ML17033B599

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NRC Inspection Report 05000335/2016012 and Preliminary White Finding (Letter and Inspection Report Only)
ML17033B599
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 02/02/2017
From: Joel Munday
Division Reactor Projects II
To: Nazar M
Florida Power & Light Co
References
EA-17-013 EA-17-013, IR 2016012
Download: ML17033B599 (13)


See also: IR 05000335/2016012

Text

OFFICIAL USE ONLY- SECURITY-RELATED INFORMATION

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

245 PEACHTREE CENTER AVENUE NE, SUITE 1200

ATLANTA, GEORGIA 30303-1257

February 2, 2017

EA-17-013

Mr. Mano Nazar

President and Chief Nuclear Officer

Nuclear Division

Florida Power & Light Co.

Mail Stop: NT3/JW

15430 Endeavor Drive

Jupiter, FL 33478

SUBJECT: ST. LUCIE PLANT - NRC INSPECTION REPORT 05000335/2016012 AND

PRELIMINARY WHITE FINDING

Dear Mr. Nazar:

On December 19, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your St. Lucie Plant, Unit 1, and inspectors discussed the results of this inspection

with Mr. Chris Costanzo, Site Vice President, and other members of your staff. On January 27,

2017, the resident inspectors presented the preliminary safety significance to Mr. Dan Deboer,

Site Director, and other members of the licensees staff. The results of this inspection are

documented in the enclosed report.

Section 4OA3 of the enclosed report documents a finding that the NRC has preliminarily

determined to be White, with low-to-moderate safety significance. This finding involved a failure

to maintain configuration control of the Unit 1 main generator inadvertent energization lockout

relay circuitry, which resulted in a reactor trip and loss of offsite power (LOOP) on August 21,

2016. We assessed the significance of the finding using the significance determination process

(SDP) and readily available information.

We intend to issue our final significance determination in writing, within 90 days from the date of

this letter. The NRCs significance determination process (SDP) is designed to encourage an

open dialogue between your staff and the NRC; however, neither the dialogue nor the written

information you provide should affect the timeliness of our final determination.

As described in NRC Inspection Manual Chapter 0612, a finding may or may not be associated

with regulatory non-compliance and, therefore, may or may not result in a violation. Based on

the review of this issue and in accordance with NRC Inspection Manual Chapter 0612, the NRC

determined that no violation of a regulatory requirement occurred.

Enclosure(s) transmitted herewith contain(s) SUNSI. When separated from enclosure(s), this

transmittal document is decontrolled.

LIMITED INTERNAL

DISTRIBUTION PERMITTED

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M. Nazar 2

Before we make a final decision, you may choose to communicate your position on the facts

and assumptions used to arrive at the finding and assess its significance by either (1) attending

and presenting at a regulatory conference, or (2) submitting your position in writing. The focus

of a regulatory conference is to discuss the significance of the finding. Written responses

should reference the inspection report number and enforcement action number associated with

this letter in the subject line.

If you request a regulatory conference, it should be held within 40 days of your receipt of this

letter. Please provide information you would like us to consider or discuss with you at least ten

days prior to any scheduled conference. If you choose to attend a regulatory conference it will

be open for public observation. If you decide to submit only a written response, it should be

sent to the NRC within 40 days of your receipt of this letter. If you choose not to request a

regulatory conference or to submit a written response, you will not be allowed to appeal the

NRCs final significance determination.

Please contact LaDonna B. Suggs, Chief, Reactor Projects Branch 3, at (404) 997-4539, or in

writing, within ten days from the issue date of this letter to notify the NRC of your intentions. If

we have not heard from you within ten days, we will continue with our significance

determination.

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for

Withholding.

Sincerely,

/RA/

Joel T. Munday, Director

Division of Reactor Projects

Docket No.: 50-335

License No.: DPR-67

Enclosure:

NRC IR 05000335/2016012

w/Attachments:

Supplemental Information

Detailed Risk Assessment (OUO-SRI)

cc Distribution via ListServ

(Cover letter and Report w/o Detailed Risk Assessment attachment)

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ML17034A050 (Cover letter w/ enclosures)

ADAMS ACCESSION NUMBER: ML17033B599 (Cover letter & IR Report only)

Entire Report w/attachment: SENSITIVE NON-PUBLICLY AVAILABLE Keyword:

SUNSI REVIEW OMPLETE NON-SENSITIVE PUBLICLY AVAILABLE MD. 3.4 Non Public A.3

By:Lundy Pressley

Cover Letter/Report Only SENSITIVE NON-PUBLICLY AVAILABLE Keyword:

SUNSI REVIEW OMPLETE NON-SENSITIVE PUBLICLY AVAILABLE SUNSI REVIEW COMPLETE

By:Lundy Pressley

OFFICE RII:DRP RII:DRP RII:DRP RII:DRP RII:DRP EICS

SIGNATURE LP via email TM via email SR LS JTM MK

NAME L Pressley T Morrissey S Roberts L Suggs JMunday M Kowal

DATE 2/1/17 2/1/17 2/1/17 2/1/17 2/ 2 /2017 2/1/17

OFFICIAL USE ONLY - SECURITY-RELATED INFORMATION

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-335

License Nos: DPR-67

Report Nos: 05000335/2016012

Licensee: Florida Power & Light Company (FP&L)

Facility: St. Lucie Plant, Unit 1

Location: 6501 South Ocean Drive

Jensen Beach, FL 34957

Dates: August 21, 2016 - December 19, 2016

Inspectors: T. Morrissey, Senior Resident Inspector

S. Roberts, Resident Inspector

J. Hanna, Senior Reactor Analyst

Approved by: Joel T. Munday, Director

Division of Reactor Projects

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Enclosure

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SUMMARY

IR 05000335/2016012; August 21, 2016 - December 19, 2016; St. Lucie Nuclear Plant, Unit 1,

Follow-up of Events and Notices of Enforcement Discretion

This report covers approximately a four-month period of inspection by resident inspectors. One

finding with preliminary significance was identified by the inspectors. The significance of

inspection findings are indicated by their color (Green, White, Yellow, Red) using Inspection

Manual Chapter (IMC) 0609, issued April 29, 2015, Significance Determination Process. The

cross-cutting aspect was determined using IMC 0310, Components Within the Cross-Cutting

Areas, dated December 4, 2014. The NRCs program for overseeing the safe operations of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 6.

Cornerstone: Initiating Events

  • To Be Determined (TBD). A self-revealing finding was identified for the licensees failure to

maintain configuration control of the inadvertent energization lockout relay manual

synchronization circuitry as required by licensee procedures MA-AA-100 and ADM-08.12,

during the October 2013 modification to the Unit 1 automatic main generator

synchronization circuit.

The performance deficiency was more than minor because it was associated with the

human performance attribute of the Initiating Events Cornerstone and it adversely affected

the associated cornerstone objective of limiting the likelihood of events that upset plant

stability and challenge critical safety functions because it resulted in an actual plant trip.

The inspectors screened the finding under the initiating events cornerstone using

Attachment 4 (October 7, 2016) and Appendix A (June 19, 2012) of Inspection Manual

Chapter 0609, Significance Determination Process (April 29, 2015). The inspectors

determined the finding required a detailed risk evaluation because the finding caused a

reactor trip and the loss of mitigation equipment relied upon to transition the plant from the

onset of the trip to a stable shutdown condition (e.g. loss of condenser and loss of

feedwater). A preliminary significance characterization of White has been assigned. The

preliminary finding involved the cross-cutting area of human performance associated with

the cross-cutting aspect of avoiding complacency because the individuals involved failed to

recognize and plan for the possibility of mistakes, latent issues, and inherent risk and failed

to implement human error reduction tools associated with configuration control. (H.12)

(Section 4OA3).

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REPORT DETAILS

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

4OA3 Followup of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report (LER) 05000335/2016-003-00, Generator Lockout

Relay Actuation During Power Ascension Results in Reactor Trip

a. Inspection Scope

On August 21, 2016, during a Unit 1 restart following a maintenance outage, the main

generator inadvertent energization lockout relay unexpectedly actuated which caused

the main generator to trip resulting in an automatic reactor trip. The relay actuation

prevented the automatic transfer of station auxiliaries to the startup transformers and

resulted in a LOOP, although offsite power remained available at the switchyard. The

inspectors reviewed the LER and associated root cause evaluation (action request (AR)

2151217) to verify the accuracy and completeness of the LER and the appropriateness

of the corrective actions. The LER was also reviewed to identify any licensee

performance deficiencies (PDs) associated with the event. Documents reviewed are

listed in the Attachment. This LER is closed.

b. Findings

Introduction: A self-revealing finding was identified for the licensees failure to maintain

configuration control of an electrical wire during the October 2013 installation of a digital

upgrade to the Unit 1 automatic main generator synchronization circuit.

Description: On August 21, 2016, during a normal power ascension for Unit 1, the

reactor tripped, from approximately 38 percent reactor power, when the inadvertent

energization generator lockout relay actuated. The relay actuation prevented the

automatic transfer of station auxiliaries to the startup transformers which resulted in a

complicated trip (i.e. loss of main feedwater, main condenser, offsite power to the safety

related buses and all reactor coolant pumps.) Offsite power remained available at the

switchyard during this event. Both emergency diesel generators started and powered

the safety related buses. Operators manually restored power to the buses after verifying

availability.

The main generator inadvertent energization lockout relay was a protective relay that

was designed to be armed when the main generator was offline and had a set point of

8000 amps. This protective feature was designed to prevent damage to the main

generator, which could be incurred through motoring in the event the output breakers

were closed unintentionally with the main generator offline. The synchronization circuit

was designed to automatically bypass the inadvertent energization lockout relay when

the main generator was synchronized to the grid, using either manual or automatic

synchronization methods.

The licensees investigation found that the inadvertent energization lockout relay

remained armed following manual synchronization of the main generator to the electrical

grid on August 21, 2016, due to a missing wire in the manual synchronization circuit.

The missing wire prevented the relay from performing its disarming function as required

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3

during main generator synchronization. The licensee replaced the missing wire and an

appropriate post maintenance test was completed. The licensee performed a root cause

evaluation (AR 2151217) and identified one root cause, which was; incorrect removal of

a wire during an October 2013 modification to restore the automatic synchronization

capabilities of the generator breakers. Corrective actions included: replacement of the

missing wire, and implementing procedure guidance for both units to verify the

inadvertent energization lockout relay was reset prior to exceeding 8000 amps.

The manual synchronization performed on August 21, 2016, was the first manual

synchronization utilized since the digital modification was installed in October 2013. The

missing wire did not impact the disarming function of the inadvertent energization lockout

relay following automatic synchronization. From June 2010, until automatic

synchronization was restored in October 2013, manual synchronization to the grid had

been utilized successfully, therefore the wire in question had been properly installed

prior to the modification in October 2013.

Licensee procedure MA-AA-100, Conduct of Maintenance, Revision 15 (2013), Section

5.11, Configuration Control, stated in part, that each site shall have a configuration

control procedure that provided step by step instructions for conducting configuration

changes in the plant. The procedure stated that configuration changes included the

lifting of leads, and installing and removing electrical jumpers. A wire is considered the

same as an electrical lead or conductor. Licensee administrative procedure ADM-

08.12, Maintenance Configuration Control, Revision 2 (2013), Section 1.2, Scope,

included configuration changes such as lifting leads, and installing and removing

electrical jumpers. Section 4.1, Configuration Control, stated in part, to perform all

component manipulations and changes per the following: detailed procedure or written

instructions.

The digital automatic synchronization modification performed in October 2013 was

installed under written instructions as work order (WO) 40038386, which implemented

engineering change (EC) 274642, SYNC/888: Auto Sync Not Working. The

instructions directed the de-termination and removal of conductors in the main generator

synchronization circuit, however the wire/conductor that was erroneously removed was

not within the scope of the WO. The licensee concluded that the wire was removed

erroneously. Therefore the removal was not performed in accordance with procedures

MA-AA-100, Conduct of Maintenance and ADM-08.12, Maintenance Configuration

Control which resulted in a loss of configuration control.

In the period between October 2013, and August 21, 2016, the licensee had only utilized

the functional automatic synchronization circuit. Therefore when using this method for

synchronization the licensee fully met Technical Specification (TS) 3.8.1.1, which

required a minimum of two physically independent alternating current (AC) circuits

between the offsite transmission network and the onsite Class 1E distribution system in

addition to TS 3.8.1.2, for shutdown, that requires one circuit between the offsite and

onsite distribution system. Therefore during this period the electrical power systems

were capable of performing their specified safety functions as detailed in the Updated

Final Safety Analysis Report (UFSAR), Chapter 8, Electric Power.

On August 21, 2016, when the licensee utilized the non-conforming manual

synchronization circuit they unknowingly introduced the susceptibility of a LOOP. The

manual synchronization was performed at approximately 1202 hours0.0139 days <br />0.334 hours <br />0.00199 weeks <br />4.57361e-4 months <br />. The LOOP

occurred at approximately 1926 hours0.0223 days <br />0.535 hours <br />0.00318 weeks <br />7.32843e-4 months <br /> with restoration of offsite power from one

electrical bus at approximately 2012 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.65566e-4 months <br /> and two electrical buses at approximately

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4

2036 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.74698e-4 months <br />. However, up until the actual moment that the inadvertent relay actuation

occurred the electrical system could have performed its specified safety function.

TS 3.8.1.1 Limiting Condition of Operation (LCO) condition d, stated that with two of the

required offsite AC circuits inoperable restore within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or be in Hot Standby with

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. The licensee was in Hot Standby immediately following the reactor trip and

restored the operability of two offsite AC circuits in approximately 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and 34 minutes,

from initial susceptibility until full restoration, and therefore, did not violate the TS and

LCO requirements.

Analysis: The failure to maintain configuration control of the inadvertent energization

lockout relay manual synchronization circuitry wire as required by licensee procedures

MA-AA-100 and ADM-08.12 was a performance deficiency (PD). Specifically, this failure

to maintain configuration control resulted in an erroneously removed wire from the

manual synchronization circuitry which resulted in a reactor trip. The PD was more than

minor because it was associated with the human performance attribute of the Initiating

Events Cornerstone. The PD adversely affected the cornerstone objective of limiting the

likelihood of events that upset plant stability and challenge critical safety functions

because the PD resulted in an actual reactor trip with complications.

The inspectors screened the finding using Inspection Manual Chapter (IMC) 0609, Initial

Characterization of Findings, Attachment 4, (October 7, 2016), under the initiating

events cornerstone because the event resulted in a transient with a reactor trip, loss of

offsite power and loss of feedwater. Attachment 4 of IMC 0609, then routed the

screening to IMC 0609, Appendix A, The Significance Determination Process (SDP) for

Findings At-Power, (June 19, 2012). Using IMC 0609, Appendix A, Exhibit 1 -

Initiating Events Screening Questions, under B. Transient Initiators the inspectors

determined the finding required a detailed risk evaluation because the finding caused

both a reactor trip and the loss of mitigation equipment relied upon to transition the plant

from the onset of the trip to a stable shutdown condition (e.g. loss of condenser and loss

of feedwater).

A preliminary significance characterization has been assigned, however the

characterization is not yet finalized. The finding does not represent an immediate safety

concern because the main generator synchronization circuit has been restored to allow

automatic bypassing of the inadvertent energization lockout relay during manual as well

as automatic synchronizations.

A Regional SRA performed the detailed risk assessment by using the NRCs

Standardized Plant Analysis Risk (SPAR) model for St. Lucie Unit 1 and setting the Plant

Centered LOOP frequency equal to 1.0 because the event actually occurred. The initial

result was approximately 2E-5 (Yellow). The dominant risk sequence was a Plant

Centered LOOP 02-11 where CST depletion occurs and long term heat removal fails.

This type of sequence contributed 80 percent (1.4E-5 / 1.73E-5) of the total internal

events CDF. Through a visit to the St. Lucie site involving simulator observations,

plant walkdowns, procedure reviews and interaction with NextEra risk staff, the analyst

further refined the analysis and gave additional credit for operator actions for:

  • Condensate Storage Tank refill from one of a number of potential sources,

including crosstie capability from Unit 2, depressurization of the steam

generators and using tools and apparatus as described in 10 CFR 50.54(hh)(2),

commonly known as B.5.(b) equipment, or Mitigating Strategies-FLEX

equipment. A comprehensive Human Error Probability representing any/all of

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5

those three potential sources was created using the SPAR-H methodology and

assigned a value of 1E-2.

  • Propping open doors and installing temporary ventilation for the Reactor Auxiliary

Building electrical equipment rooms. Certain accident sequences in the risk

results had failures of the 5A and 5B exhaust fans which would ultimately cause

failure of electrical equipment and consequently the mitigating system equipment

which is powered by it. A Human Error Probability which would limit room heat

up < 120F was created using the SPAR-H methodology and assigned a value of

1E-1.

When applied to the cutset results, these two additional factors reduced the calculated

CDF to 2E-6. The detailed risk evaluation was completed on December 5, 2016, and

was peer reviewed by another SRA on December 14, 2016. Please refer to the Detailed

Risk Assessment in the Attachment accompanying this inspection report for the

complete analysis.

Subsequently the licensee performed additional analyses that appeared to show the risk

was less than 1E-6 (Green). The SRA continued to engage the licensee in discussions

and perform sensitivity analyses based on the licensees input to verify the initial result

continued to be valid, i.e., White. The factors that the licensee asserted should be given

additional credit for in the risk model (and which the NRC agreed with) were:

  • Condensate Storage Tank unavailability was changed from 1.6E-1 to 8E-3,

based on historical data provided by the licensee from the last 3 years.

  • Recovery factor for Loss of Offsite Power Sequences was set equal to 1E-1.

(Historically the SPAR models have included recovery credit for Station Blackout

sequences, but not for LOOP sequences.)

  • Basic event representing the operators failing to initiate feed and bleed primary

injection cooling was changed from 2E-2 to 1E-2. This change was made based

on the lower decay heat level in the reactor core at 40 percent reactor power

(when the performance deficiency would cause a LOOP), thus providing the

operators approximately 50 percent more time to complete the action.

When applying these additional recovery credits, and when applying additional credit to

the CST and emergency ventilation recovery actions mentioned above (one order of

magnitude decrease in each case) the risk result remained greater than 1E-6 (White).

The preliminary finding involved the cross-cutting area of human performance and was

associated with the cross-cutting aspect of avoiding complacency because the

individuals involved failed to recognize and plan for the possibility of mistakes, latent

issues, and inherent risk and failed to implement appropriate error reduction tools.

Specifically the licensee failed to plan for the inherent risk of errors during the removal of

unnecessary conductors in the circuit and failed to implement human error reduction

tools associated with configuration control. [H.12].

Enforcement: The inspectors did not identify a violation of regulatory requirements

associated with this finding. Because the finding did not involve a violation of regulatory

requirements and the significance has not been determined, it is identified as FIN

05000335/2016012-01, Failure to Maintain Component Configuration Control Resulted

in a Complicated Reactor Trip

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6

4OA6 Meetings, Including Exit

On December 19, 2016, the resident inspectors discussed the inspection results with

Mr. Chris Costanzo, Site Vice President, and other members of the licensees staff. On

January 27, 2017, the resident inspectors presented the preliminary safety significance

to Mr. Dan Deboer, Site Director, and other members of the licensees staff. The

inspectors verified that no proprietary information was retained by the inspectors or

documented in this report.

ATTACHMENTS:

SUPPLEMENTAL INFORMATION

DETAILED RISK ASSESSMENT

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SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Summers, Regional Vice President

D. Deboer, Site Director

C. Costanzo, Site Vice President

D. Cecchett, Licensing Engineer

K. Frehafer, Licensing Engineer

M. Jones, Engineering Director

W. Parks, Operations Director

D. Pitts, Maintenance Director

R. Sciscente, Licensing Engineer

M. Snyder, Licensing Manager

R. Wright, Plant General Manager

NRC Personnel

L. Pressley, Senior Project Engineer

J. Hanna, Senior Reactor Analyst

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Attachment

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LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000335/2016012-01 FIN Failure to Maintain Component Configuration Control

Resulted in a Complicated Reactor Trip

(Section 4OA3)

Closed

05000335/2016-003-00 LER Generator Lockout Relay Actuation During Power

Ascension Results in Reactor Trip (Section 4OA3)

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LIST OF DOCUMENTS REVIEWED

Section 4OA3: Follow-up of Events and Notice of Enforcement Discretion

Miscellaneous:

LER 05000335, 2016-003-00, Generator Lockout Relay Actuation during Power Ascension

Results in Reactor Trip

PRA Analysis of St. Lucie Unit 1 August 21, 2016 Generator Lockout Event, dated January 13,

2017

Procedures:

MA-AA-100, Conduct of Maintenance, Revision 15

ADM-08.12, Maintenance Configuration Control, Revision 2

1-ARP-01-G00, Control Room Panel G RTGB 102, Revision 42

1-AOP-25.02, Ventilation Systems, Revision 6

2-EOP-01, Standard Post Trip Actions SPTA, Revision 35

2-EOP-09, Loss of Offsite Power/Loss of Forced Circulation, Revision 20

2-EOP-10, Station Blackout, Revision 25

1-FSG-02, Alternate AFW Suction Source, Revision 2

1-FSG-03, Alternate Low Pressure Feedwater, Revision 2

1-FSG-06, Alternate CST Makeup, Revision 2

Drawings:

8770-B-327, sheet 1790, Inadvertent Energization Generator Protection

8770-B-327, sheet 886, Generator Breakers 1E & 1M

8770-B-327, sheet 888, Gen. Auto & MAN. Synchronization

Miscellaneous:

WO 40038386, EC 274642, SYNC/888: Auto Sync Not Working

Job Performance Measure 0121245, Supply Demineralized Water from the Treated Water

Storage Tank to the Unit 1(2) Condensate Storage Tank, Revision 0

Job Performance Measure 0321227, Align Unit 2 CST to Supply 1C AFW Pump, Revision

6Job Performance Measure 0521517, Restoration of Electrical Equipment Room

Ventilation-Unit 1, Revision 3

Operations Training Document, Align the Unit 1A and 1B AFW Pumps to the Unit 2 CST,

Revision 4

Root Cause Analysis, Lockout Relay Automatic Reactor Trip (Complicated)

Licensee Decay Heat Calculations Assuming 38% Power, dated November 30, 2016

Enercon Calculation, Plant St. Lucie Unit 1 Electrical Equipment Room Loss of HVS-5A/B

Heatup Evaluation, Revision 0

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