Similar Documents at Salem |
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217M2101999-10-19019 October 1999 Forwards NRC Rept Number 17, Requal Tracking Rept from Operator Licensing Tracking Sys.Rept Was Used by NRC to Schedule Requalification Exam for Operators & Record Requal Pass Dates ML18107A5601999-10-18018 October 1999 Submits 30-day Fuel Clad Temp Rept,Iaw 10CFR50.46.Rept Describes Changes to Calculated Peak Clad Temp (PCT) for Salem Generating Station Large & Small Break LOCA Analyses ML18107A5531999-10-0808 October 1999 Forwards Summary Rept of Plant Startup & Power Ascension Testing for Sgs,Unit 2 Cycle 11,per Requirements of TS 6.9.1.1 ML18107A5561999-10-0707 October 1999 Requests Relief Associated with Containment Examinations at Hope Creek & Salem Generating Stations.Attachment 1 Includes Proposed Alternatives & Supporting Justification for Relief Requests ML18107A5591999-10-0505 October 1999 Informs That Nj Dept of Environ Protection Has No Comments on License Change Request S99-07 for Sgs,Units 1 & 2 ML18107A5501999-10-0505 October 1999 Provides Current Status of Pse&G Actions Re GL 98-01, Y2K Readiness of Computer Sys at Npps, for Salem Nuclear Generating Station,Units 1 & 2 & Hope Creek Nuclear Generating Station ML18107A5521999-10-0505 October 1999 Encourages NRC to Support Abb Combustion Engineering Nuclear Power Request for Priority Review of Generic TR Re Crossflow Ultrasonic Flow Measurement Sys IR 05000272/19990071999-09-28028 September 1999 Forwards Insp Repts 50-272/99-07 & 50-306/99-07 on 990721- 0831.One Potentially Safety Significant Issue Identified Dealing with Control Room Special Ventilation System.Four Addl Issues of Low Safety Significance Identified ML18107A5341999-09-22022 September 1999 Provides Data Re Operator Licensing Exam for Salem & Hope Creek Station,In Response to NRC Form 536 (7-1999) ML18107A5421999-09-22022 September 1999 Forwards Discharge Monitoring Rept for Salem Generating Station for Aug 1999.Rept Is Required by & Prepared Specifically for EPA & Nj Dept of Environ Protection ML20212B3631999-09-14014 September 1999 Forwards Rev 13 to Salem - Hope Creek Security Plan,Iaw 10CFR50.54(p).Summary of Proposed Changes to Plan,Encl. Encl Withheld ML18107A5321999-09-13013 September 1999 Forwards Revised 10CFR50.92 Evaluation to Clarify Util Response to Question Number 1 Re Amend to Modify TS 3/4 8.1, AC Power Sources. ML18107A5351999-09-13013 September 1999 Informs That NRC Has Reviewed Pse&G Request Proposing to Modify TS Which Allow EDG to Be Operated for 24 Surveillance Test During Any Mode,Iaw 10CFR50.91(b) & Has No Comments ML18107A5331999-09-13013 September 1999 Provides Notification That PSEG Intends to Utilize ASME Code Case N-481 During Second ISI Interval at Sgs Units 1 & 2 ML18107A5221999-09-0808 September 1999 Requests Approval to Use ASME Code Case N546,which Provides Alternative Qualification Requirements That Allow Personnel Most Familiar with Walkdown of Plant Sys,Like License Operators to Perform VT-2 Examinations ML18107A5231999-09-0808 September 1999 Forwards Salem Generating Station Semiannual Radioactive Effluent Release Rept for Jan-June 1999. Rept Summarizes Liquid & Gaseous Releases & Solid Waste Shipments from Salem Generating Station for Period of Jan-June 1999 ML18107A4981999-08-26026 August 1999 Forwards Response to NOV That Resulted from Predecisional Enforcement Conference Conducted on 990624.Corrective Actions:Communications to Supervisors Reinforced Employee Right & Duty to Raise Nuclear Safety Issues ML18107A5181999-08-26026 August 1999 Forwards Ninety Day Rept for ISI Activities Conducted at Sgs,Unit 2 During Ninth Extended Outage & Tenth Refueling Outage.List of Encl,Provided ML18107A5061999-08-26026 August 1999 Provides First Feedback from Observation of NRC Insp Under Pilot Nuclear Power Plant Insp Program.Attached Are Completed Insp Feedback Forms for Procedure 71111, Attachment 21 & Procedure 71151 ML18107A5051999-08-24024 August 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Request IAW Requirements of 10CFR50.91(b) & Has No Comments Re Amend to FOL Change Request S99-02 to Modify TS Re Penetration Valves ML18107A4921999-08-23023 August 1999 Provides Suppl Info Re 971024 Amend Request to Modify TS 3/4 7.7, Auxiliary Bldg Exhaust Air Filtration Sys. Util Withdraws from Request All Proposed Changes Associated with Filter Testing,Per Issuance of GL 99-02 ML18107A4911999-08-20020 August 1999 Forwards Revised Plant Attribute Libraries for Salem & Hope Creek Generating Stations,Iaw 10CFR50,App E,Vi, Emergency Response Data Sys, 3.b.Changes Are Identified by Rev Bars ML18107A4861999-08-19019 August 1999 Forwards NPDES Discharge Monitoring Rept, for Salem Generating Station for Month of Jul 1999.Rept Required by & Prepared Specifically for EPA & Nj Dept of Environ Protection ML18107A4831999-08-18018 August 1999 Submits Licensee Comments on NRC 990730 Ltr Which Provided Notification of Close Out of TAC Numbers MA0567 & MA0568 Re GL 92-01,Rev 1,Suppl 1 ML18107A4801999-08-13013 August 1999 Requests That Pse&Gs Contact in NUREG-0383, Directory of Compliance for Radioactive Matl Packages, Be Changed ML18107A4751999-08-0505 August 1999 Forwards Fitness for Duty Performance Data Rept for Six Month Period Ending 990630 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML18107A4531999-07-20020 July 1999 Forwards Discharge Monitoring Rept for Salem Generating Station, for June 1999.Rept Is Required by & Prepared for EPA & Nj Dept of Environ Protection ML18107A4431999-07-0606 July 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Pse&G License Change Request S98-17 Re Permissible Enrichment Values for New Fuel Storage & Has No Comments ML20196J6301999-07-0101 July 1999 Requests Addl Info Re Status of Decommissioning Funding for Limerick Generating Station,Units 1 & 2,Peach Bottom Atomic Power Station,Units 1,2 & 3 & Salem Nuclear Generating Station,Units 1 & 2 ML18107A4181999-06-30030 June 1999 Submits Response to NRC Request for Info Re Y2K Readiness at Npps,Per GL 98-01,suppl 1.Disclosure Encl ML20209B6751999-06-29029 June 1999 Ack Receipt of from Dr Powell in Response to NRC Re Fitness for Duty.Attachment 2 of Will Be Withheld from Public Disclosure,Per 10CFR2.790 ML18107A4131999-06-25025 June 1999 Provides Further Clarification of Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting Station SBO & Loca/Loop Loading Requirements,Per Util 990426 Ltr & Discussion with NRC ML18107A4091999-06-22022 June 1999 Forwards Discharge Monitoring Rept for May 1999,containing Info as Required by Permit NJ0005622.Rept Prepared Specifically for EPA & Nj Dept of Environ Protection ML18107A4061999-06-21021 June 1999 Provides Supplemental Info to Proposed License Amend, Modifying TS 3/4 7.7, Auxiliary Bldg Exhaust Air Filtration Sys. Info Re Acceptance Criterion Discussed ML18107A3691999-06-11011 June 1999 Forwards Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1.Original Submittal Contained Typo for year-to-date Value for Numbers of Hours Generator Was on Line (Service Hours) ML18107A3641999-06-0404 June 1999 Requests Enforcement Discretion for TS 3/4.6.2.3 Re Containment Cooling Sys for Salem Generating Station,Unit 1 ML18107A3561999-06-0303 June 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Pse&G License Change Request S99-05 & Has No Comments ML18107A3611999-05-27027 May 1999 Forwards Responses to NRC 990301 & 990323 RAIs for Salem & Hope Creek Generating Stations Relating to GL 96-05 ML18107A3301999-05-24024 May 1999 Forwards Suppl Info Re GL 95-07, Pressure Locking & Thermal Binding of Safety Related Power Operated Gate Valves. Encl Contains Methodology Used in Determination of Pressure Locking Susceptibility of PORVs Block Valves ML18107A3371999-05-21021 May 1999 Forwards NPDES Discharge Monitoring for Salem Generating Station for Apr 1999, Containing Info as Required by Permit NJ0005622 ML18107A3291999-05-20020 May 1999 Forwards Redacted Response to NRC 990322 RAI Re Notification of Licensed Operator That Tested Positive for Alcohol. Attachment 2 Withheld,Per 10CFR2.790(a)(6) ML18107A3031999-05-18018 May 1999 Provides Summary of Changes to NRC Commitments That Have Been Made But Not Reported by Other Means,Iaw with NEI Process for Managing NRC Commitments ML18107A2891999-05-13013 May 1999 Forwards Rev 36 to Pse&G Nuclear Business Unit Emergency Plan. Rev 36 Incorporates Changes to Section 1-3,6 & 7 & 9-17.Attached Copy Includes All Sections of EP for Completeness ML18107A2951999-05-12012 May 1999 Submits SG Tube Plugging Rept,Per Plant TS 4.4.6.5.a.Total of 47 Tubes Were Plugged During SG Tube Insps,Which Were Completed During Plant Tenth RFO ML18107A2861999-05-11011 May 1999 Forwards Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. COLR Rept Was Received by Util as Part of Reload SE ML18107A2481999-04-29029 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept for Salem & Hope Creek Generating Stations. Rept Summarizes Results of Radiological Environ Surveillance Program for 1998 ML18107A2511999-04-27027 April 1999 Submits 30-day Fuel Clad Temp Rept for Salem Generating Station,Units 1 & 2.Rept Describes Changes to Calculated Peak Clad Temp (PCT) for Plant Large & Small LOCA & Small Break LOCA Analyses ML18107A2631999-04-26026 April 1999 Provides Clarification on Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting SBO & Loca/ LOOP Loading Requirements ML18107A2371999-04-26026 April 1999 Forwards Corrected Response to NRC RAI Re Licensee Request for Change to TS Permissible Enrichment Values for New Fuel Storage.Incorrect Attachment Was Provided with Util 990412 Ltr to Nrc.Encl Supersedes 990412 Submittal 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML18107A5601999-10-18018 October 1999 Submits 30-day Fuel Clad Temp Rept,Iaw 10CFR50.46.Rept Describes Changes to Calculated Peak Clad Temp (PCT) for Salem Generating Station Large & Small Break LOCA Analyses ML18107A5531999-10-0808 October 1999 Forwards Summary Rept of Plant Startup & Power Ascension Testing for Sgs,Unit 2 Cycle 11,per Requirements of TS 6.9.1.1 ML18107A5561999-10-0707 October 1999 Requests Relief Associated with Containment Examinations at Hope Creek & Salem Generating Stations.Attachment 1 Includes Proposed Alternatives & Supporting Justification for Relief Requests ML18107A5501999-10-0505 October 1999 Provides Current Status of Pse&G Actions Re GL 98-01, Y2K Readiness of Computer Sys at Npps, for Salem Nuclear Generating Station,Units 1 & 2 & Hope Creek Nuclear Generating Station ML18107A5521999-10-0505 October 1999 Encourages NRC to Support Abb Combustion Engineering Nuclear Power Request for Priority Review of Generic TR Re Crossflow Ultrasonic Flow Measurement Sys ML18107A5591999-10-0505 October 1999 Informs That Nj Dept of Environ Protection Has No Comments on License Change Request S99-07 for Sgs,Units 1 & 2 ML18107A5341999-09-22022 September 1999 Provides Data Re Operator Licensing Exam for Salem & Hope Creek Station,In Response to NRC Form 536 (7-1999) ML20212B3631999-09-14014 September 1999 Forwards Rev 13 to Salem - Hope Creek Security Plan,Iaw 10CFR50.54(p).Summary of Proposed Changes to Plan,Encl. Encl Withheld ML18107A5321999-09-13013 September 1999 Forwards Revised 10CFR50.92 Evaluation to Clarify Util Response to Question Number 1 Re Amend to Modify TS 3/4 8.1, AC Power Sources. ML18107A5331999-09-13013 September 1999 Provides Notification That PSEG Intends to Utilize ASME Code Case N-481 During Second ISI Interval at Sgs Units 1 & 2 ML18107A5351999-09-13013 September 1999 Informs That NRC Has Reviewed Pse&G Request Proposing to Modify TS Which Allow EDG to Be Operated for 24 Surveillance Test During Any Mode,Iaw 10CFR50.91(b) & Has No Comments ML18107A5231999-09-0808 September 1999 Forwards Salem Generating Station Semiannual Radioactive Effluent Release Rept for Jan-June 1999. Rept Summarizes Liquid & Gaseous Releases & Solid Waste Shipments from Salem Generating Station for Period of Jan-June 1999 ML18107A5221999-09-0808 September 1999 Requests Approval to Use ASME Code Case N546,which Provides Alternative Qualification Requirements That Allow Personnel Most Familiar with Walkdown of Plant Sys,Like License Operators to Perform VT-2 Examinations ML18107A5061999-08-26026 August 1999 Provides First Feedback from Observation of NRC Insp Under Pilot Nuclear Power Plant Insp Program.Attached Are Completed Insp Feedback Forms for Procedure 71111, Attachment 21 & Procedure 71151 ML18107A5181999-08-26026 August 1999 Forwards Ninety Day Rept for ISI Activities Conducted at Sgs,Unit 2 During Ninth Extended Outage & Tenth Refueling Outage.List of Encl,Provided ML18107A4981999-08-26026 August 1999 Forwards Response to NOV That Resulted from Predecisional Enforcement Conference Conducted on 990624.Corrective Actions:Communications to Supervisors Reinforced Employee Right & Duty to Raise Nuclear Safety Issues ML18107A5051999-08-24024 August 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Request IAW Requirements of 10CFR50.91(b) & Has No Comments Re Amend to FOL Change Request S99-02 to Modify TS Re Penetration Valves ML18107A4921999-08-23023 August 1999 Provides Suppl Info Re 971024 Amend Request to Modify TS 3/4 7.7, Auxiliary Bldg Exhaust Air Filtration Sys. Util Withdraws from Request All Proposed Changes Associated with Filter Testing,Per Issuance of GL 99-02 ML18107A4911999-08-20020 August 1999 Forwards Revised Plant Attribute Libraries for Salem & Hope Creek Generating Stations,Iaw 10CFR50,App E,Vi, Emergency Response Data Sys, 3.b.Changes Are Identified by Rev Bars ML18107A4831999-08-18018 August 1999 Submits Licensee Comments on NRC 990730 Ltr Which Provided Notification of Close Out of TAC Numbers MA0567 & MA0568 Re GL 92-01,Rev 1,Suppl 1 ML18107A4801999-08-13013 August 1999 Requests That Pse&Gs Contact in NUREG-0383, Directory of Compliance for Radioactive Matl Packages, Be Changed ML18107A4751999-08-0505 August 1999 Forwards Fitness for Duty Performance Data Rept for Six Month Period Ending 990630 ML20210M7571999-08-0404 August 1999 Forwards Response to Requesting Addl Info Re Status of Decommissioning Funding for Lgs,Pbaps & Sngs. Attachment Provides Restatement of Questions Followed by Response ML18107A4431999-07-0606 July 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Pse&G License Change Request S98-17 Re Permissible Enrichment Values for New Fuel Storage & Has No Comments ML18107A4181999-06-30030 June 1999 Submits Response to NRC Request for Info Re Y2K Readiness at Npps,Per GL 98-01,suppl 1.Disclosure Encl ML18107A4131999-06-25025 June 1999 Provides Further Clarification of Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting Station SBO & Loca/Loop Loading Requirements,Per Util 990426 Ltr & Discussion with NRC ML18107A4061999-06-21021 June 1999 Provides Supplemental Info to Proposed License Amend, Modifying TS 3/4 7.7, Auxiliary Bldg Exhaust Air Filtration Sys. Info Re Acceptance Criterion Discussed ML18107A3691999-06-11011 June 1999 Forwards Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1.Original Submittal Contained Typo for year-to-date Value for Numbers of Hours Generator Was on Line (Service Hours) ML18107A3641999-06-0404 June 1999 Requests Enforcement Discretion for TS 3/4.6.2.3 Re Containment Cooling Sys for Salem Generating Station,Unit 1 ML18107A3561999-06-0303 June 1999 Informs That Nj Dept of Environ Protection Bureau of Nuclear Engineering Has Reviewed Pse&G License Change Request S99-05 & Has No Comments ML18107A3611999-05-27027 May 1999 Forwards Responses to NRC 990301 & 990323 RAIs for Salem & Hope Creek Generating Stations Relating to GL 96-05 ML18107A3301999-05-24024 May 1999 Forwards Suppl Info Re GL 95-07, Pressure Locking & Thermal Binding of Safety Related Power Operated Gate Valves. Encl Contains Methodology Used in Determination of Pressure Locking Susceptibility of PORVs Block Valves ML18107A3291999-05-20020 May 1999 Forwards Redacted Response to NRC 990322 RAI Re Notification of Licensed Operator That Tested Positive for Alcohol. Attachment 2 Withheld,Per 10CFR2.790(a)(6) ML18107A3031999-05-18018 May 1999 Provides Summary of Changes to NRC Commitments That Have Been Made But Not Reported by Other Means,Iaw with NEI Process for Managing NRC Commitments ML18107A2891999-05-13013 May 1999 Forwards Rev 36 to Pse&G Nuclear Business Unit Emergency Plan. Rev 36 Incorporates Changes to Section 1-3,6 & 7 & 9-17.Attached Copy Includes All Sections of EP for Completeness ML18107A2951999-05-12012 May 1999 Submits SG Tube Plugging Rept,Per Plant TS 4.4.6.5.a.Total of 47 Tubes Were Plugged During SG Tube Insps,Which Were Completed During Plant Tenth RFO ML18107A2861999-05-11011 May 1999 Forwards Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. COLR Rept Was Received by Util as Part of Reload SE ML18107A2481999-04-29029 April 1999 Forwards 1998 Annual Radiological Environ Operating Rept for Salem & Hope Creek Generating Stations. Rept Summarizes Results of Radiological Environ Surveillance Program for 1998 ML18107A2511999-04-27027 April 1999 Submits 30-day Fuel Clad Temp Rept for Salem Generating Station,Units 1 & 2.Rept Describes Changes to Calculated Peak Clad Temp (PCT) for Plant Large & Small LOCA & Small Break LOCA Analyses ML18107A2371999-04-26026 April 1999 Forwards Corrected Response to NRC RAI Re Licensee Request for Change to TS Permissible Enrichment Values for New Fuel Storage.Incorrect Attachment Was Provided with Util 990412 Ltr to Nrc.Encl Supersedes 990412 Submittal ML18107A2631999-04-26026 April 1999 Provides Clarification on Licensing & Design Basis for 125 Vdc Battery Margins for Sgs & HCGS for Meeting SBO & Loca/ LOOP Loading Requirements ML18107A2411999-04-22022 April 1999 Forwards Draft Revised Pages 4.1 & 4.2 of Nuclear Business Unit Emergency Plan for Hope Creek & Salem Generating Stations.Changes Are Noted in Italics ML18107A1841999-04-14014 April 1999 Forwards PSEG Annual Rept for 1998, & PECO Annual Rept for 1998. Stockholders Annual Rept of Each Owner & Cash Flow Statements Showing 1998 Actual & 1999 Projected Cash Flow with Explanation Encl ML18107A1981999-04-12012 April 1999 Responds to 990312 RAI Re Request for Change to TSs Permissible Enrichment Values for New Fuel Storage,Which Was Submitted on 990202 ML18107A1691999-04-12012 April 1999 Forwards Proprietary & non-proprietary Epips,Including Rev 17 to EPIP 807,rev 1 to NC.EP-EP.ZZ-0801(Q) & Rev 2 to NC.EP-EP.ZZ-0806(Q) & Revised EPIPs Table of Contents. Proprietary Info Withheld ML20205K4541999-04-0808 April 1999 Forwards Revised Info Re 990330 NRC Nuclear Power Reactor Licensee Financial Qualifications & Decommissioning Funding Assurance Status Rept ML18106B1491999-04-0505 April 1999 Forwards Drafts of Proposed Changes to Pages 4.1 & 4.2 of Emergency Plan,Which Are Contained on Page 4.2 & Noted in Italics & Underlined ML20205F8981999-03-31031 March 1999 Provides Info Re Status of Decommissioning Funding for LGS, Units 1 & 2,PBAPS,Units 1,2 & 3 & Sgs,Units 1 & 2,per Requirements of 10CFR50.75(f)(1) ML18106B1431999-03-31031 March 1999 Forwards Pse&G Rept on Financial Min Assurance for Period Ending 981231 for Hope Creek,Salem,Units 1 & 2 & Pbaps,Units 2 & 3,IAW 10CFR50.75 ML18107A2201999-03-30030 March 1999 Forwards Final Exercise Rept for 980303,full-participation Plume Exposure Pathway Exercise & 980505-07, full-participation Ingestion Pathway Exercise of Offsite Radiological Emergency Response for Salem & Hope Creek 1999-09-08
[Table view] Category:UTILITY TO NRC
MONTHYEARML18095A4881990-09-17017 September 1990 Requests Regional Waiver of Compliance from Tech Spec 3.6.2.3, Containment Cooling Sys. Waiver Requested in Order to Allow Replacement of Containment Fan Cooler Unit Motor #22 W/O Requiring Plant Shutdown ML18095A4901990-09-13013 September 1990 Provides Supplemental Info Applicable to Clarification of 10CFR50,App R Exemption Request Re Fire Suppression Sys for Panel 335,per NRC Request ML20059E6821990-09-0404 September 1990 Forwards Info Re Temporary Mod to Security Plan Concerning Protected Area.Info Withheld ML18095A4641990-08-31031 August 1990 Forwards Revised Response to NRC Bulletin 88-004 Re Potential pump-to-pump Interaction.Util Pursuing Permanent Solution to Issue & Will Implement Appropriate Permanent Field Change by End of Unit 1 10th Refueling Outage ML18095A4621990-08-31031 August 1990 Provides Revised Response to Generic Ltr 89-13, Svc Water Problems Affecting Safety-Related Equipment. Only HXs Exhibiting Unsatisfactory Test Results Will Be Inspected & Possibly Cleaned ML18095A4431990-08-30030 August 1990 Forwards Salem Generating Station Semiannual Radioactive Effluent Release Rept,Jan-June 1990 & Rev 6 to Odcm. ML18095A4531990-08-30030 August 1990 Forwards RERR-28, Salem Generating Station Semiannual Radioactive Effluent Release Rept for Jan-June 1990 & Revised Odcm.W/O Revised ODCM ML18095A4391990-08-29029 August 1990 Forwards Semiannual Rept Re fitness-for-duty Performance Data for 6-month Period Ending 900630,per 10CFR26.71(d).Rept Includes Testing Results,Random Testing Program Results & Confirmed Positive Tests for Specific Substances ML18095A4421990-08-28028 August 1990 Clarifies 900710 Request for Amends to Licenses DPR-70 & DPR-75,changing Sections I & M.Under Proposed Change,Section I Should Be Changed to Read Section 2.J for License DPR-70 & Section M Changed to Read Section 2.N for License DPR-75 ML20059B6611990-08-22022 August 1990 Confirms That 10 Anchor/Darling Model S350W Swing Check Valves Installed at Plant,Per NRC Bulletin 89-002.All 18 Valves Inspected & Retaining Block Studs Replaced W/Upgraded Matl.No Crack Noted on Any Studs Which Were Replaced ML20059C2861990-08-21021 August 1990 Provides Correction to 900810 Response to Request for Addl Info Re Util Request for Restatement of OL Expiration Dates ML18095A4151990-08-10010 August 1990 Forwards Response to Request for Addl Info Re Reinstatement of OL Expiration Dates Based on Original Issuance of Ols. Advises That Correct Expiration Date for OL Proposed to Be 200418 ML18095A4091990-08-0909 August 1990 Forwards Responses to NRC Comments Re Plant Simulator Certification for 10CFR55.45(b)(2),per 891228 Ltr ML18095A4061990-08-0808 August 1990 Forwards Corrected marked-up Pages for Tech Spec Table 3.3-11 Re Subcooling Margin Monitor & Reactor Vessel Level Instrumentation Sys,Per 900223 Ltr.Administrative Changes Made as Indicated ML18095A3861990-07-30030 July 1990 Forwards Listing of Station Blackout Major Audit Items Resolution Scope,Per Station Blackout Schedule Commitment ML18095A3661990-07-26026 July 1990 Forwards Decommissioning Repts for Hope Creek,Peach Bottom & Salem Nuclear Generating Stations ML18095A3761990-07-26026 July 1990 Forwards Decommissioning Repts & Certification of Financial Assurance for Plants ML18095A3721990-07-24024 July 1990 Forwards Rept & Certification of Financial Assurance for Decommissioning for Plants,Per 10CFR50.75 ML18095A3751990-07-18018 July 1990 Provides Status of Commitments Made to NRC by Util in 900109 Ltr Re NUREG-0737,Item II.D.1,per 900628 Telcon ML18095A3741990-07-18018 July 1990 Provides Supplemental Info Re Facility sub-cooling Margin Monitor ML18095A3611990-07-18018 July 1990 Responds to NRC Bulletin 90-001, Loss of Fill-Oil in Transmitters Mfg by Rosemount. ML18095A3621990-07-18018 July 1990 Forwards Corrected Tech Spec Page 3/4 3-5 for License Change Request 89-12 Submitted on 891227 & 900521 ML18095A3591990-07-13013 July 1990 Corrects Typo in 900702 Response to Generic Ltr 90-04 Re Schedule for Completion of Remaining Open Items ML18095A3471990-07-11011 July 1990 Responds to NRC 900611 Ltr Re Violations Noted in Insp Repts 50-272/90-14 & 50-311/90-14.Corrective Actions:Directive from Radiation Protection Mgt to All Radiation Protection Personnel Issued Re Control of Compliance Agreement Sheets ML18095A3451990-07-10010 July 1990 Forwards Addl Info Re License Change Request 89-03 Re Reactor Trip Sys Instrumentation ML18095A3461990-07-10010 July 1990 Responds to NRC 900608 Ltr Re Violations Noted in Insp Repts 50-272/90-12 & 50-311/90-12.Corrective Actions:Assessment of ECCS & Component Performance Undertaken & ECCS Flow Testing Procedure Upgraded to Address Human Factors ML18095A3491990-07-10010 July 1990 Forwards Jn Steinmetz of Westinghouse 900614 Ltr Re Reassessment of Util Response to Bulletin 88-002 ML18095A3481990-07-10010 July 1990 Submits Supplemental Rept Identifying Root Cause of Missed Commitment & Corrective Actions to Assure Future Compliance Re Implementation of Mods to Facility PASS ML18095A3441990-07-0909 July 1990 Provides Written Notification Re Change in Calculated Peak Clad Temp,Per 900606 Verbal Notification ML18095A3281990-07-0202 July 1990 Responds to NRC 900530 Ltr Re Violations Noted in Insp Repts 50-272/90-09 & 50-311/90-09.Corrective Actions:Util Intends to Use Nuclear Shift Supervisor as Procedure Reader & EOP, Rev 2 Under Development ML18095A3301990-07-0202 July 1990 Responds to Generic Ltr 90-04 Re Status of Licensee Implementation of Generic Safety Issues.Table Describing Status of Generic Safety Issue Implementation Encl ML18095A3391990-06-29029 June 1990 Forwards Correction to 890913 License Change Request 88-09, Consisting of Tech Spec Page 3/4 4-13 ML18095A3221990-06-28028 June 1990 Provides Supplemental Info Re 900223 Proposed Revs to Tech Specs for Reactor Vessel Level Instrumentation Sys.Tables 3.3-11a & 3.3-11b Should Be Combined Into Single Table ML18095A3231990-06-28028 June 1990 Responds to NRC 900518 Ltr Re Violations Noted in Insp Repts 50-272/90-10,50-311/90-10 & 50-354/90-07.Two Noncited Violations Disputed.Util fitness-for-duty Program Exceeds Part 26 Requirements for Positive Blood Alcohol Limits ML18095A3241990-06-28028 June 1990 Forwards Retyped Pages to 871224 License Change Request 87-15 & Modified,Per 900620 Ltr ML18095A3211990-06-26026 June 1990 Requests 30-day Extension Until 900730 to Provide Completion Schedule to Resolve Audit Findings Re Station Blackout ML18095A3161990-06-25025 June 1990 Forwards Supplemental Info Re Response to Generic Ltr 88-14. All Committed Actions Complete as of 900613 ML18095A3141990-06-25025 June 1990 Provides Schedule Change for Implementation of Control Room Mods.Schedule Modified to Address Overhead Annunciator Human Engineering Discrepancies During Phase III ML18095A3201990-06-25025 June 1990 Responds to NRC 900524 Ltr Re Violations Noted in Insp Repts 50-272/90-11 & 50-311/90-11.Corrective Actions:All Overdue Operations & Maint Procedure Files Reviewed for Outstanding Rev Requests & Procedure Upgrade Program Initiated ML18095A3001990-06-20020 June 1990 Provides Addl Info Re Application for Amend to Licenses DPR-70 & DPR-75 Concerning Turbine Valve Surveillance Interval,Per 900320 Request.Util Adding Direction to Personnel If Unnacceptable Flaws Found ML20043H6221990-06-20020 June 1990 Provides Supplemental Info Re NRC Bulletin 88-008 for Fifth Refueling Outage.Detailed Test Rept Being Prepared to Document Results of Each Individual Insp Re Insulation, Hangers & High Energy Break Areas ML18095A2991990-06-20020 June 1990 Forwards Westinghouse Affidavit Supporting 900412 Request for Withholding Proprietary Info from Public Disclosure Per 10CFR2.790 ML18095A2721990-06-0808 June 1990 Responds to NRC 900329 Ltr Re Weaknesses Noted in Insp Repts 50-272/90-80 & 50-311/90-80.Corrective Actions:Fire Doors Placed on Blanket Preventive Maint Work Order & Damaged Fire Doors Will Be Repaired Immediately ML18095A2711990-06-0606 June 1990 Submits Info in Support of 900522 Verbal Request for Relief from Requirements of ASME Section XI ML18095A2611990-06-0101 June 1990 Forwards Corrected Operating Data Rept, Page for Apr 1990 Monthly Operating Rept ML18095A2521990-06-0101 June 1990 Forwards Application in Support of Request for Renewal of NJPDES Permit NJ0005622,per Requirements of Subsection 3.2 of Plant Environ Protection Plan,Nonradiological ML18095A2591990-06-0101 June 1990 Forwards Corrected Unit Shutdown & Power Reductions, Page for Apr 1990 Monthly Operating Rept ML18095A2411990-05-30030 May 1990 Submits Special Rept 90-4 Addressing Steam Generator Tube Plugged During Fifth Refueling Outage.Plugging Completed on 900516.Cause of Tube Degradation Attributed to Normal Wear Due to Erosion/Corrosion Factors ML18095A2431990-05-30030 May 1990 Informs of Util Plans Re Facility Cycle 6 Reload Core, Expected to Achieve Burnup of 16600 Mwd/Mtu.All Postulated Events within Allowable Limits Based on Review of Basis of Cycle 6 Reload Analysis & Westinghouse SER ML18095A2531990-05-29029 May 1990 Provides Addl Info Re End of Life Moderator Temp Coefficient.Feedback Used in Steam Line Break Has No Relationship to Full Power Moderator Density Coefficient 1990-09-04
[Table view] |
Text
- Public Service Electric and Gas Company Steven E. Miltenberger Public Service Electric and Gas Company P.O. Box 236, Hancocks Bridge, NJ 08038 609-339-4199 Vice President and Chief Nuclear Officer October 21, 1988 NLR-N88176 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
REQUEST FOR TEMPORARY EXEMPTION FROM 10 CFR 50.46(a)(l)(i)
SALEM GENERATING STATION, UNIT 2 DOCKET NO. 50-311 Public Service Electric and Gas Company (PSE&G) hereby requests temporary exemption from certain administrative portions of 10 CFR 50.46(a)(l)(i) for Salem Generating Station Unit 2 in order to return to power operation. As a result the fourth refueling outage at Salem Unit 2, all the Row 1 steam generator tubes were plugged and some unrecoverable loose parts were left in the Reactor Coolant System. A safety evaluation has been performed to demonstrate no significant safety impact, including an evaluation of the Large Break LOCA analysis (see Attachments 2 and 3). However, the requirement exists to formally revise the Large Break LOCA analysis to accurately reflect and document the current plant configuration in the ECCS Appendix K model.
The amount of time required to complete the reanalysis extends well beyond the planned date for return to power operation from the fourth refueling outage. Therefore, a one-time, temporary exemption from the adminstrative requirement of 10 CFR 50.46(a)(l)(i) is necessary until the formal analysis has been completed and is available for submittal, scheduled for March 31, 1989. As discussed in Attachment 1, PSE&G has concluded that this exemption request satisfies the requirements of 10 CFR 50.12(a).
Therefore, PSE&G requests the NRC to review and approve this exemption request by October 27, 1988 in order to permit Salem Unit 2 to enter Mode 2 and return to power operation. Pursuant to the requirements of 10 CFR 170.21, a check in the amount of
$150.00 is enclosed.
0 ADOCK 05000311
~ aR1 fo301as asio21
Document Control Desk 2 10/21/88 Should you have any questions, do not hesitate to contact us.
Sincerely, Attachments (3) c Mr. J. C. Stone Licensing Project Manager Mr. R. W. Borchardt Senior Resident Inspector Mr. W. T. Russell, Administrator USNRC Region I Ms. J. Moon, Interim Chief Bureau of Nuclear Engineering Department of Environmental Protection CN 415 Trenton, NJ 08625
ATTACHMENT 1 REQUEST FOR TEMPORA.RY EXEMPTION FROM CERTAIN ADMINISTRATIVE REQUIREMENTS OF 10 CFR 50.46(a) (1) (i) .
In accordance with the requirements of 10 CFR 50.12(a), Public Service Electric and Gas Company (PSE&G) hereby requests a temporary exemption to certain administrative requirements of 10 CFR 50.46(a)(l)(i) for.Salem Generating Station Unit 2.
I.
SUMMARY
OF THE CURRENT SITUATION As a result of eddy current examinations performed during the Salem Unit 2 Fourth Refueling Outage, defective tubes were discovered in two steam generators which were indicative of the Westinghouse Series 51 Steam Generator Row 1, U-bend tangent
, cracking phenomenon. In addition to plugging the defective tubes, PSE&G decided to plug the Row 1 tubes in all four Salem Unit 2 steam generators as a precautionary measure. As a result of this decision, 2.7% of the Salem Unit 2 steam generator tubes have been plugged. The reduced flow as a result of this condition affects the peak cladding temperature and requires a Large Break LOCA ECCS reanalysis for Salem Unit 2.
During refueling operations a burnable poison rodlet assembly hold down nut, a locking weld pin and a hand held gamma measurement probe with cable connector were inadvertently dropped into the reactor cavity. Subsequent efforts to retrieve these items were unsuccessful. *As a result, a decision was made to evaluate these objects as loose parts within the reactor coolant system. The potential for a partial flow blockage to or within fuel assemblies affects of the peak cladding temperature and requires a Large Break LOCA ECCS reanalysis for Salem Unit 2.
While these events do not present any safety.concerns or operational considerations for the reasons detailed in Attachments 2 and 3, a formal reanalysis is required to confirm that Salem Unit 2 meets the applicable criteria of 10 CFR
- 50~46(b) based on the current plant configuration.
II. BASIS FOR THE EXEMPTION REQUEST For plants licensed based on the 1978 Westinghouse Large Break LOCA model, Generic Letter 86-16 requires subsequent plant changes which affect the results of the model, to be reevaluated against an updated, approved model and submitted in accordance with 10 CFR 50.46(a)(l)(i). Since the reanalysis with the new Page 1 of 5
ECCS model cannot be completed for approximately 5 months (for the reasons discussed in Section III) and because Salem Unit 2 is scheduled to enter Mode 2 on October 27, 1988, PSE&G requests a one-time, temporary exemption from 10 CFR 50.46(a)(l)(i) based on the specific circumstances discussed in Section III and the technical arguments contained in the Westinghouse Safety Evaluations pLovided in Attachments 2 and 3.
In summary the Safety Evaluations conclude that the requirements of 10 CFR 50.46(b), including the maximum peak cladding temperature (PCT) limit of 2200°F are satisfied and the safe operation of Salem Unit 2 is assured. The Safety Evaluations are based on sensitivity studies which indicate that the current maximum Large Break LOCA (LB LOCA) PCT value of 2130°F would increase by a maximum of 28°F' as a result of the tube plugging modifications and a maximum of approximately 22°F as a result of the potential flow blockage effect of the loos*e parts. However, the actual rr.axirnum LB LOCA PCT, due to the combined effects discussed above, will not change due to the offsetting effect of reduced rod internal backfill pressure of currently used fuel assemblies previously evaluated but not yet incorporated into the existing analysis. The Safety Evaluations provide sufficient information to conclude that this exemption request does not involve a* significant increase in the probability or consequences of an accident previously evaluated, does not create the possibility of a new or different kind of accident from any accident previously evaluated and does not involve a significant reduction in a margin of safety. Therefore, it can be concluded that this exemption does not involve a safety concern nor present an undue risk to the public health and safety and is consistent with the common defense and security.
III. SPECIFIC JUSTIFYING CIRCUMSTANCES This request meets the criteria established by the NRC in 10 CFR 50.12(a)(2) in that special circumstances are present which warrant. approval. Specifically, Paragraphs 50.12(a)(2)(ii),
50.12(a)(2)(iii) and 50.12(a)(2)(v) apply to the current situation. 10 CFR 50.12(a)(2)(ii) states:
"Application of the regulation in the particular circumstances would not serve the underlying purpose of the rule or is not necessary to achieve the underlying purpose of the rule. "
- PSE&G believes that the immediate submittal of the formally amended ECCS analysis is not necessary to achieve the underlying purpose of 10 CFR 50.46 provided that sufficiently detailed information is available to justify the safe operation of the
- station in accordance with the applicable regulatory requirements. Attachments 2 and 3 contain the Safety Evaluations which indicate that the sensitivity studies performed on the current ECCS analyses assure that the calculated PCT value is Page 2 of 5
bounding and in compliance with 10 CFR 50.46(b). Additionally, PSE&G commits to complete the ECCS reanalysis, using the 1981 Westinghouse ECCS model with BASH, by March 31, 1989 and provide a final report to the NRC staff for review.
10 CFR 50.12(a)(2)(iii) states:
"Compliance would result in undue hardship or other costs that are significantly in excess of those contemplated when the regulation was adopted, or that are significantly in excess of those incurred by others similarly situated."
Without approval of the temporary exemption request, PSE&G would be required to complete the ECCS reanalysis prior to return to power operation of Salem Unit 2. Completion of this reanalysis requires significant expenditures of engineering manpower by Westinghouse (i.e. developing revised computer codes, inputting amended parameters, running lengthy computer codes, verifying output results, and generating a final report and conclusion) and takes a minimum of 5 months to complete. In addition, during the time in which the analysis was being performed, Salem Unit 2 could not return to operational service even though physically ready which results in a severe financial penalty and the associated costs of replacement power. Finally, similar requests have been granted to Tennessee Valley Authority for Sequoyah Unit 1 and Pacific Gas* and Electri~ Company for Diablo Canyon Unit 2 which, if not applied to Salem Unit 2 would result in a significant cost well in excess of that incurred by others.
10 CFR 50.12(a)(2)(v) states:
"The exemption would provide only temporary relief from the applicable regulation and the licensee or applicant has made good faith efforts to comply with the regulation."
As indicated above, PSE&G is only requesting this exemption on a one-time, temporary basis and fully intends to complete the necessary reanalysis and provide a report to the NRC staff by March 31, 1989. ,In the meantime, PSE&G has completed Safety Evaluations which justify the safe operation of Salem Unit 2.
The requirements of 10 CFR 50.46(b) have been satisfied as demonstrated in the Safety Evaluations and will be applied to the reanalysis as well.
- IV. TECHNICAL CONSIDERATIONS contains a Safety Evaluation which addresses the technical concerns associated with plugging the steam generator tubes. Information is also provided in the form of the results of a sensitivity study which evaluates the effects of tube plugging on the current Large Break LOCA ECCS analysis and against the requirements of 10 CFR 50.46(b). From the detailed Page 3 of 5
discussion provided, PSE&G has concluded that this exemption request does not represent a safety concern. contains a Safety Evaluation which addresses the technical concerns associated with the presence of several loose parts in the reactor coolant system. Information is also provided in the form of the results of a sensitivity study which evaluates the effects of loose parts on the current Large Break LOCA ECCS analysis and against the requirements of 10 CFR 50.46(b). From the detailed discussion provided, PSE&G has concluded that this exemption request does not represent a safety concern.
V. ENVIRONMENTAL ASSESSMENT The regulatory requirements of 10 CFR 50.46(b) have been applied to the sensitivity study results contained in the Safety Evaluations. None of the specific limits are exceeded as a result of the requested exemption. Therefore, operation of the station with the exemption request in place does not place the station in an unacceptable or unanalyzed condition and does not affect radiological or nonradiological plant effluents. This conclusion is applicable to both the steam generator tube plugging and the loose parts monitoring issues.
Therefore, it can be concluded, that operation of Salem Unit 2 with the proposed exemption in place will not impact the environment nor result in a situation in which the environmental impact is increased beyond that already analyzed for Salem.
VI. DATE WHEN COMPLIANCE WILL BE ACHIEVED PSE&G is currently in compliance with the requirements of 10 CFR 50.46(b) and has concluded that the enclosed Safety Evaluations adequately demonstrate interim compliance with the administrative portions of 10 CFR 50.46(a)(l)(i). However, in order to assure that the ECCS model for Salem Unit 2 is properly revised to reflect the current plant configuration, PSE&G commits to complete the subject reanalysis and provide a final report to the NRC by March 31, 1989.
VII. CONCLUSION Based on the information discussed above and the Safety Evaluations provided in Attachments 2 and 3, PSE&G has concluded that:
- 1. The requirements of 10 CFR 50.46(b) regarding the results of ECCS analysis, including PCT, have been, are and will continue to be applied to Salem Unit 2.
Accordingly, PSE&G concludes that operation of Page 4 of 5
the station with the exemption request in place will satisfy the intent of 10 CFR 50.46(a)(l)(i).
- 2. The Safety Evaluations were performed to justify delaying the submittal of the formal ECCS analysis while Salem Unit 2 returns to power operation and concludes that neither the plugging of steam generator tubes nor the presence of loose parts in the reactor coolant system represent a safety concern or create an environmental impact.
- 3. The requested exemption is authorized by law and will not present an undue risk to the public health and safety, and is consistent with the common defense and security.
- 4. Special circumstances exist which justify the approval of this exemption request including the financial costs and hardships which would be incurred if approval was not granted.
- 5. The proposed exemption does not represent a situation which is unique or isolated to Salem Unit 2 but has been encountered in the industry before and successfully approved and implemented by stations such as Sequoyah and Diablo Canyon.
PSE&G requests the NRC staff to review and approve this exemption request by October 27, 1988 in order to support entry into Mode 2 and ascension to power of Salem Unit 2.
Page 5 of 5
- ATTACHMENT 2 LARGE BREAK LOCA SAFETY EVALUATION FOR SALEM UNIT 2 FOR STEAM GENERATOR TUBE PLUGGING I. BACKGROUND During the Fourth Refueling outage for Salem Unit 2, the eddy current examination of Row 1 tubes indicated 45 defective tubes on No. 24 Steam Generator and 46 defective tubes on No. 22 Steam Generator. The defects were indicative of the Westinghouse Series 51 steam Generator U-bend tangent primary water stress corrosion cracking {PWSCC) problem in Row 1 tubes. Eddy current examination of the Row 2 tubes of Nos. 22 and 24 Steam Generators and the Row 1 and Row 2 tubes in Nos. 21 and 23 Steam Generators revealed no further evidence of "low" row U-bend tangent cracking.
Subsequent to these eddy current examination results, a decision was made by PSE&G to plug all Row 1 tubes in all four Salem Unit 2 steam generators. The plugging of all the Row 1 tubes results in 2.7% of the tubes being plugged. This safety evaluation has been prepared to indicate the acceptability of up to 3.5% tube plugging.
Since there is no change in thermal design flow used as a basis for the accident analysis, the results of the evaluation indicate the change to the NSSS design temperatures and pressures is a redgction in the steam pressure of 9 psi and steam temperature of
- 1. 4 F.
II. LARGE BREAK LOCA (FSAR Section 15.4.1)
The current Large Break LOCA analysis for Salem Unit 2, performed using the Westinghouse 1978 Evaluation Model (EM) for 17x17 standard fuel resulted in a PCT of 2130°F for the limiting Cd=0.8 break. As shown in the Salem UFSAR Section 15.4.1.2, a subsequent "evaluation," done to account for NUREG-0630 burst and blockage effects, resulted in no Fa reduction. An evaluation has been performed, based upon the 78EK, to consider the effects on the analysis of the increase in the allowable steam generator tube plugging to 3.5%.
Based upon the large break LOCA sensitivity to steam generator tube plugging documented in WCAP 8986,("Perturbation Technique for Calculating ECCS Cooling Performance", February 1977), a penalty of 14°F would be estimated for a 4-loop plant with 3.5%
tube plugging. However, studies with the 1981 Evaluation Model which incorporates the NUREG-0630 burst and blockage fuel rod models, have shown a sensitivity to tube plugging which was roughly double that cited in WCAP-8986. Thus, to account for potential non-conservatism associated with the fuel rod models in the 78EM of the establisheg sensitivity, a conservative estimate of the penalty would be 28 F.
I L_
However, the analysis was also done using fuel parameters which l
are now overly conservative. Accounting for the lower rod internal backfill pressure of the 17x17 standard fuel currently in Salem Unit 2 results in a PCT benefit larger (>100°F) than the combined penalty of 28°F associated with tube plugging and approximately 22°F penalty associated with the loose parts blockage presented in Attachment 3. Thus, the net effect would be no increase in peak clad temperature. Consequently, the evaluation in Section 15.4.1.2 to address NUREG-0630 "Clad swelling and Rupture Models for LOCA Analysis" remains applicable.
Furthermore, this evaluation using the 78EM is known to be conservative with respect to more recent, approved evaluation models. Although the 1981 Evaluation Model has shown a higher sensitivity to tube plugging than the 78EM, the 1981 EM with BASH has demonstrated an even lower sensitivity to tube plugging.
Indeed, the effect of using the improved analytical modeling techniques in either of these more recent models in total would result in a net benefit and a less limiting PCT for the plant.
Based on the discussion given above, the increase in the allowable steam generator tube plugging level to 3.5% does not result in an increase in the peak clad temperature for Salem Unit
- 2. Therefore, this change is acceptable and the resulting peak clad temperature does not change the current margin and remains within the regulatory limits.
- ATTACHMENT 3 LARGE BREAK LOCA SAFETY EVALUATION FOR SALEM UNIT 2 FOR UNRECOVERED FOREIGN PARTS IN RCS I. BACKGROUND During the Salem Unit 2 Fourth Refueling Outage, it was visually determined that a burnable poison rodlet round hold down nut and weld pin were not in place, during reactor core fuel loading and repositioning in core map position c-10, in a reload core Region 2 location. The round hold down nut affixes the burnable poison rodlet top end plug to the burnable poison rodlet positioning upper plate which locates the burnable poison rodlets within the 17 x 17 fuel assembly. The top end plug has a threaded end shank, .216 inches in diameter, that is slotted to a depth to receive the positioning plate through hole and the round hold down nut with an internal .216 inches in diameter threaded hole.
The hold down nut is slotted to the same size as the rodlet top end plug threaded shank to receive a .375 inches long pin that is tack welded in the shank and nut upon completing the rodlet -
plate - nut assembly.
During core reloading in this same refueling outage, a gamma measurement hand probe, Eberline Model HP-290 was lost in the reactor vessel" When the manipulator crane trolley was moved, the probe with its cable connector was torn off and fell into the reactor cavity. At that time, only three fuel elements were loaded. These elements were off loaded to the spent fuel pit.
Neither of these aforementioned objects were found and a decision was made to evaluate these objects as loose parts within the reactor coolant system (RCS).
A potential effect of these loose parts is partial blockage of flow to the fuel assemblies or blockage within fuel assemblies.
The worst case effect of this blockage on the Large Break LOCA analysis for Salem Unit 2 is discussed below.
II. LARGE BREAK LOCA (FSAR CHAPTER 15.4.1)
The current licensing basis Large Break LOCA analysis for Salem Unit 2 was performed using the 1978 Westinghouse Evaluation Model for 17x17 standard fuel agd resulted in a Peak Cladding
- Temperature (PCT) of 2130 F for the limiting C =0.8 break. A subsequent "3-page evaluation", done to accoun~ for NUREG-0630 burst and blockage effects, resulted in no reduction to the analyzed FQ of 2.32.
To det~rmine the effect of these loose parts on the Large Break LOCA analysis an evaluation has been performed which considers locations of the loose parts within the RCS which could impact the Large Break LOCA PCT calculations. The core flow area assumed in the evaluation reflects the current Salem Unit 2 core with Westinghouse 17x17 standard fuel.
The location which was determined to have the greatest potential to impact the Large Break LOCA transient was that which would block the reactor coolant flow through the active core fuel rod assemblies. The chemical and mechanical evaluation of these loose parts within the reactor vessel environment indicates that the plastic, rubber, aluminum and tin-lead alloy of the HP-290 probe will disperse into benign particles within the reactor coolant. The remaining metal components of the lost objects will remain intact; however, some deformation can be expected. An evaluation of the size of the remaining objects indicates that only the lock pin, the ground wire and the stainless steel central wire of the HP-290 probe have the potential to enter any of the fuel assembly subchannels. The remaining objects will not be able to pass through the fuel assembly bottom nozzles.
The current licensing basis analysis for Salem resulted in a peak clad temperature at the fuel rod burst elevation of 6 ft. In this case, the temperature excursion is driven by the heat release from the zirc-water reaction on the fuel rod cladding.
The time of fuel rod burst is dependent upon the cooling provided by the positive and negative flow through the core during the blowdown portion of the transient. If the presence of the loose parts will cause the fuel rod to burst earlier than is currently predicted, an increase in PCT will result. To determine if the timing of fuel rod burst would be altered by the presence of the loose parts in the RCS, it was postulated that during the LOCA event, all the objects are lodged beneath the bottom nozzle except the lock pin, the ground wire and the HP-290 central wire which are lodged next to the hot rod in the hot assembly. In this situation flow through the subchannel adjacent to the hot rod is blocked at the core entrance and flow in the subchannel is impeded due to the presence of the lock pin and wire. The maximum effect of the flow impedance due to the presence of the lock pin and wire will occur if the objects are lodged at the burst elevation. In this case, the maximum flow redistribution resulting from the blockage will effect the local heat transfer at the burst elevation. The presence of the objects lodged in the fuel assembly bottom nozzle will have no effect on the timing of the fuel rod burst since full flow recovery will occur approximately 30 inches downstream of the blocked nozzle. Therefore, only the flow impedance in the subchannel has the potential to impact the PCT calculation. An evaluation of the maximum blockage within the subchannel at the burst elevation indicates that 36% of the subchannel or approximately 0.13% of the hot assembly would be blocked due to the presence of the lock pin and wire. A subchannel blockage of this magnitude was evaluated and found to potentially create a PCT increase of 22.21°F.
The licensing basis large break LOCA analysis for Salem was perf orrlied using fuel performance parameters which are now overly conservative. Accounting for the lower rod internal backfill pressure of the fuel currently in Salem Unit 2 results in a PCT benefit larger (>100°F) than the combined penalty of the apgroximately 22°F penalty associated with the blockage and the 28 F penalty due to the increase steam generator tube plugging presented in Attachment 2. Thus, the net effect would result in no increase in peak clad temperature.
Recent development of a Best-Estimate Large Break LOCA model and test performed to determine the effects of fuel assembly flow blockage have demonstrated that even large amounts of flow blockage (<90%) result in a PCT benefit. The benefit is related to breakup of the entrained water droplets which are present during a LOCA. However, current LOCA models developed in response to 10CFRS0.46 and Appendix K to 10CFR50 do not have the sophistication to model non~equilibrium effects and the presence of entrained water droplets during blowdown.
- Thus, sensitivity studies based on Appendix K models, result in a calculated increase in PCT. Furthermore, the expected location of the loose parts during a LOCA would be at either the top or bottom of a grid depending upon the flow direction. The local power is lower and heat transfer is much higher in the region around grids than calculated by the Westinghouse Evaluation Models. Credit for these effects would offset the 22°F penalty associated with the loose parts in the RCS.
Based on the discussion given above, the presence of the loose parts will not result in an increase in peak clad temperature for Salem Unit 2. Therefore, the continued operation of Salem Unit 2 with th5 loose parts in the RCS is acceptable. A calculated PCT of 2130 F is low enough that there are no concerns for meeting the maximum local Zirconium water reaction limit of less than 17%, the core wide Zirconium water reaction of less than 1%, the ability to retain a coolable geometry as a result of thermal effects, or the ability to cool the reactor long-term.