ML071430289
ML071430289 | |
Person / Time | |
---|---|
Site: | Cooper |
Issue date: | 05/22/2007 |
From: | Howell A NRC/RGN-IV/DRP |
To: | Minahan S Nebraska Public Power District (NPPD) |
References | |
EA-07-090 IR-07-007 | |
Download: ML071430289 (39) | |
See also: IR 05000298/2007007
Text
May 22, 2007
EA 07-090
Stewart B. Minahan, Vice
President-Nuclear and CNO
Nebraska Public Power District
P.O. Box 98
Brownville, NE 68321
SUBJECT: COOPER NUCLEAR STATION - NRC SPECIAL INSPECTION
REPORT 05000298/2007007
Dear Mr. Minahan:
On April 24, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed a special
inspection at your Cooper Nuclear Station. This inspection examined activities associated with
the Emergency Diesel Generator 2 failure that occurred on January 18, 2007. During this
event the emergency diesel generator automatically isolated from the electrical bus following an
over-current condition as a result of a voltage regulator failure. The NRCs initial evaluation
satisfied the criteria in NRC Management Directive 8.3, NRC Incident Investigation Program,
for conducting a special inspection. The basis for initiating the special inspection is further
discussed in the Charter, which is included as Attachment 2 to the enclosed report. The
determination that the inspection would be conducted was made by the NRC on January 26,
2007, and the inspection started on January 29, 2007.
The enclosed special inspection report documents the inspection findings which were discussed
on April 24, 2007, with Mr. Mike Colomb, General Manager of Plant Operations, and other
members of your staff. The inspection examined activities conducted under your license as
they relate to safety and compliance with the Commissions rules and regulations and with the
conditions of your license. The team reviewed selected procedures and records, observed
activities, and interviewed personnel.
The enclosed report discusses one finding that appears to have low to moderate safety
significance (White). As described in Section 6.0 of this report, the NRC concluded that the
failure to establish appropriate procedural controls for evaluating the use of parts of
indeterminate quality prior to their installation in safety-related systems resulted in Emergency
Diesel Generator 2 failure on January 18, 2007. The safety significance of this finding was
assessed on the basis of the best available information, including influential assumptions, using
the applicable Significance Determination Process and was preliminarily determined to be a
White (i.e., low to moderate safety significance) finding. Attachment 3 of this report provides a
detailed description of the preliminary risk assessment. In accordance with NRC Inspection
Nebraska Public Power District -2-
Manual Chapter (IMC) 0609, Significance Determination Process, we intend to complete our
evaluation using the best available information and issue our final determination of safety
significance within 90 days of this letter.
This finding does not represent an immediate safety concern because of the corrective actions
you have taken. These actions included the installation of properly dedicated voltage regulator
components for Emergency Diesel Generator 2 following the failure that occurred on
January 18, 2007.
Also, this finding constitutes an apparent violation of NRC requirements and is being
considered for escalated enforcement action in accordance with the NRC Enforcement Policy.
The current Enforcement Policy is included on the NRCs Web site at www.nrc.gov; select
About NRC, How We Regulate, Enforcement, then Enforcement Policy.
Before we make a final decision on this matter, we are providing you an opportunity (1) to
present to the NRC your perspectives on the facts and assumptions, used by the NRC to arrive
at the finding and its significance, at a Regulatory Conference or (2) submit your position on the
finding to the NRC in writing. If you request a Regulatory Conference, it should be held within
30 days of the receipt of this letter and we encourage you to submit documentation at least one
week prior to the conference in an effort to make the conference more efficient and effective. If
a Regulatory Conference is held, it will be open for public observation. If you decide to submit
only a written response, such submittal should be sent to the NRC within 30 days of the receipt
of this letter.
Please contact Michael Hay at (817) 860-8144 within 10 business days of the date of this letter
to notify the NRC of your intentions.
If you choose to provide a written response, it should be clearly marked as a Response to An
Apparent Violation in Inspection Report No. 05000298/2007007: EA-07-090 and should
include: (1) the reason for the apparent violation, or, if contested, the basis for disputing the
apparent violation; (2) the corrective steps that have been taken and the results achieved; (3)
the corrective steps that will be taken to avoid further violations; and (4) the date when full
compliance will be achieved. Your response may reference or include previously docketed
correspondence, if the correspondence adequately addresses the required response. If an
adequate response is not received within the time specified or an extension of time has not
been granted by the NRC, the NRC will proceed with its enforcement decision or schedule a
Since the NRC has not made a final determination in this matter, no Notice of Violation is being
issued for the inspection finding at this time. In addition, please be advised that the number
and characterization of the apparent violation described in the enclosed inspection report may
change as a result of further NRC review.
The report also documents one NRC-identified finding, which was evaluated under the risk
significance determination process as having very low safety significance (Green). This finding
was determined to involve a violation of NRC requirements. However, because of the very low
safety significance and because it is entered into your corrective action program, the NRC is
Nebraska Public Power District -3-
treating this finding as a noncited violation consistent with Section VI.A.1 of the NRC
Enforcement Policy. If you contest the noncited violation in this report, you should provide a
response within 30 days of the date of this inspection report, with the basis for your denial, to
the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington,
DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory
Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011-4005; the
Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington,
DC 20555-0001; and the NRC Resident Inspectors at the Cooper Nuclear Station.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its
enclosures will be made available electronically for public inspection in the NRC Public
Document Room or from the Publicly Available Records (PARS) component of NRCs
document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html.
Sincerely,
/RA/
Arthur T, Howell III, Director
Division of Reactor Projects
Docket: 50-298
License: DPR-46
Enclosure: NRC Inspection Report 05000298/2007007
Attachment 1: Supplemental Information
Attachment 2: Special Inspection Charter
Attachment 3: Significance Determination Evaluation
cc w/Enclosure:
Gene Mace P. V. Fleming, Licensing Manager
Nuclear Asset Manager Nebraska Public Power District
Nebraska Public Power District P.O. Box 98
P.O. Box 98 Brownville, NE 68321
Brownville, NE 68321
Michael J. Linder, Director
John C. McClure, Vice President Nebraska Department of
and General Counsel Environmental Quality
Nebraska Public Power District P.O. Box 98922
P.O. Box 499 Lincoln, NE 68509-8922
Columbus, NE 68602-0499
Nebraska Public Power District -4-
Melanie Rasmussen, Radiation Control
Chairman Program Director
Nemaha County Board of Commissioners Bureau of Radiological Health
Nemaha County Courthouse Iowa Department of Public Health
1824 N Street Lucas State Office Building, 5th Floor
Auburn, NE 68305 321 East 12th Street
Des Moines, IA 50319
Julia Schmitt, Manager
Radiation Control Program Ronald D. Asche, President
Nebraska Health & Human Services and Chief Executive Officer
Dept. of Regulation & Licensing Nebraska Public Power District
Division of Public Health Assurance 1414 15th Street
301 Centennial Mall, South Columbus, NE 68601
P.O. Box 95007
Lincoln, NE 68509-5007 Kevin V. Chambliss, Director of
Nuclear Safety Assurance
H. Floyd Gilzow Nebraska Public Power District
Deputy Director for Policy P.O. Box 98
Missouri Department of Natural Resources Brownville, NE 68321
P. O. Box 176
Jefferson City, MO 65102-0176 John F. McCann, Director, Licensing
Entergy Nuclear Northeast
Director, Missouri State Emergency Entergy Nuclear Operations, Inc.
Management Agency 440 Hamilton Avenue
P.O. Box 116 White Plains, NY 10601-1813
Jefferson City, MO 65102-0116
Keith G. Henke, Planner
Chief, Radiation and Asbestos Division of Community and Public Health
Control Section Office of Emergency Coordination
Kansas Department of Health 930 Wildwood, P.O. Box 570
and Environment Jefferson City, MO 65102
Bureau of Air and Radiation
1000 SW Jackson, Suite 310 Chief, Radiological Emergency
Topeka, KS 66612-1366 Preparedness Section
Kansas City Field Office
Daniel K. McGhee, State Liaison Officer Chemical and Nuclear Preparedness
Bureau of Radiological Health and Protection Division
Iowa Department of Public Health Dept. of Homeland Security
Lucas State Office Building, 5th Floor 9221 Ward Parkway
321 East 12th Street Suite 300
Des Moines, IA 50319 Kansas City, MO 64114-3372
Nebraska Public Power District -5-
Electronic distribution by RIV:
Regional Administrator (BSM1)
DRP Director (ATH)
DRS Director (DDC)
DRS Deputy Director (RJC1)
Senior Resident Inspector (NHT)
Branch Chief, DRP/C (MCH2)
Senior Project Engineer, DRP/C (WCW)
Team Leader, DRP/TSS (CJP)
RITS Coordinator (MSH3)
Only inspection reports to the following:
L. Trocine, OEDO RIV Coordinator (LXT)
ROPreports
CNS Site Secretary (SEF1)
OE Mail
M. Ashley, NRR (MAB)
M. Vasquez (GMV)
V. Dricks (VLD)
W. Maier (WAM)
SUNSI Review Completed: _WCW ADAMS: : Yes G No Initials: __WCW
- Publicly Available G Non-Publicly Available G Sensitive : Non-Sensitive
R:\_REACTORS\CNS\2007\CNS2007-07 RP Special.wpd_
RIV:DRS RI:DRP/C SRA:DRS C:DRP/C ACES
SPRutenkroger NHTaylor MFRunyan MCHay MHaire
E-WCWalker T-Walker /RA/ /RA/ /RA/
5/14/07 5/17/07 5/9/07 5/17/07 5/10/07
D:DRP
ATHowell III
/RA/
5/22/07
OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket.: 50-298
License: DPR-46
Report: 05000298/2007007
Licensee: Nebraska Public Power District
Facility: Cooper Nuclear Station
Location: P.O. Box 98
Brownville, Nebraska
Dates: January 28 through April 24, 2007
Inspectors: N. Taylor, Resident Inspector
S. Rutenkroger, PHD, Reactor Inspector
Approved By: Arthur T. Howell III, Director
Division of Reactor Projects
-1- Enclosure
SUMMARY OF FINDINGS
IR 05000298/2007007; 01/28/07 - 04/24/07; Cooper Nuclear Station. Special Inspection in
response to Emergency Diesel Generator 2 failure on January 18, 2007.
This report documents the special inspection activities conducted by one resident inspector and
one reactor inspector. One apparent violation and one non-cited violation were identified. The
significance of the issues is indicated by their color (Green, White, Yellow, or Red) and was
determined by the significance determination process in Inspection Manual Chapter 0609.
Findings for which the significance determination process does not apply are indicated by the
severity level of the applicable violation. The NRC's program for overseeing the safe operation
of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight
Process, Revision 3, dated July 2000.
A. NRC-Identified and Self-Revealing Findings
Cornerstone: Mitigating Systems
- TBD. The team identified an apparent violation of 10 CFR Part 50, Appendix B,
Criterion V, "Instructions Procedures, and Drawings," for the failure to establish
procedural controls for evaluating the use of parts of indeterminate quality prior
to their installation in safety-related applications. This procedural deficiency
resulted in the installation of a voltage regulator circuit board of indeterminate
quality that adversely affected the function of Emergency Diesel Generator 2.
Specifically, following installation of the part on November 11, 2006, failure of the
part occurred following 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br /> of operation resulting in an over-voltage trip of
Emergency Diesel Generator 2 on January 18, 2007.
The finding is greater than minor because it is associated with the equipment
performance cornerstone objective to ensure the availability, reliability, and
capability of systems that respond to initiating events to prevent undesirable
consequences. Using NRC Inspection Manual Chapter 0609, Significance
Determination Process, Phase 1 Worksheet, a Phase 2 evaluation was required
because the finding resulted in the loss of the safety function of Emergency
Diesel Generator 2 for greater than the Technical Specification completion time.
The Phase 2 evaluation concluded that the finding was of low to moderate safety
significance. A Phase 3 preliminary significance determination analysis also
determined the finding was of low to moderate safety significance.
- Green. The team identified three examples of a noncited violation of Technical
Specification 5.4.1.a involving the failure to establish adequate maintenance
procedures for work performed on Emergency Diesel Generator 2. These
inadequate procedures failed to identify a degraded condition in the voltage
regulator off-manual-auto switch and contributed to an over-voltage trip of
Emergency Diesel Generator 2 that occurred on November 13, 2006.
-2- Enclosure
The finding is more than minor because it is associated with the Mitigating
Systems cornerstone attribute of procedure quality and affects the associated
cornerstone objective to ensure the availability, reliability, and capability of
systems that respond to initiating events. Specifically, the performance
deficiency resulted in: (1) the failure to discover a degraded condition in the
Emergency Diesel Generator 2 voltage regulator, and (2) an over-voltage trip
during the tuning of Emergency Diesel Generator 2 on November 13, 2006.
Using the Manual Chapter 0609 Appendix G, "Shutdown Operations Significance
Determination Process," Phase 1 Checklist, the finding is determined to have
very low safety significance because one operable diesel generator was still
capable of supplying power to the class 1E electrical power distribution
subsystems. This finding has a cross-cutting aspect in the area of human
performance in that the licensees procedures were not complete and provided
inadequate instructions for conducting maintenance associated with Emergency
Diesel Generator 2.
-3- Enclosure
REPORT DETAILS
1.0 Special Inspection Report
The NRC conducted this special inspection to better understand the circumstances
surrounding the failure of Emergency Diesel Generator (EDG) 2 that occurred on
January 18, 2007. The failure of EDG 2 occurred during a routine monthly surveillance
test following approximately four hours of operation. The cause of the event was the
result of a failure of a voltage regulator card that had been installed in November 2006.
In accordance with NRC Management Directive 8.3, NRC Incident Investigation
Program, it was determined that this event met the deterministic criteria and had
sufficient risk significance to warrant a special inspection.
The team used NRC Inspection Procedure 93812, Special Inspection Procedure, to
conduct the inspection. The special inspection team reviewed procedures, corrective
action documents, as well as design and maintenance records for the equipment of
concern. The team interviewed key station personnel regarding the event, reviewed the
root cause analysis, and assessed the adequacy of corrective actions. A list of specific
documents reviewed is provided in Attachment 1. The charter for the special inspection
is provided as Attachment 2.
2.0 Review of EDG Voltage Regulator Problems
The team conducted a review of all work orders, surveillance test records, and condition
reports associated with the electrical components of EDG 2 written from January 2004
through January 2007. The following discusses several discrete periods of degraded
performance of the EDG 2 voltage regulator.
EDG 2 Voltage Regulator Performance in 2005
On three occasions in 2005, operators initiated condition reports (CRs) documenting
difficulties maintaining stable reactive load on EDG 2. In all reported occurrences,
kilovolt-ampere-reactive (KVAR) step changes, ranging from 100-300 KVAR, and spikes
up to 2000 KVAR were received during manipulation of the lower-raise voltage regulator
switch in the control room. This remote switch sends demand signals to the motor
operated potentiometer (MOP) providing a reference voltage signal to the voltage
regulator. On the basis of these observations, the licensee replaced the EDG 2 MOP in
December 2005. In addition, the licensee initiated a preventive maintenance (PM) plan
in June 2006 implementing MOP cleaning and inspection activities every operating cycle
and MOP replacement every third operating cycle.
The team noted there were five similar condition reports pertaining to EDG 1 in the
2000-2007 time period. The KVAR changes documented in these condition reports
were consistent with MOP issues affecting EDG 2. The team noted that corrective
actions consisting of the previously discussed PM activities appeared adequate to
address the problem.
-4- Enclosure
The licensee evaluated the impact of these KVAR step changes on the operability of the
EDGs after each occurrence. The KVAR rating of the EDGs is 5000 KVAR, and the
maximum reactive load seen during these transients was approximately 2000 KVAR.
During these KVAR step changes, the licensee did not observe any frequency or real
load changes, and all acceptance criteria of the surveillance test procedures were
satisfied. As such, the licensee determined the operability of the EDGs was not affected
by the KVAR swings, but that the KVAR changes were indicative of a degraded
condition in the voltage regulator system. The team reviewed the licensees evaluation
for this degraded condition and determined it adequately provided reasonable
assurance of operability.
EDG 2 Voltage Regulator Performance in 2006
Despite the installation of a new MOP in December 2005, unpredictable KVAR changes
began occurring again early in 2006. In addition to KVAR swings during manipulation of
the lower-raise voltage regulator switch, the licensee noted KVAR swings during steady
state operation of EDG 2. This new trend suggested that a failure mechanism existed
that was unrelated to the MOP. In response to this trend, the licensee initiated CR-
CNS-2006-2729 and developed actions to review the overall health of the voltage
regulating system and utilized vendor support to develop actions to resolve the problem.
One of the actions coming from the CR was to perform extenistive troubleshooting
during Refueling Outage 23 (RE23), specifically directed at cleaning the MOP and
checking circuit continuity throughout the voltage regulator system. Work Order (WO)
4514076 was created to perform this task on EDG 2.
EDG 2 Over-Voltage Event on November 11, 2006
One of the troubleshooting steps included in WO 4514076 was to wipe the R13
feedback adjust potentiometer on the voltage regulator printed circuit board. This
involved turning a small screw on the potentiometer and exercising the slide wire
resistor through its full range of travel. During performance of this step on November 8,
2006, the resistor failed due to an open circuit condition. The licensee had anticipated
problems with the printed circuit board and initiated a contingency in the WO to replace
the board with a spare.
Replacement of the printed circuit board required a tuning process to establish the
correct voltage regulator response. WO 4514076 contained the procedural guidance to
complete this task. This tuning process involved, in part, running EDG 2 unloaded,
initiating small voltage changes, measuring the time response of the ensuing voltage
transient, and making incremental adjustments in the position of the R13 potentiometer.
During this process the licensee had several pieces of test equipment installed to
monitor the EDG output voltage response.
During the unloaded run of EDG 2 for this activity, operations personnel shut the
machine down because of unexpected fuel rack movement (the team reviewed this
condition and determined that this was normal fuel rack behavior that did not affect EDG
2 operability). While the EDG was shutdown, electrical technicians investigated a
potential problem with an installed oscilloscope being used as test equipment. The
-5- Enclosure
technicians connected a variac to the oscilloscope and introduced a 60 volt test signal.
The technicians realized immediately that they had failed to disconnect the oscilloscope
from the voltage regulator system and disconnected it. Unknown at the time to the
technicians, this erroneous act resulted in blowing a fuse on one of three phases of the
voltage regulator potential transformer, adversely affecting the voltage regulator
summing network that senses generator output voltage. As a result, during the
subsequent restart of EDG 2, the voltage regulator sensed an artificially low output
voltage and drove voltage up until the EDG 2 over-voltage trip occurred at 6125 volts.
The performance aspects of this event resulted in a non-cited violation of NRC
requirements, which is described in NRC Integrated Inspection Report 05000298/2006005 (ML070360639).
EDG 2 Over-voltage Event on November 13, 2006
On November 13, 2006, the licensee replaced the blown fuse and continued with the
voltage regulator tuning process. The process required operators to make small
changes in voltage around rated voltage, after which engineers reviewed the ensuing
voltage transient as recorded on a strip chart. This was an iterative process that
involved several voltage changes. Approximately ten seconds after one voltage change
EDG 2 experienced a pair of voltage spikes; the first to approximately 5500 volts and
the second to greater than 5900 volts, resulting in an over-voltage EDG trip.
In response to this event, the licensee initiated CR-CNS-2006-9096. The licensee
conducted significant troubleshooting efforts to ascertain the cause of the over-voltage
condition. These troubleshooting efforts included continuity checks, testing of voltage
regulator connectors, and five monitored test runs of EDG 2. Unable to find a definitive
cause for the trip, the licensee contacted a nuclear field service contractor experienced
in voltage regulator maintenance. In the apparent cause report attached to CR-CNS-
2006-9096, the licensee reported that on the basis of the troubleshooting conducted, the
acceptable operation of EDG 2 in the five test runs, and the vendors experience, the
apparent cause of the trip was the erratic behavior of one or both of the potentiometers
of the voltage regulator card. The team reviewed the design of the voltage regulator,
vendor instructions, industry maintenance guidelines, and industry operating experience,
and was unable to find any information that corroborated this apparent cause. The
apparent cause report suggested corrective actions to improve the training of those
involved in voltage regulator maintenance and to develop a voltage regulator testing
procedure to allow onsite personnel to tune the voltage regulator.
Following the completion of troubleshooting, EDG 2 was run without incident in a
number of surveillance tests, including a sequential load test, at the end of the RE23
outage. In addition, a routine four-hour surveillance test was completed successfully on
December 12, 2006.
EDG 2 Over-voltage Event on January 18, 2007
On January 18, 2007, the licensee conducted Surveillance Procedure 6.2DG.101,
Diesel Generator 31 Day Operability Test. After approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> and 13
minutes at full load, the EDG 2 output breaker tripped open on an over-current
-6- Enclosure
condition, followed immediately by an over-voltage trip of EDG 2. During the transient,
the KVAR loading of the machine reached a peak of 10,667 KVAR and the output
current reached a peak of approximately 1700 amps when the EDG output circuit
breaker and the bus tie breaker to the safety related bus tripped open on over-current.
With EDG 2 disconnected from the bus, output voltage rose rapidly until the machine
tripped on over-voltage at 6009 volts.
Following this third over-voltage trip of EDG 2, the licensee formed a root cause analysis
team and completed a significant troubleshooting effort with vendor support. Unable to
locate a failed component, the licensee replaced the suspect voltage regulator card and
performed a six hour loaded run of EDG 2. Based on acceptable performance during
this test and the belief that the degraded condition that caused the January 18th trip no
longer existed, the licensee declared EDG 2 operable on January 22, 2007.
3.0 Root Cause and Immediate Corrective Actions
Root Cause for Voltage Regulator Failures
As documented in CR-CNS-2007-00480, the licensee determined that the root cause of
the January 18, 2007 trip of EDG 2 was that the original procurement process did not
provide technical requirements to reduce the probability of infant mortality failure in the
voltage regulator board in the EDG voltage regulating subsystem. The team reviewed
the licensees root cause methodology and agreed with this conclusion.
The procurement error associated with the voltage regulator card occurred in the Fall of
1973 and involved the inadequate procurement of a commercial grade component for
use in safety related applications. The team noted that in the late 1980's, the NRC
conducted a series of inspections to understand licensees procurement and
commercial-grade dedication programs. These inspections resulted in the NRC
providing additional guidance related to acceptable licensee commercial grade
procurement and dedication programs. Specifically, the NRC issued Generic Letter 91-
05, Licensee Commercial-Grade Procurement and Dedication Programs that provided
guidance for complying with the requirements of 10 CFR Part 50, Appendix B, Quality
Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, specifically
related to assuring the quality of items purchased and installed in safety related
applications.
The team reviewed Engineering Procedure 3-CNS-DC-138.2, Dedication, Revision 1,
and determined that it had been adequately revised to define expectations for the
dedication of commercial-grade components based on the new guidance. The team
noted that during the years in which substandard procurement practices were in place
that components of indeterminate quality had been accepted into the warehouse as
spare parts acceptable for use in safety- related applications. The team determined that
the licensee had failed to establish adequate procedural guidance to evaluate the use
of these parts of indeterminate quality prior to their installation in safety-related
applications.
The enforcement aspects of this issue are fully described in Section 6 of this report.
-7- Enclosure
Immediate Corrective Actions
In response to the failure of EDG 2 on January 18, 2007, the licensee formed an
integrated response team and staffed the Outage Control Center to track the status of
troubleshooting efforts.
A prompt assessment was performed to determine whether the cause of the failure of
EDG 2 was applicable to EDG 1. The licensee demonstrated that during RE23, EDG 2
had undergone a significant amount of invasive voltage regulator maintenance. In
addition, EDG 2 twice experienced over-voltage trips during the outage. EDG 1 had not
demonstrated this behavior and did not undergo any invasive voltage regulator
maintenance. On the basis of these facts, the licensee determined that EDG 1
operability was not affected by the failure of EDG 2.
The licensee began a rigorous failure modes and effects analysis (FMEA), focusing on
the condition of any electrical component that could affect the control circuit in the
voltage regulator assembly. The FMEA included continuity checks, verification of relay
settings, and an in-situ test of the suspect voltage regulator printed circuit board. The
board passed the in-situ test with no anomalies, and was then replaced with a spare part
obtained from another nuclear utility. After tuning the new circuit board, the licensee
conducted a six hour surveillance run on EDG 2 followed by a full load reject test. No
anomalies were noted during the surveillance testing.
On the basis of the FMEA results and the successful completion of the surveillance test,
the licensee declared EDG 2 operable on January 22, 2007.
4.0 Review of Licensee Troubleshooting Efforts
The team examined vendor manuals, industry maintenance guidelines, and circuit
drawings for the Basler series boost static regulator (SBSR) voltage regulator and
compiled a list of all components, which could fail in a manner as to potentially replicate
the January 18 event. The team reviewed relevant operating experience to identify
additional failure mechanisms experienced at other facilities. The team then compared
the independently generated list to the licensees FMEA to determine whether any
failure modes had not been considered or eliminated inappropriately.
In addition, the team observed a regularly scheduled surveillance test of EDG 1 on
January 29, 2007, conducted in accordance with Procedure 6.1DG.101, Diesel
Generator 31 Day Operability Test. The team observed control room and local
indications during EDG startup and steady state operations, reviewed the data collected
and the completed surveillance package. The team noted no anomalies in the
performance of EDG 1.
The team reviewed the licensees analysis concerning the potential effects that the high
voltage and current conditions could have on affected electrical equipment during the
three EDG 2 over-voltage transients described above. The team reviewed vendor
documentation, procurement records, drawings, relay setpoint calculations and
-8- Enclosure
conducted interviews with design and system engineering staff. The team determined
that the protective devices installed, such as the over-voltage and over current relays,
provided adequate protection for EDG 2 and connected equipment.
During troubleshooting following the failure, a maintenance technician discovered two
loose terminal screws on the back of the EDG 2 OFF-MANUAL-AUTO switch (OMAS).
The licensee had concluded that this was a potential cause of the January 18 failure.
The team reviewed the design of the switch, its function in the circuit, and conducted
several interviews with the technician who discovered the condition. On the basis of the
intermittent nature of the OMAS discontinuity and the prolonged nature of the transient
on January 18 (at least 30 seconds in duration), the team determined that the OMAS
discontinuity was a possible but implausible mode of failure. The team shared this view
with licensee management during a debrief on February 1, 2007.
The team identified several examples of failure modes that were not considered or
eliminated without a technical basis, each of which was brought to the attention of
licensee management during a debrief on February 1, 2007. Following these
discussions the licensee performed additional EDG 2 inspections on February 8, 2007,
and performed eight hour loaded runs on February 8 and February 12, 2007. These
additional inspections and loaded runs did not identify any deficient conditions.
5.0 Offsite Testing of Suspect Voltage Regulator Card
Following the over-voltage event on January 18, 2007, the licensee conducted an in-situ
test of the voltage regulator printed circuit board to identify potential failure mechanisms.
This test was similar to a factory acceptance test in that it powered up the board to
identify hard component failures. No such failures were detected during the in-situ
testing.
The licensee sent the board to a commercial test laboratory where, under vendor
supervision and with input from CNS engineering staff, a series of visual and electrical
tests were conducted to identify failure modes. The laboratory identified that a zener
diode on the printed circuit was in a failed state. CNS demonstrated that this failed
zener diode could have caused the over-voltage event that occurred on January 18,
2007.
The failed circuit board was one of two circuit boards commercially purchased in 1973
that were evaluated by the CNS staff as acceptable for use in safety related applications
without obtaining reasonable assurance that the parts were of sufficient quality to
support safety-related diesel generator functions. After the failure mode was identified,
the team challenged the licensee regarding the treatment of the spare circuit board still
in the warehouse. The licensee subsequently placed the spare circuit board in a
blocked status pending further testing or evaluation of its level of quality.
-9- Enclosure
6.0 Procurement of Spare Voltage Regulator Card
a. Inspection Scope
The team reviewed the quality assurance controls associated with the voltage regulator
printed circuit board that contained the failed zener diode. Specifically, the team
reviewed pertinent procurement documents and quality assurance program guidance to
determine whether the requirements of 10 CFR 50 Appendix B, Quality Assurance
Criteria for Nuclear Power Plants and Fuel Reprocessing Plants, were satisfied.
b. Findings
Introduction. The team identified an apparent violation of 10 CFR Part 50, Appendix B,
Criterion V, Instructions, Procedures, and Drawings, involving the failure to establish
appropriate procedural controls for evaluating the use of parts of indeterminate quality
prior to their installation in safety-related applications. This deficiency resulted in the
installation of a defective voltage regulator circuit board in EDG 2 that failed after 35
hours of operation.
Description. On January 18, 2007, approximately three hours and thirteen minutes into
a loaded surveillance run, EDG 2 experienced an automatic trip because of a voltage
regulator printed circuit board failure. The licensees root cause report, documented in
CR-CNS-2007-00480, determined that the cause of the failure was that the original
procurement process did not provide technical requirements to reduce the probability of
infant mortality failure in the voltage regulator board. The board had been installed in
EDG 2 on November 11, 2006, as corrective maintenance to repair a failure of a
potentiometer on the previously installed circuit board.
The licensee determined that the failed circuit board had been purchased from the
Basler Electric Company in 1973, but that the procurement of the part had not specified
any technical requirements from the vendor. In effect, the part was purchased as a
commercial grade item from a non-Appendix B source and placed into storage as an
essential component, ready for use in safety-related applications, without any
documentation of its suitability for that purpose. The licensee determined that the
specification of proper technical requirements, such as inspections and/or testing, would
have provided an opportunity to discover the latent defect prior to installing the card in
an essential application.
The team noted that in February 1992, the NRC had conducted an inspection at CNS to
review the implementation of Nebraska Public Power Districts (NPPD) programs for the
procurement and dedication of commercial grade items used in safety-related
applications. The results, documented in NRC Inspection Report 05000298/1992-201,
consisted of several identified deficiencies of the CNS quality assurance program.
These deficiencies described that NPPD had been purchasing commercial grade items
and dedicating them based solely on a part number verification, and warehousing these
parts as ready for essential use. The report stated this practice was insufficient to
-10- Enclosure
provide reasonable assurance that the parts were suitable for essential applications, and
as a result, parts of indeterminate quality had been inappropriately labeled as essential.
In response to these deficiencies, CNS made improvements to the existing quality
assurance program and performed a review of all commercial grade procurements
made during the period of the inspection (January 1990 through February 1992). The
team noted these process improvements failed to address that substandard qualification
of essential components potentially occurred since new construction, and that any
essential parts commercially procured prior to 1990, were potentially of indeterminate
quality. This resulted in the licensees failure to establish procedural controls to evaluate
the adequacy of these previously procured commercial grade parts that were deemed
acceptable for use in safety related applications.
The team reviewed the current requirements of Administrative Procedure 0.40.4,
Planning, Revision 2 and Site Services Procedure 1-CNS-MP-115, Material Issues
and Staging, Revision 6. Procedure 0.40.4 establishes the steps taken by work
planners to select the correct quality class part for a given work order, and provides
instructions for planners if the required part safety classification does not match the
available asset. Procedure 1-CNS-MP-115 defines the activities taken by the
warehouse personnel to verify that parts obtained from the warehouse satisfy the
requirements identified by the work planners. These program requirements included
checks for shelf life, post work testing, and other appropriate barriers. However, as
previously discussed, neither procedure evaluated the use of parts that were
inadequately procured for use in safety related applications prior to 1990. On the basis
of the deficiencies in the CNS procurement program previously identified by the NRC,
and a review of site quality procedures, the team determined that the licensee had failed
to establish appropriate procedural controls for evaluating the use of parts of
indeterminate quality prior to their installation in safety-related applications.
The team noted that if the licensee had implemented administrative controls to review
the suitability of pre-1990 procurement items prior to their use in safety-related
applications, then the licensee could have had the opportunity to discover the
inadequate measures taken to qualify the voltage regulator circuit boards for essential
applications. Given this information, the licensee could have either procured a new
board from an essential source, or dedicated the old part using Engineering Procedure
3-CNS-DC-138.2, Dedication. Procedure 3-CNS-138.2 directs the user to Engineering
Procedure 3-CNS-DC-138, Technical Evaluation Process, for the identification of
critical characteristics important to provide reasonable assurance that a part is ready for
essential use. Attachment 3 to Procedure 3-CNS-DC-138 provides examples of
appropriate critical characteristics, one of which is a burn-in endurance test. The team
reviewed industry standards for such tests, including MIL-STD-750D, Department of
Defense Test Method Standard for Semiconductor Devices, which recommends a
96 hour0.00111 days <br />0.0267 hours <br />1.587302e-4 weeks <br />3.6528e-5 months <br /> burn in test. Given that the voltage regulator card failed after approximately 35
hours of service, the team concluded that a burn-in or other equivalent test would have
given CNS the opportunity to discover the latent defect. To better understand current
CNS standards for acceptance of safety-related electrical components, the inspectors
reviewed Change Evaluation Document (CED) 6017822, that is being implemented to
install new circuit cards in the Average Power Range Monitor system. Purchase
-11- Enclosure
Order 4500055181 procured the new circuit cards and imposed a burn-in test prior to
shipment. The team also noted that the non-safety related electrical components for
CEDs 6010820 and 6016542, being implemented to install new reactor water level and
feedwater control systems, have been energized on site for testing for over one year in
an attempt to complete logic verification and identify latent defects.
The team noted that the failure to evaluate these parts of indeterminate quality resulted
in the failure to identify the latent defect in the voltage regulator circuit board in EDG 2.
Specifically, this deficiency resulted in installing a voltage regulator circuit board of
indeterminate quality in EDG 2 on November 11, 2006, that experienced an infant
mortality failure after 35 hours4.050926e-4 days <br />0.00972 hours <br />5.787037e-5 weeks <br />1.33175e-5 months <br /> of operation on January 18, 2007.
Analysis: This finding is considered to be a performance deficiency because the
licensee failed to establish appropriate procedural guidance to ensure that commercially
procured components are of sufficient quality prior to their installation in safety related
applications. This finding is more than minor because it is associated with the
equipment performance attribute of the Mitigating Systems cornerstone and adversely
affects the cornerstone objective of ensuring the availability, reliability, and capability of
systems that respond to initiating events.
The team evaluated the issue using the Significance Determination Process (SDP)
Phase 1 Screening Worksheet provided in Manual Chapter 0609, Appendix A,
"Significance Determination of Reactor Inspection Findings for At-Power Situations."
The screening indicated that a Phase 2 analysis was required because the finding
represents a loss of safety function for EDG 2 for greater than its Technical
Specification allowed completion time. The Phase 2 and 3 evaluations preliminarily
concluded that the finding was of low to moderate safety significance (See Attachment 3
for details).
Enforcement: 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and
Drawings, requires, in part, that activities affecting quality shall be prescribed by
procedures of a type appropriate to the circumstances and shall include appropriate
acceptance criteria for determining that important activities have been satisfactorily
completed. Contrary to this, the licensee failed to establish appropriate procedural
controls for evaluating the use of parts of indeterminate quality prior to their installation
in safety-related applications. This deficiency resulted in the installation of a voltage
regulator circuit board of indeterminate quality in EDG 2 that prematurely failed after 35
hours of operation. This issue was entered into the licensee's corrective action program
as CR-CNS-2007-00480. Pending determination of the findings final safety
significance, this finding is identified as Apparent Violation (AV) 05000298/2007007-
001, "Inadequate Procedures Result in Failure of Emergency Diesel Generator Voltage
Regulator."
-12- Enclosure
7.0 Review of EDG 2 Maintenance Procedures
a. Inspection Scope
The team assessed the maintenance procedures and work orders used to perform
preventive and corrective maintenance activities on EDG 2 between 2005 and the failure
on January 18, 2007. In addition to reviewing the written procedures, the team
interviewed procedure writers and maintenance technicians to determine if the work
instructions provided were adequate to achieve their intended objectives.
b. Findings
Introduction: The team identified three examples of a Green noncited violation (NCV) of
TS 5.4.1.a regarding inadequate maintenance procedures associated with EDG 2.
Description: Maintenance Procedure (MP) 7.3.8.2, Diesel Generator Electrical
Examination and Maintenance, is performed by the licensee approximately every
eighteen months and is intended to perform inspections and preventive maintenance on
engine and generator electrical components. This procedure was conducted on EDG 2
on March 14, 2006, and November 8, 2006. MP 7.3.8.2, Revision 19, contained a
specific section on voltage regulator maintenance that included instructions to check
lugs and screw terminals for tightness and integrity. The team noted that the scope of
the voltage regulator checks was limited to only those components within the voltage
regulator cabinet. This deficiency prevented maintenance technicians from identifying
that loose terminal screws existed on the voltage regulator OFF-MANUAL-AUTO switch
(OMAS) because it is physically located on the EDG 2 metering panel. These loose
terminal connections were discovered during troubleshooting efforts following the
January 18, 2007, failure of EDG 2. The licensee demonstrated that these loose
terminations represented a degraded condition that could cause an over-voltage event
similar in nature to that experienced on January 18, 2007. MP 7.3.8.2 was inadequate
in that it did not contain sufficient procedural guidance to identify the degraded
conditions in voltage regulator system components outside the voltage regulator
cabinet. The licensee documented this performance deficiency in CR-CNS-2007-00794.
In the second example, WO 4514076 was planned for the RE23 refueling outage as an
assigned corrective action from CR-CNS-2006-2729. The intent of the work order was
to perform a thorough inspection of EDG 2 voltage regulator system components to
identify the cause of continued voltage and reactive load perturbations experienced
during surveillance testing. WO 4514076 contained specific instructions for checking
the integrity of electrical connections in the EDG 2 voltage regulator cabinet and
metering panel. On the basis of interviews conducted with the system engineer who
wrote the work instructions, the team learned the engineer had intended for the
maintenance personnel to specifically check the terminal screws on the OMAS switch
for tightness. The guidance to perform this check was contained in a note at the front of
the procedure and not in the individual work order step for the switch. As a result, the
OMAS switch connections were not checked for tightness, resulting in another missed
opportunity to discover the loose terminal connections on the switch. The licensee
documented this performance deficiency in CR-CNS-2007-01021.
-13- Enclosure
In the third example, WO 4514076 contained inadequate instructions for tuning the EDG
2 voltage regulator during the RE23 refueling outage. On November 11, 2006, the
printed circuit board in the EDG 2 voltage regulator was replaced to correct a degraded
potentiometer. WO 4514076 contained instructions for tuning the new voltage regulator
card following installation, but was inadequate in that it contained acceptance criteria
that were inappropriate for the voltage regulators installed at CNS. The instructions
directed maintenance personnel to adjust the R13 potentiometer to obtain quarter wave
dampening in the EDG output voltage response. The technicians noted that adjusting
R13 did not change the amplitude of the sinusoidal response, and determined that the
acceptance criteria in WO 4514076 could not be satisfied. Technicians then set the
R13 potentiometer resistance on the new card to the same value as found on the old
card. During subsequent measurements of the voltage regulator response, the
technicians noted that the time required for the output voltage to oscillate through one
complete cycle had increased from 3.1 to 3.8 seconds. The technicians accepted this
new response characteristic without any engineering evaluation, procedural guidance, or
vendor technical reference demonstrating its acceptability. A subsequent evaluation
performed by engineering demonstrated that this change did not interfere with the safety
function of the EDG. Additionally, EDG 2 experienced an over-voltage trip on November
13, 2006, during the tuning process. In condition report CR-CNS-2006-9096, the
licensee documented the apparent cause of the EDG trip as the erratic behavior of one
or both of the potentiometers on the voltage regulator card and went on to explain that
industry operating experience and vendors both recognize that this over-voltage trip
could have been caused by the tuning process. The corrective actions proposed in the
apparent cause report included improvements to the EDG voltage regulator tuning
process and additional training for maintenance personnel performing the activity. The
licensee documented this procedural inadequacy in CR-CNS-2007-1307.
Analysis: The performance deficiency associated with this finding involved the
licensees failure to provide adequate instructions for performing maintenance on
EDG 2. The finding is more than minor because it is associated with the Mitigating
Systems cornerstone attribute of procedure quality and affects the associated
cornerstone objective to ensure the availability, reliability, and capability of systems that
respond to initiating events. Specifically, the performance deficiency resulted in: (1) the
failure to discover a degraded condition in the EDG 2 voltage regulator, and (2) an over-
voltage trip during the tuning of EDG 2 on November 13, 2006. Using the Manual
Chapter 0609 Appendix G, "Shutdown Operations Significance Determination Process,"
Phase 1 Checklist, the finding is determined to have very low safety significance
because one operable diesel generator was still capable of supplying power to the class
1E electrical power distribution subsystems.
This finding has a cross-cutting aspect in the area of human performance in that the
licensees procedures were not complete and provided inadequate instructions for
persons conducting maintenance on safety related equipment.
Enforcement. Technical Specification 5.4.1.a requires that written procedures be
established, implemented, and maintained, covering the activities specified in
Regulatory Guide 1.33, Revision 2, Appendix A, dated February 1978. Regulatory
Guide 1.33, Appendix A, Section 9 (a), requires that maintenance affecting the
-14- Enclosure
performance of safety-related equipment should be performed in accordance with
written procedures. Contrary to this, Maintenance Procedure 7.3.8.2 and Work Order 4514076 did not contain adequate instructions to identify the degraded condition of the
EDG 2 OFF-MANUAL-AUTO switch. In addition, Work Order 4514076 did not contain
adequate instructions for the tuning of EDG 2 following the replacement of the voltage
regulator printed circuit board, resulting in an over-voltage trip of EDG 2 on November
13, 2006. Because the finding is of very low safety significance and has been entered
into the licensees corrective action program in Condition Reports CR-CNS-2007-00794,
CR-CNS-2007-01021, and CR-CNS-2007-01307, this violation is being treated as an
NCV consistent with Section VI.A of the Enforcement Policy: NCV 05000298/2007007-
002, "Inadequate Procedures for Conducting Maintenance on Emergency Diesel
Generator 2.
8.0 Long-Term Corrective Actions
The team interviewed system and design engineering personnel to ascertain the long
term plans the licensee intends to implement to improve EDG electrical performance.
The licensee has already implemented measures to improve their ability to monitor EDG
performance during surveillance testing through the installation of special test
equipment. Future plans include installation of permanent external test connections to
minimize the unavailability time required to hook up the test equipment for each
scheduled surveillance.
The licensee has initiated actions to establish technical requirements for burn-in or other
equivalent testing for safety-related DG system circuit boards. Additionally, the licensee
plans to define other safety related systems with circuit boards that need similar
treatment.
The licensee also plans to implement several modifications to improve EDG reliability in
upcoming refueling outages. The changes include installation of a digital MOP during
the next refueling outage and replacement of the entire voltage regulator system with a
digital system in the subsequent outage.
9.0 Potential Generic Issues
The team noted that CNS submitted an operating experience report to alert the industry
of the potential failure of zener diodes in Basler SBSR voltage regulators. The team did
not identify any potentially generic issues during the inspection.
-15- Enclosure
4OA6 Meetings, Including Exit
On February 1, 2007, the preliminary results of this inspection were presented to
Mr. M. Colomb and other members of his staff who acknowledged the findings.
Following additional in-office reviews, the final results of the inspection were presented
to Mr. Colomb and his staff on April 24, 2007. The team confirmed that the supporting
details in this report contained no proprietary information.
ATTACHMENT 1: SUPPLEMENTAL INFORMATION
ATTACHMENT 2: SPECIAL INSPECTION CHARTER
ATTACHMENT 3: SIGNIFICANCE DETERMINATION EVALUATION
-16- Enclosure
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee Personnel
M. Bergmeier, Operations Support Group Supervisor
D. Buman, System Engineering Manager
K. Cohn, Engineering Support
M. Dickerson, Design Engineering
J. Flaherty, Licensing Engineer
P. Fleming, Licensing Manager
C. Gaedeke, Maintenance
T. Hottovy, Equipment Reliability Manager
J. Larson, Quality Assurance Supplier Supervisor
M. McCormack, Electrical Systems/I&C Engineering Supervisor
E. McCutchen, Regulatory Affairs Senior Licensing Engineer
M. Metzger, System Engineer
B. Morris, Maintenance Support Superintendent
R. Noon, Root Cause Team Leader, Corrective Action & Assessments
S. Norris, Assistant Operations Manager
R. Rexroad, System Engineering
K. Sutton, Risk Management Supervisor
D. Willis, Operations Manager
NRC Personnel
S. Graves, Reactor Inspector
M. Haire, Enforcement Specialist
R. McIntyre, Quality & Vendor Branch A
R. Pettis, Quality & Vendor Branch A
P. Prescott, Quality & Vendor Branch A
S. Rutenkroger, PHD, Reactor Inspector
S. Schwind, Senior Resident Inspector
N. Taylor, Resident Inspector
D. Thatcher, Chief, Quality & Vendor Branch A
A1-1 Attachment 1
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
05000298/2007007-01 AV Inadequate Procedures Result in Failure of Emergency
Diesel Generator Voltage Regulator
Opened and Closed
05000298/2007007-02 NCV Inadequate Procedures for Conducting Maintenance on
LIST OF ACRONYMS
AV Apparent Violation
CFR Code of Federal Regulations
CNS Cooper Nuclear Station
CR condition report
EDG emergency diesel generator
FMEA failure modes and effects analysis
KVAR kilovolt-ampere-reactive
MOP motor operated potentiometer
MP maintenance procedure
NCV noncited violation
NPPD Nebraska Public Power District
NRC U.S. Nuclear Regulatory Commission
OMAS off-manual-auto switch
PM preventive maintenance
RE23 refueling outage 23
SBSR series boost static regulator
SDP significance determination process
WO work order
LIST OF DOCUMENTS REVIEWED
Procedures Reviewed:
Administrative Procedure 0.40.4, Planning, Revision 2
Site Service Procedure 1-CNS-MP-15, Material Issues and Staging, Revision 6
Engineering Procedure 3-CNS-DC-138, Technical Evaluation Process, Revision 1
Engineering Procedure 3-CNS-DC-138.2, Dedication, Revision 1
A1-2 Attachment 1
Quality Assurance Instruction QAI-9, Guidelines for Establishing Quality Classifications of
Components and Materials, Draft 10/3/73
Condition Reports:
CR-CNS-2005-00938, CR-CNS-2005-07806, CR-CNS-2005-08336, CR-CNS-2006-02091, CR-
CNS-2006-02140, CR-CNS-2006-00279, CR-CNS-2006-02963, CR-CNS-2006-05149, CR-
CNS-2006-08798, CR-CNS-2006-08999,CR-CNS-2006-09096, CR-CNS-2006-09301, CR-
Work Orders:
4338439, 4424754, 4458094, 4472125, 4499755, 4514076, 4536182, 4535878, 4536371,
4548656, 4548698, 4548841, 4548860, 4551090
Controlled Drawings:
Basler Electric Company drawing 9032100910, Revision N01
Basler Electric Company drawing 9072400910, Revision N03
14EK-0144, Rev. N17
BR 3012, Sheet #3, Rev. N17
BR 3012, Sheet #6, Rev. N15
0223R0558, Sheet #33, Rev. N22
14DK0921, Rev. N01
BR 3257, Sheet 48H, Rev. N01
BR 3251, Sheet 11, Rev. N17
G5-262-743, Sheet 10A, Rev. N03
Miscellaneous Documents:
Purchase Order 73440, September 21, 1973
Nonconformance Report 002, October 27, 1973
Purchase Order 75149, November 15, 1973
Certificate of Compliance for Purchase Order 75149, December 3, 1973
CNS Vendor Manual VM-0246 [Basler Type SBSR HV Series Boost Exciter-Regulator]
A1-3 Attachment 1
Instruction Manual SM-100, Synchronous Motors, Generators, D.C. Exciters & Brushless
Equipment, Ideal Electric (no date)
Memo from Ideal Electric and Manufacturing Company to Cooper Bessemer Company, dated
8-28-70 (provided specific ratings for CNS generators)
CNS Design Criteria Document, DCD-1, Diesel Generators
EPRI Technical Report 1011110, Basler SBSR Voltage Regulators for Emergency Diesel
Generators, Final Report, November 2004
NUREG/CR-6819, Vol. 1, Common-Cause Failure Event Insights, Emergency Diesel
Generators
NRC Information Notice 96-23, Fires in Emergency Diesel Generator Exciters During
Operation Following Undetected Fuse Blowing, April 22, 1996
IEEE Standard 336-1971, Installation, Inspection and Testing Requirements for
Instrumentation and Electric Equipment During The Construction of Nuclear Power Generating
Stations
A1-4 Attachment 1
SPECIAL INSPECTION CHARTER
January 25, 2007
MEMORANDUM TO: Nicholas H. Taylor, Resident Inspector, Cooper Nuclear Station
Project Branch C, Division of Reactor Projects
Dr. Scott P. Rutenkroger, Reactor Inspector
Engineering Branch 1, Division of Reactor Safety
FROM: Arthur T. Howell III, Director, Division of Reactor Projects /RA/ AVegel for
SUBJECT: SPECIAL INSPECTION CHARTER TO EVALUATE THE COOPER
NUCLEAR STATION EMERGENCY DIESEL GENERATOR FAILURE
A Special Inspection Team is being chartered in response to the Cooper Nuclear Station
emergency diesel generator (EDG) failure. The EDG failed during surveillance testing on
January 18, 2007. You are hereby designated as the Special Inspection Team members.
Mr. Taylor is designated as the team leader. The assigned senior reactor analyst (SRA) to
support the team is Mike Runyan.
A. Basis
On January 18, 2007, during performance of a monthly surveillance test, Emergency
Diesel Generator 2 automatically isolated from the electrical bus following an over-
current condition. The licensee determined this condition resulted from a high voltage
condition. The licensee has preliminarily identified the cause of the failure to be either:
(1) a loose electrical connection affecting the voltage regulator circuit, or (2) a latent
failure of the voltage regulator printed circuit board. The licensee has experienced
previous voltage regulator problems, resulting in replacement of EDG 2 voltage
regulator components during the last refueling outage (RE23). The most recent failure
of EDG 2, and previous licensee efforts to identify and correct EDG 2 voltage regulator
problems, draws into question the effectiveness of the licensees corrective actions.
Additionally, prior to the failure on January 18, 2007, EDG voltage regulator
troubleshooting and postmaintenance activities have resulted in additional automatic trips due to high voltage conditions.
This Special Inspection Team is chartered to review the circumstances related to
historical and present EDG 2 voltage regulator problems and assess the effectiveness
of the licensees actions for resolving these problems. The team will also assess the
effectiveness of the immediate actions taken by the licensee in response to the EDG 2
failure that occurred on January, 18, 2007.
A2-1 Attachment 2
B. Scope
The team is expected to address the following:
1. Develop an understanding of the EDG degraded conditions and failures related
to voltage regulator problems.
2. Assess licensee effectiveness in identifying previous EDG voltage regulator
problems, evaluating the cause of these problems, and implementation of
corrective actions to resolve identified problems.
3. Identify and assess additional actions planned by the licensee in response to the
declining performance of the EDG 2 voltage regulator, including the timeline for
completion of these actions.
4. Assess the licensees root cause evaluation, the extent of condition, and the
licensees common mode evaluation.
5. Evaluate pertinent industry operating experience and potential precursors to the
January 18 event, including the effectiveness of licensee actions taken in
response to the operating experience.
6. Determine if there are any potential generic issues related to the failure of the
EDG 2 voltage regulator. Promptly communicate any potential generic issues to
Region IV management.
7. Determine if the Technical Specifications were met when the EDG failed.
8. Collect data as necessary to support a risk analysis.
C. Guidance
Inspection Procedure 93812, Special Inspection, provides additional guidance to be
used by the Special Inspection Team. Your duties will be as described in Inspection
Procedure 93812. The inspection should emphasize fact-finding in its review of the
circumstances surrounding the event. It is not the responsibility of the team to examine
the regulatory process. Safety concerns identified that are not directly related to the
event should be reported to the Region IV office for appropriate action.
The Team will report to the site, conduct an entrance, and begin inspection no later than
January 28, 2007. While on site, you will provide daily status briefings to Region IV
management, who will coordinate with the Office of Nuclear Reactor Regulation, to
ensure that all other parties are kept informed. A report documenting the results of the
inspection should be issued within 30 days of the completion of the inspection.
This Charter may be modified should the team develop significant new information that
warrants review. Should you have any questions concerning this Charter, contact me at
(817) 860-8144.
A2-2 Attachment 2
SIGNIFICANCE DETERMINATION EVALUATION
Significance determination process Phase 1:
In accordance with NRC Inspection Manual Chapter 0609, Appendix A, Significance
Determination of Reactor Inspection Findings for At-Power Situations, the inspectors
conducted a significance determination Phase 1 screening and determined that the
finding resulted in loss of the safety function of Emergency Diesel Generator 2 for
greater than the Technical Specification allowed completion time. Therefore, a
Significance Determination Process Phase 2 evaluation was required.
Significance determination process Phase 2:
In accordance with Manual Chapter 0609, Appendix A, Attachment 1, User Guidance
for Determining the Significance of Reactor Inspection Findings for At-Power
Situations, the inspectors evaluated the EDG 2 failure using the Risk-Informed
Inspection Notebook for Cooper Nuclear Station, Revision 2.
Assumptions
1. The Phase 2 analysis assumed that the EDG 2 was unable to perform its
function beginning on November 16, 2006. This date assumes that the failure of
the voltage regulator was a run-time degradation (consistent with the licensees
root cause) and recognizes that in the licensees risk model EDG 2 must be
capable of providing its safety function for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following an accident. This
resulted in an applied exposure time of 64 days.
2. Recovery credit was not appropriate due to the lack of a useable procedure or
operator training in operating the EDG 2 voltage regulator in the manual mode
during a loss of offsite power.
3. The loss of EDG 2 affects the full mitigation credit for other safety functions on
the Loss of Offsite Power worksheet (reference special useage rule 1.6).
4. Phase 2 Analysis Results: The Phase 2 analysis indicated that the significance
of the finding was potentially Greater than Green. The dominant accident
sequence involved a loss of offsite power with recovery within the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> life of
the CNS batteries, and a loss of offsite power without high pressure injection and
recovery within one hour. Completion of all applicable sequences in the Loss of
Offsite Power worksheet resulted in one sequence with a score of 8, three
sequences with a score of 7 and one sequence with a score of 6. Based on this
result the issue screened as White in the SDP Phase II analysis.
A3-1 Attachment 3
Significance determination process Phase 3:
The analyst estimated the risk increase resulting from the EDG 2 voltage regulator
failure. The diesel was run at the following times with durations reported as the period
of time that the voltage regulator was energized (all of these operational runs were
conducted after the performance deficiency occurred):
Date of EDG Run Duration of EDG Run
November 13, 2006 1 hr 30 min
November 14, 2006 6 hrs 46 min
November 15, 2006 1 hr 35 min
November 16, 2006 9 hrs 23 min
November 17, 2006 5 hrs 3 min
November 18, 2006 2 hrs 28 min
December 12, 2006 5 hrs 41 min
January 18, 2007 4 hrs 16 min (point of failure)
Assumptions:
1. It is assumed that the voltage regulator degraded only during times that it was
energized, which is closely correlated to engine runtime. This implies that no
degradation occurred while the EDG was secured and in a standby status. It is
further assumed that the failure was a deterministic outcome set to occur after a
specific number of operating hours. Therefore, it is assumed that EDG 2 would
have failed to run at four hours following a loss of offsite power (LOOP) demand
at any time during the 37 day period from its last successful surveillance test on
December 12, 2006, until the test failure that occurred on January 18, 2007.
Prior to this date, EDG 2 would have run and failed at 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> for the 24 day
period from November 18, 2006, to December 12, 2006. The EDG was run for
approximately 17 hours1.967593e-4 days <br />0.00472 hours <br />2.810847e-5 weeks <br />6.4685e-6 months <br /> in the two days preceding November 18, 2006. Because
very little exposure existed prior to November 18, 2006, this date is chosen as
the cutoff for this analysis.
2. The voltage regulator could not have been repaired in place or replaced with a
new unit in time to affect the outcome of any of the core damage sequences.
Also, procedures did not exist and training was not conducted to operate the
EDG in a manual voltage regulation mode. Therefore, it is assumed that the
EDG 2 voltage regulator failure would not have been recoverable for any
accident sequence.
A3-2 Attachment 3
3. For the purpose of this analysis, it is assumed that EDG 2 would not be
unavailable or fail to operate for the first four hours or 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> of its hypothetical
start demand during the 37 day and 24 day exposure periods, respectively. This
introduces a slight inconsistency to the risk estimate, but because it would
similarly affect both the base and current case, it does not significantly influence
the result of this analysis.
4. Common cause vulnerabilities for EDG 1 did not exist, that is, the failure mode is
assumed to be independent in nature. This is because the root cause
investigation determined that the failure was the result of an infant mortality of a
voltage regulator conponent, which had been installed for only two months. The
same component in EDG1 had been installed for several years and had
operated reliably beyond the "burn-in" period without experiencing failure from
manufacturing defects.
The CNS SPAR model, Revision 3.31, dated October 10, 2006, was used in the
analysis. A cutset truncation of 1.0E-12 was used. Average test and maintenance was
assumed.
To represent the assumed failure of EDG 2, the basic event EPS-DGN-FR-DG1B
(diesel generator 1B fails to run) was set to one. A flag set house event for DG1B out
of service was added to the EDG1B fault tree and set to FALSE in the base case, and
TRUE in the current case in order to remove non-minimal cutsets. Also, the common
cause probability for fail-to-run events was restored to its nominal value.
Internal Events Analysis:
A. Risk Estimate for the 37-day period between December 12, 2006 and
January 18, 2007:
During this exposure period, EDG 2 is assumed to have been capable of running for
four hours. The LOOP frequency used in the analysis was adjusted to reflect the
situation that only LOOPs with durations greater than four hours would result in a risk
increase attributable to the voltage regulator failure. The base LOOP frequency is
3.59E-2/yr. The 4-hour non-recovery of offsite power is 0.1566. The 4-hour non-
recovery of diesel generators is 0.4835. To account for having only one EDG to recover
during the first four hours (since recovery of EDG 2 is assumed to be running during the
first four hours of the event), the EDG non-recovery factor was adjusted to the square
root of the base non-recovery factor. This adjusts the recovery from a one out of two
EDG recovery to a one out of one recovery. This factor is (0.4835)1/2 = 0.695. Therefore
the adjusted LOOP frequency, representing the frequency of LOOPs that are not
recovered in four hours by either restoring offsite power or recovering a failure of EDG 1
is 3.59E-2(0.1566)(0.695) = 3.91E-3/yr. For the base case, the adjusted LOOP
frequency considers that both EDGs are hypothetically recoverable. Therefore the base
case LOOP frequency is 3.59E-2(0.1566)(0.4835) = 2.72E-3/yr.
A3-3 Attachment 3
Resetting event time t=0 to four hours following the LOOP event requires that the
recovery factors for offsite power and the EDGs be adjusted. For example, in two hour
sequences in SPAR, the basic event for non-recovery of offsite power should be
adjusted to the non-recovery at 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, given that recovery has failed at four hours.
An adjustment to account for the diminishment of decay heat must be considered. This
is because the magnitude of decay heat at four hours following shutdown is less than in
the early moments following a reactor trip, and the timing of core damage sequences is
affected by this fact. In the SPAR model, recovery times for either offsite power, EDGs,
or both are set at the intervals of 30 minutes, two hours, four hours, eight hours, and ten
hours. The analyst determined that the average decay heat level in the first 30 minutes
is approximately two times the average level that exists between four and five hours
following shutdown. Therefore, baseline 30-minute SPAR model sequences, that
essentially account for boil-off to fuel uncovery were adjusted to one hour sequences.
The two hour sequences model safety relief valve failures to close, and are based more
on inventory control than core heat production. Therefore, no adjustment was made for
these sequences. The analyst determined that decay heat rates leveled out quickly
following shutdown and could find no basis for adjusting the times associated with the
four, eight, and ten hour sequences.
The following table presents the adjusted offsite power non-recovery factors for the
event times that are relevant in the SPAR core damage cutsets:
SPAR SPAR base SPAR base SPAR base Modified
recovery offsite power offsite power offsite power SPAR
time non-recovery non-recovery at non-recovery at recovery
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> + SPAR (Column 4
recovery time in divided by
Column 1 Column 3)
30 min. 0.7314 0.1566 0.12051 0.769
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.3181 0.1566 0.09637 0.615
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.1566 0.1566 0.06718 0.429
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.06718 0.1566 0.04040 0.258
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.05070 0.1566 0.03346 0.214
1. A SPAR recovery time of 1.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> is used, as discussed above, to account for the lessening of decay heat.
The following table presents the analogous non-recovery factor adjustments for EDG 1
recovery times for the current case (it is assumed that EDG 2 is not recoverable):
A3-4 Attachment 3
SPAR SPAR base non- SPAR base SPAR base Modified
recovery recovery for two EDG non- EDG non- SPAR
time EDGs recovery at 4 recovery at 4 recovery
hours for 1 EDG hours + SPAR (Column 4
(square root of recovery time in divided by
0.4835) Column 1 Column 3)
(square root)
30 min. 0.8570 0.695 0.6511 0.937
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.6482 0.695 0.612 0.881
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.4835 0.695 0.544 0.783
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.2959 0.695 0.439 0.632
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.2374 0.695 0.397 0.571
1. A SPAR recovery time of 1.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> is used, as discussed above, to account for the lessening of decay heat.
The following table presents the EDG non-recoveries used for the base case (both
EDGs are assumed available for recovery in the base case):
SPAR SPAR base non- SPAR base SPAR base Modified
recovery recovery for two EDG non- EDG non- SPAR
time EDGs recovery at 4 recovery at 4 recovery
hours hours + SPAR (Column 4
recovery time in divided by
Column 1 Column 3)
30 min. 0.8570 .4835 0.42401 0.877
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.6482 .4835 0.3742 0.774
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.4835 .4835 0.2959 0.612
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.2959 .4835 0.1926 0.398
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.2374 .4835 0.1576 0.326
1. A SPAR recovery time of 1.0 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> is used, as discussed above, to account for the lessening of decay heat.
The SPAR base case was updated to reflect the new LOOP frequency and non-
recovery times for offsite power and EDGs (column 5 figures).
The SPAR base case update result, after applying the applicable revised LOOP
frequency and offsite power and EDG recovery figures, was 1.039E-5/yr. The current
case result, with the EDG 2 fail-to-run set to one and the flag set house event set to
TRUE, and the changed recoveries inserted for offsite power and the EDGs was
5.373E-5/yr.
A3-5 Attachment 3
Therefore, the estimated ICCDP of the 37-day period during which EDG 2 was assumed
to be in a condition that guaranteed its failure at four hours is (5.373E-5/yr. - 1.039E-
5/yr.) (37 days/365 days/yr.) = 4.4E-6/yr.
B. Risk Estimate for the 24-day period between November 18, 2006 and
December 12, 2006:
During this exposure period, EDG 2 is assumed to have been capable of running for 10
hours. The LOOP frequency used in the analysis was adjusted to reflect the situation
that only LOOPs with durations greater than 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> would result in a risk increase
attributable to the voltage regulator failure. The base LOOP frequency is 3.59E-2/yr.
The 10-hour non-recovery of offsite power is 5.070E-2. The 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> non-recovery of
diesel generators is 0.2374. To account for having only one EDG to recover during the
first 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> (since recovery in this analysis only applies to the postulated failure of
EDG 1), the EDG non-recovery factor was adjusted to the square root of the base non-
recovery factor. This adjusts the recovery from a one out of two EDG recovery to a one
out of one recovery. This factor is (0.2374)1/2 = 0.487. Therefore, the adjusted LOOP
frequency, representing the frequency of LOOPs that are not recovered in ten hours by
either restoring offsite power or recovering a failure of EDG 1, is 3.59E-2(5.070E-
2)(0.487) = 8.86E-4/yr. For the base case, the adjusted LOOP frequency considers that
both EDGs are hypothetically recoverable. Therefore, the base case LOOP frequency
is 3.59E-2(5.070E-2)(0.2374) = 4.32E-4/yr.
The analyst considered an adjustment to account for the diminishment of decay heat as
in the four hour case above. The analyst determined that the average decay heat level
in the first 30 minutes is approximately three times the average level that exists between
10 and 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> following shutdown. Therefore, the baseline 30 minute SPAR models,
that essentially account for boil-off to fuel uncovery were adjusted to 1.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />
sequences. The two hour sequences model safety relief valve failures to close, and are
based more on inventory control than core heat production. Therefore, no adjustment
was made for these sequences. Sequences of four and eight hours were increased by
30 minutes each, but no change was made to the 10 hour1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> sequences.
The following table presents the adjusted offsite power non-recovery factors for the
event times that are relevant in the SPAR core damage cutsets:
A3-6 Attachment 3
SPAR SPAR base SPAR base SPAR base Modified
recovery offsite power offsite power offsite power SPAR
time non-recovery non-recovery at non-recovery at recovery
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> + (Column 4
SPAR recovery divided by
time in Column Column 3)
1
30 min. 0.7314 0.0507 0.04271 0.842
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.3181 0.0507 0.0404 0.797
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.1566 0.0507 0.03212 0.633
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.06718 0.0507 0.02412 0.475
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.05070 0.0507 0.0220 0.434
1. A SPAR recovery time of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> is added to 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, as discussed above, to account for the falloff of decay heat.
2. The SPAR recovery time is increased by 30 minutes, as discussed above.
The following table presents the analogous non-recovery factor adjustments for EDG 1
recovery times:
SPAR SPAR base non- SPAR base SPAR base Modified
recovery recovery for two EDG non- EDG non- SPAR
time EDGs recovery at 10 recovery at 10 recovery
hours for 1 EDG hours + SPAR (Column 4
(square root of recovery time in divided by
0.2374) Column 1 Column 3)
(square root)
30 min. 0.8570 0.4872 0.4511 0.926
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.6482 0.4872 0.439 0.901
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.4835 0.4872 0.3882 0.796
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.2959 0.4872 0.3212 0.659
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.2374 0.4872 0.300 0.616
1. A SPAR recovery time of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> is added to 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, as discussed above, to account for the falloff of decay heat.
2. The SPAR recovery time is increased by 30 minutes, as discussed above.
The following table presents the EDG recoveries used for the base case (both EDGs are
assumed available for recovery in the base case):
A3-7 Attachment 3
SPAR SPAR base non- SPAR base SPAR base Modified
recovery recovery for two EDG non- EDG non- SPAR
time EDGs recovery at 10 recovery at 10 recovery
hours for 1 EDG hours + SPAR (Column 4
recovery time in divided by
Column 1 Column 3)
30 min. 0.8570 0.2374 0.20301 0.855
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 0.6482 0.2374 0.1926 0.811
4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> 0.4835 0.2374 0.15022 0.633
8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> 0.2959 0.2374 0.10302 0.434
10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br /> 0.2374 0.2374 0.0898 0.378
1. A SPAR recovery time of 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> is added to 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />, as discussed above, to account for the falloff of decay heat.
2. The SPAR recovery time is increased by 30 minutes, as discussed above.
The SPAR base case was updated to reflect the new LOOP frequency and non-
recovery times for offsite power and EDGs (column 5 figures).
The SPAR base case update result, after applying the applicable revised LOOP
frequency and offsite power and EDG recovery figures, was 1.008E-5/yr. The current
case result, with the EDG 2 fail-to-run set to one and the flag set house event set to
TRUE and the changed recoveries inserted for offsite power and the EDGs, was
2.830E-5/yr.
Therefore, the estimated ICCDP of the 24-day period during which EDG 2 was assumed
to be in a condition that guaranteed its failure at 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, is (2.830E-5/yr. - 1.008E-5/yr.)
(24 days/365 days/yr.) = 1.2E-6/yr.
Total Internal Events Result:
Exposure Period
37-Day (12/12/06 - 01/18/07) 4.4E-6/yr.
24-Day (11/18/06 - 12/12/06) 1.2E-6/yr.
Total Internal Events Result 5.6E-6/yr.
Sensitivity of EDG 2 Recovery:
In the analysis presented above, it was assumed that EDG 2 could not be recovered in
time to lower the risk of the relevant core damage sequences. This was because the
failed voltage regulator could not be repaired or replaced quickly and operation of the
emergency diesel generator in a manual voltage regulation mode was not a subject of
operator training and not explicitly expressed in plant procedures. As a sensitivity to this
assumption, a low bounding (highest allowance for recovery) case for operating the
A3-8 Attachment 3
EDG in manual voltage regulation mode was considered using the SPAR-H
methodology. The results of this analysis are presented in the table below.
Performance Diagnosis (0.01) Action (0.001)
Shaping Factor
Available Time Extra Time (0.1) >5 Times Required (0.1)
Stress High (2) High (2)
Procedures Incomplete (20) Incomplete (20)
Experience/Training Low (10) Low (3)
Total1 0.288 0.012
Overall Total HRA 0.3
1. This reflects the result using the formula for cases where 3 or more negative PSFs are present.
The nominal time for performing the actions was small compared to the minimum time
of four hours available to restore power following failure of EDG 2 at four hours into the
event. The Class 1E batteries are capable of supplying eight hours of power. For the
core damage sequences that comprise most of the risk relative to this finding, it is
assumed that EDG 1 fails initially and the Division 1 battery begins to deplete. Division
1 dc is necessary for control of the RCIC system. EDG 2 is assumed to fail after four
hours of run time, and therefore the Division 1 batteries have four hours of remaining
capacity at this time. Therefore, extra credit for time available was applied for both
diagnosis and action. High stress was assumed because the station would be in a
blackout condition. Procedures for manual operation were not available, but credit for
incomplete procedures was applied as a bounding assumption. Low training and
experience was assumed because the plant staff had not performed this mode of
operation and had not received training.
The result of the SPAR-H analysis was a failure probability of 0.3. Although there are
some short-term sequences in the SPAR results, corresponding to the failure of dc-
powered high pressure injection sources, their contribution to core damage was less
than two percent of the total risk. Therefore, for the purposes of this sensitivity
assessment, as an adequate first-order approximation, the non-recovery probability of
0.3 was applied to every core damage sequence. The result is presented in the
following table:
Exposure Period
37-Day (12/12/06 - 01/18/07) 1.3E-6/yr.
24-Day (11/18/06 - 12/12/06) 3.6E-7/yr.
Total Internal Events Result 1.7E-6/yr.
A3-9 Attachment 3
External Events:
The risk increase from fire initiating events was reviewed and determined to have a
small impact on the risk of the finding. Only two fire scenarios were identified where
equipment damage could cause a LOOP to occur. One was a control room fire that
affected either Vertical Board F or Board C. The second was a fire in the Division 2
critical switchgear. For the control room fires, the scenario probabilities are remote
because of the confined specificity of their locations and the fact that a combination of
hot shorts of a specific polarity are needed to cause a LOOP. In addition, recovery from
a LOOP induced in this manner would be likely to succeed because a minimum of four
hours would be available (based on an 8-hour battery capacity and a four hour depletion
of the Division 1 battery that provides power to the reactor core isolation cooling system)
prior to the EDG 2 failure, power would presumably be available in the switchyard, and
the breaker manipulations needed to complete this task would be possible and within
the capability of an augmented plant staff that would respond to the event.
The other class of fires that would result in a LOOP were those that require an
evacuation of the control room. In this case, plant procedures require offsite power to
be isolated from the vital buses and the preferred source of power, the Division 2 EDG,
is used to power the plant. With the assumption that the Division 2 EDG will fail four
hours into the event, a station blackout would occur at this time. The sequences that
could lead to core damage would include a failure of the Division 1 EDG, such that
ultimate success in averting core damage would rely on recovery of either EDG or of
offsite power. A review of the onsite electrical distribution system did not reveal any
particular difficulties in restoring switchyard power to the vital buses in this scenario,
especially given that at least four hours are available to accomplish this task.
In general, the fire risk importance for this finding is small compared to that associated
with internal events because onsite fires do not remove the availability of offsite power in
the switchyard, whereas, in the internal events scenarios, long-term unavailability of
offsite power is presumed to occur as a consequence of such events as severe weather
or significant electrical grid failures.
The CNS IPEEE Internal Fire Analysis screened the fire zones that had a significant
impact on overall plant risk. When adjusted for the exposure period of this finding, the
cumulative baseline core damage frequency for the zones that had the potential for a
control room evacuation (and a procedure-induced LOOP) or an induced plant centered
LOOP was approximately 3.6E-7/yr. The methods used to screen these areas were not
rigorous and used several bounding assumptions. The analyst qualitatively assumed
that the increase in risk from having EDG 2 in a status where it is assumed to fail at four
hours would likely be somewhat less than one order of magnitude above the baseline, or
3.6E-6/yr. This is easily demonstrated by an assumption that failure to re-connect
offsite power within a period of at least four hours is well less than 10 percent. Based
on these considerations, the analyst concluded that the risk related to fires would not be
sufficiently large to change the risk characterization of this finding.
The seismicity at CNS is low and would likely have a small impact on risk for an EDG
issue.
A3-10 Attachment 3
As a sensitivity, data from the RASP External Events Handbook was used to estimate
the scope of the seismic risk particular to this finding. The generic median earthquake
acceleration assumed to cause a loss of offsite power is 0.3g. The estimated frequency
of earthquakes at CNS of this magnitude or greater is 9.828E-5/yr. The generic median
earthquake frequency assumed to cause a loss of the diesel generators is 3.1g, though
essential equipment powered by the EDGs would likely fail at approximately 2.0g. The
seismic information for CNS is capped at a magnitude of 1.0g with a frequency of
8.187E-6. This would suggest that an earthquake could be expected to occur with an
approximate frequency of 9.0E-5/yr that would remove offsite power but not damage
other equipment important to safe shutdown. In the internal events discussion above, it
was estimated that LOOPs that exceeded four hours duration would occur with a
frequency of 3.91E-3/yr. Most LOOP events that exceed the four hour duration would
likely have recovery characteristics closely matching that from an earthquake. The ratio
between these two frequencies is 43. Based on this, the analyst qualitatively concluded
that the risk associated with seismic events would be small compared to the internal
result.
Flooding could be a concern because of the proximity to the Missouri River. However,
floods that would remove offsite power would also likely flood the EDG compartments
and therefore not result in a significant change to the risk associated with the finding.
The switchyard elevation is below that of the power block by several feet, but it is not
likely that a slight inundation of the switchyard would cause a loss of offsite power. The
low frequency of floods within the thin slice of water elevations that would remove offsite
power for at least four hours, but not render the diesel generators inoperable, indicates
that external flooding would not add appreciably to the risk of this finding.
Based on the above, the analyst determined that external events did not add
significantly to the risk of the finding.
Large Early Release Frequency:
In accordance with Manual Chapter 0609, Appendix A, Attachment 1, Step 2.6,
"Screening for the Potential Risk Contribution Due to LERF," the analyst reviewed the
core damage sequences to determine an estimate of the change in large early release
frequency caused by the finding.
The LERF consequences of this performance deficiency were similar to those
documented in a previous SDP Phase 3 evaluation regarding a misalignment of gland
seal water to the service water pumps. The final determination letter was issued on
March 31, 2005 and is located in ADAMS, Accession No. ML050910127. The following
excerpt from this document addressed the LERF issue:
The NRC reevaluated the portions of the preliminary significance determination related
to the change in LERF. In the regulatory conference, the licensee argued that the
dominant sequences were not contributors to the LERF. Therefore, there was no
change in LERF resulting from the subject performance deficiency. Their argument was
A3-11 Attachment 3
based on the longer than usual core damage sequences, providing for additional time to
core damage, and the relatively short time estimated to evacuate the close in population
surrounding Cooper Nuclear Station.
LERF is defined in NRC Inspection Manual Chapter 0609, Appendix H, Containment
Integrity Significance Determination Process as: the frequency of those accidents
leading to significant, unmitigated release from containment in a time frame prior to the
effective evacuation of the close-in population such that there is a potential for early
health effect. The NRC noted that the dominant core damage sequences documented
in the preliminary significance determination were long sequences that took greater than
12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> to proceed to reactor pressure vessel breach. The shortest calculated interval
from the time reactor conditions would have met the requirements for entry into a
general emergency (requiring the evacuation) until the time of postulated containment
rupture was 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The licensee stated that the average evacuation time for CNS,
from the declaration of a General Emergency was 62 minutes.
The NRC determined that, based on a 62-minute average evacuation time, effective
evacuation of the close-in population could be achieved within 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Therefore, the
dominant core damage sequences affected by the subject performance deficiency were
not LERF contributors. As such, the NRCs best estimate determination of the change
in LERF resulting from the performance deficiency was zero.
In the current analysis, the total contribution of the 30-minute sequences to the current
case CDF is only 0.17% of the total. For two hour sequences, the contribution is only
0.04 percent. That is, almost all of the risk associated with this performance deficiency
involves sequences of duration four hours or longer following the loss of all ac power.
Based on the average 62 minute evacuation time as documented above, the analyst
determined that large early release did not contribute to the significance of the current
finding.
References:
GE-NE-E1200141-04R2, Table 5-1, Shutdown Power at Cooper Nuclear Station
(proprietary)
Green Screen Source Data, External Events PRA model, Nine Mile Point, Unit 1
NUREG/CR-6890, Reevaluation of Station Blackout Risk at Nuclear Power Plants,
Analysis of Loss of Offsite Power Events: 1986-2004"
A3-12 Attachment 3