ML14224A150

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Inspection Report 05000331/2014003; 04/01/2014 - 06/30/2014, Duane Arnold Energy Center; Maintenance Effectiveness, Operability Determinations and Functionality Assessments, and Identification and Resolution of Problems
ML14224A150
Person / Time
Site: Duane Arnold NextEra Energy icon.png
Issue date: 08/11/2014
From: Christine Lipa
NRC/RGN-III/DRP/B1
To: Richard Anderson
NextEra Energy Duane Arnold
References
IR-14-003
Download: ML14224A150 (49)


See also: IR 05000331/2014003

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE RD. SUITE 210

LISLE, IL 60532-4352

August 11, 2014

Mr. Richard L. Anderson

Vice President

NextEra Energy Duane Arnold, LLC

3277 DAEC Road

Palo, IA 52324-9785

SUBJECT: DUANE ARNOLD ENERGY CENTER - NRC INTEGRATED INSPECTION

REPORT 05000331/2014003

Dear Mr. Anderson:

On June 30, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated

inspection at your Duane Arnold Energy Center. The enclosed report documents the results of

this inspection, which were discussed on July 21, 2014, with you and other members of your

staff.

Based on the results of this inspection, three NRC-identified findings of very low safety

significance were identified. The findings involved violations of NRC requirements. However,

because of their very low safety significance, and because the issues were entered into your

corrective action program, the NRC is treating the issues as non-cited violations (NCVs) in

accordance with Section 2.3.2 of the NRC Enforcement Policy. Additionally, two licensee-

identified violations are listed in Section 4OA7 of this report.

If you contest the subject or severity of any NCV, you should provide a response within 30 days

of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a

copy to the Regional Administrator, U.S. Nuclear Regulatory Commission - Region III,

2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector

Office at the Duane Arnold Energy Center. In addition, if you disagree with the cross-cutting

aspect assigned to any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region III, and the NRC Resident Inspector at the Duane Arnold Energy Center.

R. Anderson -2-

In accordance with Title 10 of the Code of Federal Regulation 2.390, Public Inspections,

Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter

and its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Christine Lipa, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-331

License No. DPR-49

Enclosure:

Inspection Report 05000331/2014003

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-331

License No: DPR-49

Report No: 05000331/2014003

Licensee: NextEra Energy Duane Arnold, LLC

Facility: Duane Arnold Energy Center

Location: Palo, IA

Dates: April 1 through June 30, 2014

Inspectors: L. Haeg, Senior Resident Inspector

J. Steffes, Resident Inspector

D. Oliver, Reactor Inspector

S. Shah, Reactor Engineer

V. Myers, Health Physicist

R. Elliott, Reactor Engineer

C. Norton, Project Manager

Approved by: Christine Lipa, Chief

Branch 1

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS ........................................................................................................... 2

REPORT DETAILS ....................................................................................................................... 5

Summary of Plant Status ........................................................................................................... 5

1. REACTOR SAFETY ....................................................................................................... 5

1R01 Adverse Weather Protection (71111.01) .............................................................. 5

1R04 Equipment Alignment (71111.04) ........................................................................ 6

1R05 Fire Protection (71111.05) ................................................................................... 7

1R06 Flooding (71111.06) ............................................................................................. 7

1R11 Licensed Operator Requalification Program (71111.11) ...................................... 8

1R12 Maintenance Effectiveness (71111.12) ................................................................ 9

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) ........ 12

1R15 Operability Determinations and Functionality Assessments (71111.15) ............ 13

1R18 Plant Modifications (71111.18) .......................................................................... 17

1R19 Post-Maintenance Testing (71111.19) ............................................................... 17

1R22 Surveillance Testing (71111.22) ........................................................................ 18

2. RADIATION SAFETY ................................................................................................... 19

2RS5 Radiation Monitoring Instrumentation (71124.05) .............................................. 19

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06) ...................... 20

4. OTHER ACTIVITIES .................................................................................................... 26

4OA1 Performance Indicator (PI) Verification (71151) ................................................. 26

4OA2 Identification and Resolution of Problems (71152) ............................................ 27

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153) ............... 33

4OA6 Management Meetings ...................................................................................... 33

4OA7 Licensee-Identified Violations ............................................................................ 33

SUPPLEMENTAL INFORMATION ............................................................................................... 1

KEY POINTS OF CONTACT..................................................................................................... 1

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED ......................................................... 2

LIST OF DOCUMENTS REVIEWED......................................................................................... 3

LIST OF ACRONYMS USED .................................................................................................. 10

SUMMARY OF FINDINGS

Inspection Report 05000331/2014003; 04/01/2014 - 06/30/2014, Duane Arnold Energy Center;

Maintenance Effectiveness, Operability Determinations and Functionality Assessments, and

Identification and Resolution of Problems.

This report covers a three-month period of inspection by resident inspectors and announced

baseline inspections by regional inspectors. Three Green findings were identified by the

inspectors. The findings were considered non-cited violations (NCVs) of Nuclear Regulatory

Commission (NRC) regulations. The significance of inspection findings is indicated by their

color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection

Manual Chapter (IMC) 0609, Significance Determination Process (SDP), dated June 2, 2011.

Cross-cutting aspects are determined using IMC 0310, Aspects Within the Cross-Cutting

Areas effective date January 1, 2014. All violations of NRC requirements are dispositioned in

accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process Revision 5, dated February 2014.

NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding of very low safety significance (Green) and

associated non-citied violation of Duane Arnold Energy Center (DAEC) Renewed

Operating License Condition 2.C.(3), for the failure to implement compensatory

measures for non-functional fire suppression deluge systems. Specifically, the licensee

did not establish hourly fire patrols within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of discovering the non-functional status

of deluges 3 and 4 in accordance with Technical Requirements Manual (TRM) Limiting

Condition for Operation (TLCO) 3.11.4, Fire Suppression Deluge and Sprinkler

Systems, Condition A.2. The licensee documented the issue in the corrective action

program (CAP) as condition reports (CRs) 01959153, 01964875, 01964878, 01968702,

01968720 and 01971501; and implemented fire patrols until the deluge systems were

satisfactorily tested per TRM requirements.

The performance deficiency was determined to be more than minor and a finding in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, because it impacted the Reactor Safety - Initiating Events Cornerstone of

Protection Against External Factors to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. The inspectors also determined that if left uncorrected, the performance

deficiency would have the potential to lead to a more significant safety concern. The

inspectors applied IMC 0609, Attachment 4, Initial Characterization of Findings, to this

finding. The inspectors answered Yes to question E.2(2), Does the finding involve

fixed fire protection systems or the ability to contain a fire within Table 3 - SDP Appendix

Router, and transitioned to IMC 0609, Appendix F, Fire Protection Significance

Determination Process. The inspectors processed the finding in accordance with Fire

Protection SDP Phase 1 Screening in IMC 0609, Appendix F, Attachment 1 and

answered Yes to Step 1.3, Task 1.3.1 question, Is the reactor able to reach and

maintain safe shutdown (either hot or cold) condition? Therefore, the finding screened

as very low safety significance (Green).

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The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Consistent Process in the Human Performance area and

involving individuals using a consistent systematic approach to make decisions. [H.13]

(Section 1R15.1)

Cornerstone: Mitigating Systems

  • Green. The inspectors identified a finding of very low safety significance (Green) and

associated non-cited violation of 10 CFR 50, Appendix B, Criterion V, Instructions,

Procedures, and Drawings, for the failure to prescribe a procedure appropriate to the

circumstances for work order planning as related to the failure of under-voltage relay

127-SB2. Specifically, procedure MA-AA-203-1001, Work Order Planning, Section 4.2,

Step 2, inappropriately allowed the selection of model work orders without verification of

the acceptance criteria, requirements for as-found/as-left data, set points, and other

related information. The issue was entered into the licensees CAP for resolution as

CRs 01972812 and 01972807; and the licensee took actions to add a verification step to

procedure MA-AA-203-1001, Section 4.2, Step 2, to verify the procedure being

referenced contained the relevant information to the work task being accomplished.

The inspectors determined that the issue of concern represented a performance

deficiency because it was the result of the licensees failure to prescribe a procedure

appropriate for the circumstances. The performance deficiency was determined to be

more than minor and a finding in accordance with IMC 0612, Power Reactor Inspection

Reports, Appendix B, Issue Screening, because if left uncorrected, the performance

deficiency would have the potential to lead to a more significant safety concern. The

inspectors applied IMC 0609, Attachment 4, Initial Characterization of Findings, to this

finding. The inspectors answered No to all questions within Table 3 - SDP Appendix

Router, and transitioned to IMC 0609, Appendix A, The Significance Determination

Process for Findings At-Power. Per Exhibit 2 - Mitigating Systems Screening

Questions, the inspectors determined that because the finding did not represent an

actual loss of function (redundant loss of power instrumentation remained operable

during the period of the 127-SB2 inoperability), the finding screened as very low safety

significance (Green).

The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Evaluation in the Problem Identification and Resolution area and

involved the organization thoroughly evaluating issues to ensure that resolutions

address causes and extent of conditions commensurate with their safety significance.

[H.13] (Section 4OA2.5)

Cornerstone: Barrier Integrity

  • Green. A finding of very low safety significance and associated non-citied violation of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was

identified by the inspectors for the licensees failure to accomplish procedure EN-AA-

203-1001, Operability Determinations/Functionality Assessments. Specifically, on

multiple occasions but as recently as March 20, 2014, the licensee failed to properly

evaluate operability following intermittent downward spikes of the A refueling floor

exhaust duct - high radiation monitor (RIS-4131A). The improper operability evaluations

3

resulted in not declaring RIS-4131A inoperable when appropriate, improper prioritization

of investigation of the cause, and untimely resolution of the degraded conditions. The

licensee entered the inspectors concerns into the CAP as CR 01954560. The licensee

invoked a policy to properly assess operability in the interim, completed a prompt

operability determination (POD) to evaluate intermittent downward spikes, completed a

past operability review (POR), and ultimately identified the cause and implemented

repairs to RIS-4131A.

The inspectors determined that the issue of concern represented a performance

deficiency because it was the result of the licensees failure to meet a procedural

requirement, and the cause was reasonably within the licensees ability to foresee and

correct and should have been prevented. The performance deficiency was determined

to be more than minor and a finding in accordance with IMC 0612, Power Reactor

Inspection Reports, Appendix B, Issue Screening, because it impacted the Barrier

Integrity Cornerstone Attribute of structure, system, and component (SSC) and Barrier

Performance, and adversely affected the Cornerstone objective of maintaining

containment and radiological barrier functionality. The inspectors applied IMC 0609,

Attachment 4, Initial Characterization of Findings, to this finding. The inspectors

answered No to all questions within Table 3 - SDP Appendix Router, and transitioned

to IMC 0609, Appendix A, The Significance Determination Process for Findings At-

Power. Per Exhibit 3 - Barrier Integrity Screening Questions, the inspectors answered

No to questions B.1 and B.2, and Yes to question C.1, therefore, the finding screened

as very low safety significance (Green).

The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Human Performance, Consistent Process, and involving

individuals using a consistent, systematic approach to make decisions. [H.13]

(Section 1R12.1)

Licensee-Identified Violations

Violations of very low safety or security significance or Severity Level IV that were

identified by the licensee have been reviewed by the NRC. Corrective actions taken or

planned by the licensee have been entered into the licensees CAP. These violations

and CAP tracking numbers are listed in Section 4OA7 of this report.

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REPORT DETAILS

Summary of Plant Status

Duane Arnold Energy Center (DAEC) operated at full power for the entire inspection period

except for brief down-power maneuvers to accomplish rod pattern adjustments or to conduct

planned surveillance testing activities.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.1 External Flooding

a. Inspection Scope

The inspectors evaluated the design, material condition, and procedures for coping with

the design basis probable maximum flood. The evaluation included a review to check

for deviations from the descriptions provided in the Updated Final Safety Analysis Report

(UFSAR) for features intended to mitigate the potential for flooding from external factors.

As part of this evaluation, the inspectors checked for obstructions that could prevent

draining, checked that the roofs did not contain obvious loose items that could clog

drains in the event of heavy precipitation, and determined that barriers required to

mitigate the flood were in place and operable. Additionally, the inspectors performed a

walkdown of the protected area to identify any modification to the site which would inhibit

site drainage during a probable maximum precipitation event or allow water ingress past

a barrier. The inspectors also walked down underground bunkers/manholes subject to

flooding that contained multiple train or multiple function risk-significant cables. The

inspectors also reviewed the abnormal operating procedure (AOP) for mitigating the

design basis flood to ensure it could be implemented as written. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one external flooding sample as defined in Inspection

Procedure (IP) 71111.01-05.

b. Findings

No findings were identified.

.2 Readiness For Impending Adverse Weather Condition - Extreme Heat/Drought

Conditions

a. Inspection Scope

The inspectors performed a detailed review of the licensees procedures and

preparations for operating the facility during an extended period of time when ambient

outside temperature was high and the ultimate heat sink was experiencing elevated

temperatures. The inspectors focused on plant specific design features and

implementation of the procedures for responding to or mitigating the effects of these

conditions on the operation of the facilitys River Water Supply, Emergency Service

5

Water, Residual Heat Removal Service Water, and electrical substation systems.

Inspection activities included a review of the licensees adverse weather procedures,

daily monitoring of the off-normal environmental conditions, and that operator actions

specified by plant specific procedures were appropriate to ensure operability of the

facilitys normal and emergency cooling systems. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one readiness for impending adverse weather condition

sample as defined in IP 71111.01-05.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04)

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk significant

systems:

  • B Control Building Chiller (CBC) subsystem with the A CBC subsystem out of

service for planned maintenance (PM);

  • Intake Structure Ventilation System; and

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, the UFSAR, Technical Specification (TS) requirements, outstanding

work orders (WOs), CRs, and the impact of ongoing work activities on redundant trains

of equipment in order to identify conditions that could have rendered the systems

incapable of performing their intended functions. The inspectors also walked down

accessible portions of the systems to verify system components and support equipment

were aligned correctly and operable. The inspectors examined the material condition of

the components and observed operating parameters of equipment to verify that there

were no obvious deficiencies. The inspectors also verified that the licensee had properly

identified and resolved equipment alignment problems that could cause initiating events

or impact the capability of mitigating systems or barriers and entered them into the

corrective action program (CAP) with the appropriate significance characterization.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted three quarterly partial system walkdown samples as

defined in IP 71111.04-05.

b. Findings

No findings were identified.

6

1R05 Fire Protection (71111.05)

.1 Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk significant

plant areas:

  • Pre-Fire Plan (PFP) -RB-757; Pre-Fire Plan Reactor Building El. 757,

Revision 0;

  • PFP-RB-812; Pre-Fire Plan Reactor Building El. 812, Revision 0;
  • PFP-TB-780; Pre-Fire Plan Turbine Building El. 780, Revision 0;
  • PFP-RB-828; Pre-Fire Plan Reactor Building El. 828, Revision 0; and
  • PFP-RB-855; Pre-Fire Plan Reactor Building El. 855, Revision 0.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and implemented adequate

compensatory measures for out-of-service, degraded or inoperable fire protection

equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event.

Using the documents listed in the Attachment to this report, the inspectors verified that

fire hoses and extinguishers were in their designated locations and available for

immediate use; that fire detectors and sprinklers were unobstructed; that transient

material loading was within the analyzed limits; and fire doors, dampers, and penetration

seals appeared to be in satisfactory condition. The inspectors also verified that minor

issues identified during the inspection were entered into the licensees CAP.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted five routine resident inspector tour samples as defined in

IP 71111.05-05.

b. Findings

No findings were identified.

1R06 Flooding (71111.06)

.1 Underground Vaults

a. Inspection Scope

The inspectors selected underground bunkers/manholes subject to flooding that

contained cables whose failure could disable risk-significant equipment. The inspectors

determined whether any cables were submerged, that splices were intact, and that

appropriate cable support structures were in place. In those areas where dewatering

7

devices were used, such as a sump pump, the inspectors determined whether the

device was functional and level alarm circuits were set appropriately to ensure that the

cables would not be submerged. In those areas without dewatering devices, the

inspectors verified that drainage of the area was available, or that the cables were

qualified for submergence conditions. The inspectors also reviewed the licensees

corrective action documents with respect to past submerged cable issues identified in

the CAP to verify the adequacy of the corrective actions. The inspectors performed a

walkdown of the following underground bunkers/manholes subject to flooding:

  • Manholes 1MH104, 105, 106, and 107.

Specific documents reviewed during this inspection are listed in the Attachment to this

report.

This inspection constituted one underground vaults sample as defined in

IP 71111.06-05.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program (71111.11)

.1 Resident Inspector Quarterly Review of Licensed Operator Requalification (71111.11Q)

a. Inspection Scope

On June 2, 2014, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification training to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas of the crew:

  • licensed operator performance;
  • clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one resident inspector quarterly review of licensed operator

requalification sample as defined in IP 71111.

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b. Findings

No findings were identified.

.2 Resident Inspector Quarterly Observation During Periods of Heightened Activity or Risk

(71111.11Q)

a. Inspection Scope

On May 20, 2014, the inspectors observed a crew of licensed operators during the

performance of a downpower evolution to perform a rod pattern adjustment. This was

an activity that required heightened awareness or was related to increased risk. The

inspectors evaluated the following areas of the crew:

  • licensed operator performance;
  • clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

The performance in these areas was compared to pre-established operator action

expectations, procedural compliance and task completion requirements. Documents

reviewed are listed in the Attachment to this report.

This inspection constituted one resident inspector quarterly observation during periods of

heightened activity or risk sample as defined in IP 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12)

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following

risk-significant systems:

  • Intake Structure Ventilation system;
  • Area and Process Radiation Monitors; and
  • Safety-Related Electrical Relays for the Standby and Start-Up Transformers.

The inspectors reviewed events such as where ineffective equipment maintenance had

resulted in valid or invalid automatic actuations of engineered safeguards systems and

independently verified the licensee's actions to address system performance or condition

problems in terms of the following:

9

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and

components (SSCs)/functions classified as (a)(2), or appropriate and adequate

goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted three routine quarterly evaluation samples as defined in

IP 71111.12-05.

b. Findings

(1) Failure to Accomplish Procedure for Repetitive Malfunctions of Refuel Floor Radiation

Monitor

Introduction: A finding of very low safety significance and associated non-cited violation

(NCV) of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, was identified by the inspectors for the licensees failure to accomplish

procedure EN-AA-203-1001, Operability Determinations/Functionality Assessments.

Specifically, on multiple occasions but as recently as March 20, 2014, the licensee failed

to properly evaluate operability of intermittent downward spikes of the A refueling floor

exhaust duct - high radiation monitor (RIS-4131A). The improper operability evaluations

resulted in not declaring RIS-4131A inoperable when appropriate, improper prioritization

of investigation of the cause, and untimely resolution of the degraded conditions.

Description: On February 21, 2014, operators in the main control room received an

unexpected alarm associated with the A refueling floor exhaust duct - high radiation

monitor (RIS-4131A). Upon further investigation, the licensee determined that a

downscale condition had occurred on the radiation monitor and the condition was

spurious, in that following a reset of the alarm, the downscale condition cleared. The

licensee documented the downscale condition in the CAP as CR 01942767,

documented that there is reasonable assurance that RIS-4131A remains able to

perform its safety function, therefore, RIS-4131A is operable, and the CR was closed to

trending.

During the week of March 3, 2014, the inspectors reviewed the extent of the downscale

conditions for RIS-4131A over the prior year. The inspectors noted five prior CRs dating

back to April of 2013 that documented similar spurious downscale alarms for RIS-4131A.

For each occurrence, the downscale alarm was reset, the radiation monitor was verified

to be indicating normally after the alarm reset and during the daily channel check, and

the CRs were closed to trend. However, following a downscale occurrence in October of

2013, the licensee generated a trend CR that documented the ongoing issues with

10

downscale alarms from RIS-4131A, and generated a condition evaluation to determine

why prior work orders performed to correct the downscale conditions had not been

effective. In November of 2013, DAEC Nuclear Oversight generated a CR also

recognizing the stations inability to correct the unknown condition with the radiation

monitor that was resulting in the repetitive downscale alarms.

Following additional downscale conditions on March 20 and April 1, 2014; and the

inspectors recollection that Revision 16 was made to licensee procedure

EN-AA-203-1001, Operability Determinations/Functionality Assessments, on

February 11, 2014, the inspectors questioned the licensees closing to trend downscale

conditions of RIS-4131A. In particular, the inspectors noted that EN-AA-203-1001

was revised to require more rigorous, systematic, and consistent

operability/functionality/reportability (OFR) screenings and immediate operability

determinations (IODs) for all CRs involving TS SSCs. The inspectors were concerned

that the licensee was not: 1) ensuring that the periodic inoperable conditions of the

radiation monitor were being properly evaluated under EN-AA-203-1001, 2) recognizing

that a degraded condition existed with RIS-4131A, and 3) establishing the appropriate

timeliness of resolution.

Specifically, EN-AA-203-1001, Section 4.1.2 required in part, that if the shift manager

receives notice that a SSC described in the current licensing basis is affected by a

degraded condition, the shift manager shall: perform the OFR screening using

instructions in Section 4.2. Section 4.2.1.1 of EN-AA-203-1001 required, in part, that

the shift manager shall perform the OFR screening of CRs that identify a degraded

condition. Attachment 1 of EN-AA-203-1001, OFR Screening, required in part, that

the required action for degraded conditions of TS SSCs is to perform an IOD. The

inspectors determined that the March 20 and April 1, 2014, downscale conditions of

RIS-4131A represented a degraded condition for RIS-4131A, and OFR and IOD

screenings had not been performed. In particular, EN-AA-203-1001, Section 4.3.1

required in part, that if the condition affects a TS SSC, the shift manager shall complete

the IOD without delay and in a controlled manner using the best available information,

and Section 4.3.6 required in part, that the shift manager prepares the IOD using the

guidance in EN-AA-203-1001-F04, AR Operability Notes Worksheet, to determine the

IOD content. Additionally, Section 4.3.9 required in part, that if the IOD raises a

question of past operability, then the shift manager shall request a prompt operability

determination (POR).

Based on the inspectors questions/concerns above, the licensee generated

CR 001954560 on April 3, 2014. Corrective actions included invoking a policy to

properly assess operability until final corrective actions were taken (logging of TS

LCO 3.3.6.1, Primary Containment Isolation Instrumentation, and 3.3.6.2, Secondary

Containment Isolation Instrumentation, entries during momentary inoperable

conditions), completing a prompt operability determination (POD) to evaluate operability

of the instrument and to evaluate for compensatory measures (RIS-4131A was

determined to be operable but degraded), and completing a past operability review.

Based on determining that RIS-4131A was operable but degraded, the station elevated

and prioritized investigation into the cause of the downward spikes, and ultimately

identified the cause and implemented repairs to RIS-4131A.

11

Analysis: The inspectors determined that the issue of concern represented a

performance deficiency because it was the result of the licensees failure to meet

procedural requirements, and the cause was reasonably within the licensees ability to

foresee and correct and should have been prevented.

The performance deficiency was determined to be more than minor and a finding

because it impacted the Barrier Integrity Cornerstone Attribute of SSC and Barrier

Performance, and adversely affected the Cornerstone objective of maintaining

containment and radiological barrier functionality. Specifically, the degraded condition of

RIS-4131A adversely impacted defense-in-depth provided by the primary and secondary

containment isolation refueling floor exhaust duct - high radiation function.

The inspectors applied Inspection Manual Chapter (IMC) 0609, Attachment 4, Initial

Characterization of Findings, to this finding. The inspectors answered No to all

questions within Table 3 - Significance Determination Process (SDP) Appendix Router,

and transitioned to IMC 0609, Appendix A, The Significance Determination Process for

Findings At-Power. Per Exhibit 3 - Barrier Integrity Screening Questions, the

inspectors answered No to questions B.1 and B.2, and Yes to question C.1,

therefore, the finding screened as very low safety significance (Green).

The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Human Performance, Consistent Process, and involving

individuals using a consistent, systematic approach to make decisions. Specifically, on

numerous occasions, improper operability decisions were made with respect to

intermittent downward spiking of RIS-4131A. By not using the systematic operability

process to evaluate the intermittent downward spikes, ongoing malfunctions of

RIS-4131A were accepted for an extended period of time. [H.13]

Enforcement: Title 10 CFR Part 50 Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires, in part, that activities affecting quality shall be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with these instructions.

Contrary to the above, on multiple occasions but as recently as March 20, 2014, the

licensee failed to properly accomplish procedure EN-AA-302-1001, Operability

Determinations/Functionality Assessments, Revision 16, following intermittent

downward spiking of the A refueling floor exhaust duct - high radiation monitor

(RIS-4131A).

Because this violation was of very low safety significance and because the issue was

entered into the licensees CAP as CR 01954560, consistent with Section 2.3.2 of the

Enforcement Policy it is being treated as a NCV. (NCV 05000331/2014003-01, Failure

to Accomplish Procedure for Repetitive Malfunctions of Refuel Floor Radiation

Monitor).

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk for the

maintenance and emergent work activities affecting risk-significant and safety-related

12

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

  • B Standby Diesel Generator (SBDG) unavailability during gasket replacements;
  • Cable Spreading Room Suppression system failed surveillance test;
  • Work Week 1424 plant risk; and
  • Plant risk during Core Spray surveillance testing and Emergency Core Cooling

System Instrument PMs.

These activities were selected based on their potential risk-significance relative to the

Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted five maintenance risk assessment and emergent work

control samples as defined in IP 71111.13-05.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15)

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

LS1861D (Reactor Protection System (RPS) Channel B2) found to be high out of

the TS-required calibration value;

  • Fire Protection System Deluge 3 & 4 lack of TRM surveillance test; and
  • Alternate Depressurization System accumulator sizing issue.

The inspectors selected these potential operability/functionality issues based on the risk

significance of the associated components and systems. The inspectors evaluated the

technical adequacy of the evaluations to ensure that TS operability or functionality was

properly justified and the subject component or system remained available such that no

unrecognized increase in risk occurred. The inspectors compared the operability,

functionality and design criteria in the appropriate sections of the TS, TRM, and UFSAR

to the licensees evaluations to determine whether the components or systems were

13

operable or functional. Where compensatory measures were required to maintain

operability or functionality, the inspectors determined whether the measures in place

would function as intended and were properly controlled. The inspectors determined,

where appropriate, compliance with bounding limitations associated with the evaluations.

Additionally, the inspectors reviewed a sampling of corrective action documents to verify

that the licensee was identifying and correcting any deficiencies associated with

operability and functionality evaluations.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted four operability evaluation samples as defined in

IP 71111.15-05.

b. Findings

(1) Failure to Establish Fire Patrols as Compensatory Actions in Accordance with the Fire

Protection Program

Introduction: The inspectors identified a finding of very low safety significance (Green)

and associated NCV of DAEC Renewed Operating License Condition 2.C.(3), for the

failure to implement compensatory measures for non-functional fire suppression deluge

systems. Specifically, the licensee did not establish hourly fire patrols within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of

discovering the non-functional status of deluges 3 and 4 in accordance with TRM

TLCO 3.11.4, Fire Suppression Deluge and Sprinkler Systems, Condition A.2.

Description: On March 6, 2014 the licensee transitioned their fire protection program to

National Fire Protection Association (NFPA) 805, Performance-Based Standard for Fire

Protection for Light Water Reactor Electric Generating Plants, 2001 Edition. As part of

the transition analysis, the licensee documented in FHA-200, Fire Protection Design

Documentation, Appendix F, Fire Safety Analysis, that deluge systems 3 and 4,

associated with Reactor Feedwater Pumps 1P-1B and 1P-1A, respectively, had been

determined to be of high safety significance in the event of a fire. Being of high safety

significance, controls and testing requirements for deluge systems 3 and 4 were

incorporated into TRM Section 3.11.4, Fire Suppression Deluge and Sprinkler

Systems, for periodic testing to ensure functionality. In accordance with Technical

Surveillance Requirement (TSR) 3.11.4.4, these deluges were required to be air flow

tested on 36 month basis.

On April 17, 2014 while reviewing License Renewal Interim Staff Guidance

LR-ISG-2012-02, Aging Management of Internal Surfaces, Fire Water Systems,

Atmospheric Storage Tanks, and Corrosion Under Insulation, the licensee discovered

that procedures did not exist for air flow testing of deluges 3 and 4. Prior to transition to

NFPA 805, under 10 CFR 50, Appendix R, these deluges were not required to be air

flow tested at any point. Therefore, prior to April 17, 2014, fire suppression deluges

3 and 4 had never been air flow tested. The licensee determined that because no

physical impairment was apparent for the deluges, there existed a reasonable

expectation of functionality. The licensee declared the TSR 3.11.4.4 missed and

invoked TSR 3.0.3 to perform a risk assessment for the missed surveillance and

manage the risk impact until the next available window to air flow test the deluges.

14

In part, TSR 3.0.3 stated that, if it is discovered that a Surveillance was not performed

within its specified Frequency, then compliance with the requirement to declare the

TLCO not met may be delayed, from the time of discovery, up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or up to the

limit of the specified Frequency, whichever was greater. This delay period is permitted

to allow performance of the Surveillance. A risk evaluation shall be performed for any

Surveillance delayed greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and the risk impact shall be managed. On

May 9, 2014, the resident inspectors challenged the licensees use of TSR 3.0.3 to delay

the performance of air flow testing based on IMC 0326, Appendix A, Section A.03 that

stated, in part, Surveillance Requirement 3.0.3 may not be applied when a licensee

discovers that a Technical Specifications surveillance has never been performed. In

cases where a specified safety function or a necessary and related support function

required for operability has never been performed, then a reasonable expectation of

operability does not exist. Although the statement referred to the Technical

Specifications, the inspectors determined that the IMC 0326 statement also applied to

the TRM TSRs after discussions with the NRC Technical Specification Branch.

On May 29, 2014, the licensee directed that a Condition Evaluation be performed to

determine the use of TSR 3.0.3 and its appropriateness to the circumstances and further

directed that a functionality assessment be performed. On June 10, 2014, the licensees

Condition Evaluation confirmed that use of TSR 3.0.3 was not appropriate given

TSR 3.11.4.4 air flow testing for deluge systems 3 and 4 had never been performed

(i.e. not missed). The inspectors noted that TSR 3.0.1 stated, in part, that TSRs shall

be met during the MODES or other specified conditions in the Applicability for individual

TLCOs, unless otherwise stated in the TSR. Failure to meet a Surveillance, whether

such failure is experienced during the performance of the Surveillance or between

performances of the Surveillance, shall be failure to meet the TLCO. Failure to perform

a Surveillance within the specified Frequency shall be failure to meet the TLCO

expect as provided in TSR 3.0.3. On June 10, 2014, the licensee declared fire

suppression deluge systems 3 and 4 non-functional, entered TLCO 3.11.4, Condition A

and established hourly fire watches in the Reactor Feedwater Pump area. See

Section 4OA7 of this report that provides additional background information for a

Licensee-Identified Violation associated with this issue.

The issues were documented in CRs 01959153, 01964875, 01964878, 01968702,

01968720 and 01971501. Corrective actions included establishing procedures to air

flow test the systems and prompted changes to EN-AA-203-1001, Operability

Determinations/Functionality Assessments, to add clarification that a missed

surveillance is not the same as a surveillance that has never been performed. On

July 4, 2014, the licensee successfully tested, in accordance with the approved

procedures, and restored functionality of the automatic fire suppression deluge systems

3 and 4.

Analysis: The inspectors determined that the issue of concern represented a

performance deficiency because it was the result of the licensees failure to establish an

hourly fire patrol in accordance with TLCO 3.11.4 required action Condition A.2.

Specifically, on May 9, 2014, the inspectors raised the question about the licensee

invoking TSR 3.0.3 and performing a risk assessment associated with a system which

had never been tested before, where a reasonable expectation of functionality did not

exist. The performance deficiency was within the licensees ability to foresee and

correct and should have been prevented because the licensee had a process in place to

15

address the status of the deluge system 3 and 4 functionality through the Operability

Determination/Functionality Assessment procedure.

The performance deficiency was determined to be more than minor and a finding in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, because it impacted the Reactor Safety - Initiating Events Cornerstone of

Protection Against External Factors to limit the likelihood of events that upset plant

stability and challenge critical safety functions during shutdown as well as power

operations. The inspectors also determined that if left uncorrected, the performance

deficiency would have the potential to lead to a more significant safety concern.

The inspectors applied IMC 0609, Attachment 4, Initial Characterization of Findings, to

this finding. The inspectors answered Yes to question E.2(2), Does the finding involve

fixed fire protection systems or the ability to contain a fire within Table 3 - SDP Appendix

Router, and transitioned to IMC 0609, Appendix F, Fire Protection Significance

Determination Process. The inspectors processed the finding in accordance with Fire

Protection SDP Phase 1 Screening in IMC 0609, Appendix F, Attachment 1 and

answered Yes to Step 1.3, Task 1.3.1 question, Is the reactor able to reach and

maintain safe shutdown (either hot or cold) condition? Therefore, the finding screened

as very low safety significance (Green).

The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Consistent Process in the Human Performance area and

involving individuals using a consistent systematic approach to make decisions.

Specifically, the licensee did not systematically consider and apply the aforementioned

TRM statements and EN-AA-203-1001 procedure (which establishes a process

consistent with IMC 0326); in order to correctly assess the non-functional status of

deluges 3 and 4 upon discovery that TSR 3.11.4.4 was never performed. [H.13]

Enforcement: Duane Arnold Energy Center Renewed Operating License Condition

2.C.(3), Fire Protection Program, stated, in part that Duane Arnold shall implement

and maintain in effect all provisions of the approved fire protection program that comply

with 10 CFR 50.48(a) and 10 CFR 50.48(c). Fire protection program procedure

FP-AB-100, DAEC Fire Protection Program, section 3.4.4(3), stated in part, that for

NFPA 805 credited Fire Protection System and Features, TLCOs and compensatory

measures were prescribed by the TRM.

Contrary to the above, on April 17, 2014, the licensee failed to institute compensatory

measures for non-functional fire suppression deluge systems as required by

Duane Arnold Energy Center Renewed Operating License Condition 2.C.(3).

Specifically, the licensee did not establish an hourly fire patrol within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of

discovering the non-functional status of deluges 3 and 4 in accordance with TRM

TLCO 3.11.4, Fire Suppression Deluge and Sprinkler Systems, Condition A.2.

Because this violation was of very low safety significance and because the issue was

entered into the licensees CAP as CRs 01959153, 01964875, 01964878, 01968702,

01968720 and 01971501, consistent with Section 2.3.2 of the Enforcement Policy it is

being treated as a NCV. (NCV 05000331/2014003-02, Failure to Establish Fire

Patrols as Compensatory Actions in Accordance with the Fire Protection

Program).

16

1R18 Plant Modifications (71111.18)

a. Inspection Scope

The inspectors reviewed the following modification:

  • A Control Building Chiller (CBC) condenser head replacement following

discovery of internal surface pitting during PM.

The inspectors reviewed the configuration changes and associated 10 CFR 50.59 safety

evaluation screening against the design basis, the UFSAR, and the TS, as applicable, to

verify that the modification did not affect the operability or availability of the affected

system. The inspectors, as applicable, observed ongoing and completed work activities

to ensure that the modification was installed as directed and consistent with the design

control documents; the modification operated as expected; post-modification testing

adequately demonstrated continued system operability, availability, and reliability; and

that operation of the modification did not impact the operability of any interfacing

systems. As applicable, the inspectors verified that relevant procedure, design, and

licensing documents were properly updated. Lastly, the inspectors discussed the plant

modification with operations, engineering, and training personnel to ensure that the

individuals were aware of how the operation with the plant modification in place could

impact overall plant performance.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one modification sample as defined in IP 71111.18-05.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing (71111.19)

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities to verify that

procedures and test activities were adequate to ensure system operability and functional

capability:

  • A CBC testing following PM;
  • B SBDG testing following ventilation system PM; and

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion); and test

17

documentation was properly evaluated. The inspectors evaluated the activities against

TSs, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various

NRC generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted four post-maintenance testing samples as defined in

IP 71111.19-05.

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

  • Surveillance Test Procedure (STP) 3.0.0-01, Instrument Checks, Revision 142

reactor coolant system (RCS);

(Routine);

  • STP 3.5.3-02; RCIC System Operability Test, Revision 46 (Routine);
  • STP 3.5.1-01B; B Core Spray System Operability Test, Revision 15 (in-service

test (IST));

  • STP 3.3.1.1-13; Turbine Control Valve EOC RPT Logic & RPS Instrumentation

Functional Test, Revision 15 (Routine);

  • STP 3.5.1-02A; A LPCI System Operability Tests, Revision 14 (Routine); and
  • STP 3.5.1-03A; A Core Spray System Simulated Automatic Actuation,

Revision 9 (Routine).

The inspectors observed in-plant activities and reviewed procedures and associated

records to determine the following:

  • did preconditioning occur;
  • the effects of the testing were adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

  • acceptance criteria were clearly stated, demonstrated operational readiness, and

were consistent with the system design basis;

  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency was

in accordance with TSs, the UFSAR, procedures, and applicable commitments;

18

  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

  • test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

  • where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

  • where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

  • where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

  • prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

  • equipment was returned to a position or status required to support the

performance of its safety functions; and

  • all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

These inspections constituted five routine samples, one in-service test sample, and one

reactor coolant system leak detection surveillance testing inspection sample, as defined

in IP 71111.22, Sections-02 and-05.

b. Findings

No findings were identified.

2. RADIATION SAFETY

Cornerstones: Occupational and Public Radiation Safety

2RS5 Radiation Monitoring Instrumentation (71124.05)

This inspection constituted a partial sample as defined in IP 71124.05-05.

.1 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down effluent radiation monitoring systems, including at least one

liquid and one airborne system. Focus was placed on flow measurement devices and all

19

accessible point-of-discharge liquid and gaseous effluent monitors of the selected

systems. The inspectors assessed whether the effluent/process monitor configurations

aligned with Offsite Dose Calculation Manual (ODCM) descriptions and observed

monitors for degradation and out-of-service tags.

b. Findings

No findings were identified.

.2 Calibration and Testing Program (02.03)

Process and Effluent Monitors

a. Inspection Scope

The inspectors selected effluent monitor instruments (such as gaseous and liquid) and

evaluated whether channel calibration and functional tests were performed consistent

with radiological effluent TSs/ODCM. The inspectors assessed whether: (a) the

licensee calibrated its monitors with National Institute of Standards and Technology

traceable sources; (b) the primary calibrations adequately represented the plant nuclide

mix; (c) when secondary calibration sources were used, the sources were verified by the

primary calibration; and (d) the licensees channel calibrations encompassed the

instruments alarm set-points.

The inspectors assessed whether the effluent monitor alarm setpoints were established

as provided in the ODCM and station procedures.

For changes to effluent monitor setpoints, the inspectors evaluated the basis for

changes to ensure that an adequate justification existed.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06)

This inspection constituted one complete sample as defined in IP 71124.06-05.

.1 Inspection Planning and Program Reviews (02.01)

Event Report and Effluent Report Reviews

a. Inspection Scope

The inspectors reviewed the radiological effluent release reports issued since the last

inspection to determine if the reports were submitted as required by the ODCM/TSs.

The inspectors reviewed anomalous results, unexpected trends, or abnormal releases

identified by the licensee for further inspection to determine if they were evaluated, were

entered in the CAP, and were adequately resolved.

The inspectors selected radioactive effluent monitor operability issues reported by the

licensee as provided in effluent release reports, to review these issues during the onsite

20

inspection, as warranted, given their relative significance and determine if the issues

were entered into the CAP and adequately resolved.

b. Findings

No findings were identified.

Offsite Dose Calculation Manual and Final Safety Analysis Report Review

a. Inspection Scope

The inspectors reviewed UFSAR descriptions of the radioactive effluent monitoring

systems, treatment systems, and effluent flow paths so they could be evaluated during

inspection walkdowns.

The inspectors reviewed changes to the ODCM made by the licensee since the last

inspection against the guidance in NUREG-1302 and 0133, and Regulatory

Guides 1.109, 1.21, and 4.1. When differences were identified, the inspectors reviewed

the technical basis or evaluations of the change during the onsite inspection to

determine whether they were technically justified and maintain effluent releases as-low-

as-reasonably-achievable.

The inspectors reviewed licensee documentation to determine if the licensee has

identified any non-radioactive systems that have become contaminated as disclosed

either through an event report or the ODCM since the last inspection. This review

provided an intelligent sample list for the onsite inspection of any 10 CFR 50.59

evaluations and allowed a determination if any newly contaminated systems have an

unmonitored effluent discharge path to the environment, whether any required ODCM

revisions were made to incorporate these new pathways, and whether the associated

effluents were reported in accordance with Regulatory Guide 1.21.

b. Findings

No findings were identified.

Groundwater Protection Initiative Program

a. Inspection Scope

The inspectors reviewed reported groundwater monitoring results and changes to the

licensees written program for identifying and controlling contaminated spills/leaks to

groundwater.

b. Findings

No findings were identified.

Procedures, Special Reports, and Other Documents

a. Inspection Scope

The inspectors reviewed Licensee Event Reports, event reports and/or special reports

related to the Effluent Program issued since the previous inspection to identify any

21

additional focus areas for the inspection based on the scope/breadth of problems

described in these reports.

The inspectors reviewed Effluent Program implementing procedures, particularly those

associated with effluent sampling, effluent monitor set-point determinations, and dose

calculations.

The inspectors reviewed copies of licensee and third party (independent) evaluation

reports of the Effluent Monitoring Program since the last inspection to gather insights

into the licensees program and aid in selecting areas for inspection review (smart

sampling).

b. Findings

No findings were identified.

.2 Walkdowns and Observations (02.02)

a. Inspection Scope

The inspectors walked down selected components of the gaseous and liquid discharge

systems to evaluate whether equipment configuration and flow paths align with the

documents reviewed in Section 02.01 above and to assess equipment material

condition. Special attention was made to identify potential unmonitored release points

(such as open roof vents in boiling water reactor turbine decks, temporary structures

butted against turbine, auxiliary or containment buildings), building alterations which

could impact airborne, or liquid effluent controls, and ventilation system leakage that

communicates directly with the environment.

For equipment or areas associated with the systems selected for review that were not

readily accessible due to radiological conditions, the inspectors reviewed the licensee's

material condition surveillance records, as applicable.

The inspectors walked down filtered ventilation systems to assess for conditions such as

degraded high-efficiency particulate air/charcoal banks, improper alignment, or system

installation issues that would impact the performance or the effluent monitoring capability

of the effluent system.

As available, the inspectors observed selected portions of the routine processing and

discharge of radioactive gaseous effluent (including sample collection and analysis) to

evaluate whether appropriate treatment equipment was used and the processing

activities align with discharge permits.

The inspectors determined if the licensee has made significant changes to their effluent

release points (e.g., changes subject to a 10 CFR 50.59 review or require NRC approval

of alternate discharge points).

As available, the inspectors observed selected portions of the routine processing and

discharging of liquid waste (including sample collection and analysis) to determine if

appropriate effluent treatment equipment is being used and that radioactive liquid waste

is being processed and discharged in accordance with procedure requirements and

aligns with discharge permits.

22

b. Findings

No findings were identified.

.3 Sampling and Analyses (02.03)

a. Inspection Scope

The inspectors selected effluent sampling activities, consistent with smart sampling, and

assessed whether adequate controls have been implemented to ensure representative

samples were obtained (e.g. provisions for sample line flushing, vessel recirculation,

composite samplers, etc.).

The inspectors selected effluent discharges made with inoperable (declared

out-of-service) effluent radiation monitors to assess whether controls were in place

to ensure compensatory sampling was performed consistent with the radiological

effluent TSs/ODCM and that those controls were adequate to prevent the release of

unmonitored liquid and gaseous effluents.

The inspectors determined whether the facility was routinely relying on the use of

compensatory sampling in lieu of adequate system maintenance, based on the

frequency of compensatory sampling since the last inspection.

The inspectors reviewed the results of the Inter-Laboratory Comparison Program to

evaluate the quality of the radioactive effluent sample analyses and assessed whether

the Inter-Laboratory Comparison Program includes hard-to-detect isotopes, as

appropriate.

b. Findings

No findings were identified.

.4 Instrumentation and Equipment (02.04)

Effluent Flow Measuring Instruments

a. Inspection Scope

The inspectors reviewed the methodology the licensee uses to determine the effluent

stack and vent flow rates to determine if the flow rates were consistent with radiological

effluent TS/ODCM UFSAR values, and that differences between assumed and actual

stack and vent flow rates did not affect the results of the projected public doses.

b. Findings

No findings were identified.

Air Cleaning Systems

a. Inspection Scope

The inspectors assessed whether surveillance test results since the previous inspection

for TS required ventilation effluent discharge systems (high-efficiency particulate air and

23

charcoal filtration), such as the standby gas treatment system and the

containment/auxiliary building ventilation system, met TS acceptance criteria.

b. Findings

No findings were identified.

.5 Dose Calculations (02.05)

a. Inspection Scope

The inspectors reviewed all significant changes in reported dose values compared to the

previous radiological effluent release report (e.g., a factor of 5, or increases that

approach Appendix I criteria) to evaluate the factors which may have resulted in the

change.

The inspectors reviewed radioactive liquid and gaseous waste discharge permits to

assess whether the projected doses to members of the public were accurate and based

on representative samples of the discharge path.

The inspectors evaluated the methods used to determine the isotopes that are included

in the source term to ensure all applicable radionuclides are included within detectability

standards. The review included the current Part 61 analyses to ensure hard-to-detect

radionuclides are included in the source term.

The inspectors reviewed changes in the licensees offsite dose calculations since the

last inspection to evaluate whether changes were consistent with the ODCM and

Regulatory Guide 1.109. The inspectors reviewed meteorological dispersion and

deposition factors used in the ODCM and effluent dose calculations to evaluate whether

appropriate factors were being used for public dose calculations.

The inspectors reviewed the latest Land Use Census to assess whether changes

(e.g., significant increases or decreases to population in the plant environs, changes

in critical exposure pathways, the location of nearest member of the public or critical

receptor, etc.) have been factored into the dose calculations.

For the releases reviewed above, the inspectors evaluated whether the calculated doses

(monthly, quarterly, and annual dose) are within the 10 CFR Part 50, Appendix I, and TS

dose criteria.

The inspectors reviewed, as available, records of any abnormal gaseous or liquid tank

discharges (e.g., discharges resulting from misaligned valves, valve leak-by, etc.) to

ensure the abnormal discharge was monitored by the discharge point effluent monitor.

Discharges made with inoperable effluent radiation monitors, or unmonitored leakages,

were reviewed to ensure that an evaluation was made of the discharge to satisfy

10 CFR 20.1501 so as to account for the source term and projected doses to the public.

b. Findings

No findings were identified.

24

.6 Groundwater Protection Initiative Implementation (02.06)

a. Inspection Scope

The inspectors reviewed monitoring results of the Groundwater Protection Initiative to

determine if the licensee implemented its program as intended and to identify any

anomalous results. For anomalous results or missed samples, the inspectors assessed

whether the licensee identified and addressed deficiencies through its CAP.

The inspectors reviewed identified leakage or spill events and entries made into

10 CFR 50.75 (g) records. The inspectors reviewed evaluations of leaks or spills and

reviewed any remediation actions taken for effectiveness. The inspectors reviewed

onsite contamination events involving contamination of ground water and assessed

whether the source of the leak or spill was identified and mitigated.

  • On October 11, 2012, approximately 200 to 700 gallons of radioactively

contaminated water leaked to the ground from the Condensate Storage Tank pit

through a failed seal. The inspectors reviewed the licensees notification to the NRC

(Event No. 48403), the licensees ground water monitoring program, completed

remediation, as well as the licensees plan to install additional sample wells for better

characterization of the spill.

For unmonitored spills, leaks, or unexpected liquid or gaseous discharges, the

inspectors assessed whether an evaluation was performed to determine the type and

amount of radioactive material that was discharged by:

  • Assessing whether sufficient radiological surveys were performed to evaluate the

extent of the contamination and the radiological source term and assessing whether

a survey/evaluation had been performed to include consideration of hard-to-detect

radionuclides.

  • Determining whether the licensee completed offsite notifications, as provided in its

Groundwater Protection Initiative implementing procedures.

The inspectors reviewed the evaluation of discharges from onsite surface water bodies

that contain or potentially contain radioactivity and the potential for ground water leakage

from these onsite surface water bodies. The inspectors assessed whether the licensee

was properly accounting for discharges from these surface water bodies as part of their

effluent release reports.

The inspectors assessed whether on-site ground water sample results and a description

of any significant on-site leaks/spills into ground water for each calendar year were

documented in the Annual Radiological Environmental Operating Report for the

Radiological Environmental Monitoring Program or the Annual Radiological Effluent

Release Report for the Radiological Effluent TSs.

For significant, new effluent discharge points (such as significant or continuing leakage

to ground water that continues to impact the environment, if not remediated), the

inspectors evaluated whether the ODCM was updated to include the new release points.

25

b. Findings

No findings were identified.

.7 Problem Identification and Resolution (02.07)

a. Inspection Scope

The inspectors assessed whether problems associated with the Effluent Monitoring and

Control Program were being identified by the licensee at an appropriate threshold and

were properly addressed for resolution in the licensees CAP. In addition, they

evaluated the appropriateness of the corrective actions for a selected sample of

problems documented by the licensee involving radiation monitoring and exposure

controls.

b. Findings

No findings were identified.

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Physical Protection

4OA1 Performance Indicator (PI) Verification (71151)

.1 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage performance indicator

for the period from the second quarter 2013 through the first quarter 2014. To determine

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the Nuclear Energy Institute Document 99-02, Regulatory Assessment

Performance Indicator Guideline, Revision 7, dated August 31, 2013, were used. The

inspectors reviewed the licensees operator logs, RCS leakage tracking data, issue

reports, event reports and NRC Integrated Inspection Reports for the period of

April, 2013 through March, 2014, to validate the accuracy of the submittals. The

inspectors also reviewed the licensees issue report database to determine if any

problems had been identified with the PI data collected or transmitted for this indicator

and none were identified. Documents reviewed are listed in the Attachment to this

report.

This inspection constituted one reactor coolant system leakage sample as defined in

IP 71151-05.

b. Findings

No findings were identified.

26

.2 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors reviewed licensee submittals for the Occupational Exposure Control

Effectiveness Performance Indicator for the fourth quarter 2013. The inspectors used PI

definitions and guidance contained in the Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline, Revision 7, dated

August 2013, to determine the accuracy of the Performance Indicator data reported

during those periods. The inspectors reviewed the licensees assessment of the

Performance Indicator for occupational radiation safety to determine if the indicator-

related data was adequately assessed and reported. To assess the adequacy of the

licensees Performance Indicator data collection and analyses, the inspectors discussed

with radiation protection staff the scope and breadth of its data review and the results of

those reviews. Documents reviewed are listed in the Attachment to this report.

The inspectors reviewed a licensee-identified issue that occurred on October 8, 2013,

and was documented as a licensee-identified NCV of TS 5.7.2 in NRC Inspection Report 05000331/2013005. The licensee previously did not report this as a PI occurrence.

Upon discussion with the licensee, the licensee has determined that the issue was an

occurrence of the Occupational Exposure Control Effectiveness PI in accordance

with Nuclear Energy Institute Document 99-02. This licensee has entered this issue into

their CAP as CR 01971250. This will result in the change for this PI from zero to one

occurrence. This change will not result in a change in regulatory significance to this PI.

This inspection constituted a partial occupational exposure control effectiveness sample

as defined in IP 71151-05.

b. Findings

No findings were identified.

However, the inspectors identified a minor violation of 10 CFR 50.9 Completeness and

Accuracy of information for one occurrence that was not reported. Specifically, the

Occupational Exposure Controls Effectiveness PI occurrence on October 8, 2013 was

not initially reported and then not corrected when NRC issued IR 2013-005 as discussed

above. Because this results in the change for this PI from zero to one occurrence, and

does not result in a change in regulatory significance of this PI, this is considered a

minor violation.

4OA2 Identification and Resolution of Problems (71152)

.1 Routine Review of Items Entered into the Corrective Action Program

a. Inspection Scope

As part of the various baseline inspection procedures discussed in previous sections of

this report, the inspectors routinely reviewed issues during baseline inspection activities

and plant status reviews to verify they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: identification of the problem was complete and accurate; timeliness was

27

commensurate with the safety significance; evaluation and disposition of performance

issues, generic implications, common causes, contributing factors, root causes, extent-

of-condition reviews, and previous occurrences reviews were proper and adequate; and

that the classification, prioritization, focus, and timeliness of corrective actions were

commensurate with safety and sufficient to prevent recurrence of the issue. Documents

reviewed are listed in the Attachment to this report.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings were identified.

.2 Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily condition report packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

The inspectors performed a review of the licensees CAP and associated documents to

identify trends that could indicate the existence of a more significant safety issue. The

inspectors review was focused on repetitive equipment issues, but also considered the

results of daily inspector CAP item screening discussed in Section 4OA2.2 above,

licensee trending efforts, and licensee human performance results. The inspectors

review nominally considered the 6-month period of January 2014 through June 2014,

although some examples expanded beyond those dates where the scope of the trend

warranted.

The review also included issues documented outside the normal CAP in major

equipment problem lists, repetitive and/or rework maintenance lists, departmental

problem/challenges lists, system health reports, quality assurance audit/surveillance

reports, self-assessment reports, and Maintenance Rule assessments. The inspectors

compared and contrasted their results with the results contained in the licensees

28

CAP trending reports. Corrective actions associated with a sample of the issues

identified in the licensees trending reports were reviewed for adequacy.

This inspection constituted one semi-annual trend inspection sample as defined in

IP 71152-05.

b. Findings

No findings were identified.

.4 Annual Sample: Review of Operator Workarounds

a. Inspection Scope

The inspectors evaluated the licensees implementation of their process used to identify,

document, track, and resolve operational challenges. Inspection activities included, but

were not limited to, a review of the cumulative effects of the operator workarounds on

system availability and the potential for improper operation of the system, for potential

impacts on multiple systems, and on the ability of operators to respond to plant

transients or accidents.

The inspectors performed a review of the cumulative effects of operator workarounds.

The documents listed in the Attachment to this report were reviewed to accomplish the

objectives of the inspection procedure. The inspectors reviewed both current and

historical operational challenge records to determine whether the licensee was

identifying operator challenges at an appropriate threshold, had entered them into their

CAP and proposed or implemented appropriate and timely corrective actions which

addressed each issue. Reviews were conducted to determine if any operator challenge

could increase the possibility of an Initiating Event, if the challenge was contrary to

training, required a change from long-standing operational practices, or created the

potential for inappropriate compensatory actions. Additionally, all temporary

modifications were reviewed to identify any potential effect on the functionality of

Mitigating Systems, impaired access to equipment, or required equipment uses for which

the equipment was not designed. Daily plant and equipment status logs, degraded

instrument logs, and operator aids or tools being used to compensate for material

deficiencies were also assessed to identify any potential sources of unidentified operator

workarounds.

These inspections constituted one operator workaround annual inspection sample as

defined in IP 71152-05.

b. Findings

.5 Selected Issue Follow-Up Inspection: Standby Transformer Relay Root Cause

Evaluation

a. Inspection Scope

The inspectors reviewed Root Cause Evaluation (RCE) 01934040, Under-voltage Relay

Failed, associated with the January 17, 2014, surveillance test failure of Standby

Transformer under-voltage relay 127-SB2. The inspectors assessed whether the

licensees determination of the root and contributing causes, corrective actions, and

29

effectiveness measures were appropriate. The finding below describes a finding and

violation identified by the inspectors during their review.

This inspection constituted one in-depth problem identification and resolution sample as

defined in IP 71152-05.

b. Findings

(1) Failure to Prescribe Work Order Planning Procedure Appropriate to the Circumstances

Introduction: The inspectors identified a finding of very low safety significance (Green)

and associated NCV of 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, for the failure to prescribe a procedure appropriate to the circumstances

for work order planning as related to the failure of under-voltage relay 127-SB2.

Specifically, procedure MA-AA-203-1001, Work Order Planning, Section 4.2, Step 2,

inappropriately allowed the selection of model work orders without verification of the

acceptance criteria, requirements for as-found/as-left data, set points, and other related

information.

Description: On January 17, 2014, the licensee performed STP 3.3.8.1-05B, 1A4 4KV

Emergency Transformer Supply Under-Voltage Calibration. During performance of the

STP, two trip circuit contacts on Standby Transformer supply under-voltage relay

127-SB2 did not open as expected. Upon further investigation, the licensee discovered

that the 11-12 and 13-14 127-SB2 contacts had been configured incorrectly. The

contacts were arranged in series with a third contact 19-20, such that upon a reduction

of supply voltage, two contacts would open, but one contact remained closed and would

have prevented the relay trip signal from tripping the Standby Transformer supply

breaker when voltage reduced to less than 2450 Volts. The function of the 127-SB2

relay was to sense a loss of offsite power, open the Standby Transformer supply

breaker, and provide a permissive signal to the 1A4 4KV essential bus to allow the bus

to be reenergized by the B SBDG. The contact configuration was such that this

function would have been inhibited had it been called upon.

Technical Specification 3.3.8.1, Loss of Power Instrumentation, required in part,

relay 127-SB2 to be operable in Modes 1, 2 and 3. The failed STP on January 17, 2014,

demonstrated that the 127-SB2 relay was inoperable and the required action to satisfy

the TS was to place the channel in trip within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of discovery (Condition A.1) and if

that was not achieved, declare the associated SBDG inoperable immediately

(Condition C.1). Upon the discovery of the inoperable relay, the licensee declared the

B SBDG inoperable to comply with LCO 3.3.8.1, Condition C.1. The licensee

documented the issue in CR 01934040 and performed a POR. The prompt operability

review (POR) noted that relay 127-SB2 had been replaced on September 16, 2013, as

part of WO 40126852. Further review noted that no in-field, post-installation functional

testing had been performed or identified as part of the WO instructions. Therefore, relay

127-SB2 had been inoperable from September 16, 2013, to January 17, 2014, or 120

days. During this timeframe, the relay miss-configuration had gone unrecognized and

the TS required actions unfulfilled, resulting in the licensee operating in a condition

prohibited by Technical Specifications. The event was reported by the licensee as

Licensee Event Report (LER) 2014-001-00 and 2014-001-01 in accordance with

10 CFR 50.73(a)(2)(i)(B). See Section 4OA3.1 in reference to the above mentioned

LERs and Section 4OA7 for an associated licensee-identified violation.

30

As part of the event analysis called out by CR 01934040, the licensee performed an

RCE in accordance with procedure PI-AA-100-1005, Root Cause Analysis, Revision 9.

The RCE identified two root causes and two contributing causes. The first root cause

was that existing procedural guidance was inadequate to correctly setup the relay per

procedure RELAY-080-08, General Electric Under-Voltage Relay Type NGV,

Revision 10, which WO 40126852 referenced for calibration of relay 127-SB2. The

licensee determined that RELAY-080-08 did not define set-point criteria and relay

configuration. The corrective action to prevent recurrence was to make changes to

RELAY-080-08 to state that when a relay or contact is replaced, the configuration of the

relay or contact shall match the installed relay and applicable drawings. Furthermore,

the procedure was changed to record allowable dropout voltage as specified in

applicable drawings and that a maintenance supervisor or engineer shall verify the

correct set-point information.

The second root cause was that existing procedural guidance was inadequate to

correctly test the relay per procedure MD-024, Post Maintenance Testing Program,

Revision 23, that stated calibration alone was an adequate post maintenance test for

protective relays. The corrective action to prevent recurrence was to modify procedure

MD-024 to require at a minimum, return to service testing of TS-required equipment to

ensure that functionality and operability requirements are met.

The resident inspectors reviewed the RCE and found the licensees root and contributing

causes, as well as the corrective actions, appropriate to the circumstances with one

exception. A contributing cause was identified by the licensee associated with WO

planning being inadequate to identify relay configuration and acceptance criteria. The

licensees corrective action to address this contributing cause was to provide a briefing

to WO planners that procedure MA-AA-203-1001, Section 4.2 stated, in part that

acceptance criteria, requirements for as-found/as-left data, set points, and other related

information must be copied verbatim from the controlled procedure, and that if that

requirement was not going to be conducted, the expectation was that the requirements

were verified to ensure that the information was in fact contained in the procedure being

referenced. Procedure PI-AA-100-1005, Section 4.10, Step 2 stated in part, that

corrective actions should be specific and address each root and contributing cause.

Further, Section 4.10, Step 3 stated, in part that all corrective actions shall be consistent

with the SMART approach - (Specific, Measurable, Achievable, Relevant, and Timely)

(refer to PI-AA-205). Per procedure PI-AA-205, Condition Evaluation and Corrective

Action, Revision 25, a Relevant corrective action is one in which the action is aligned

with the issue that it is intended to resolve and will correct the problem.

The inspectors questioned the licensees corrective action to provide a briefing of

expectations to WO planners given the apparent procedural weakness in

MA-AA-203-1001. Specifically, Section 4.2 of MA-AA-203-1001 provided WO planners

with several options/steps that could be used to create work task instructions. The

corrective action to address the contributing cause only addressed Option/Step 3 in

Section 4.2 but made no reference to Option/Step 2 which stated that Controlled

procedures may be referenced in the work task instructions and included in the work

order package. The inspectors were concerned that using Option 2, as it existed, did

not ensure that WO planners verify the controlled document referenced contained the

appropriate acceptance criteria, as-found/as-left data, set points, and other related

information relevant to the circumstances.

31

The existing procedural error-trap that was not addressed as part of the RCE

contributing cause corrective action was documented in CRs 01972812 and 01972807.

Condition Report 01972807 specifically added a verification step as part of procedure

MA-AA-203-1001, Section 4.2, Step 2, to verify the procedure being referenced

contained the relevant information to the work task being accomplished.

Analysis: The inspectors determined that the issue of concern represented a

performance deficiency because it was the result of the licensees failure to prescribe a

procedure appropriate for the circumstances. Specifically, on June 18, 2014, procedure

MA-AA-203-1001, Work Order Planning, Section 4.2, Step 2, inappropriately allowed

the selection of model work orders without verification of the acceptance criteria,

requirements for as-found/as-left data, set points, and other related information. The

performance deficiency was within the licensees ability to foresee and correct and

should have been prevented because the licensee had a process in place to

appropriately identify, evaluate and correct issues noted as part of the Root Cause

Evaluation process.

The performance deficiency was determined to be more than minor and a finding in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Screening, because if left uncorrected, the performance deficiency would have the

potential to lead to a more significant safety concern. Specifically, MA-AA-203-1001 was

deficient, in that a WO planner could select a model work order without a required

verification of the work objectives to ensure correct equipment configuration and

functional testing was performed.

The inspectors applied IMC 0609, Attachment 4, Initial Characterization of Findings, to

this finding. The inspectors answered No to all questions within Table 3 - SDP

Appendix Router, and transitioned to IMC 0609, Appendix A, The Significance

Determination Process for Findings At-Power. Per Exhibit 2 - Mitigating Systems

Screening Questions, the inspectors determined that because the finding did not

represent an actual loss of function (redundant loss of power instrumentation remained

operable during the period of the 127-SB2 inoperability), the finding screened as very

low safety significance (Green).

The inspectors determined that the performance characteristic of the finding that was the

most significant causal factor of the performance deficiency was associated with the

cross-cutting aspect of Evaluation in the Problem Identification and Resolution area and

involved the organization thoroughly evaluating issues to ensure that resolutions

address causes and extent of conditions commensurate with their safety significance.

Specifically, the licensee correctly identified the need to ensure work orders either

contained appropriate acceptance criteria, as-found/as-left data, set points, and other

related information relevant to the circumstances, but failed to fully evaluate the

adequacy of the contributing cause corrective action and its applicability to the work

order planning procedure as a whole.

Enforcement: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures,

and Drawings, requires in part, that activities affecting quality shall be prescribed by

documented procedures of a type appropriate to the circumstances.

Contrary to the above, on June 18, 2014, the licensee failed to prescribe a work order

planning procedure appropriate for the circumstances. Specifically, procedure

MA-AA-203-1001, Work Order Planning, Revision 1, was not appropriate in that it did

32

not ensure that appropriate configuration and testing criteria were verified prior to

developing work orders.

Because this violation was of very low safety significance and because the issue was

entered into the licensees CAP as CRs 01972812 and 01972807, consistent with

Section 2.3.2 of the Enforcement Policy it is being treated as a NCV.

(NCV 05000331/2014003-03, Failure to Prescribe Work Order Planning Procedure

Appropriate to the Circumstances).

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000331/2014-001-00 and 05000331/2014-001-01:

Condition Prohibited by Technical Specifications - Past Inoperability of Standby

Transformer Under-Voltage Relay

This event, which occurred on January 17, 2014, involved the Standby Transformer

under-voltage relay 127-SB2 which was found inoperable during surveillance testing and

was inoperable since it was replaced on September 16, 2013. See Section 4OA2.5

above for a detailed description of the event and an associated NRC-identified NCV.

The inspectors reviewed LERs05000331/2014001-00 and 05000331/2014001-01

against reporting requirements and found no issues. A licensee-identified violation

associated with this event and the enforcement aspects are discussed in Section 4OA7

below. Documents reviewed are listed in the Attachment to this report. These LERs are

closed.

This inspection constituted one event follow-up sample as defined in IP 71153-05.

4OA6 Management Meetings

.1 Exit Meeting Summary

On July 21, 2014, the inspectors presented the inspection results to Mr. G. Pry, Plant

General Manager, and other members of the licensee staff. The licensee acknowledged

the issues presented. The inspectors confirmed that none of the potential report input

discussed was considered proprietary.

.2 Interim Exit Meetings

An interim exit was conducted for the inspection results for the areas of radiation

monitoring instrumentation, radioactive gaseous and liquid effluent treatment, and

occupational exposure control effectiveness performance indicator verification with

Mr. R. Anderson, Site Vice President, on June 13, 2014. The inspectors confirmed that

none of the potential report input discussed was considered proprietary.

4OA7 Licensee-Identified Violations

The following violations of very low significance (Green) were identified by the licensee

and are violations of NRC requirements which meet the criteria of the NRC Enforcement

Policy for being dispositioned as NCVs.

  • Duane Arnold Energy Center Renewed Operating License Condition 2.C.(3),

Fire Protection Program, stated, in part that Duane Arnold shall implement and

33

maintain in effect all provisions of the approved fire protection program that

comply with 10 CFR 50.48(a) and 10 CFR 50.48(c).

Contrary to the above, on March 6, 2014, the licensee transitioned their fire

protection program to NFPA 805 without having tested or having procedures to

test fire suppression deluge systems 3 and 4. Specifically, procedure

FP-AB-100, DAEC Fire Protection Program, Section 3.4.4, stated in part that,

NFPA 805, Section 3.2.3(1) provides the requirements for establishing

procedures that address inspection, testing and maintenance for fire protection

systems and features credited by NFPA 805. Section 3.4.4(2), stated in part

that, fire protection systems are periodically inspected and tested in accordance

with established procedures recommended by equipment manufacturers or by

nationally recognized organizations such as the NFPA. Procedure

FP-AA-04-1000, Fire Protection Maintenance, Testing, Impairment and

Compensatory Actions, Section 4.2.1.1, stated in part that, procedures shall be

established for any testing on fire protection systems, equipment and features.

Section 1R15.1 above provides additional background description for this

licensee-identified violation. The inspectors determined the finding could be

evaluated using the SDP in accordance with IMC 0609, Significance

Determination Process, Attachment 0609.04, Initial Characterization of

Findings, Table 3 - SDP Appendix Router and IMC 0609, Appendix F,

Attachment 1, Fire Protection Significance Determination Process Phase 1

Worksheet. Because the inspectors answered Yes to the Step 1.3, Task 1.3.1

question Is the reactor able to reach and maintain safe shutdown (either hot or

cold) condition? the finding screened as very low safety significance (Green).

The licensee documented the issue in CR 01959153; created appropriate testing

procedures to demonstrate deluge 3 and 4 functionality, and satisfactorily air flow

tested the deluge systems in accordance with approved procedures.

that if any 4.16 kV emergency bus under-voltage (degraded voltage) channel

was inoperable, that the associated Diesel Generator (DG) be declared

inoperable within one hour from discovery of loss of initiation capability for

feature(s) in one or both divisions as well as placing the channel in trip within

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Contrary to the above on September 19, 2013, the licensee failed to declare the

B DG inoperable and entered a condition prohibited by TSs. Specifically,

WO 40126852 was completed to replace relay 127-SB2, 1A4 4KV Emergency

Transformer Supply Under-voltage, due to dirty contacts. However, 127-SB2

was returned to service without post maintenance testing appropriate to the

circumstances. This resulted in 127-SB2 being in an inoperable status when the

required action to declare the B DG inoperable within one hour was not

accomplished. Section 4OA2.5 above provides additional background

description for this licensee-identified violation. The licensee documented the

conditions prohibited by TSs for relay 127-SB2 in CRs 01934167 and 01934040.

The inspectors determined the finding could be evaluated using the SDP in

accordance with IMC 0609, Significance Determination Process, Attachment

0609.04, Initial Characterization of Findings, Table 3 - Appendix Router and

IMC 0609 Appendix A, The Significance Determination Process for Findings At

Power, Exhibit 2 - Mitigating Systems Screening Questions. Because the

34

inspectors answered No to all questions in Section A, the finding screened as

very low safety significance (Green). Section 4OA2.5 describes the corrective

actions taken by the licensee.

ATTACHMENT: SUPPLEMENTAL INFORMATION

35

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

R. Anderson, Site Vice President

G. Pry, Plant General Manager

K. Kleinheinz, Site Engineering Director

W. Bentley, Maintenance Director

M. Davis, Emergency Preparedness and Licensing Manager

K. Peveler, Nuclear Oversight Manager

R. Wheaton, Operations Director

R. Porter, Radiation Protection Manager

D. Olsen, Chemistry Manager

J. Schwertfeger, Security Manager

C. Hill, Training Manager

B. Murrell, Licensing Engineer Analyst

L. Swenzinski, Licensing Engineer

C. Casey, Chemistry Supervisor

Nuclear Regulatory Commission

C. Lipa, Chief, Reactor Projects Branch 1

M. Chawla, Project Manager, NRR

Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000331/2014003-01 NCV Failure to Accomplish Procedure for Repetitive Malfunctions

of Refuel Floor Radiation Monitor (Section 1R12.1)05000331/2014003-02 NCV Failure to Establish Fire Patrols as Compensatory Actions in

Accordance with the Fire Protection Program

(Section 1R15.1)05000331/2014003-03 NCV Failure to Prescribe Work Order Planning Procedure

Appropriate to the Circumstances (Section 4OA2.5)

Closed

05000331/2014003-01 NCV Failure to Accomplish Procedure for Repetitive Malfunctions

of Refuel Floor Radiation Monitor (Section 1R12.1)05000331/2014003-02 NCV Failure to Establish Fire Patrols as Compensatory Actions in

Accordance with the Fire Protection Program

(Section 1R15.1)05000331/2014003-03 NCV Failure to Prescribe Work Order Planning Procedure

Appropriate to the Circumstances (Section 4OA2.5)

05000331/2014-001-00; LER Condition Prohibited by Technical Specifications - Past

-01 Inoperability of Standby Transformer Under-Voltage Relay

(Section 4OA3.1)

Discussed

None

2

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather Protection

AOP 903; Severe Weather; Revision 39

OP-AA-102-1002; Seasonal Readiness; Revision 4

AOP 410; Loss of River Water Supply/High River Bed Elevation/Low River Water Depth;

Revision 27

AOP 902; Flood; Revision 51

Condition Evaluation (CE) 01942883-01; Inventory of Flood Materials per WO 40249718-01 and

AOP 902

CE 01957698-01; Conduct a Rework Evaluation for Rainwater Leaking into the RCIC Room

Through Hatch

CR 01942883; Inventory of Flood Material per WO 40249718-01 and AOP 902

CR 01949252; Frequency Based PM Needed for Flooding Preps

CR 01957698; Rainwater Leaking into RCIC Room Through Hatch

CR 01963290; Storm Drain Entrance Almost Completely Blocked by Gravel

CR 01969659; Doors, Bottom Seal Improvements Mitigate Potential Water Intrusion

CR 01969674; Flood/Conduit Seals Capability for Flood Protection

CR 01969689; Conduit Internal Seal Inspections/Flood Inspections

CR 01972529; Water Found in MH107 Following Storm/Heavy Rain

CR 01972989; Water Intrusion into Various Reactor Building and Essential Switchgear Room

CR 01973136; Initiate Work Order to Seal Penetration - AOP 902

CR 01973155; Initiate Work Order to Relocate Gasoline/Diesel Storage Tanks - AOP 902

CR 01973261; Rain Water Entering CSC Building during Severe Weather

CR 01973305; AOP 902 Flood Entry Due to Cedar River Water Level

CR 01973311; Safety CR Rain Water Intrusion at Cable Spreading Room Door

CR 01973646; Water Intrusion into Refuel Floor and RCIC Room

POD 01957698-01; Rainwater Leaking into RCIC Room through Hatch; Revision 0

1R04 Equipment Alignment

Operating Instruction (OI) 710, Intake Structure HVAC System, Revision 14

DCR985A; Intake Structure Air Compressors

DCR985B; Power Separation for Instrument Air Compressors

OI 255A2; Control Rod Drive System Valve Lineup and Checklist; Revision 5

OP-AA-102-1003; Guarded Equipment; Revision 5

OI 255A2; Control Rod Drive System Valve Lineup and Checklist; Revision 5

OI 710; Intake Structure HVAC System; Revision 14

OI 730A1; Control Building HVAC System Electrical Lineup; Revision 3

OI 730A4; Plant Chilled Water System Valve Lineup; Revision 17

OI 730A6; Control Building HVAC System Control Panel Lineup; Revision 9

BECH-M161; P&ID Air Conditioning System Control Building; Revision 53

BECH-M169<2>; P&ID Control Building Cooling System; Revision 22

BECH-M169<3>; P&ID Control Building Chillers 1VCH001A and 1VCH001B; Revision 13

3

DCR985A; Intake Structure Air Compressors

DCR985B; Power Separation for Instrument Air Compressors

1R05 Fire Protection

STP NS13B005; WK3-Portable Fire Extinguishing Equipment Inspection

STP NS13B005; Portable Fire Extinguishing Equipment

CR 01974458; Violation of Fire Hazards Analysis for Fire Zone OAG

CR 01974441; Violation of Administrative Control Procedure (ACP) 1412.2, Control of

Combustibles

CR 01974230; Poor Housekeeping in the Turbine Building Exhaust Fan Penthouse

FHA-200; NFPA 805 Fire Protection Design Document; Revision 16

FHA-400; Duane Arnold Energy Center Fire Protection Program; Revision 14

FP-AB-100; Fire Protection Program; Revision 0

ACP 1412.2; Control of Combustibles; Revision 41

ACP 1412.4; Impairments to Fire Protection Systems; Revision 69

PFP-RB-757; Pre-Fire Plan Reactor Building El. 757; Revision 0

PFP-RB-812; Pre-Fire Plan Reactor Building El. 812; Revision 0

PFP-RB-828; Pre-Fire Plan Reactor Building El. 828; Revision 1

PFP-RB-855; Pre-Fire Plan Reactor Building El. 855; Revision 1

PFP-TB-780; Pre-Fire Plan Turbine Building El. 780; Revision 0

STP NS13F006; Structural Steel Fireproofing Inspection; Revision 17

STP NS13B005; WK3-Portable Fire Extinguishing Equipment Inspection

STP NS13B005; Portable Fire Extinguishing Equipment

CR 01964471; Deluge #2 Leak Getting Worse

CR 01966499; Missing Items During Fire Brigade Inventory

CR 01966736; Leakage on Primary Line Upstream of Isolation

CR 01966799; HPCI Deluge #2 FPR-14-7114

1R06 Flooding

ECPM SECT 4.4; Electrical Manhole Inspection Frequency; Revision 1

WO 40308721; SUS99.09 Inspect Manholes MH104, MH105, MH106 and MH107

BECH-E350<1>; Underground Duct Bank Layout; Revision 7

BECH-E351<1>; Manhole Details; Revision 2

CR 01965875; Manhole MH104, MH105; MH106, MH107 Inspect Results May 14, 2014

CR 01966371; DNA - CAS Operator Observed Water Flowing From Manhole

CR 01972529; Water Found in MH107 Following Storm/Heavy Rain

CR 01974836; Run Boroscope through Conduit Y156A to Check for Obstruction

1R11 Licensed Operator Requalification Program

OP-020; Area Inspections; Revision 26

Reactivity Management Plan; Downpower for Control Rod Sequence Exchange; May 2014

CE 01967067; Tar-Like Substance Found on Floor of the Condenser Bay; Revision 1

CR 01967056; CV1097A Has a 5-10 DPM Packing Leak

CR 01967057; V03-0245 LS-1070A Lower Isolation Packing Leak

CR 01967058; CV1064 in Steam Tunnel Has 10-15 DPM Leak from Packing

CR 01967067; Identified Abnormal Leakage on Condenser Bay Floor

4

1R12 Maintenance Effectiveness

CR 01943118; 1K016A Intake Air Compressor Tripped Again

CR 01944636; TC7715A Leaking Air

CR 01944627; 1VT050A Excessive Leakage

CR 01944750; 1K016A Failed Once Again

CR 01952071; Air Leak Past Fitting Upstream of Check Valve V77-0019

CR 01960690; 1K016A Intake Air Compressor is Short Cycling

CR 01960301; 1K016A Intake Air Compressor Found Not Cycling

CR 01961140; 1K016A Found Tripped

CR 01961192; V77-0022 Has an Air Leak

CR 01962708; 1K016A Not Carrying Load at Intake Structure

CR 01966760; Air Dryer was Found in Service but not Purging

CR 01967005; DO7713A Positioner Inlet Supply Line Leaking Air

CR 01969340; DNA-River Water Supply HVAC Controllers Not Installed per Specifications

CR 01970330; 1K-16A Exhaust Line Air Fryer Not Functioning

CR 01942767; Unexpected Alarm on RIS-4131A

CR 01949942; Unexpected Alarm on A Fuel Pool Rad Monitor Downscale

CR 01953813; Annunciator 1C03A (C-1) Fuel Pool Exhaust RIS-4131A/B Rad Monitor

CR 01954560; Momentary Alarms Associated with RIS-4131A

CR 01867785; Unexpected Alarm from RIS-4131A

CR 01867929; Momentary Spike Down on RR4131

CR 01877344; Fuel Pool Exhaust RIS-4131A/B Downscale/Inoperable Alarm Activated & Reset

CR 01909908; RIS-4131A Spiked Downscale

CR 01911385; Fuel Pool Exhaust RIS-4131A/B Downscale/Inoperable Alarm Activated & Reset

CR 01912005; CRs and WRs are not Automatically Crossed Referenced to WOs

CR 01912041; Trend - RIS-4131A/B Downscale/Inoperable Alarms not Fixed

CR 01920482; No Equipment Reliability Issues for the Refuel Floor Radiation Monitor

CR 01935047; Trend - Increased Trend in Relay Issues

1R13 Maintenance Risk Assessments and Emergent Work Control

WPG-2; On-Line Risk Management Guideline; Revision 65

WMA-AA-100; Risk Management Program; Revision 0

EN-AA-105; Probabilistic Risk Assessment (PRA) Program; Revision 0

Operators Risk Report; June 26, 2014

Operators Logs; May 30-31, 2014, and June 9, 16, 17, 2014

WO 40239697-01; E/S4599B: Replace Electrolytic Capacitors

STP 3.5.1-03A; A Core Spray System Simulated Automatic Actuation; Revision 9

WPG-1; Work Process Guideline; Revision 61

OP-AA-104-1007; Online Aggregate Risk; Revision 2

WM-AA-100-1000; Work Activity Risk Management; Revision 1

OP-AA-102-1003; Guarded Equipment; Revision 5

Work Week 1424 Work Activity Risk Management Summary and Weekly Probabilistic Risk

Analysis

AOP 410; Loss of River Water Supply/High River Bed Elevation/Low River Water Depth;

Revision 27

EP-AA-105 (DAEC); Maintaining Equipment Important to Emergency Preparedness (DAEC

Specific Information); Revision 3

EP-AA-105; Maintaining Equipment Important to Emergency Response; Revision 4

Operators Risk Report; June 26, 2014

5

Operators Logs; May 30-31, 2014, and June 9, 16, 17, 2014

WO 40239697-01; E/S4599B: Replace Electrolytic Capacitors

WO 40293372-01; 94-K7333B Replace Relay

WO 40249563-01; AV7318B-O: Calibrate Positioner

WO 40267914-01; 1VEF036B: MA-Inspect Unit

WO 40310673-01; 1G-31 Lube Oil Cooler Heat Exchanger

STP 3.3.8.1-04B; 1A4 4KV Emergency Bus Under-voltage Relay Calibration; Revision 2

M063-033; B Control Building Chiller Mechanical Drawing (1VCH001B); Revision 6

M063-036; Control Building Chiller Condenser 1E235A Fabricated Head; Revision 0

CE 01965912; Kaman 2 High Alarms

CR 01973110; Kaman 2 Auto Check Source Needs Repositioning

CR 01972939; Emergency Service Water System Unavailability in Maintenance Rule Yellow

Status

CR 01948954; Unplanned TS and TRM Entries due to Door Timeout

CR 01949651; Unplanned Standby Filter Unit/Control Building Boundary LCO Entry on

Door 402

CR 01945507; Possible Missed Surveillance; 1/2 of 3.4.5-03 Not Completed

1R15 Operability Determinations and Functionally Assessments

CR 01946048; Apparent Cause Evaluation Report, LS1861D Calibration Found out of

Tolerance

EN-AA-203-1001; Operability Determinations/Functionality Assessments; Revision 16

FP-AA-104-1000; Fire Protection Maintenance, Testing, Impairment and Compensatory Action;

Revision 0

FP-AB-100; DAEC Fire Protection Program; Revision 0

ACP 107.0; Surveillance Tests

ACP 111.0; Inspection, Test Control and Testing; Revision 6

ACP 1412.4; Impairments to Fire Protection Systems, Revision 70

ACE 1966869; Standby Liquid Control Foreign Material; Revision 2

POR 1966869; Standby Liquid Control Foreign Material Past Operability Review

CE 01964875-01; NRC Question on Use of TSR 3.0.3 and the TRM

CR 01946048; Apparent Cause Evaluation Report, LS1861D Calibration Found Out of

Tolerance

CR 01959153; No Air Flow Testing Procedures Exist for TRM Deluge Systems

CR 01963691; TRM Surveillance Requirements Not Performed

CR 01963696; Missed TRM Surveillance for Hose Stations

CR 01964875; NRC Question on Use of TSR 3.0.3 and the TRM

CR 01964878; NFPA Requirements for Air Flow Testing

CR 01971501; TLCO Times for Fire Detection and Suppressions Challenged

CR 01966869; Standby Liquid Control Foreign Material

Procedure Change Request (PCR) 01968702; EN-AA-203-1001 - Operability

Determinations/Functionality Assessments

PCR 01968720; ACP 107.0 - Surveillance Tests

TWR 01976300; Provide Training on the Proper Use of SR 3.0.3 and TSR 3.0.3

CR 01956085; CAL-M98-058 (Alternate Depressurization System Accumulator Size

Verification) Inputs Error

CR 01956930; Investigate Potential Non-Conservative TS SR 3.5.1.3

6

1R18 Plant Modifications

CR 01961603; Errors on Original Code Data Reports for Condenser

CR 01961294; S&L Draft Evaluation Not Favorable for 1E235A Return to Service

CR 01960576; A Control Building Chiller Condenser 1E235A Return Head Has Corrosion

1R19 Post-Maintenance Testing

STP 3.5.1-05; HPCI System Operability Test; Revision 58

WO 40170771; MO2247-O, Lube and Inspect Gearbox and Limit Switch

WO 40176867; MO2318-O; Inspect Lube Gearbox and Limit Switch

WO 40175686; 1P218-M, Inspect & Perform PI Test

STP 3.8.1-06B; B Standby Diesel Generator Operability Test (Fast Start); Revision 15

WO 40184541; 1P229C-M, Change Out Upper Motor Bearing (RHR)

CR 01844913; C RHR Motor Oil Reservoir Found Metal Shavings

WO 40107646; Replace Electrolytic Capacitors

WO 40168715; MO 2515-O, Lube & Inspect

WO 40173426; Calibrate TE 2406 (Maintenance Run)

WO 40172163; FI 2509: Calibrate

WO 40172161; FIC2509: Replace MPU Board

WO 40172164; FT2509: Calibrate

STP 3.5.3-02; RCIC System Operability Test; Revision 37

MD-062; Work Order Task(s); Revision 7

MD-024; Post Maintenance Testing Program; Revision 78

STP 3.5.1-02A; A LPCI System Operability Tests; Revision 14

STP 3.5.3-02; RCIC System Operability Test; Revision 44

CAL-E90-008; In-Service Testing Program Instrument Accuracy; Revision 17

POD 1971819; Instrument Accuracy Accounted for in RCIC Flow Rate in STP 3.5.3-02

CR 01964910; NRC Question Regarding PI 2302, HPCI Booster Pump Suction PI

CR 01967624; FI2509 Indicated 395 GPM During RCIC Operability Test

CR 01967794; DNA - Margin to RCIC Tech Spec Flow Requirement is Low

CR 01971819; Instrument Accuracy Accounted for in RCIC Flow Rate STP

1R22 Surveillance Testing

STP 3.3.6.1-32; RCIC Exhaust Diaphragm Channel Functional Test; Revision 4

ACP 107; Surveillance Tests; Revision 17

STP 3.0.0-01; Surveillance Test Procedure Instrument Checks; Revision 142

STP 3.3.6.1-32; RCIC Exhaust Diaphragm Channel Functional Test; Revision 4

STP 3.5.1-01B; B Core Spray System Operability Test; Revision 15

STP 3.3.1.1-13; Turbine Control Valve EOC RPT Logic and RPS Instrument Function Test;

Revision 15

STP 3.5.1-03A; A Core Spray System Simulated Automatic Actuation; Revision 9

STP NS930002; Main Turbine Stop and Combined Intermediate Valves Test; Revision 5

APED-E41-002; Process Diagram High Pressure Coolant Injection System

CAL-M91-010; Recommended Discharge Pressure for HPCI Main Pump Test; Revision 1

CAL-M91-011; Recommended Discharge Pressure for RCIC Main Pump Test; Revision 0

CE 1961465-01; Evaluate Minimum HPCI Pump Discharge Pressure During Operability STPs

CE 1961479-01; Evaluate Minimum RCIC Pump Discharge Pressure During Operability STPs

CR 01961465; DNA AR: HPCI STPs May Contain an Incorrect Pump Discharge Pressure

7

CR 01961479; DNA AR: RCIC STPs Minimum Pump Discharge Pressure Less Than CAL

M91011

CR 01967068; SV and ISV Position Indication Problems for STP NS930002

CR 01968205; ODMI for MSR Drain Tank Dump Valve Leak By

PCR 1961750; Change STPs 3.5.1-05, 3.5.1-09, 3.5.1-10 Minimum HPCI Pump Discharge

Pressure

2RS5 Radiation Monitoring Instrumentation

STP 3.0.0-01; Surveillance Test Procedure Instrument Checks; Revision 142

STP NS790301; GSW Radiation Monitor Calibration

STP NS791011; K8 Calibration

STP NS791013; K10 Calibration

OI 920; Drywell Sump Systems; Revision 46

2RS6 Radioactive Gaseous and Liquid Effluent Treatmen

PCP 8.7; Alarm Setpoints for Liquid Rad Monitors; Revision 17

PCP 8.4; Alarm Setpoints and Efficiency for GE Offgas Stack Rad Monitor; Revision 10

EV-AA-100; Fleet Ground Water Protection Program; Revision 2

ACP 1411.35; The DAEC Groundwater Protection Program; Revision 8

STP 3.6.4.3-03-A; SBGT Sys HEPA/CHAR Filter Efficiency Test

STP 3.6.4.3-03-B; SBGT Sys HEPA/CHAR Filter Efficiency Test

NS790505; Effluent Noble Gas Sampling & Analysis; Revision 3

NS790601; Effluent P & I Sampling & Analysis; Revision 24

EV-AA-100-1001-F01; 10 CFR 50.75(g) Documentation; various dates

Duane Arnold Energy Center Operations and Maintenance Activity Assessment of Unplanned

Releases; July 12, 2013

EN 48403; Offsite Notification Due to Leak From Condensate Storage Tank Containment Pit

Sump; October 12, 2012

Five Year Review of the DAEC GWPP Monitoring Plan; August 13, 2013

Ground Water Protection Initiative Site Conceptual Model; May 29, 2013

CR 01812156; CST Pit Sump Seal Leaking

CR 01827363; Structural Monitoring, CST Foundation Floor Surface Cracks

CR 01820689; Degraded Drain Piping Found in Turbine Building Basement

CE 01905073; Tritium and Cesium 137 Identified in Conduit Water - 2013

4OA1 Performance Indicator Verificaiton

CR 01910625; Walkdown Scope Increase

CR 01971250; TS Hi-Rad Violation Not Characterized Correctly: NRC PI Q413

MSPI Basis Document; Revision 16

NRC PI Data Calculation, Review and Approvals; RCS Leakage; 2nd Quarter 2013 through

1st Quarter 2014

OI 920; Drywell Sump System; Revision 46

CR 01866940; Very Slight Increasing Trend in Drywell Unidentified Leakage

CR 01867793; Drywell Equipment Sump Did Not Auto Pump

CR 01871786; Equipment Sump Inconsistent Pump Volumes Today

CR 01872165; DWEDS Totalizer FQ3708 Drift Due to 1P-037A Control Circuit De-energized

CR 01872166; Abnormal DW Identified Leakage Calculation Due to FQ3708 Drift

CR 01879703; Drywell Equipment Drain Pump, 1P-37B, Did Not Auto Pump

8

CR 01886976; DWEDS Has Not Pumped for Greater Than 8 Hours

CR 01887568; Level Switch is Sticking

CR 01887570; Drywell Floor Drain Leakage Calculated High

CR 01951939; Potential Adverse Trend - Sump Pump Issues

CR 01965584; Equipment Sump Failed to Pump at 1200

CR 01910625; Walkdown Scope Increase

CR 01971250; TS Hi-Rad Violation not Characterized Correctly: NRC PI Q413

4OA2 Identification and Resolution of Problems

RCE 01934040; Under-voltage Relay Failed Root Cause Evaluation

MA-AA-203-1001; Work Order Planning; Revision 1

Relay-G080-08; General Electric Under-voltage Relay Type NGV; Revision 11

STP 3.3.8.1-05B; 1A4 4KV Emergency Transformer Supply Under-voltage Calibration;

Revision 2

WO 40136277-01; STP 3.3.8.1-05-B 4KV Transformer Supply Under-voltage

MD-024; Post Maintenance Testing Program; Revision 78

MA-AA-202; Work Order Execution Process; Revision 8

MD-062; Work Order Task(s); Revision 6

MA-AA-201; Work Order Identification, Screening and Validation Process

WM-AA-200; Work Management Process Overview; Revision 8

AD-AA-103; Nuclear Safety Culture Program; Revision 5

PI-AA-100-1002; Procedure for Failure Investigation Process; Revision 9

OP-AA-100-1002; Plant Status Control Management; Revision 2

PI-AA-101-1000; Focused Self-Assessment Planning, Conduct and Reporting; Revision 10

ACP 1410.2; LCO Tracking and Safety Function Determination Program; Revision 32

AD-AA-100-1006; Procedure and Work Instruction Use and Adherence; Revision 3

PI-AA-204; Condition Identification and Screening; Revision 24

PI-AA-205; Condition Evaluation and Corrective Action; Revision 25

PI-AA-100-1005; Root Cause Analysis; Revision 9

PI-AA-100-1007; Apparent Cause Evaluation; Revision 8

CR 01934040; STP 3.3.8.1-05-B, 4KV Emergency Transformer Under-voltage Failed

CR 01934167; 127/SB2 Standby Transformer 1X4 Under-voltage Relay Wrong Configuration

CR 01941895; Reportability Review Due Date Set Past LER 60 Day Due Date

CR 01972812; Contributing Cause Actions for Under-voltage Relay RCE #1934040

PCR 01972807; MA-AA-203-1001 - Work Order Planning

9

LIST OF ACRONYMS USED

ACP Administrative Control Procedure

ADAMS Agencywide Document Access Management System

AOP Abnormal Operating Procedure

CAP Corrective Action Program

CBC Control Building Chiller

CE Condition Evaluation

CFR Code of Federal Regulations

CR Condition Report

DAEC Duane Arnold Energy Center

DG Diesel Generator

IOD Immediate Operability Determination

IMC Inspection Manual Chapter

IP Inspection Procedure

kV Kilovolt

LCO Limiting Condition for Operation

LER Licensee Event Report

LPCI Low Pressure Coolant Injection

NCV Non-Cited Violation

NFPA National Fire Protection Association

NRC U.S. Nuclear Regulatory Commission

ODCM Offsite Dose Calculation Manual

OFR Operability/Functionality/Reportability

OI Operating Instruction

PARS Publicly Available Records System

PCR Procedure Change Request

PFP Pre-Fire Plan

PI Performance Indicator

PM Planned Maintenance

POD Prompt Operability Determination

POR Prompt Operability Review

RCE Root Cause Evaluation

RCIC Reactor Core Isolation Cooling

RCS Reactor Coolant System

RPS Reactor Protection System

SBDG Standby Diesel Generator

SDP Significance Determination Process

SSC Structure, System, and Component

STP Surveillance Test Procedure

TLCO Technical Requirements Manual Limiting Condition for Operation

TRM Technical Requirements Manual

TSR Technical Surveillance Requirement

TS Technical Specification

UFSAR Updated Final Safety Analysis Report

WO Work Order 10

R. Anderson -2-

In accordance with Title 10 of the Code of Federal Regulation 2.390, Public Inspections,

Exemptions, Requests for Withholding, of the NRC's "Rules of Practice," a copy of this letter

and its enclosure, and your response (if any) will be available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records System (PARS)

component of NRC's Agencywide Documents Access and Management System (ADAMS),

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Christine Lipa, Chief

Branch 1

Division of Reactor Projects

Docket No. 50-331

License No. DPR-49

Enclosure:

Inspection Report 05000331/2014003

w/Attachment: Supplemental Information

cc w/encl: Distribution via LISTSERV

DISTIRBUTION w/encl:

Anthony Bowers Carole Ariano

RidsNrrDorlLpl3-1 Resource Linda Linn

RidsNrrPMDuaneArnold Resource DRPIII

RidsNrrDirsIrib Resource DRSIII

Cynthia Pederson Patricia Buckley

Darrell Roberts Carmen Olteanu

Steven Orth ROPreports.Resource@nrc.gov

Allan Barker

DOCUMENT NAME: Duane Arnold IR 2014 003

Publicly Available Non-Publicly Available Sensitive Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" =

Copy with attach/encl "N" = No copy

OFFICE RIII RIII RIII RIII

NAME RNg for CPhillips:rj CLipa

DATE 08/11/14 08/11/14

OFFICIAL RECORD COPY