On 12/31/15, at approximately 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br />, during shift turnover panel walk-downs, a licensed operator identified that the High Pressure Coolant Injection ( HPCI) flow controller output indication was showing zero percent. The controller was in automatic with the set point at 5000 gpm, which would typically result in a controller output value of 100%.
This condition would have prevented the HPCI system from performing its design function in the event of an accident.
The HPCI system was declared inoperable and the appropriate Technical Specification Action was entered.
Other standby systems (Reactor Core Isolation Cooling and low pressure emergency core cooling systems) remained operable.
Troubleshooting of the flow controller and related circuitry identified a failed signal converter.
The signal converter was replaced and the HPCI system was declared operable at approximately 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br /> on 12/31/15.
There were no actual safety consequences associated with this event. |
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Category:Letter
MONTHYEARIR 05000277/20240032024-11-0404 November 2024 Integrated Inspection Report 05000277/2024003 and 05000278/2024003 ML24284A2842024-10-10010 October 2024 (Wcgs), Revision of One Form That Implements the Radiological Emergency Response Plan (RERP) RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24281A1012024-10-0707 October 2024 Senior Reactor and Reactor Operator Initial License Examinations ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24240A1692024-09-18018 September 2024 Cy 2023 Summary of Decommissioning Trust Fund Status ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification ML24221A2582024-09-0606 September 2024 Response to Request for Re-Engagement Regarding the Subsequent License Renewal Environmental Review for Peach Bottom Atomic Power Station, Units 2 and 3 05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum IR 05000277/20240052024-08-29029 August 2024 Updated Inspection Plan for Peach Bottom Atomic Power Station, Units 2 and 3 (Report 05000277/2024005 and 05000278/2024005) ML24235A0342024-08-23023 August 2024 U.S. Nuclear Regulatory Commission’S Analysis of Constellation Energy Generation’S Decommissioning Funding Status Report IR 05000277/20240102024-08-23023 August 2024 Fire Protection Team Inspection Report 05000277/2024010 and 05000278/2024010 ML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 IR 05000277/20240022024-08-14014 August 2024 Integrated Inspection Report 05000277/2024002 and 05000278/2024002 IR 05000482/20240052024-08-14014 August 2024 Updated Inspection Plan for Wolf Creek Generating Station (Report 05000482/2024005) ML24225A1692024-08-12012 August 2024 10 CFR 50.46 Annual Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24214A3232024-08-0101 August 2024 Response to Request for Additional Information - Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations ML24208A0962024-07-25025 July 2024 57243-EN 57243 - Rssc Wire & Cable LLC, Dba Marmon - Part 21 Notification ML24206A1252024-07-24024 July 2024 Revision of Three Procedures and Two Forms That Implement the Radiological Emergency Response Plan (RERP) ML24191A0612024-07-0606 July 2024 Independent Spent Fuel Storage Installation (ISFSI) - Annual Radioactive Effluent Release Report ML24178A4142024-06-26026 June 2024 Revision of One Procedure and One Form That Implement the Radiological Emergency Response Plan (RERP) ML24178A3672024-06-26026 June 2024 Correction to 2023 Annual Radioactive Effluent Release Report – Report 47 ML24177A1512024-06-24024 June 2024 Post Accident Monitoring Instrumentation Report ML24166A1172024-06-20020 June 2024 Regulatory Audit Summary Regarding Proposed Alternative Schedule to Complete Decommissioning Beyond 60 Years RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000277/20243012024-06-13013 June 2024 Initial Operator Licensing Examination Report 05000277/2024301 and 05000278/2024301 RS-24-058, Regarding Subsequent License Renewal Environmental Review2024-06-0505 June 2024 Regarding Subsequent License Renewal Environmental Review ML24151A6482024-06-0303 June 2024 Changes in Reactor Decommissioning Branch Project Management Assignments for Some Decommissioning Facilities ML24150A2722024-05-29029 May 2024 Annual Radiological Environmental Operating Report 81, January 1, 2023 Through December 31, 2023 ML24150A0032024-05-28028 May 2024 Request for Exemptions from 10 CFR 50.82(a)(8)(i)(A) and 10 CFR 50.75(h)(1)(iv) and Proposed Amendment to the Decommissioning Trust Agreement ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 RS-24-055, 2023 Corporate Regulatory Commitment Change Summary Report2024-05-17017 May 2024 2023 Corporate Regulatory Commitment Change Summary Report ML24134A1792024-05-13013 May 2024 Supplemental Information in Support of Request for Alternative Schedule to Complete Decommissioning Beyond 60 Years of Permanent Cessation of Operations IR 05000277/20240012024-05-13013 May 2024 Integrated Inspection Report 05000277/2024001 and 05000278/2024001 IR 05000277/20245012024-05-0808 May 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000277/2024501 and 05000278/2024501 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24121A1832024-04-30030 April 2024 Pre-Submittal Meeting Presentation Material Peach Bottom ECCS Compensated Level System Replacement Project ML24118A0032024-04-27027 April 2024 2023 Annual Radioactive Effluent Release Report - Report 47 ML24120A2762024-04-23023 April 2024 Independent Spent Fuel Storage Installation (ISFSI) Facility - Annual Radioactive Effluent Release Report 66 January 1, 2023 Through December 31, 2023 CNL-24-033, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-04-17017 April 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24107A2462024-04-15015 April 2024 Submittal of Changes to Technical Specifications Bases ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition ML24102A0472024-04-11011 April 2024 Operator Licensing Examination Approval 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report RS-24-023, Report on Status of Decommissioning Funding.2024-03-22022 March 2024 Report on Status of Decommissioning Funding. IR 05000277/20244022024-03-12012 March 2024 Cybersecurity Inspection Report 05000277/2024402 and 05000278/2024402 (Cover Letter Only) ML24061A2642024-03-0101 March 2024 Revision of Two Procedures That Implement the Radiological Emergency Response Plan (RERP) for Wolf Creek Generating Station (WCGS) Commissioners ML24060A1192024-02-29029 February 2024 Notification of Conduct of a Fire Protection Team Inspection 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition 05000277/LER-2024-001, Automatic Reactor Scram Due to an Invalid Generator Lockout2024-03-21021 March 2024 Automatic Reactor Scram Due to an Invalid Generator Lockout 05000278/LER-2023-002, Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit2023-12-14014 December 2023 Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit 05000278/LER-2023-001, Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion2023-11-0707 November 2023 Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion 05000277/LER-2022-002, Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded2022-12-15015 December 2022 Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded 05000277/LER-2022-001, Automatic Reactor Scram Due to Loss of Power to Both RPS Buses2022-07-15015 July 2022 Automatic Reactor Scram Due to Loss of Power to Both RPS Buses 05000277/LER-2021-003, Manual Reactor Scram Due to Degrading Condenser Vacuum2022-01-12012 January 2022 Manual Reactor Scram Due to Degrading Condenser Vacuum ML21196A4852021-07-16016 July 2021 LER 2-2021-002-00 for Peach Bottom Atomic Power Station, Unit 2, Safety Relief Valve Inoperability Due to Nitrogen Leakage from Braided Hose Wear 05000278/LER-2017-0012017-12-20020 December 2017 Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 3 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line 05000277/LER-2017-0012017-03-0808 March 2017 Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection, LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 2 Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection 05000278/LER-2016-0012016-11-22022 November 2016 Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function, LER 16-001-00 for Peach Bottom, Unit 3, Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function 05000277/LER-2016-0012016-11-11011 November 2016 Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications, LER 16-001-00 for Peach Bottom, Unit 2, Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications 05000278/LER-2015-0012016-02-26026 February 2016 Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter, LER 15-001-00 for Peach Bottom, Unit 3, Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter ML13058A0432013-02-22022 February 2013 Submittal of Independent Spent Fuel Storage Installation (ISFSI) Cask Event Report ML1007702362010-03-12012 March 2010 60-Day Security Event Report 2-10-S01 ML0927401622009-09-30030 September 2009 LER 09-S01-00 for Peach Bottom, Units 2 & 3 Regarding Unescorted Access Granted to Contract Worker Who Did Not Provide Complete Work History Information ML1015505682009-07-10010 July 2009 Event Notification for Peach Bottom on Elevated Tritium Levels Found in On-Site Well ML0434503772004-12-10010 December 2004 LER-04-S01-00 for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3, 60 Day Security Event Report 2-04-S01 ML19095A7391976-12-0505 December 1976 Reporting Abnormal Occurrence No. 50-278-74-33 at Peach Bottom Atomic Power Station for Failure of Main Steam Line High Flow Switch dPIS-3-2-116C to Trip During Surveillance Test 2024-09-05
[Table view] |
comments regarding burden estimate to the FO1A, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulator/ Commission. Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc gov, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
Unit Conditions Prior to the Event Unit 3 was in Mode 1 and operating at approximately 100% rated thermal power when the event occurred. There were no structures, systems or components out of service that contributed to this event.
Description of the Event
On 12/31/15, at approximately 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br />, during shift turnover panel walk-downs, a licensed operator identified that the High Pressure Coolant Injection (HPCI) (EIIS:BJ) flow controller (EIIS:FIC) output indication was showing zero percent. The controller was in automatic with the set point at 5000 gpm, which would typically result in a controller output value of 100%. This condition would have prevented the HPCI system from performing its design function in the event of an accident. The HPCI system was declared inoperable and the appropriate Technical Specification Action was entered. Other standby systems (Reactor Core Isolation Cooling and low pressure emergency core cooling systems) remained operable.
This condition was reported to the NRC on 12/31/15 at approximately 1315 hours0.0152 days <br />0.365 hours <br />0.00217 weeks <br />5.003575e-4 months <br /> pursuant to the requirements of 10CFR 50.72(b)(3)(v)(D) (Event Notification 51630).
Subsequent troubleshooting of the HPCI system determined that a signal converter in the HPCI control circuitry had failed, resulting in the HPCI system not being capable of providing a sufficient flow rate if it had been required for a design basis event. The signal converter was replaced. HPCI was satisfactorily tested and returned to an operable status on 12/31/15 at approximately 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br />. The elapsed time from discovery to the time when the system was returned to service was approximately 14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> and 40 minutes.
Analysis of the Event
The HPCI system is part of the Emergency Core Cooling System (ECCS) network that provides cooling water to the reactor vessel for certain design basis events. The HPCI system uses a turbine driven pump that is designed to provide core cooling for a wide range of reactor pressures. As a result of this failure, upon receipt of an initiation signal, the HPCI turbine would have started, but the flow controller would have provided a flow demand of 0%. This would cause the governor control valve to close, stopping the turbine shortly after receiving the initiation signal.
A documented walk down of this panel on 12/30/15 at approximately 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> shows that the flow controller indicated 100% at that time. In addition, the operator also observed the controller at 100% at approximately 0400 on 12/31/15. It was observed during shift turnover walk downs at approximately 0630 hours0.00729 days <br />0.175 hours <br />0.00104 weeks <br />2.39715e-4 months <br /> to be at 0%. Therefore, the duration of inoperability prior to discovering the condition was at most approximately 2-1/2 hours. During the inoperability time period, other core cooling systems (Automatic Depressurization System (ADS) (EIIS: RV), Core Spray (EIIS: BM) and Low Pressure Coolant Injection (EIIS: BO)) were operable and could have adequately comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Infocollects Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
responded to a design basis event to maintain the plant in a safe condition. The Reactor Core Isolation Cooling (RCIC) system (EIIS: BN) was also operable during this time period. This event is not considered to be risk significant. There were no actual safety consequences associated with this event.
This event is being reported in accordance with 10CFR 50.73(a)(2)(v)(D), as a condition that could have prevented the fulfillment of the safety function of a system needed to mitigate the consequences of an accident. This LER also satisfies the reporting obligations of 10CFR Part 21, as stated in 10CFR 21.2(c).
Cause of the Event
Troubleshooting of the HPCI system determined that a signal converter in the HPCI control circuitry had failed. The signal converter converts the HPCI Flow Controller 4-20 mA output to a 10-50 mA signal that is required by the HPCI Electronic Governor Module.
The signal converter is manufactured by Moore Industries, Model #SCT/4-20MA/10-50MA and supplied by Nutherm International. The signal converter had been installed and tested in October 2015 during the recent refueling outage.
Following its failure on 12/31/15, it was sent off site for failure analysis. A failed transistor in the signal converter was identified. When replaced with a new transistor, the new transistor also failed during functional tests, suggesting it was the result of another sub-component within the signal converter. Additional testing and analysis could not determine what other sub-component had failed.
Corrective Actions
The signal converter was replaced. HPCI was satisfactorily tested and returned to an operable status on 12/31/15 at approximately 2110 hours0.0244 days <br />0.586 hours <br />0.00349 weeks <br />8.02855e-4 months <br />.
The failure has been classified as a latent manufacturing issue resulting in an infant mortality of the device. Similar installed equipment has been in operation for a period of time adequate for identifying this type of failure. The replacement signal converter has been in-service since 12/31/15 with satisfactory performance. Additional corrective actions are being evaluated in accordance with the corrective action program.
Previous Similar Occurrences LERs 3-04-001 and 3-05-001 both reported a failure of a HPCI flow controller due to failure of an internal power supply. The corrective actions taken for the previous events would not have been expected to prevent this recent event.