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Abstract While at power during surveillance testing, the HPCI turbine exhaust rupture diaphragm alarm annuciated following startup of the Unit'3 HPCI Turbine.
Investigation revealed that the inner rupture disc, PSD3-23-6, had ruptured.
Since the outer disc had not ruptured, the HPCI turbine remained operable until it was intentionally removed from service to replace the inner rupture disc.
Prior to removing the turbine from service, the systems required by Technical Specification 4.5.C.2 (RCIC, ADS, LPCI, and Core Spray) were verified to be operable.
Cause of the event is under investigation.
The rupture disc was replaced and HPCI was declared operable following surveillance test verification.
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, nne,.a. mu n n Description of the Event:
On January 6,1984, Peach Bottom Atomic Power Station was operating under normal conditions with both Units 2 and 3 at 100%
power.
At approximately 10:30 a.m., while conducting a surveillance test (ST-1.1 'HPCI Logic System Functional Test') on the Unit 3 HPCI system, the turbine exhaust rupture diaphragm alarm annuciated following startup of the HPCI turbine.
This alarm sences a pressure of greater than 10 psig between the inner and outer rupture discs located in series in a 16" line which taps off the turbine exhaust line and itself exhausts to the torus. room.
Investigation revealed that the inner rupture disc,
.PSD3-23-6 (manufactured by Continental Disc Corporation), had ruptured.
The setpoint_of the rupture disc is 175 psig.
The outer rupture disc, PSD3-23-7, had not ruptured, and therefore the HPCI turbine was not declared inoperable at that time.
At 4:44 p.m. on January 6,1984, the HPCI turbine was intentionally removed from service and declared inoperable in order to replace the inner rupture disc.
At 8:31 p.m. on January 6, 1984, the HPCI turbine, which was out of service for three hours and forty-seven minutes, was declared operable and returned to service following surveillance test (ST-6. 5 ) verification,.
As of January l',1984, the newly imposed 10CFR50.72 (b) (2) (iii) requires reporting an inoperable HPCI system within four hours on the Emergency Notification System (ENS).
Administrative Procedure A-31, Rev. 8 " Procedure for Notification of NRC",
addresses this new reporting requirement, however, the four hour report was not made.
The notification error was due to an administrative oversight as a result of an unfamiliarity with the new reporting requirements.
The NRC Site Inspector was notified of the reporting error.
Senior station personnel were informed on January 9,1984 of the importance of being familiar with the new reporting requirements.
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e,.msm.nn Consequences of the Event:
The outer rupture disc, PSD3-23-7, did not rupture therefore the HPCI system remained in service at the time of the occurrence.
Prior to blocking the HPCI system out of service, the Reactor Core Isolation Cooling System, Automatic Depressurization System, Low Pressure Coolant Injection System, and Core Spray systems were verified as operable as required by Technical Specification 4.5.C.2.
The HPCI system was returned to service within four hours after being declared inoperable.
Cause of the Event
Determination of the cause of the event is under investigation.
The scope of the investigation includes: 1) verifying the proper material of the rupture discf 2) a review of the piping configuration of the turbine exhaust line, 3) investigating the performance of the vacuum breakers between the torus air space and turbine exhaust line, 4) investigating'the turbine exhaust i
stop/ check-vdive performance, and 5) obtaining dynamic pressure test data of the turbine exhaust system.
A supplemental report will be submitted following completion of the investigation.
I
Corrective Actions
ST 6.5 HPCI Pump, Valve, Flow, Cooler Test verified the Turbineexhaustpressureindic[atednormallyduringthe operability of the HPCI system after the inner rupture disc was replaced.
test and the system was returned to service.
A subsequent ST-6.5 l
was successfully completed on January 30, 1984 with all functions indicating normally.
L Previous Similar Occurrences LER's: 3-83-15/3L-0, 3-82-23/3L-0.
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PHILADELPHIA ELECTRIC COMPANY 23O1 MARKET STREET P.O. BOX 8699 PHILADELPHIA. PA.19101 (2153841-4000 March 30, 1984 Docket No. 50-278 Document Control Desk
.U.S. Nuclear Regulatory Commission Washington, DC 20555
SUBJECT:
Licensee Event Report
Dear Dr. Murley:
This LER deals with the failure of the Unit No. 3 HPCI turbine exhaust inner' rupture disc, PSD3-23-6, while performing surveillance testing on the HPCI system.
Reference:
Docket No. 50-278 Report Number:
3-84-01 Revision Number:
01 Event Date:
January 6, 1984
= Report Date:
March 30, 1984 Facility:
Peach Bottom Atomic Power Station RD #1, Delta, PA 17314 This LER is submitted pursuant to.the requirements of 10 CFR' 50.73 (a) (2) (v).
The revised portion of this LER is identified by a vertical bar in the margin.
Very truly yours, W. T. Ullrich Superintendent Nuclear Generation Division
!cc:
- - Mr. A. R. Blough Site Inspector Dr. Thomas E. Murley, USNRC
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| 05000278/LER-1984-001-02, Revised LER 84-001-02:on 840106,turbine Exhaust Rupture Diaphragm Alarm Annunicated Following Startup of HPCI Turbine.Caused by Rupture of Inner Rupture Disc.Inner Rupture Disc Replaced | Revised LER 84-001-02:on 840106,turbine Exhaust Rupture Diaphragm Alarm Annunicated Following Startup of HPCI Turbine.Caused by Rupture of Inner Rupture Disc.Inner Rupture Disc Replaced | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1984-001, :on 840106,HPCI Turbine Exhaust Rupture Diaphragm Alarm Annunciated Following Startup.Caused by Inner Rupture Disk PSD3-23-6 Ruptured.Inner Rupture Disc Replaced |
- on 840106,HPCI Turbine Exhaust Rupture Diaphragm Alarm Annunciated Following Startup.Caused by Inner Rupture Disk PSD3-23-6 Ruptured.Inner Rupture Disc Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1984-001, :on 840117,during Surveillance Testing of RHR B Injection Valve Mo 2-10154B,valve Failed to Reopen.Caused by Warping of Bakelite Coil & Core Housing within Motor Control Ctr.Thermal Overload Device Replaced |
- on 840117,during Surveillance Testing of RHR B Injection Valve Mo 2-10154B,valve Failed to Reopen.Caused by Warping of Bakelite Coil & Core Housing within Motor Control Ctr.Thermal Overload Device Replaced
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000277/LER-1984-002-01, :on 840321,partial Actuation of Primary Containment Isolation Sys Caused Main Steam Tunnel Ventilation Trip.Caused by Burned Out Coil in Relay 16A-K24. Relay & Isolation Logic Replaced |
- on 840321,partial Actuation of Primary Containment Isolation Sys Caused Main Steam Tunnel Ventilation Trip.Caused by Burned Out Coil in Relay 16A-K24. Relay & Isolation Logic Replaced
| | | 05000278/LER-1984-002, :on 840124,reactor Heatup Rate of 111 F/H Occurred During Unit Startup.Caused by Calculation Error. Heatup Rate Reduced by Reactor Operator |
- on 840124,reactor Heatup Rate of 111 F/H Occurred During Unit Startup.Caused by Calculation Error. Heatup Rate Reduced by Reactor Operator
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000277/LER-1984-003-01, Revised LER 84-003-01:on 840131,heatup Rate Exceeded Tech Spec Limits.Caused by Personnel Error.Operator Disciplined. Memo Issued to All Licensed Operators Re Tech Spec Rate | Revised LER 84-003-01:on 840131,heatup Rate Exceeded Tech Spec Limits.Caused by Personnel Error.Operator Disciplined. Memo Issued to All Licensed Operators Re Tech Spec Rate | | | 05000277/LER-1984-003, :on 840131,operator Failed to Take Corrective Action Rapidly Enough to Contain Reactor Coolant Temp, Allowing Heatup Rate to Reach 120 F.Caused by Personnel Error.Operator Disciplined |
- on 840131,operator Failed to Take Corrective Action Rapidly Enough to Contain Reactor Coolant Temp, Allowing Heatup Rate to Reach 120 F.Caused by Personnel Error.Operator Disciplined
| | | 05000278/LER-1984-003-01, :on 840329,core Spray Logic Fuse 14A-F2B Blew During Instrument Surveillance Testing Due to Shorted Socket on Indicating Light 14A-DS26B.Shorted Socket Removed from Logic Circuit & Fuse Replaced |
- on 840329,core Spray Logic Fuse 14A-F2B Blew During Instrument Surveillance Testing Due to Shorted Socket on Indicating Light 14A-DS26B.Shorted Socket Removed from Logic Circuit & Fuse Replaced
| | | 05000278/LER-1984-004, :on 840125,reactor Coolant Temp Dropped Below 120 F When Feedwater Inadvertently Pumped Into Reactor Vessel.Caused by Operator Error.Level Restored to Normal & Main Steam Line Drains Opened |
- on 840125,reactor Coolant Temp Dropped Below 120 F When Feedwater Inadvertently Pumped Into Reactor Vessel.Caused by Operator Error.Level Restored to Normal & Main Steam Line Drains Opened
| | | 05000277/LER-1984-004-01, :on 840213,during Local Leak Rate Tests on RHR Sys B Valves,Packing Leak Discovered on Test Line Isolation Valve MO2-10-34B.Caused by Loose Packing.Packing Tightened & Valve Stroke Tested |
- on 840213,during Local Leak Rate Tests on RHR Sys B Valves,Packing Leak Discovered on Test Line Isolation Valve MO2-10-34B.Caused by Loose Packing.Packing Tightened & Valve Stroke Tested
| | | 05000277/LER-1984-005-01, :on 840323,partial Actuation of Primary Containment Isolation Sys Occurred.Caused by Power Loss to Portion of Primary Containment Isolation Sys Due to Blown Fuse from Shorted Coil in Relay 1GA-K56 |
- on 840323,partial Actuation of Primary Containment Isolation Sys Occurred.Caused by Power Loss to Portion of Primary Containment Isolation Sys Due to Blown Fuse from Shorted Coil in Relay 1GA-K56
| 10 CFR 50.73(a)(2) | | 05000278/LER-1984-005, :on 840209,reactor Auto Scram on High Neutron Flux Occurred Due to Runback & Subsequent Relay Failure in Main Turbine Electrohydraulic Control Sys.Caused by Faulty Relay Contact.Relay Replaced |
- on 840209,reactor Auto Scram on High Neutron Flux Occurred Due to Runback & Subsequent Relay Failure in Main Turbine Electrohydraulic Control Sys.Caused by Faulty Relay Contact.Relay Replaced
| 10 CFR 50.73(a)(2) | | 05000278/LER-1984-006-01, :on 840426,inconsistency in Temp Indications for Main Steam Line Tunnel Exhaust Duct Noted.Investigation Showed TE-5931A & TE-5931B Pulled Out of Exhaust Duct.Caused by Improper Scaffolding Installation |
- on 840426,inconsistency in Temp Indications for Main Steam Line Tunnel Exhaust Duct Noted.Investigation Showed TE-5931A & TE-5931B Pulled Out of Exhaust Duct.Caused by Improper Scaffolding Installation
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000277/LER-1984-006, :on 840328,routine Sample of Water Taken from High Pressure Svc Water Piping Discovered Contaminated. Caused by HX Leaking Into Discharge Pond Via Piping Sys. HX Repaired |
- on 840328,routine Sample of Water Taken from High Pressure Svc Water Piping Discovered Contaminated. Caused by HX Leaking Into Discharge Pond Via Piping Sys. HX Repaired
| | | 05000278/LER-1984-007-01, :on 840602,HPCI Sys Made Inoperable for Maint Work W/Reactor Pressure Greater than 105 Psig.Caused by Failure of Personnel to Realize HPCI Inoperability Would Violate Tech Specs.Individual Counseled |
- on 840602,HPCI Sys Made Inoperable for Maint Work W/Reactor Pressure Greater than 105 Psig.Caused by Failure of Personnel to Realize HPCI Inoperability Would Violate Tech Specs.Individual Counseled
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1984-007, :on 840403,reactor Water Cleanup Sys Isolated on High Temp.Caused by Loss of Electrical Power to Temp Indicating Switch TIS-12-99.Maint Shorted Hot Lead to Ground Causing Fuse 12A-F1 to Blow.Fuse Replaced |
- on 840403,reactor Water Cleanup Sys Isolated on High Temp.Caused by Loss of Electrical Power to Temp Indicating Switch TIS-12-99.Maint Shorted Hot Lead to Ground Causing Fuse 12A-F1 to Blow.Fuse Replaced
| 10 CFR 50.73(a)(2) | | 05000277/LER-1984-008-01, Revised LER 84-008-01:on 840427,standby Gas Treatment Sys Solenoid Valve SV-00009 Failed to Operate Properly, Preventing Fan a Inlet & Outlet Dampers from Opening.Cause of Solenoid Failure Under Investigation | Revised LER 84-008-01:on 840427,standby Gas Treatment Sys Solenoid Valve SV-00009 Failed to Operate Properly, Preventing Fan a Inlet & Outlet Dampers from Opening.Cause of Solenoid Failure Under Investigation | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000278/LER-1984-008-01, :on 840610,three through-wall Cracks Discovered in Loop Jet Pump B Instrumentation Penetration Reducer to safe-end Weld.Caused by Igscc.Circumferential Indications on Welds Repaired |
- on 840610,three through-wall Cracks Discovered in Loop Jet Pump B Instrumentation Penetration Reducer to safe-end Weld.Caused by Igscc.Circumferential Indications on Welds Repaired
| | | 05000277/LER-1984-008, :on 840427,solenoid Valve SV-00009 of Standby Gas Treatment Sys Failed.Caused by Measurement Error of Differential Pressure Switch.Defective Solenoid Replaced & Switches Will Be Replaced & Tested |
- on 840427,solenoid Valve SV-00009 of Standby Gas Treatment Sys Failed.Caused by Measurement Error of Differential Pressure Switch.Defective Solenoid Replaced & Switches Will Be Replaced & Tested
| | | 05000277/LER-1984-009, :on 840516,during Refueling Outage,False lo-lo Reactor Level Initiation Signal Caused HPCI & RCIC to Attempt to Start When Both Power Supplies for ECCS Channel a Logic Feeds Removed.Supply Feeds Restored |
- on 840516,during Refueling Outage,False lo-lo Reactor Level Initiation Signal Caused HPCI & RCIC to Attempt to Start When Both Power Supplies for ECCS Channel a Logic Feeds Removed.Supply Feeds Restored
| 10 CFR 50.73(a)(2) | | 05000278/LER-1984-009-01, :on 840801,HPCI Sys Declared Inoperable Due to Identification of Mechanical Failure of Second HPCI Steam Supply Line Hanger 3-23-DBN-S4.Cause Unknown.Hanger Repaired & HPCI Returned to Svc |
- on 840801,HPCI Sys Declared Inoperable Due to Identification of Mechanical Failure of Second HPCI Steam Supply Line Hanger 3-23-DBN-S4.Cause Unknown.Hanger Repaired & HPCI Returned to Svc
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1984-010, :on 840607,w/unit Shutdown for Refueling & Major Mod outage,through-wall Crack Discovered in Loop a Jet Pump Instrumentation Penetration Reducer to safe-end Weld.Caused by IGSCC |
- on 840607,w/unit Shutdown for Refueling & Major Mod outage,through-wall Crack Discovered in Loop a Jet Pump Instrumentation Penetration Reducer to safe-end Weld.Caused by IGSCC
| 10 CFR 50.73(a)(2)(i) | | 05000278/LER-1984-010-01, :on 840816,loss of Power to Portion of Primary Containment Isolation Sys Outboard Isolation Logic Caused Partial Actuation.Caused by Grounded Leads on Primary Side of Unit 2 Pump Transformer A.Logic Reset |
- on 840816,loss of Power to Portion of Primary Containment Isolation Sys Outboard Isolation Logic Caused Partial Actuation.Caused by Grounded Leads on Primary Side of Unit 2 Pump Transformer A.Logic Reset
| 10 CFR 50.73(a)(2) | | 05000277/LER-1984-011, :on 840608,acetylene Leak Occurred During Drywell Preheat Welding.Caused by Leak Where Hose Crimped to Std Screw Connection.Personnel Evacuated & Addl Ventilation Used to Expel Gas |
- on 840608,acetylene Leak Occurred During Drywell Preheat Welding.Caused by Leak Where Hose Crimped to Std Screw Connection.Personnel Evacuated & Addl Ventilation Used to Expel Gas
| | | 05000278/LER-1984-011-01, :on 840821,sudden Runback of Three Reactor Feed Pumps Resulted in Reactor Low Level Scram,Groups I,Ii & III Isolations & Automatic Initiation of HPCI & Rcic.Caused by Intermittent Failure of Component |
- on 840821,sudden Runback of Three Reactor Feed Pumps Resulted in Reactor Low Level Scram,Groups I,Ii & III Isolations & Automatic Initiation of HPCI & Rcic.Caused by Intermittent Failure of Component
| 10 CFR 50.73(a)(2) | | 05000278/LER-1984-012-01, :on 840912,section of Standby Gas Treatment Sys Duct Work in Reactor Bldg Sump Room Collapsed.Caused by Valving Error During Transfer of Equipment Cell Exhaust. Ductwork Repaired |
- on 840912,section of Standby Gas Treatment Sys Duct Work in Reactor Bldg Sump Room Collapsed.Caused by Valving Error During Transfer of Equipment Cell Exhaust. Ductwork Repaired
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1984-012, :on 840628,w/unit in Cold Shutdown for Refueling,Surveillance Testing Discovered Inoperable Horizontal Fire Damper in Cable Spreading Room.Caused by Missing Spring Closure Device |
- on 840628,w/unit in Cold Shutdown for Refueling,Surveillance Testing Discovered Inoperable Horizontal Fire Damper in Cable Spreading Room.Caused by Missing Spring Closure Device
| | | 05000277/LER-1984-013, :on 840629,diesel Driven Fire Pump Started Automatically & Flooding Occured at Elevation 116 Ft of Turbine Bldg.Caused by Break in Elbow in Fire Header.Both Fire Pumps Removed from Svc & Tested |
- on 840629,diesel Driven Fire Pump Started Automatically & Flooding Occured at Elevation 116 Ft of Turbine Bldg.Caused by Break in Elbow in Fire Header.Both Fire Pumps Removed from Svc & Tested
| 10 CFR 50.73(a)(2)(x) | | 05000278/LER-1984-013-01, :on 840921,during Surveillance Test,Hpci Turbine Exhaust Rupture Diaphragm Alarm Annunicated Following Startup of Turbine.Caused by Ruptured Inner Rupture Disc PSD3-23-6.Disc Replaced |
- on 840921,during Surveillance Test,Hpci Turbine Exhaust Rupture Diaphragm Alarm Annunicated Following Startup of Turbine.Caused by Ruptured Inner Rupture Disc PSD3-23-6.Disc Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1984-014, :on 840716,continuous Firewatch Removed from Cable Spreading Room W/O Realizing That Firewatch Still Needed Due to out-of-svc Cardox Sys.Condition Discovered & Firewatch Reestablished on 840719 |
- on 840716,continuous Firewatch Removed from Cable Spreading Room W/O Realizing That Firewatch Still Needed Due to out-of-svc Cardox Sys.Condition Discovered & Firewatch Reestablished on 840719
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000278/LER-1984-014-01, :on 841114,reactor Scram Occurred While Attempting to Replace Recirculation Pump B.Caused by Power Spike from Cold Water from Idle Recirculation Loop. Operating Procedure for Pump Startup Revised |
- on 841114,reactor Scram Occurred While Attempting to Replace Recirculation Pump B.Caused by Power Spike from Cold Water from Idle Recirculation Loop. Operating Procedure for Pump Startup Revised
| 10 CFR 50.73(a)(2) | | 05000278/LER-1984-015-02, :on 841126,HPCI Turbine Exhaust Rupture Diaphragm Alarm Annunciated.Caused by Failure of Inner Rupture Disk PSD3-23-6.Rupture Disk Replaced |
- on 841126,HPCI Turbine Exhaust Rupture Diaphragm Alarm Annunciated.Caused by Failure of Inner Rupture Disk PSD3-23-6.Rupture Disk Replaced
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000277/LER-1984-015, :on 840709,smoke Detector Alarms Activated W/O Cause.Hourly Fire Patrol Established & Detectors Removed, Violating Tech Spec 3.14.D.3 Rev.Personnel Will Review Tech Spec Revs to Avoid Deviation |
- on 840709,smoke Detector Alarms Activated W/O Cause.Hourly Fire Patrol Established & Detectors Removed, Violating Tech Spec 3.14.D.3 Rev.Personnel Will Review Tech Spec Revs to Avoid Deviation
| 10 CFR 50.73(a)(2)(1) | | 05000277/LER-1984-016, :on 840727,liquid Penetration Exams of Reactor Pressure Vessel Jet Pump Inlet Riser Safe Ends Revealed crack-like Indications.Caused by Igscc.Addl Radiographic & Liquid Dye Penetrant Exams Will Be Performed |
- on 840727,liquid Penetration Exams of Reactor Pressure Vessel Jet Pump Inlet Riser Safe Ends Revealed crack-like Indications.Caused by Igscc.Addl Radiographic & Liquid Dye Penetrant Exams Will Be Performed
| 10 CFR 50.73(a)(2)(1) |
|