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Category:Licensee Event Report (LER)
MONTHYEAR05000277/LER-2024-003, Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum2024-09-0505 September 2024 Automatic Reactor Scram Following Main Turbine Trip Due to Degraded Condenser Vacuum 05000277/LER-2024-002, Uncoordinated DC Circuits Cause Unanalyzed Condition2024-04-0808 April 2024 Uncoordinated DC Circuits Cause Unanalyzed Condition 05000277/LER-2024-001, Automatic Reactor Scram Due to an Invalid Generator Lockout2024-03-21021 March 2024 Automatic Reactor Scram Due to an Invalid Generator Lockout 05000278/LER-2023-002, Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit2023-12-14014 December 2023 Main Steam Isolation Valves Stroke Times Exceed Technical Specification Limit 05000278/LER-2023-001, Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion2023-11-0707 November 2023 Standby Liquid Control Pump Inoperable for Greater than LCO Window Due to Gas Intrusion 05000277/LER-2022-002, Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded2022-12-15015 December 2022 Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Degraded 05000277/LER-2022-001, Automatic Reactor Scram Due to Loss of Power to Both RPS Buses2022-07-15015 July 2022 Automatic Reactor Scram Due to Loss of Power to Both RPS Buses 05000277/LER-2021-003, Manual Reactor Scram Due to Degrading Condenser Vacuum2022-01-12012 January 2022 Manual Reactor Scram Due to Degrading Condenser Vacuum ML21196A4852021-07-16016 July 2021 LER 2-2021-002-00 for Peach Bottom Atomic Power Station, Unit 2, Safety Relief Valve Inoperability Due to Nitrogen Leakage from Braided Hose Wear 05000277/LER-2021-001, High Pressure Coolant Injection System Declared Inoperable Due to Instrument Power Inverter Failure2021-06-24024 June 2021 High Pressure Coolant Injection System Declared Inoperable Due to Instrument Power Inverter Failure 05000277/LER-2020-002, Degraded Condition Due to RPV Instrument Nozzle Leakage2020-12-22022 December 2020 Degraded Condition Due to RPV Instrument Nozzle Leakage 05000277/LER-2020-001, Emergency Diesel Generator Shutdown Due to Intercooler Low Pressure Results in Condition Prohibited by Technical Specifications2020-04-24024 April 2020 Emergency Diesel Generator Shutdown Due to Intercooler Low Pressure Results in Condition Prohibited by Technical Specifications 05000278/LER-2019-001, Failure of Reactor Mode Switch Results in Condition Prohibited by Technical Specifications2019-12-19019 December 2019 Failure of Reactor Mode Switch Results in Condition Prohibited by Technical Specifications 05000277/LER-2019-001, Regarding Emergency Bus Breaker Relay Failure Results in Loss of Safety Function2019-04-11011 April 2019 Regarding Emergency Bus Breaker Relay Failure Results in Loss of Safety Function 05000277/LER-2018-002-01, Emergency Diesel Generator Air Inlet Check Valve Failure Results in a Condition Prohibited by Technical Specifications2019-03-0404 March 2019 Emergency Diesel Generator Air Inlet Check Valve Failure Results in a Condition Prohibited by Technical Specifications 05000278/LER-2018-002-01, Reactor Coolant System Pressure Boundary Leakage Resulting in Technical Specification Required Shutdown2018-12-21021 December 2018 Reactor Coolant System Pressure Boundary Leakage Resulting in Technical Specification Required Shutdown 05000278/LER-2018-004, Failure of a Main Steam Isolation Valve to Fully Close2018-11-30030 November 2018 Failure of a Main Steam Isolation Valve to Fully Close 05000278/LER-2018-003, Automatic Reactor Scram Due to Loss of Two Condensate Pumps2018-11-29029 November 2018 Automatic Reactor Scram Due to Loss of Two Condensate Pumps 05000278/LER-2018-002, Reactor Coolant System Pressure Boundary Leakage Resulting in Technical Specification Required Shutdown2018-11-19019 November 2018 Reactor Coolant System Pressure Boundary Leakage Resulting in Technical Specification Required Shutdown 05000277/LER-2018-002, Unit 3, Emergency Diesel Generator Air Inlet Check Valve Failure Results in a Condition Prohibited by Technical Specifications2018-08-10010 August 2018 Unit 3, Emergency Diesel Generator Air Inlet Check Valve Failure Results in a Condition Prohibited by Technical Specifications 05000278/LER-2018-001, Reactor Core Isolation Cooling System Pressure Switch Failure Results in Condition Prohibited by TS2018-06-21021 June 2018 Reactor Core Isolation Cooling System Pressure Switch Failure Results in Condition Prohibited by TS 05000277/LER-2018-001, Fire Safe Shutdown Requirements Not Met for Spurious Operation of Valves at a High-Low Pressure Interface2018-05-11011 May 2018 Fire Safe Shutdown Requirements Not Met for Spurious Operation of Valves at a High-Low Pressure Interface 05000278/LER-1917-001, Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line2017-12-20020 December 2017 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line 05000277/LER-2017-001, Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection2017-03-0808 March 2017 Regarding Emergency Diesel Generator Exhaust Stacks Nonconforming Design for Tornado Missile Protection 05000278/LER-2016-001, Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function2016-11-22022 November 2016 Regarding Leak in High Pressure Coolant Injection Drain Pipe Results in a Loss of Safety Function 05000277/LER-2016-001, Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications2016-11-11011 November 2016 Regarding Leak in High Pressure Service Water Pipe Results in Condition Prohibited by Technical Specifications 05000278/LER-2015-001, Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter2016-02-26026 February 2016 Regarding Loss of High Pressure Coolant Injection System Function as a Result of Failed Flow Controller Signal Converter 05000277/LER-2015-001, Regarding Condition Prohibited by Technical Specification Due to Insufficient Remote Shutdown System Surveillance Testing2015-10-20020 October 2015 Regarding Condition Prohibited by Technical Specification Due to Insufficient Remote Shutdown System Surveillance Testing 05000277/LER-2014-003, Regarding Containment Leakage Limit Exceeded Due to Through-Seat Leakage of Feed Water Check Valves2014-12-0505 December 2014 Regarding Containment Leakage Limit Exceeded Due to Through-Seat Leakage of Feed Water Check Valves 05000277/LER-2014-001, Regarding Unanalyzed Condition Due to Broken Wires in Breakers Used for Appendix R Post-Fire Safe Shutdown2014-07-17017 July 2014 Regarding Unanalyzed Condition Due to Broken Wires in Breakers Used for Appendix R Post-Fire Safe Shutdown 05000278/LER-2013-001, Re Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies2013-11-22022 November 2013 Re Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies ML13058A0432013-02-22022 February 2013 Submittal of Independent Spent Fuel Storage Installation (ISFSI) Cask Event Report 05000278/LER-2012-003, Regarding Loss of Control Room Emergency Ventilation Function Due to Failure of Ventilation Fan to Start2012-11-29029 November 2012 Regarding Loss of Control Room Emergency Ventilation Function Due to Failure of Ventilation Fan to Start 05000277/LER-2012-002, Regarding Common Cause Inoperability of Reactor Protection System Turbine Control Valve Instruments2012-11-21021 November 2012 Regarding Common Cause Inoperability of Reactor Protection System Turbine Control Valve Instruments 05000277/LER-2012-001, Regarding Laboratory Analysis Identities Safety Relief Valves and Safety Valve Set Point Deficiencies2012-11-0202 November 2012 Regarding Laboratory Analysis Identities Safety Relief Valves and Safety Valve Set Point Deficiencies 05000278/LER-2012-002, Regarding Failure of Primary Containment Isolation Valve Due to Foreign Material Results in Condition Prohibited by TS2012-08-22022 August 2012 Regarding Failure of Primary Containment Isolation Valve Due to Foreign Material Results in Condition Prohibited by TS 05000278/LER-2012-001, For Peach Bottom Atomic, Unit 3 Regarding Concurrent Inoperability of Two Trains of Core Spray Pressure Switches Results in Condition Prohibited by TS2012-06-13013 June 2012 For Peach Bottom Atomic, Unit 3 Regarding Concurrent Inoperability of Two Trains of Core Spray Pressure Switches Results in Condition Prohibited by TS 05000278/LER-2011-004, Regarding HPCI Cable Routing Error Results in Degraded Post Fire Safe Shutdown (Fssd) Analysis2012-01-13013 January 2012 Regarding HPCI Cable Routing Error Results in Degraded Post Fire Safe Shutdown (Fssd) Analysis 05000277/LER-2011-005, For Peach Bottom, Unit 2, Regarding Inoperability of Qualified Offsite Power Circuit Due to Design Weakness2011-12-15015 December 2011 For Peach Bottom, Unit 2, Regarding Inoperability of Qualified Offsite Power Circuit Due to Design Weakness 05000278/LER-2011-001, Regarding Containment Isolation Valve Inability to Close for a Design Basis Event Due to Degraded Lubricant2011-12-0909 December 2011 Regarding Containment Isolation Valve Inability to Close for a Design Basis Event Due to Degraded Lubricant 05000277/LER-2011-004, For Peach Bottom, Unit 2, Regarding Oil Leak Resulting in E1 Emergency Diesel Generator Inoperability2011-11-22022 November 2011 For Peach Bottom, Unit 2, Regarding Oil Leak Resulting in E1 Emergency Diesel Generator Inoperability 05000278/LER-2011-003, For Peach Bottom Unit 3, Regarding Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Thread Seal Leak2011-11-18018 November 2011 For Peach Bottom Unit 3, Regarding Automatic Depressurization System Safety Relief Valve Actuator Diaphragm Thread Seal Leak 05000278/LER-2011-002, For Peach Bottom Unit 3 - Residual Heat Removal Leaking Relief Valve Results in Condition Prohibited by Technical Specifications2011-11-17017 November 2011 For Peach Bottom Unit 3 - Residual Heat Removal Leaking Relief Valve Results in Condition Prohibited by Technical Specifications 05000277/LER-2011-003, Regarding Delayed Relay Operation Results in E-3 Emergency Diesel Generator Actuation During Surveillance Testing2011-10-21021 October 2011 Regarding Delayed Relay Operation Results in E-3 Emergency Diesel Generator Actuation During Surveillance Testing 05000277/LER-2011-002, For Peach Bottom, Units 2 and 3 - Condition Prohibited by Technical Specifications Due to Degraded Spent Fuel Pool Racks Boraflex Panels2011-07-29029 July 2011 For Peach Bottom, Units 2 and 3 - Condition Prohibited by Technical Specifications Due to Degraded Spent Fuel Pool Racks Boraflex Panels 05000277/LER-2011-001, For Peach Bottom Unit 2 High Pressure Coolant System Inoperable Due to Leaking Cooling Water Header Relief Valve2011-05-0606 May 2011 For Peach Bottom Unit 2 High Pressure Coolant System Inoperable Due to Leaking Cooling Water Header Relief Valve 05000277/LER-2010-004, Regarding Improper Credit for Function of Off-Site Power Source Transformer Load Tap Changer2010-11-24024 November 2010 Regarding Improper Credit for Function of Off-Site Power Source Transformer Load Tap Changer 05000277/LER-2010-003, Regarding Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies2010-11-19019 November 2010 Regarding Laboratory Analysis Identifies Safety Relief Valves and Safety Valve Set Point Deficiencies 05000277/LER-2010-002, Regarding Improperly Fastened Rod Hanger Results in Inoperable Subsystem of Emergency Service Water2010-11-15015 November 2010 Regarding Improperly Fastened Rod Hanger Results in Inoperable Subsystem of Emergency Service Water 05000277/LER-2010-001, Regarding Multiple Slow Control Rods Results in Condition Prohibited by Technical Specifications2010-03-19019 March 2010 Regarding Multiple Slow Control Rods Results in Condition Prohibited by Technical Specifications 2024-09-05
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Abstract
On 01/29/2024 at 1202 hours0.0139 days <br />0.334 hours <br />0.00199 weeks <br />4.57361e-4 months <br />, Unit 2 experienced a Generator lockout, Turbine trip and automatic Reactor Scram. All control rods inserted, and all safety systems responded as designed. Reactor level was initially maintained by Feedwater and pressure controlled with bypass valves. During the scram response, condenser vacuum degraded due to the loss of Turbine steam seals, resulting in level and pressure control being transferred to Reactor Core Isolation Cooling (RCIC) and High Pressure Coolant Injection (HPCI), respectively.
The cause of the Generator lockout is under investigation, with the suspected cause being a spurious trip of the Audio Tone system. The system has been removed from service with a redundant system providing the protective function. The Audio Tone system is scheduled for replacement in the 2024 refueling outage.
This event is reportable under 10CFR50.73(a)(2)(iv)(A) due to manual or automatic actuation of systems listed in 10CFR50.73(a)(2)(iv)(B) including the Reactor Protection System, containment isolation signals, actuation of an emergency core cooling system and Reactor Core Isolation Cooling. An ENS notification was made within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the event and was updated within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, reference ENS 56936.
(See Page 2 for required number of digits/characters for each block)
(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/) Page 3 of 3 cooling system and RCIC. An ENS notification was made within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of the event and was updated within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, reference ENS 56936.
Safety Consequences
The reactor Scram occurred as designed and resulted in no safety consequences. All safety systems responded as expected. As described above, the temporary degradation in condenser vacuum resulted in use of the RCIC system to control level for a portion of the response, but this did not challenge the ability to safely shutdown and cool down the unit.
Corrective Actions
Immediate corrective actions were taken to remove the affected Audio Tone system (TTR-1) from service and utilize the fully redundant TTR-2 system. The TTR-1 Audio Tone drawer has been replaced and a new set of cables has been identified and tested. After the completion of additional testing, this system will be maintained in a standby condition as a spare. The Audio Tone system is scheduled for a complete replacement in the upcoming 2024 refueling outage.
The corrective action to address the condenser vacuum degradation is to revise the procedure which sets the sealing steam pressure control valve to ensure it will receive the appropriate demand signal when needed.
Previous Similar Events
Peach Bottom has not experienced a Scram due to a Generator lockout in at least 10 years. The station experienced a trip of the Audio Tone system for an offsite source due to cable degradation in 2001 (Ref. EN 38241).