ML032100780

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IR 05000269-03-003, IR 05000270-03-003, IR 05000287-03-003, on 04/06 - 06/28/2003, Duke Energy Corp; Oconee Nuclear Station; Maintenance Effectiveness, Personnel Performance During Non-routine Plant Evolutions, and Other Activities
ML032100780
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 07/28/2003
From: Haag R
NRC/RGN-II/DRP/RPB1
To: Rosalyn Jones
Duke Energy Corp
References
IR-03-003
Download: ML032100780 (42)


See also: IR 05000269/2003003

Text

July 28, 2003

Duke Energy Corporation

ATTN: Mr. R. A. Jones

Site Vice President

Oconee Nuclear Station

7800 Rochester Highway

Seneca, SC 29672

SUBJECT: OCONEE NUCLEAR STATION - NRC INTEGRATED INSPECTION

REPORT 05000269/2003003, 05000270/2003003, AND 05000287/2003003

Dear Mr. Jones:

On June 28, 2003, the NRC completed an inspection at your Oconee Nuclear Station. The

enclosed report documents the inspection findings which were discussed on July 1, 2003, with

you and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

Based on the results of this inspection, there were four NRC-identified findings of very low

safety significance (Green). These findings were determined to involve violations of NRC

requirements. However, because of their very low safety significance and because they have

been entered into your corrective action program, the NRC is treating these issues as a non-

cited violations (NCVs), in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

Additionally, one licensee-identified NCV is listed in Section 4OA7 of this report. If you contest

any of the NCVs in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the United States Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the

Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Oconee facility.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

DEC 2

(ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Robert Haag, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Docket Nos.: 50-269, 50-270, 50-287

License Nos.: DPR-38, DPR-47, DPR-55

Enclosure: NRC Integrated Inspection Report 05000269/2003003, 05000270/2003003, and

05000287/2003003 w/Attachment - Supplemental Information

cc w\encl.:

L. E. Nicholson R. Mike Gandy

Compliance Manager (ONS) Division of Radioactive Waste Mgmt.

Duke Energy Corporation S. C. Department of Health and

Electronic Mail Distribution Environmental Control

Electronic Mail Distribution

Lisa Vaughn

Legal Department (ECIIX) County Supervisor of

Duke Energy Corporation Oconee County

422 South Church Street 415 S. Pine Street

Charlotte, NC 28242 Walhalla, SC 29691-2145

Anne Cottingham Lyle Graber, LIS

Winston and Strawn NUS Corporation

Electronic Mail Distribution Electronic Mail Distribution

Beverly Hall, Acting Director M. T. Cash, Manager

Division of Radiation Protection Nuclear Regulatory Licensing

N. C. Department of Environmental Duke Energy Corporation

Health & Natural Resources 526 S. Church Street

Electronic Mail Distribution Charlotte, NC 28201-0006

Henry J. Porter, Director Peggy Force

Div. of Radioactive Waste Mgmt. Assistant Attorney General

S. C. Department of Health and N. C. Department of Justice

Environmental Control Electronic Mail Distribution

Electronic Mail Distribution

DEC 3

Distribution w/encl:

L. Olshan, NRR

A. Hiser, NRR

L. Slack, RII, EICS

RIDSNRRDIPMLIPB

PUBLIC

OFFICE RII:DRP RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE MXS1 GAH2 ETR MSL1 for MSL1 for MSL1 for DWJ

NAME MShannon GHutto ERiggs SVias MScott JBlake DJones

DATE 7/28/2003 7/28/2003 7/28/2003 7/24/2003 7/24/2003 7/24/2003 7/28/2003

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

OFFICE RII:DRS RII:DRS RII:DRS RII:DRS

SIGNATURE GWL1 REC1 MSL1 for MSL1 for

NAME GLaska RCarroll RMaxey RCortes

DATE 7/24/2003 7/28/2003 7/24/2003 7/24/2003

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

PUBLIC DOCUMENT YES NO

OFFICIAL RECORD COPY DOCUMENT NAME: C:\ORPCheckout\FileNET\ML032100780.wpd

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-269, 50-270, 50-287

License Nos: DPR-38, DPR-47, DPR-55

Report No: 50-269/03-03, 50-270/03-03, 50-287/03-03

Licensee: Duke Energy Corporation

Facility: Oconee Nuclear Station, Units 1, 2, and 3

Location: 7800 Rochester Highway

Seneca, SC 29672

Dates: April 6, 2003 - June 28, 2003

Inspectors: M. Shannon, Senior Resident Inspector

A. Hutto, Resident Inspector

E. Riggs, Resident Inspector

J. Blake, Senior Project Manager (Section 1R08)

D. Jones, Senior Health Physicist (Section 4OA5.1D)

G. Laska, Operator Licensing Examiner (Section 1R11.2)

M. Scott, Senior Reactor Inspector (Sections 1R02 and 1R17)

K. Maxey, Reactor Inspector (Sections 1R02 and 1R17)

R. Cortes, Reactor Inspector (Sections 1R02 and 1R17)

S. Vias, Senior Reactor Inspector (Sections 1R02, 1R17 and

40A5.1A-C)

R. Carroll, Senior Project Inspector (Sections 1R20)

Approved by: Robert Haag, Chief

Reactor Projects Branch 1

Division of Reactor Projects

Enclosure

CONTENTS

Page

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . S1

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R02 Evaluation of Changes, Tests, or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04 Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R05 Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R07 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R08 Inservice Inspection Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R11 Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7

1R12 Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R13 Maintenance Risk Assessments and Emergent Work Evaluations . . . . . . . . . 11

1R14 Personnel Performance During Non-routine Plant Evolutions . . . . . . . . 12

1R15 Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R17 Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R19 Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

1R20 Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1R22 Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 21

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 22

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

4OA7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 27

ATTACHMENT: SUPPLEMENTAL INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

List of Acronyms . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-7

SUMMARY OF FINDINGS

IR 05000269/2003-003, IR 05000270/2003-003, IR 05000287/2003-003; Duke Energy

Corporation; 04/06/2003 - 06/28/2003; Oconee Nuclear Station; Maintenance Effectiveness,

Personnel Performance During Non-routine Plant Evolutions, and Other Activities.

The inspection was conducted by the resident Inspectors and eight regional based inspectors:

one senior project manager; one senior project engineer; one senior health physicist; two senior

reactor inspectors; one operator licensing examiner; and two reactor inspectors. The

inspectors identified four Green findings, which were identified as NCVs. The significance of

most findings is indicated by their color (Green, White, Yellow, Red) using IMC 0609,

Significance Determination Process (SDP). Findings for which the SDP does not apply may

be Green or be assigned a severity level after NRC management review. The NRC's program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Action, was identified by the inspectors for failure to promptly identify the degraded

standby shutdown facility (SSF) diesel cooling water seals in the problem investigation

process (PIP) program.

This finding was considered to be more than minor based on the fact that subsequent

analysis of the grommets noted significant degradation and this analysis would likely not

have been performed without initiation of the PIP. Therefore, if the cause of the

degradation was left uncorrected, the mitigation systems cornerstone objective of

ensuring the continued reliability of equipment needed to respond to initiating events

would be affected. In addition, continued degradation of the grommets would become a

more significant safety concern. This issue was considered to be of low safety

significance (Green) because the grommets were replaced during the SSF diesel

overhaul before they failed in service. (Section 1R12.2)

Criterion XVII Quality Assurance Records, was identified by the inspectors for failure to

maintain sufficient records [logs] to furnish evidence of activities affecting quality [TS

Limiting Conditions for Operation (LCOs)]. Specifically, operator logs provided

insufficient data to reconstruct the activities related to the June 22, 2003, Unit 1

Engineered Safeguards (ES) power supply failure, which affected the Engineered

Safeguards Protection System (ESPS) Digital Automatic Actuation Logic Channels 2, 4,

6, and 8.

The ESPS automatic initiation of ES functions to mitigate accident conditions is

assumed in the accident analysis and is required to ensure that consequences of

analyzed events do not exceed the accident analysis predictions. The failure to

adequately document TS LCO entry and action times for the failed automatic ES

actuation circuitry was considered to be more than minor because it impacted the

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operators ability to accurately implement the TS LCO action statements, and if left

uncorrected, this type of improper documentation could become a more significant

safety concern. The finding was considered to be of very low safety significance based

on the fact that the ES power supply was returned to service before any LCO condition

would have required the unit to be in Mode 3. (Section 1R14b.(1))

  • Green. A NCV of TS 3.3.7 Condition A , Engineered Safeguards Protection System

(ESPS) Digital Automatic Actuation Logic Channels, was identified by the inspectors

when it was discovered that the licensee failed to declare a number of ES configured

system components inoperable following the loss of ESPS digital channels 2, 4, 6, and

8.

The ESPS automatic initiation of ES functions to mitigate accident conditions is

assumed in the accident analysis and is required to ensure that consequences of

analyzed events do not exceed the accident analysis predictions. Consequently, this

issue is more than minor, in that by not recognizing the importance of the lost automatic

ES initiation function and taking the compensatory actions of TS 3.3.7, the mitigating

systems cornerstone objective of ensuring the continued reliability of equipment needed

to respond to initiating events was affected. However, this issue was determined to be

of very low safety significance, based on the fact that there was no loss of function of

the Low Pressure Service Water system or the Keowee Hydro Units resulting from the

loss of ESPS Digital Automatic Actuation Logic Channels 2, 4, 6, and 8. Additionally,

the ES power supplies were restored and digital channels returned to service prior to

exceeding any TS allowed outage times for the affected components. (Section

1R14b.(2))

Cornerstone: Initiating Events

identified by the inspectors, in that measures taken to preclude the installation of non-

conforming replacement parts and the ability to evaluate the suitability of replacement

during the Quality Assurance (QA) receipt inspection process were not adequate.

Specifically, this was identified for inadequate QA review during receipt inspections that

resulted in the licensee installing one non-conforming Control Rod Drive Mechanisms

(CRDM) (Split Nut) Flange Ring on Unit 2, and discovering, prior to the installation in

Unit 3, 68 CRDMs and 552 CRDM Hold Down Bolts that did not meet the design and

procurement specifications.

This finding was more than minor because non-conforming material was actually

installed in Unit 2. However, it was determined to be of very low safety significance

because there was not a loss of system function. (Section 40A5.1C)

B. Licensee Identified Violations

One violation of very low safety significance, which was identified by the licensee has

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensees corrective action program. This violation is listed

in Section 4OA7.

Report Details

Summary of Plant Status:

Unit 1 operated at 100 percent rated thermal power (RTP) during the inspection period except

for one power reduction. The unit was reduced to approximately 50 percent RTP on May 17,

2003, following a safety group 4 dropped rod. The rod was recovered and the unit was

returned to 100 percent RTP on May 18, 2003.

Unit 2 operated at 100 percent RTP during the inspection period except for two power

reductions. The unit was reduced to approximately 88 percent RTP on April 13, 2003, to

perform turbine valve movement testing. The unit was returned to 100 percent power later that

same day. On June 22, 2003, the unit was reduced to approximately 87 percent RTP to again

perform turbine valve movement testing. The unit was returned to 100 percent power later that

same day.

Unit 3 entered the report period at 93 percent RTP with an end of core life coastdown in

progress. The unit was shutdown on April 26, 2003, for a refueling outage. Following the

outage, the unit entered Mode 1 on June 14, 2003, and reached 100 percent RTP on June 18,

2003. On June 28, 2003, the unit was reduced to 15 percent RTP and the turbine taken off-line

for turbine balancing. The report period ended with the unit at 15 percent RTP.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R02 Evaluations of Changes, Tests or Experiments

a. Inspection Scope

The inspectors reviewed selected samples of evaluations to confirm that the licensee

had appropriately considered the conditions under which changes to the facility,

Updated Final Safety Analysis Report (UFSAR), or procedures may be made, and tests

conducted, without prior NRC approval. The inspectors reviewed evaluations for nine

changes and additional information, such as calculations, supporting analyses, the

UFSAR, and drawings to confirm that the licensee had appropriately concluded that the

changes could be accomplished without obtaining a license amendment. The nine

evaluations reviewed are listed in the Attachment to this report.

The inspectors also reviewed samples of changes such as design changes, UFSAR

changes, commercial grade dedication packages, equipment problem issues, and like-

for-like evaluations for which the licensee had determined that evaluations were not

required, to confirm that the licensees conclusions to screen out these changes were

correct and consistent with 10CFR50.59. The twenty-one screened out changes

reviewed are listed in the List of Documents Reviewed.

The inspectors also reviewed an audit of the 10CFR50.59 process and selected

Problem Investigation Process reports (PIPs) to confirm that problems were identified at

2

an appropriate threshold, were entered into the corrective action process, and

appropriate corrective actions had been initiated.

b. Findings

(1) Introduction: One Unresolved Item (URI) was identified in that potentially the air

temperature inside of the units control room boards (vertical and unit boards) may reach

a higher than anticipated value than previously understood during design basis events.

Description: During the review of an UFSAR change to Section 3.11.5, Loss of

Ventilation, the inspectors observed the control room area temperature maximum was

stated to be 120 degrees F. The section did not address control board interior

temperature rise nor did it discuss the maximum value that could be reached inside

boards for the discussed event. The inspectors realized that other events not discussed

in the reviewed section could cause a loss of forced ventilation to the boards. When the

licensee was informed that the heat generating temperature sensitive electronics interior

to the boards may see a higher temperature than the control room ambient temperature,

PIP O-03-04052 was written on the issue. During normal operations, Technical

Specification (TS) 3.7.16 limits the control room general area temperature to 80

degrees F.

The temperature difference between the ambient control room temperature and the

interior temperature of the boards was not clearly documented. Forced ventilation to the

boards and to the control room is postulated to be lost during such events as loss of

offsite power and seismic occurrences. There is a degraded control room ventilation

abnormal procedure. All related event and abnormal procedures do not address control

board interior temperatures nor do they have special instructions for reducing the interior

temperature of the boards during the loss of forced ventilation cooling. With the loss of

forced ventilation, a rise in temperature inside the board may occur and this rise may be

greater than that experienced in the control room inhabited space where control room

temperature is measured. Such a rise may be detrimental to critical electronic

equipment operation.

The aforementioned PIP stated that there was reasonable assurance that the equipment

inside of the control boards is operable during the event scenarios. This was based on

calculations that determined that the general area temperature rise after six hours would

be approximately 90 degrees F (calculation OSC-6667). The licensee stated that the

most limiting equipment in the boards has continuous duty temperature of 122 degrees

F, which is 32 degrees F higher than the six hour rise value. The event and abnormal

procedures are written to limit the time without forced ventilation. Further, the licencee

indicated in PIP O-00-4643, that the time required to restore cooling following a loss of

offsite power event was estimated to be less than 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. PIP O-03-4052 indicated

that an operability evaluation would be performed to further investigate the relationship

between the temperature inside the main control boards and the control rooms on all

three units.

The inspectors were aware that there are some passive vents and holes in the top of the

control boards and louvers on the side of the boards could possibly dissipate board

interior heat buildup. Further, the inspectors were aware of procedures and equipment

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in other locations that could be relied upon for safe shutdown purposes should the

abandonment of the control room be required.

However, the following issues require additional review by the licensee: an

understanding of the peak temperature reached in each unique control cabinet in each

control room space; the critical electronic components needed for plant operation during

the postulated events; the suitability of equipment in the control boards to withstand

environmental temperature such as records documenting the component vendors

continuous duty temperatures for the considered critical parts; and, critical components

locations relative to possible warm spots on the boards should also be understood

(board thermal profile relative to component location).

Until the licensee can demonstrate a clear understanding of the thermal effects on

control room board components during a postulated loss of control board forced cooling

occurrence, this issue will be identified as URI 05000269,270,287/2003003-001:

Control Room Board Component Thermal Reliability.

(2) Introduction: An URI was identified concerning Oconee UFSAR Section 3.6.1.3 that was

changed on May 17, 2001, under the old 50.59 program revision. During a review of the

change, the inspectors were concerned that the change may involve an unreviewed

safety question (USQ) under the old rule or a departure from a method of evaluation

under the new rule.

Discussion: The UFSAR change was associated with high energy line break (HELB) on

a main feedwater line. The escaping water/steam is assumed to disable the 4160 Volt

breakers for at least the motor driven emergency feedwater (EFW) pumps and for the

high pressure injection HPI pumps. The change increased the time allowed for initiation

of EFW and (HPI) after the HELB from 15 minutes to 30 minutes and from 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to 8

hours, respectively.

The 1998 UFSAR version used RETRAN program analysis and the lower equipment

recovery times that kept the reactor coolant system (RCS) subcooled and capable of

natural circulation (minimally voided) due to the small amount of water loss. Under the

May 2001 revision, the licensee used RELAP 5 program and extended times for

equipment recovery of EFW and HPI. This results in significant voiding in the RCS, loss

of subcooling, increased number of cycles of the pressurizer safety valves, loss of

natural circulation, and reliance on the boiler/condenser mode (BCM) of decay heat

removal for up to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> without safety injection. Under BCM, the expansion and

collapsing of the RCS remaining volume would cause some pressure spikes within the

RCS. This evaluation was based on licensee calculation OSC-7299, Revision 1. Page

4 of the 10 CFR 50.59 evaluation discusses RELAP5 in that:

The analytical model utilized to evaluate these effects was changed from RETRAN

to RELAP5 because of the significant RCS voiding that will occur and the

importance of boiler condenser mode of decay heat removal. The version of

RELAP5 used is similar [to] a version approved by the NRC for use by Frametone

Technologies in small break loss of coolant accident (SBLOCA) UFSAR analysis of

OTSG plants. Additionally, the NRC has approved this version for use by Duke

4

Power Company in both SBLOCA and large break loss of coolant accident

(LBLOCA) mass and energy release analysis. The additional delays in EFW and

HPI restoration result in a transient that is essentially a small break LOCA.

The inspectors were concerned that this change appears to represent an USQ, as

defined by the previous version of 10 CFR 50.59. (The evaluation was completed under

the old 10 CFR 50.59 rule on May 17, 2001, and the licensee implemented the revised

rule on July 2, 2001). In this scenario, the pressurizer safety valves are challenged to lift

and reseat multiple times while passing steam and then water until EFW is recovered.

The licensee did not consider that the increased number of cycles of these valves would

increase the probability of a malfunction (i.e., sticking open) and create the possibility of

an accident of a different type (loss of coolant). With a stuck open valve and no safety

injection, core damage would result. The licensees evaluation states that RELAP 5 has

been approval for LOCA analysis, but it is not clear as to the acceptability of this method

of evaluation for HELB. Furthermore the concept of allowing the RCS to become

significantly voided, saturated, without natural circulation, without HPI for eight hours,

and reliance on BCM for decay heat removal, appears to be a departure from a method

of evaluation as described in the UFSAR, which would require prior NRC approval under

the current regulation. Until the NRC completes its review of the above issue, it will be

identified as URI

05000269,270,287/2003003-002: HELB Accident Scenario Review.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted partial equipment alignment walkdowns to evaluate the

operability of selected redundant trains or backup systems while the other train or

system was inoperable or out of service. The walkdowns included, as appropriate,

reviews of plant procedures and other documents to determine correct system lineups

and verification of critical components to identify any discrepancies which could affect

operability of the redundant train or backup system. The following systems were

included in this review:

  • Unit 2 HPI trains 2A and 2B while the 2C HPI pump was out of service for preventive

maintenance

  • Unit 2 train A low pressure injection (LPI) while the B train of LPI was out of service

for maintenance

  • Units 1 and 2 primary instrument air system with the backup instrument air

compressor out of service for preventive maintenance

b. Findings

No findings of significance were identified.

5

.2 Complete System Walkdown.

a. Inspection Scope

The inspectors conducted a detailed review of the alignment and condition of the Unit 3

component cooling (CC) system. The inspectors utilized licensee procedures and other

documents listed in the Attachment to verify proper system alignment.

The inspectors also verified electrical power requirements, labeling, hangers, support

installation, and associated support system status. The operating pump was examined

to ensure that any noticeable vibration was not excessive, bearings were not hot to the

touch, and the pump was adequately ventilated. The walkdown also included an

evaluation of the system piping and supports against the following considerations:

  • Piping and pipe supports did not show evidence of water hammer
  • Hangers were properly sized and were within the setpoints
  • Piping insulation was adequate and showed no evidence of prior system leaks
  • Component foundations were not degraded

A review of PIPs and maintenance work orders was performed to verify that material

condition deficiencies did not significantly affect the ability of the CC system to perform

its design functions and that appropriate corrective action was being taken by the

licensee.

The inspectors also held discussions with the system and design engineers on

temporary modifications, future modifications, and operator workarounds to ensure that

the impact on the equipment functionality was properly evaluated.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

a. Inspection Scope

The inspectors conducted tours in thirteen areas of the plant to verify that combustibles

and ignition sources were properly controlled, and that fire detection and suppression

capabilities were intact. The inspectors selected the areas based on a review of the

licensees safe shutdown analysis and the probabilistic risk assessment based

sensitivity studies for fire related core damage sequences. Inspection of the following

areas were conducted during this inspection period:

  • Units 1 and 2 and Unit 3 HPI Rooms (2)
  • Units 1, 2 and 3 Equipment Rooms (3)

6

  • Units 1, 2 and 3 LPI/RBS Rooms (5)
  • Keowee Hydro Units (2)
  • Unit 2 Turbine Building Switchgear Area (1)

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

.1 Unit 3 Low Pressure Injection System Cooler Test

a. Inspection Scope

The inspectors reviewed TT/3/A/0150/061, Unit 3 Low Pressure Injection System Cooler

Test, used to gather data for the LPI cooler performance evaluation. This testing was

performed to ensure that the cooler is able to meet TS and design basis requirements.

The inspection focused on compliance with the procedure requirements and appropriate

data collection during the testing. The inspectors also reviewed design calculation

OSC - 4338 Revision 7, to ensure that the LPI heat exchanger, based on the test data,

was capable of performing its design function per the calculation.

b. Findings

No findings of significance were identified.

.2 Unit 1 Reactor Building Cooling Units (RBCU) Performance Test

a. Inspection Scope

The inspectors reviewed Unit 1 RBCU Performance Test, PT/0/A/0160/006, used to

gather data for the RBCU performance evaluation. This testing was performed to verify

that the RBCU cooling capacity meets TS and design basis requirements. The

inspection focused on compliance with the procedure requirements and appropriate

data collection during the testing. The inspectors also reviewed design calculation

OSC - 5665, Attachment 27, which calculated the RBCU capacity factors from the

obtained test data.

b. Findings

No findings of significance were identified.

7

1R08 Inservice Inspection (ISI) Activities

a. Inspection Scope

Unit 3 Steam Generator (SG) Inspection

The inspectors reviewed the implementation of the licensees program for monitoring the

performance of the U3 once-through steam generators (OTSG). The inspector

observed examinations and reviewed selected inspection records for:

- Eddy current examination (ET) data for eleven OTSG tubes.

- Tube plugging operations including quality control verification of tube locations.

- In-situ pressure testing data used to evaluate SG tube structural and leak tight

integrity of thirteen SG tubes (twelve in SG A and one in SG B)

- Certifications for ten Quality Assurance (QA) Level III Eddy Current Data Analysts

- SG tube repair (plugging) lists generated as a result of the Unit 3 SG ET inspection.

The above activities and records were compared to the TS, License Amendments, and

applicable industry established performance criteria to verify compliance. Documents

reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Simulator Scenarios

a. Inspection Scope

The inspectors observed licensed operator simulator training on June 27, 2003. The

scenario involved a dropped rod, a reactor trip, a steam generator tube leak in the 1B

steam generator, and a main steam line break. The inspectors also observed entry into

the emergency action levels (Unusual Event and Alert). The inspectors observed crew

performance in terms of: communications; ability to take timely and proper actions;

prioritizing, interpreting, and verifying alarms; correct use and implementation of

procedures, including the alarm response procedures; timely control board operation

and manipulation, including high-risk operator actions; and oversight and direction

provided by the shift supervisor, including the ability to identify and implement

appropriate TS actions.

8

b. Findings

No findings of significance were identified.

.2 Annual Operating Test Results

a. Inspection Scope

Following the completion of the annual operating examination testing cycle, which ended

on May 9, 2003, the inspectors reviewed the overall pass/fail results of the biennial

written examination, the individual Job Performance Measure operating tests, and the

simulator operating tests administered by the licensee during the operator licensing

requalification cycle. These results were compared to the thresholds established in

Manual Chapter 609 Appendix I, Operator Requalification Human Performance

Significance Determination Process.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Maintenance Effectiveness Reviews

a. Inspection Scope

The inspectors reviewed the licensees effectiveness in performing routine maintenance

activities. This review included an assessment of the licensees practices pertaining to

the identification, scoping, and handling of degraded equipment conditions, as well as

common cause failure evaluations. For each item selected the inspectors performed a

detailed review of the problem history and surrounding circumstances, evaluated the

extent of condition reviews as required, and reviewed the generic implications of the

equipment and/or work practice problem. For those systems, structures, and

components (SSCs) scoped in the maintenance rule per 10 CFR 50.65, the inspectors

verified that reliability and unavailability were properly monitored and that 10 CFR 50.65

(a)(1) and (a)(2) classifications were justified in light of the reviewed degraded

equipment condition. The inspectors reviewed the following item:

PIP O-03-02888, Turbine Driven Emergency Feedwater Pump Steam Nozzle Bolt

Failure Issue

b. Findings

No findings of significance were identified.

9

.2 Effectiveness of Standby Shutdown Diesel Preventive Maintenance and Problem

Identification

a. Inspection Scope

The inspectors observed the 10-year overhaul of the Standby Shutdown Facility (SSF)

diesel, and selected for further review, those problems which were identified by outside

contractors. Specifically, the inspectors reviewed problems being identified by Engine

Service, Inc. contractors who were contracted by the licensee to provide technical

oversight for the 10-year overhaul of the SSF diesel engines and to assist with the

maintenance activities. For this inspection activity, the inspectors reviewed the daily

field service reports provided by the contractors to the licensee to evaluate the

adequacy of previous maintenance activities and to verify that problems identified by the

contractors were being appropriately documented in the licensees corrective action

program.

b. Findings

Introduction: Two separate issues were identified as a result of this inspection:

(1) A Green non-cited violation (NCV) was identified by the inspectors for failure to

promptly identify degraded SSF diesel cooling water seals in the PIP program.

(2) An URI was identified, in that the licensee failed to implement the 6-year

recommended diesel manufacturer (EMD) preventive maintenance grommet

replacements. Consequently, at 10 years some of the grommets were found to be

at or near failure. Failure of the grommets could have led to diesel coolant leaks

and loss of cooling to the diesel. This issue will remain unresolved pending

completion of a Phase 3 risk review.

Description: During the June 2002, SSF diesel overhaul, the inspectors discussed

diesel equipment problems with the maintenance contractors from Engine Systems, Inc.

(ESI) who were providing technical oversight for the SSF diesel overhaul. The day shift

ESI contractor noted that the SSF diesel coolant grommets, located on the cylinder

heads (power packs), had been found degraded. He informed the inspectors that this

adverse condition would be provided to the licensee in a daily field service report. The

inspectors subsequently discussed the degraded grommet condition with maintenance

management to ensure that they were aware of the potential problem. The June 18,

2002, ESI daily field service report documented that Cylinder 7 on Engine B, had

deformed grommets on the cylinder head, unable to determine if the deformities were

from overheating or from installation damage. The June 19, 2002, ESI daily field

service report documented that Cylinder 8 on Engine A, had deformed head

grommets.

On June 27, 2002, prior to returning the diesel to service and after noting that a PIP

report had not been initiated, the inspectors discussed the deformed grommet issue with

licensee management. On June 28, 2002, PIP O-02-03526 was initiated to capture the

potential degraded grommet condition.

10

Subsequent discussions with engineering noted that some of the deformed grommets

were going to be sent off for analysis. At this time, the inspectors also noted that the

grommets from Cylinder 7 on Engine B and Cylinder 8 on Engine A had not been

segregated from the grommets from the other 26 cylinders. It was also noted that the

licensee could not account for all of the replaced grommets, in that only 282 of the 336

replaced grommets could be located.

During various discussions regarding the grommets, the licensee noted that the diesel

manufacturer (EMD) had recommended a 6-year replacement interval for these

grommets. However, the grommets were being replaced on a 10-year interval and the

EMD owners group was discussing the possibility of EMD changing the replacement

interval to 12 years.

In October 2002, the remaining 282 grommets were sent off to ESI for analysis. On

May 8, 2003, the results of the ESI analysis were received by the licensee. The report

noted that Diesel engines used in standby service see thermal cycling which

contributes to the hardening of these grommets. Therefore, the recommended

replacement interval is on a 6 year calendar basis. ESIs analysis concluded the

following: 31 grommets were approaching the end of life; 6 grommets had been torn

during removal and that a new grommet cannot be readily torn by hand, the ability to

tear these grommets indicates their pliability has been compromised, likely due to aging

and their brittle nature indicates they were near the end of life; 43 grommets show a

high degree of brittleness and degradation, these are considered abnormal to a typical

reseal interval, It can be assumed these grommets were still capable of performing

their sealing function, and the state of brittleness and separation they exhibit indicates

they have exceeded their useful life; and last 19 grommets were distorted into a D

shape, considered to be classic examples of cylinder combustion leaks and with no

reported leaks, it must be assumed they performed their sealing function; however,

these grommets have exceeded their useful life. EMD went on to state that Continued

operation with grommets exposed to combustion gases will lead to failure and coolant

leaks.

EMD concluded the analysis with the following: Many of the components examined in

this investigation were at or near failure, and although no coolant leaks were reported,

combustion leaks were definitely occurring in some cylinders. Coolant leaks were likely

to follow, as those cylinders grommets exposed to combustion gases would have

continued to decay until their sealing ability was exhausted. EMD also stated that

Diesel engines in standby service experience more severe thermal cycling at each

surveillance run as compared to engines in continuous duty. This thermal cycling

promotes age-hardening in these seals, and the recommended 6-year maintenance

interval is a preventive maintenance practice that must be adhered to for continued

reliability.

Analysis

The issue of not initially writing a PIP to capture the ESI identified grommet degradation

was considered to be greater than minor based on the fact that subsequent analysis of

the grommets noted significant degradation and this analysis would likely not have been

performed without initiation of the PIP. Therefore, if the cause of the degradation was

11

left uncorrected, the mitigation systems objective of ensuring the continued reliability of

equipment needed to respond to initiating events would be affected. In addition,

continued degradation of the grommets would become a more significant safety

concern. This issue was considered to be of low safety significance (Green) because

the grommets were replaced during the SSF diesel overhaul before they failed in

service.

The issue of not performing the recommended grommet replacements was considered

to be more than minor in that the degraded grommets affected the equipment reliability

of a mitigation system (i.e., the SSF diesel). The finding was first evaluated in the

Phase 1 SDP based on the degraded reliability of a mitigating system under the Reactor

Safety Cornerstone. Based on the manufacturers conclusion that the grommets had

exceeded their useful life and that continued operation with grommets exposed to

combustion gases would lead to failure and coolant leaks, it was assumed that the

finding represented an actual loss of safety function of the SSF diesel, as the loss of

coolant could preclude operation of the diesel for its 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> mission time. Since this

system was designated as a risk significant system per 10 CFR 50.65, a Phase 2

analysis was performed. The Phase 2 analysis indicated that the issue could be greater

than Green; therefore, a Phase 3 analysis was required. Pending completion of the

Phase 3 analysis, the issue of not implementing the manufacturers recommendations

for replacement of the SSF diesel coolant grommets will be identified as URI

05000269,270,287/2003003-03: Failure to Implement Manufacturers Recommendations

for Replacement of SSF Diesel Coolant Grommets. This issue is in the licensees

corrective action program as PIP O-02-03526.

Enforcement

10 CFR 50, Appendix B, Criterion XVI, requires that measures shall be established to

assure that conditions adverse to quality, such as...deficiencies, deviations, defective

material and equipment, and non-conformances are promptly identified. The licensees

quality assurance (QA) program implements this requirement through Nuclear Station

Directive 208, Problem Investigation Process, Revision 22. Section 208.6, Problem

Identification, states that a PIP should be initiated within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of recognition of the

issue. Contrary to 10 CFR 50 Appendix B, Criterion XVI, following the June 19, 2002,

identification of the degraded grommets which could be the result of improper

installation, a PIP was not initiated until June 28, 2002, which was after all of the SSF

diesel grommets had been replaced. This inadequate corrective action issue is being

treated as an NCV, consistent with Section VI.A.1 of the enforcement policy and is

identified as NCV 05000269,270,287/2003003-04: Failure to Identify the SSF Degraded

Grommets as a Deficient Condition in the PIP Corrective Action Program. This issue is

in the licensees corrective action program as PIP O-02-03526.

1R13 Maintenance Risk Assessment and Emergent Work Evaluations

a. Inspection Scope

The inspectors evaluated, as appropriate for the selected SSCs listed below: (1) the

effectiveness of the risk assessments performed before maintenance activities were

conducted; (2) the management of risk; (3) that, upon identification of an unforseen

12

situation, necessary steps were taken to plan and control the resulting emergent work

activities; and (4) that maintenance risk assessments and emergent work problems

were adequately identified and resolved.

  • PIP O-03-3584, Unexpected Closure of 1HP-5 Letdown Isolation Valve, caused by

failure of an improperly installed control air solenoid

  • IP/0/A/2005/003, Keowee Hydro Station Westinghouse Voltage Regulator Test,

performed as part of troubleshooting for failed voltage regulator

  • PIP O-03-2925, Increased HPI Motor Cable Insulation Leakage
  • Preventive Maintenance on Unit 2 Electro Hydraulic Control (EHC) System per Work

Orders 98592430 and 98592429

  • PIP O-03-3800, Unit 3 RC-4 Power Operated Relief Valve (PORV) Block Valve

Leakage and Repair

opened when attempting to depressurize the steam generator

  • PIP O-03-04140, Identification of Risk Assessment Error for Previous Repair of

3RC-4. Credit was inappropriately given for availability of the steam generators

although the RCS loops were not filled.

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-routine Plant Evolutions

a. Inspection Scope

The inspectors reviewed, the operating crews performance during selected non-routine

events and/or transient operations to determine if the response was appropriate to the

event. As appropriate, the inspectors: (1) reviewed operator logs, plant computer data,

or strip charts to determine what occurred and how the operators responded;

(2) determined if operator responses were in accordance with the response required by

procedures and training; (3) evaluated the occurrence and subsequent personnel

response using the SDP; and (4) confirmed that personnel performance deficiencies

were captured in the licensees corrective action program. The non-routine evolution

reviewed during this inspection period included the following:

  • Loss of 700 Gallons of RCS in Unit 3 Due to Over-pressurization of LPI Suction (PIP

O-03-02362)

  • Unit 1 Dropped Rod and Subsequent Recovery
  • Failure of the Unit 1 Channel B Engineered Safeguards (ES) Power Supply

13

b. Findings

(1) Introduction: A Green NCV was identified by the inspectors for failure to maintain

sufficient records [logs] to furnish evidence of activities affecting quality [TS Limiting

Conditions In Operations (LCOs)].

Description: On June 22, 2003, the Unit 1 ES channel B power supply failed. This

failure, caused a loss of power to the Engineered Safeguards Protection System (ESPS)

Digital Automatic Logic Channels 2, 4, 6, and 8. Subsequently, the inspectors reviewed

the licensees operator logs and TS tracking systems. The inspectors noted that the

operator logs provided insufficient data to reconstruct the activities related to the ES

power supply failure. The inspectors noted that the documented time for declaring the

components related to ES channels 2, 4, 6, and 8 per TS 3.3.7, had been improperly

changed and backdated from 9:55 a.m. to 9:15 a.m. In addition, the time of discovery

of the failed power supply was backdated to 8:15 a.m., although the ES channel B

power supply was functioning properly at that time. The logs did not provide any

justification for this change. Also, the inspectors noted that the logs indicated the

control room operators were informed of the loss of power to the ES digital channels at

8:51 a.m.; however, the TS tracking documents noted that the ES digital channels

became inoperable at 8:55 a.m. The various times were considered to be important

because they provided evidence for activities associated with meeting the 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> action

statement of TS 3.3.7 for placing the associated components in their ES positions or

declaring the components inoperable.

Analysis: The ESPS automatic initiation of ES functions to mitigate accident conditions

is assumed in the accident analysis and is required to ensure that consequences of

analyzed events do not exceed the accident analysis predictions. The failure to

adequately document TS LCO entry and action times for the failed automatic ES

actuation circuitry was considered to be more than minor because it impacted the

operators ability to accurately implement the TS LCO action statements, and if left

uncorrected, this type of improper documentation could become a more significant

safety concern. The finding was considered to be of very low safety significance

(Green) based on the fact that the ES power supply was returned to service before any

LCO condition would have required the unit to be in Mode 3. This observation was

based on the inspectors review of the associated completed surveillances and use of

computer alarm summaries as a basis for the initial failure time.

Enforcement: TS 5.4.1 requires that written procedures be established, implemented,

and maintained covering activities related to procedures recommended in Regulatory

Guide 1.33 Rev. 2, Appendix A, 1978. Regulatory Guide 1.33, Section 1(g),

Administrative Procedures, requires log entries. 10 CFR 50, Appendix B, Criterion XVII,

Quality Assurance Records, requires that sufficient records shall be maintained to

furnish evidence of activities affecting quality. Contrary to the above, sufficient

logkeeping and TS tracking records were not sufficiently maintained to furnish evidence

of activities related to TS LCO action statements. Because the finding is of very low

safety significance and has been entered into the corrective action program as PIP O-

03-04408, this violation is being treated as NCV 05000269/2003003-05: Failure to

Maintain Sufficient Records (logs) to Furnish Evidence of Activities Affecting Quality (TS

LCOs).

14

(2) Introduction: A Green NCV of TS 3.3.7 Condition A , Engineered Safeguards Protection

System (ESPS) Digital Automatic Actuation Logic Channels, was identified by the

inspectors when it was discovered that the licensee failed to declare a number of ES

configured system components inoperable following the loss of ES digital channels 2, 4,

6, and 8 as required.

Description: As indicated in (1) above, the June 22, 2003, power supply failure of Unit 1

ES Analog Channel B resulted in the subsequent loss of Unit 1 ES Digital Actuation

Channels 2, 4, 6, and 8. Upon declaring one or more ES digital automatic actuation

logic channels inoperable, TS LCO 3.3.7 Condition A .1, requires that ES configured

components associated with that channel be placed in their ES configuration, or

Condition A.2 requires that the components associated with that channel be declared

inoperable. The inspectors determined that the licensee failed to either place the

affected components in their ES configuration or declare them inoperable within one

hour as required by the TS. Since placing the affected components in their ES

configuration would in this case violate unit safety or operational considerations, the

licensee was required to declare the components inoperable within one hour and enter

the associated component TS LCO. Specifically, the licensee failed to enter TS 3.3.17

Condition A, one channel of the emergency power switching logic (EPSL) automatic

transfer function inoperable [channel B from ES channel 2], TS 3.3.21 Condition A, one

channel of the EPSL Keowee Hydro Unit (KHU) emergency start function inoperable

[channel B from ES channel 2], and TS 3.7.7 Condition A, one required low pressure

service water (LPSW) pump inoperable [LPSW pump B from ES channel 4].

Analysis: The ESPS automatic initiation of ES functions to mitigate accident conditions

is assumed in the accident analysis and is required to ensure that consequences of

analyzed events do not exceed the accident analysis predictions. Consequently, this

issue is more than minor, in that by not recognizing the importance of the lost automatic

ES initiation function and taking the compensatory actions of TS 3.3.7, the mitigating

systems cornerstone objective was affected. However, this issue was determined to be

of very low safety significance (Green), based on the fact that there was no loss of

function of the LPSW system or the KHUs resulting from the loss of ESPS Digital

Automatic Actuation Logic Channels 2, 4, 6, and 8. Additionally, the ES power supplies

were restored and digital channels returned to service prior to exceeding any TS allowed

outage times for the affected components.

Enforcement: TS 3.3.7 Condition A .1 requires that ES configured components

associated with an inoperable ESPS Digital Automatic Actuation Logic Channel be

placed in their ES configuration, or TS 3.3.7 Condition A.2 requires that the components

associated with the inoperable channel be declared inoperable. Contrary to the above,

the licensee failed to place all effected ES components in their ES configuration or

declare the associated components inoperable following the loss of ES digital channels

2, 4, 6, and 8. Because this finding is of very low safety significance and has been

entered into the corrective action program as PIP O-03-04408, this violation is being

treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy. It will

be identified as NCV 05000269/2003003-06: Failure to Declare ES Configured

Components Inoperable per TS.

15

1R15 Operability Evaluations

Quarterly Operability Evaluations

a. Inspection Scope

The inspectors reviewed selected operability evaluations affecting risk significant

mitigating systems, to assess, as appropriate: (1) the technical adequacy of the

evaluations; (2) whether continued system operability was warranted; (3) whether other

existing degraded conditions were considered; (4) if compensatory measures were

involved, whether the compensatory measures were in place, would work as intended,

and were appropriately controlled; and (5) where continued operability was considered

unjustified, the impact on TS LCO. The inspectors reviewed the following items for

operability evaluations:

Flange Assembly Does Not Meet ASME Requirements

  • PIP O-03-03042 Increased Containment Sump Leakage in Unit 1 From RCS and

LPSW Leakage

  • PIP O-03-02226, 2B and 1C HPI Motor Vibration Increase Following New Pump

Installations

  • PIP O-03-3183, Increased Leakage From the 1B1 RCP Seal
  • PIP O-03-02492, Unit 1 RCS Leakage From Incore Instrument Tank
  • PIP O-03-3036, The 1A LPI Motor Space Heaters Have Not Functioned Since June

2001

  • PIP O-03-02569, Evidence of Borated Water Leakage Down Inside Primary Shield

Walls Below the Unit 3 Reactor Vessel

  • PIP O-03-02268, Indications of Increased RCS Leakage in Unit 1

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

.1 Feedwater Whip Restraint Modification

a. Inspection Scope

The inspectors reviewed minor modification (ONOE) -17539, Modify Two Pipe Whip

Restraints on Unit 3 Main Feedwater Piping, to verify that the feedwater whip restraints

16

had been properly adjusted as per the design drawings following replacement of the

bolting material and clevises.

The inspectors observed work in progress during the removal and replacement of the

whip restraints and reviewed the work documentation for setting the whip restraints

following return to normal operating temperatures of the feedwater piping.

The inspectors reviewed the following documents during the inspection:

  • MP/O/A/3019/004, Revision 53, Hangers - QA Condition 1 and 4 - Removal,

Installation or Modification

  • Work Request/Work Orders 98590970 (11) making final adjustments hot
  • Design Drawing O-494, Main Feedwater Pipe Whip Restraint
  • PIP O-01-01408, Adequacy of Existing Feedwater Pipe Rupture Restraints,

Corrective Action 7

In addition, the inspectors discussed with engineering the adjustments made to the whip

restraints once hot temperature operations were reached.

b. Findings

No findings of significance were identified.

.2 Biennial Plant Modification Review

a. Inspection Scope

The inspectors evaluated design change packages for nine modifications in the Barrier

Integrity and Mitigating Systems cornerstone areas, to evaluate the modifications for

adverse affects on system availability, reliability, and functional capability. The

modifications and the associated attributes reviewed are as follows:

ONOE- 10642, Upgrade Seismic Supports and Add Isolation Valve 3N-305 to Nitrogen

Line

6 Materials/Replacement Components

6 Flowpaths

6 Pressure Boundary

6 Structural

6 Process Medium

6 Failure Modes

ONOE- 12107, Upgrade Discharge LPSW Piping from the Motor Driven EFW coolers to

1LPSW-527

6 Materials/Replacement Components

17

6 Structural

6 Process Medium

ONOE- 15414, Replace Valve 2LP-15 with Item DMV-1296, 2A LPI Discharge to RBS

Pump Spray and HPI Suction

6 Materials/Replacement Components

6 Pressure Boundary

6 Structural

ONOE- 12094, Modification of Unit 2 RC Vent System Supports/Restraints

6 Materials/Replacement Components

6 Structural

ONOE- 12800, Provide Clearance Between the Valve Body of 2SF-101 and SSF RC

Makeup Pump Discharge Piping

6 Materials/Replacement Components

6 Pressure Boundary

6 Structural

ONOE- 17011, Upgrade 3-CCW-269 to Meet EQ Requirements

6 Materials/Replacement Components

Nuclear Station Modification (NSM) 33090, Add RBCU Time Delay Relays

6 Energy needs

6 Seismic qualification

6 Response time

6 Operations procedures

6 Modes bounded by the existing analysis

NSM 23053, Automatic Feedwater Isolation System

6 Environmental Qualification

6 Response Time - Testing

6 Modes bounded by existing analysis

NSM 23092, 600 V MCC and Load Center

6 Energy Needs

6 Seismic qualification

6 Control signals appropriate under accident conditions

6 Failure modes bounded by the existing analysis

For selected modification packages, the inspectors observed the as-built configuration.

Documents reviewed included procedures, engineering calculations, modifications

design and implementation packages, work orders, site drawings, corrective action

documents, applicable sections of the UFSAR, supporting analyses, TS, and design

basis information. Documents reviewed are listed in the Attachment to this report.

The inspectors also reviewed selected PIPs associated with modifications to confirm

that problems were identified at an appropriate threshold, were entered into the

corrective action process, and appropriate corrective actions had been initiated.

18

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (PMT)

a. Inspection Scope

The inspectors reviewed PMT procedures and/or test activities, as appropriate, for

selected risk significant mitigating systems to assess whether: (1) the effect of testing

on the plant had been adequately addressed by control room and/or engineering

personnel; (2) testing was adequate for the maintenance performed; (3) acceptance

criteria were clear and adequately demonstrated operational readiness consistent with

design and licensing basis documents; (4) test instrumentation had current calibrations,

range, and accuracy consistent with the application; (5) tests were performed as written

with applicable prerequisites satisfied; (6) jumpers installed or leads lifted were properly

controlled; (7) test equipment was removed following testing; and (8) equipment was

returned to the status required to perform its safety function. The inspectors observed

testing and/or reviewed the results of the following tests:

  • PT/2/A/0202/11, 2C High Pressure Injection Pump Inservice Testing (IST)

Following Mechanical Seal Cleaning and Inspection

Failed to Lift as Specified Pressure During IST

  • PIP O-03-02831, 3HP23, Letdown Storage Tank Outlet Isolation, Failed IST

Stroke Test

  • PT/3/A/0152/007, Core Flood System valve Stroke Test, IST Stroke Test

Following Inadvertent Backseating of Core Flood Isolation Valve 2CF-2 During

Maintenance per PIP O-03-03061

  • IP/0/A/0203/001A, Low Pressure Injection System Borated Water Storage Tank

Level Instrument Calibration, calibration of level instrument reviewed following

indication of false level reading per PIP O-03-0316

  • TT/3/A/0600/022, Turbine Driven Emergency Feedwater (TDEFW) Pump Speed

Response During AFIS Initiation Test, Following AFIS Modification

Cooler Developed a Water Leak

b. Findings

No findings of significance were identified.

19

1R20 Refueling and Outage Activities

a. Inspection Scope

The inspectors conducted reviews and observations for selected licensee outage

activities to ensure that: (1) the licensee considered risk in developing the outage plan;

(2) the licensee adhered to the outage plan to control plant configuration based on risk;

(3) that mitigation strategies were in place for losses of key safety functions; and (4) the

licensee adhered to operating license and TS requirements. Between April 26, 2003,

and June 15, 2003, the following activities related to the Unit 3 refueling outage were

reviewed for conformance to the applicable procedure and selected activities associated

with each evaluation were witnessed:

  • defueled (no Mode) operations
  • refueling operations
  • reduced inventory and mid-loop conditions for installation and removal of steam

generator nozzle dams

  • activities involving the reactor vessel head replacement
  • reactor startup
  • Mode changes from Mode 6 (Refueling) to Mode 1 (Power Operation)
  • system lineups during major outage activities and Mode changes
  • final containment walkdown prior to startup

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed surveillance tests and/or reviewed test data of the selected

risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS,

UFSAR, and licensee procedure requirements. In addition, the inspectors determined if

the testing effectively demonstrated that the SSCs were ready and capable of

performing their intended safety functions.

  • PT /1/A/0600/013, 1A Motor Driven Emergency Feedwater Pump Test [IST]
  • PT/3/A/0151/20, Penetration 20 Leak Rate Test (3PR-1 and 3PR-2) [local leak

rate test (LLRT)]

20

  • PT/3/A/0151/019, Penetration 19 Leak Rate Test (3PR-5 and 3PR-6) [LLRT]
  • PT/0/A/0600/021, Standby Shutdown Facility Diesel Generator Operation
  • PT2/A0202/011, 2B HPI Pump test [IST]
  • PT/3/A/0251/019, Main Steam Atmosphere Dump Valve Functional Test
  • 1P/0/A/0305/001P, Reactor Protective System Channel D RC Pressure

Instrument Calibration

  • IP/A/0380/004C, SSF D/G Water Expansion Tank Level Instrument Calibration
  • IP/0/A/305/0005D Reactor Building High Pressure Trip Channel D

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed and evaluated the licensees conduct of a simulator based

emergency preparedness drill held on June 10, 2003. The drill scenario involved

tornado damage to the Unit 1 turbine building with a subsequent loss of all AC power.

Additionally, Unit 3 developed a steam generator tube leak as part of the drill scenario.

The inspectors observed the scenario from the simulator control room and the Technical

Support Center. The inspectors observed performance of the licensees ability to

correctly classify the event and notify state and county authorities. For this drill, the

scenario progressed to a site area emergency. The drill scenario did not provide an

opportunity for the emergency response organization to make protective action

recommendations. The inspectors also reviewed the post-drill critique that was

conducted by the licensee evaluators.

b. Findings

No findings of significance were identified.

21

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Initiating Events, Mitigating Systems, and Barrier Integrity Cornerstones

a. Inspection Scope

The inspectors reviewed the PIs listed in the table below (for all three units), to deter-

mine their accuracy and completeness against requirements in Nuclear Energy Institute

(NEI) 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2.

Cornerstone: Initiating Events

Performance Indicator Verification Period Records Reviewed

Unplanned Scrams * Licensee Event Reports

  • NRC Inspection Reports

3rd and 4th

  • Monthly Operating

Scrams with Loss of Normal quarter, 2002,

Reports

Heat Removal and

  • operator logs

1st quarter, 2003

Unplanned Power Changes * licensee power history

curves

Cornerstone: Barrier Integrity

Performance Indicator Verification Period Records Reviewed

Reactor Coolant System * daily plant chemistry

Specific Activity 3rd and 4th data

quarter, 2002,

Reactor Coolant System and * daily status reports

Leakage 1st quarter, 2003 * operator logs

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed an in-depth review of issues entered into the licensees

corrective action program. The samples selected were within the cornerstone of

mitigating systems and involved risk significant systems. The inspectors reviewed the

actions taken to determine if the licensee had adequately addressed the following

attributes:

22

  • Complete, accurate, and timely identification of the problem
  • Evaluation and disposition of operability and reportability issues
  • Consideration of previous failures, extent of condition, generic or common cause

implications

  • Prioritization and resolution of the issue commensurate with the safety significance
  • Identification of the root cause and contributing causes of the problem
  • Identification and implementation of corrective actions commensurate with the safety

significance of the issue

The following issue and corrective actions were reviewed:

  • PIP O-03-02482, Darkened Oil Found in the 2C LPI Pump Bearing

b. Findings

No findings of significance were identified.

4OA3 Event Followup

.1 Unit 1 Dropped Rod

On May 17, 2003, Unit 1 dropped Safety Group 4, Rod 9 during rod movement

verification surveillance testing at 100 percent RTP. The dropped rod was a result of a

blown fuse on one of the control rod drive motor phases. The operators reduced power

to less than 55 percent as a result of the dropped rod. The inspectors responded to the

site and verified that TS and core operating limits report requirements were met by the

licensee for quadrant power tilt ratio, axial flux, and rod alignment. The inspectors also

verified that the appropriate abnormal operating procedures were implemented by the

operators. Repairs were made, the rod was subsequently recovered, and the unit was

returned to 100 percent power on May 18, 2003.

.2 Standby Shutdown Facility Cable Routing

The inspectors followed up on a 10 CFR 50.72, eight hour notification made by the

licensee for an unanalyzed condition relating to the licensee's discovery of safe

shutdown cabling routed through an Appendix R, III.G.3 area. These cables included

control and indication wiring for several valves that isolate the reactor coolant system

from potential leakage paths during safe shutdown. The inspectors walked down the

cabling to verify the licensees assessment of the condition and reviewed the adequacy

of the compensatory measures put in place.

.3 Failure of the Engineered Safeguards Channel B Power Supply

The inspectors reviewed the licensees response to the failure of the engineered

23

safeguards channel B power supply. The failure resulted in multiple TS LCO entries

and included a loss of the digital engineered safeguards digital actuation circuits. In

addition, multiple alarms were received in the control room. Following the initial loss,

discussions were conducted with the licensee concerning the failure of the power

supply, the various TS LCO entries, and ongoing repair efforts. Followup of the ES

power supply failure is discussed further in Section 1R14 of this report.

4OA5 Other Activities

.1 Unit 3 Reactor Vessel Head Replacement Project (RVHRP)

A. Engineering Preparation and Implementation for the RVHRP

a. Inspection Scope

The inspectors reviewed engineering preparations including: selected Design

Modification Packages, engineering calculations, analyses, and drawings for the

Oconee RVHRP, in order to assess adequacy and completeness. To obtain a greater

understanding of the entire project scope, the inspectors also held discussions with

project management. To determine that proper Code Sections and Editions were

applicable for this RVHRP, the inspectors also reviewed applicable sections of the

Oconee Final Safety Analysis Report and various scope documents.

b. Findings

No findings of significance were identified.

B. Review of RVHRP Lifting and Transportation Program Activities

a. Inspection Scope

The inspectors reviewed the adequacy of the RVHRP lifting program as described in

Modification Package ON-33112, Part AS1, Reactor Vessel Head Rigging and

Handling, assuring that it was prepared in accordance with regulatory requirements,

appropriate industrial codes and standards, and verified that the maximum anticipated

loads to be lifted would not exceed the capacity of the lifting equipment and supporting

structures.

The inspectors examined the RVHRP lifting equipment including the Polar Crane, a

down-ender placed inside the Reactor Building, three four-point lift systems, three skid

systems and a Self Propelled Modular Transport.

The inspectors reviewed the adequacy of the transport programs, procedures, work

packages, and load test records, to assure that they had been prepared and/or tested in

accordance with regulatory requirements, appropriate industrial codes, and standards.

The inspectors also reviewed the licensee's analyses for buried piping located beneath

the transport path as documented in Modification Package ON-53112, Part AS4,

Reactor Vessel Head Transport, to ensure that piping would not be damaged.

24

b. Findings

No findings of significance were identified.

C. Quality Assurance (QA) Oversight

a. Inspection Scope

The inspectors reviewed licensee procedures relative to QA oversight of contractor

activities for the RVHRP replacement. In addition, the inspectors discussed

procurement and quality control inspection of various parts, including the Control Rod

Drive Mechanisms (CRDM), Hold Down Bolts, and CRDM (Split Nut) Flange Ring that

were utilized in the attachment of the CRDMs to the Reactor Vessel CRDM flanges.

The inspectors also reviewed a sample of PIPs, non-conformance reports, Purchase

Orders, and Receiving Inspection Reports (Form SCD-311A) pertaining to the above

parts. The inspectors also reviewed the Unit 3 Reactor Vessel Head Penetration

Preservice Inspection conducted in February 2003. The Unit 3 Oconee replacement

reactor vessel head contains sixty-nine alloy 690 penetration tubes that are shrunk fit in

the reactor vessel head and attached with alloy 152/52 partial penetration J-groove

welds. The inspectors reviewed aspects of the inspection program that provided a

baseline of the condition of the accessible outside diameter and inside diameter

surfaces of the vessel head penetration tubes and the partial penetration J-groove welds

attaching the penetration tubes to the reactor vessel head. The review included Scope

of Work, Procedures, Personnel Certifications, Equipment Certifications, and

examination results.

b. Findings

Introduction: The inspectors identified a Green NCV of 10CFR50.55a(g)(4), which

requires meeting the ASME Boiler and Pressure Vessel Code,Section XI, IWA-7000,

Replacement, and of 10 CFR 50, Appendix B, Criterion VII, Control of Purchased

Material, Equipment, and Services. This resulted in the licensee installing one non-

conforming CRDM (Split Nut) Flange Ring on Unit 2, assembly #18, and discovering

prior to the installation in Unit 3, 68 CRDM (Split Nut) Flange Rings and 552 CRDM Hold

Down Bolts that did not meet the design and procurement specifications.

Description: In April 2003, while the licensee was performing an inspection during the

replacement of the reactor vessel head project, they determined that the CRDM Hold

Down Bolts, and CRDM (Split Nut) Flange Rings did not receive proper QA reviews of

the mechanical/chemical properties and non-destructive examinations (NDE) as

specified in the procurement and design specifications. These reviews and testing were

conducted during the initial mechanical/chemical and NDE testing performed by

independent testing facilities, and subsequently during the receipt inspections performed

by Framatome ANP, who was acting as the contractor for the RVHRP project, and

finally the licensee.

While performing Supply Chain Directive, SACD311, Rev. 1, Receipt Inspection &

Testing of QA Condition Items, the licensee failed to identify that the CRDM (Split Nut)

Flange Rings did not meet the required design and procurement specifications (i.e., a

25

yield strength of 100 ksi and a tensile strength of 125 ksi) for material quality as stated

in the Certificate of Compliance and as defined by ASME SA-320, Grade L43. The

CRDM (split nut) flange rings also did not meet the NDE ultrasonic testing (UT) as

described in ASME Section III, Sub-Article NB-2580 Examination of Bolts, Nuts and

Studs, specifically NB-2586 Ultrasonic Examination for Sizes Over 4 in., requiring the

examination be performed at a nominal frequency of 2.25 Mhz. Also the 552 CRDM

Hold Down Bolts for Unit 3 did not meet the same NDE-UT testing as described in

ASME Section III, Sub-Article NB-2580 Examination of Bolts, Nuts and Studs. Although

not a code requirement, the examination was called for by the design and procurement

specification.

A QA review, performed prior to installation of the components during Unit 3 End of

Cycle (EOC) 20 refueling outage (RFO) in the spring of 2003, led to the identification of

of one non-conforming CRDM (Split Nut) Flange Ring for CRDM Assembly #18 installed

on Unit 2 during the Unit 2 U2EOC19 RFO in the fall of 2002, and removal of 68

uninstalled, non-conforming CRDM (Split Nut) Flange Rings from the site for failure to

meet the mechanical property requirements of the components. This non-conforming

condition was not identified during the Unit 2 EOC19 RFO.

Based on the discovery that one non-conforming CRDM (Split Nut) Flange Ring was

installed on Unit 2, the licensee performed an engineering evaluation that is

documented in Framatome ANP Document 32-5027297-00, Operability Assessment of

CRDM Nut Ring with Reduced Tensile Strength Material. The one CRDM (Split Nut)

Flange Ring installed on Unit 2 was declared to be operable, but degraded, and could

remain in place until the end of the current Unit 2 operating cycle (which is scheduled to

end in the spring of 2004) when the reactor vessel head will be replaced. New CRDM

(Split Nut) Flange Rings with different heat numbers were procured and installed on the

Unit 3 head. The inspectors reviewed the methodology utilized in the engineering

evaluation for the non-conforming flange ring and found that the review was thorough.

The evaluation involved the redoing of all the ASME Code-required calculations for the

connection using the actual strength of the material supplied rather than the minimum

strength required by the material specification.

Analysis: The inspectors determined that this finding was associated with an inadequate

receipt inspection for the above parts. The finding was more than minor because

non-conforming material was actually installed in Unit 2. This deficiency was evaluated

under the SDP. Since there was no loss of function, the Initiating Events and Mitigation

Systems cornerstones were not impacted. The SDP Phase 1 RCS Barrier cornerstone

required an evaluation under SDP Phase 2. A regional senior reactor analyst performed

a SDP Phase 3 analysis and determined that since there was not a loss of function of

the system, there was no increase in risk. The finding was evaluated as Green (very

low safety significance).

Enforcement: 10CFR50.55a(g)(4) specifies in part that components classified as ASME

Code Class 1, Class 2, and Class 3 meet the requirements set forth in Section XI of the

ASME Boiler and Pressure Vessel Code. The ASME Boiler and Pressure Vessel Code,

Section XI, 1989 Edition, with no Addenda, subsection IWA-7220, states in part that

Prior to authorizing the installation of an item to be used for replacement, the Owner

shall conduct an evaluation of the suitability of that item.

26

Also, 10CFR50, Appendix B, Criterion VII, Control of Purchased Material, Equipment,

and Services, states that Measures shall be established to assure that purchased

material, equipment, and services, whether purchased directly or through contractors

and subcontractors, conform to the procurement documents. These measures shall

include provisions, as appropriate, for source evaluation and selection, objective

evidence of quality furnished by the contractor or subcontractor, inspection at the

contractor or subcontractor source, and examination of products upon delivery.

Contrary to the above, during the Unit 2 EOC19 RFO in the fall of 2002, measures taken

to evaluate the suitability of replacement parts were not adequate in that they did not

preclude the installation of one non-conforming CRDM (Split Nut) Flange Ring on CRDM

Assembly #18 on Unit 2. The same QA reviews of the remainder of the 68 CRDM (Split

Nut) Flange Rings and 552 CRDM Hold Down Bolts in the warehouse did not identify the

non-conforming parts prior to the attempt to install them on the Unit 3 reactor vessel

head. Because the finding is of very low safety significance and because the issue is in

the licensees corrective action program under PIPs O-03-2211, O-03-2132, O-03-2177

and O-03-2171, it is being treated as an NCV, consistent with Section VI.A.1 of the NRC

Enforcement Policy. Accordingly, it will be identified as NCV 05000270,287/2003003-

07: Failure to Detect Non-Conforming Parts During Receipt Inspections.

D. Radiation Protection

a. Inspection Scope

Radiation safety controls for removal of the Unit 3 reactor vessel head and preparation

of the head for temporary storage were reviewed and evaluated. Licensee procedures

for posting, surveying, and controlling access to radiologically significant areas were

assessed for adequacy. During tours of the Auxiliary Building and the Unit 3

Containment Building, the inspectors evaluated radiological postings and barricades

against current radiological surveys and procedurally established radiological controls.

Radiation Work Permits (RWPs) issued for the RVHRP were reviewed for incorporation

of established access controls. RWP specified alarm setpoints for electronic dosimeters

were also evaluated against current radiological surveys. Health Physics Technician

(HPT) proficiency in providing job coverage and occupational workers adherence to

RWP requirements were evaluated through worker interviews, work area tours and job

site observations. The inspectors observed radiation dose rates measured by an HPT in

the work areas adjacent to the vessel head after it was placed on the head stand. The

observed work area dose rates were compared to the licensees most current

documented survey results.

As Low As Reasonably Achievable (ALARA) planning and controls for the RVHRP were

reviewed and evaluated for consistency with Section IV, ALARA Planning, of the

licensees System ALARA Manual. ALARA Planning Worksheets, ALARA controls,

dose estimates, dose tracking, exposure controls including temporary shielding,

contamination and airborne radioactivity controls, project staffing and training,

emergency contingencies, and temporary storage of the original reactor head assembly

were reviewed and discussed with the licensee. RWPs issued for the RVHRP and their

associated ALARA job briefing packages were examined for incorporation of the ALARA

controls established for the project. Worker adherence to those controls was assessed

27

through job site observations during the movement of original reactor head assembly to

the head stand.

Through the above reviews and observations, the licensees radiation safety program

implementation and practices for the RVHRP were evaluated by the inspectors for

consistency with 10 CFR 20 requirements and approved licensee procedures. Licensee

plans, procedures, and records reviewed during the inspection are listed in the

Attachment to this report.

b. Findings

No findings of significance were identified.

.2 Institute of Nuclear Power Operations (INPO) Report Review

The inspectors reviewed the final report issued by INPO on April 28, 2003, for the

evaluation that was conducted at the Oconee facility during the weeks of August 5,

2002, and August 12, 2002. The inspectors did not identify any safety issues in the

INPO report that either warranted further NRC followup or that had not already been

addressed by the NRC.

4OA6 Management Meetings

Exit Meeting Summary

The inspectors presented the inspection results to Mr. Ron Jones, Site Vice President,

and other members of licensee management at the conclusion of the inspection on

July 1, 2003. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any of the material examined during the

inspection should be considered proprietary. No proprietary information was identified

4OA7 Licensee Identified Violation

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements, which meets the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a NCV.

C TS Surveillance Requirement (SR) 3.4.12.5 specifies, in part, the required channel

functional test frequency of the PORV to be within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after decreasing RCS

temperature to less than or equal to 325 degrees F. On June 8, 2003, at 4:25 p.m.,

RCS temperature was lowered to less than 325 degrees F. On June 9, 2003, at 4:00

p.m., it was discovered that the channel functional test of the Unit 3 PORV had not

been completed. The functional test was subsequently completed satisfactorily at

3:26 a.m., on June 10, 2003. The circumstances involving this missed surveillance

are described in PIP O-03-03840. Because the subsequent performance of the

missed TS SR was satisfactorily, this violation is of very low safety significance, and is

being treated as a NCV.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

S. Batson, Mechanical/Civil Engineering Manager

J. Batton, Oconee Steam Generator Engineer

D. Baxter, Engineering Manager

N. Constance, Operations Training Manager

C. Curry, Maintenance Manager

T. Curtis, Reactor & Electrical Systems Manager

D. Covar, Training Instructor

C. Eflin, Requalification Supervisor

W. Foster, Safety Assurance Manager

P. Fowler, Access Services Manager, Duke Power

T. Gillespie, Operations Manager

B. Hamilton, Station Manager

B. Jones, Training Manager

R. Jones, Site Vice President

T. King, Security Manager

B. Lowrey, Steam Generator Engineer

L. Nicholson, Regulatory Compliance Manager

R. Repko, Superintendent of Operations

J. Smith, Regulatory Affairs

J. Twiggs, Manager, Radiation Protection

J. Weast, Regulatory Compliance

NRC

L. Reyes, Regional Administrator, Region II

V. McCree, Deputy Director, Division of Reactor Projects, Region II

B. Haag, Chief, Branch 1, Division of Reactor Projects, Region II

C. Carpenter, Chief, Inspection Program Branch, NRR

L. Olshan, Project Manager

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000269,270,287/2003 URI Control Room Board Component Thermal

003-01 Reliability (Section 1R02b.(1))

05000269,270,287/2003 URI HELB Accident Scenario Review (Section

003-02 1R02b.(2))

Attachment

2

05000269,270,287/2003 URI Failure to Implement Manufacturers

003-03 Recommendations for Replacement of

SSF Diesel Coolant Grommets (Section

1R12.2)

Opened and Closed

05000269,270,287/2003 NCV Failure to Identify the SSF Degraded

003-04 Grommets as a Deficient Condition in

the PIP Corrective Action Program

(Section 1R12.2)05000269/2003003-05 NCV Failure to Maintain Sufficient Records

(logs) to Furnish Evidence of Activities

Affecting Quality (TS LCOs) (Section

1R14b.(1))05000269/2003003-06 NCV Failure to Declare ES Configured

Components Inoperable per TS (Section

1R14b.(2))

05000270,287/2003003-07 NCV Failure to Detect Non-Conforming Parts

during Receipt Inspections (Section

40A5.1C)

Items Discussed

None

LIST OF DOCUMENTS REVIEWED

(Sections 1R02 and 1R17)

Screened Out Items

NSM 12995, Temporary Wiring Procedure

NSM 23092, 600 V MCC and Load Center

NSM 53065, UFSAR revision Section 9.5.1.4.3 Cable Splicing

ONOE- 10642, Upgrade Seismic Supports and Add Isolation Valve 3N-305 to Nitrogen

Line

ONOE- 12107, Upgrade Discharge LPSW Piping from the MDEFDWPM coolers to

1LPSW-527 ONOE- 15414, Replace Valve 2LP-15 with Item DMV-1296 2A LPI

Discharge to RBS Pump Spray and HPI Suction

ONOE- 12094, Modification of Unit 2 RC Vent system Supports/Restraints

ONOE- 12800 ,Provide Clearance Between the Valve Body of 2SF-101 and SSF RC

Makeup Pump Discharge Piping

3

ONOE- 17011, Upgrade 3-CCW-269 to Meet EQ Requirements

ONOE-16856, Revise OSS-0254.00-00-1028

ONOE-16872, UST TAC Sheets

ONOE-16876, Revise Controlled Documents for RM-23A Module

ONOE-16990, Revise Test Acceptance Criteria Sheets for ECCW

ONOE-17068, Adjustable Trip Setting Correction for MCCs

NSM 23092, 600/208 VAC Load Capacity, Rev. 0

ONOE 11721, Include Alarm Setpoints of Stations Transformers in EDB and the OAC, 1

ONOE 14030, Modify Keowee Auxiliary Power Alignment Circuitry

ONOE 14409, Add fuses Between QA1 and Non-QA1 LPI Pump Circuits

ONOE 15256, Upgrade of Red Bus x/y Metering Transformers

ONOE-16712, Revise Maintenance Rule Design Basis Document to Add Reactor Building

Ventilation Functions

Evaluations

NSM 33090, Voltage Adequacy Project NSM-ON-33090/AL3 (RBCU Three Minute Delay),

NSM-23053, Automatic Feedwater Isolation System

Calculation OSC-5325, ECCW Lake Level Verification

EP 3A 1800-01, Revision 39, Turbine Building Flooding [emergency operating porcedure]

NSM 13058, MSLB Leak Detection Circuitry

ONOE 15735, Removed ESF Signal to 3LP-21 and 22

UFSAR Section 3.11.5, Loss of Ventilation

PIPS

PIP O-99-0204

PIP O-91-0121

PIP O-96-0387

PIP O-00-1845

PIP O-98-3062

PIP O-98-2221

PIP-O-01-04635

PIP-O-02-02669

PIP-O-02-00619

PIP-O-02-00054

Audits

Assessment Report Number GO-02-01(NPA)(50.59)(ALL), Applicability Determination and 10

CFR 50.59 Process Evaluation, Assessment Dates 2/4/02 - 2/7/02

PIP-O-03-01300, Level II Assessment of Frametome ANP Compliance to Oconee Contractor

Agreements, 2/18/03 - 2/18/03

PIP-O-03-01736, Level II Assessment 2MOD03001, Review of ONS Temporary Mod Process

4

Calculations

OSC-5267, Flow from UST to Hotwell - MSN-291

OSC-6901, Determination of Average Reactor Building Temperature (Type IV), Rev. 3

04158901-1SP, 12VDC Power Supply, SE P/N 50015966-001

Other Documents Reviewed

MARF #79

(Section 1R04)

Drawings

OFD-114A-1.4, Units 1 & 3 Flow Diagram of CC System (Drain Tank), Revision 5

OFD-144A-3.1, Unit 3 Flow Diagram of CC System (Supply and Return),

Revision 7

OFD-144A-3.2, Unit 3 Flow Diagram of CC System (Reactor Building and Heat Exchangers),

Revision 11

OFD-144A-3.3, Unit 3 Flow Diagram of CC System (Control Rod Drive Service Structure and

Filters), Revision 6

Procedures

Selected Licensee Commitment 16.9.10, CC and HPI Seal Injection to Reactor Coolant

Pumps (RCP)

AP/3/1700/014, Loss of Normal HPI Makeup and/or RCP Seal Injection

AP/3/1700/016, Abnormal Reactor Coolant Pump Operation

AP/3/1700/020, Loss of Component Cooling

UFSAR

Section 6.2.3, Containment Isolation System

Section 9.2.1, Component Cooling System

(Section 1R08)

Procedures

Framatome Technologies Procedure 54-ISI-400-11, Multifrequency Eddy Current Examination

of Tubing, (with Procedure Qualification 54-PQ-400) and Change Notice 30-5027221-00 for

Oconee Unit 3 EOC20 Requirements, dated April 22, 2003

Eddy Current Acquisition Guidelines for Duke Power Companys Once-Through Steam

Generators (OTSG), Rev. 9, April 22, 2003

Data Management Guidelines, Rev. 0, April 23, 2003

Eddy Current Analysis Guidelines for Duke Power Companys Once-Through Steam

Generators (OTSG), Rev. 6, April 22, 2003

5

Other Documents

Framatome ANP Engineering Information Record 51-5028238-00, In-Situ Pressure Test

Summary for Oconee Unit 3 (May 2003)

Duke Power Steam Generator Management Program SGMEP 105, OTSG Specific Assessment

of Potential Degradation Mechanisms for Oconee Unit 3 EOC 20, April 28, 2003

(Sections 40A5.1A-C)

Procedures

Procedure QEP 07.12-3,10CFR50.65(a)(4) Assessment

Procedure QEP 07-12, 10CFR50.59 Evaluations and 10CFR50.65 Assessments

NSD 403, Shutdown Risk Management (Modes 4, 5, 6, and No-Mode) per 10CFR 50.65 (a)(4),

Rev. 11.

NSD 415, Operational Risk Management (Modes 1, 2, 3) per 10CFR 50.65 (a)(4), Rev. 1.

NSD 209, 10CFR50.59 Process, Rev. 9.

Mcinnes Steel Company Ultrasonic Test (UT) Procedure No. UT-SA388-95, Rev. 0

General Nuclear Corporation, Magnetic Particle Examination, Wet Continuous Method GNC-

054, Rev. 1

Supply Chain Directive, SACD311, Rev. 1, Receipt Inspection & Testing of QA Condition Items

Other Documents

Modification Package - RV Head Components Modification, Modification #33112, Part No. AM7,

Rev. 0.

Reactor Vessel Closure Head Replacement Project, Oconee Nuclear Power Plant Units 1, 2, &

3, Input Document for Replacement RVCHA Licensing and Safety Evaluation April 2003.

Modification Package - Reactor Vessel Head Rigging and Handling, Modification # ON33112,

Part No. AS1, Rev. 1.

Modification Package Review - Replacement of Reactor Vessel Closure Head, Service

Structure and Associated Components, Modification # ON33112, Part No. 000, Rev. 0

(including 10CFR50.59 Screen).

Specification for Reactor Vessel for Duke Power Company, March 19, 1973

Oconee Unit 3, Rector Vessel Head Penetration Preservice Inspection, February 2003

Input Document for Replacement RVCHA Licensing and Safety Evaluation, April 2003

Oconee Unit 3 Reactor Vessel Head Penetration Preservice Inspection - February 2003, Final

Report

Various site engineering drawings including Head Movement Drawings from Mammoet

Various FANP calcs and NCRs

Framatome ANP Document 32-5027297-00, Operability Assessment of CRDM Nut Ring with

Reduced Tensile Strength Material

PIPs: O-03-2132, O-03-2211, O-03-2177, O-03-2171, O-03-2922, O-03-2998, O-03-2844, O-

03-1218, O-03-2898

Framatome ANP NCRs: 6025753, 32-5027297-00, 6024468, 6024579, 6025325

Purchase Orders (POs): NS146-001, NS146-002, ON52461, ON13513

Receipt Inspection Reports for: PO NS146-001, PO NS146-002, PO ON52461, PO ON13513

Corrective Action Reports (CARs): 6025777-00

6

(Section 40A5.1D)

Procedures, Plans, and Manuals

Standard Health Physics Procedure (SH) SH/0/B/2000/005, Posting of Radiation Control

Zones, Revision (Rev.) 1

SH/0/B/2000/012, Access Controls for High, Extra High, and Very High Radiation Areas,

Rev. 1

Duke Power Company System ALARA Manual,Section IV, ALARA Planning, Rev. 15,

10/15/02

Radiation Protection (RP) Job Coverage Plan, Rev. 1, 4/9/03

RP-012, Surveillance Plan, Rev. 0, 4/15/03

Records

ALARA Planning Worksheet - Unit 3 Reactor Head Replacement - Install and Remove

Scaffolding (Equipment Chase Area and Reactor Head Stand)

ALARA Planning Worksheet - Unit 3 RHRP Install Shielding, Encapsulate Reactor Head and

Decon Activities

ALARA Planning Worksheet - Unit 3 Reactor Head Replacement - Remove and Install

Interferences in Equipment Chase Area

ALARA Planning Worksheet - Unit 3 Reactor Head Replacemant - Electrical/Mechanical

Disconnects and Reconnects, Remove/Install Interferences, CRD Remmoval

ALARA Planning Worksheet - Unit 3 Reactor Head Replacement - Install and Remove

Lifting Equipment, Remove ORVH and Install RRVH

Radiation Survey Report 050603-30, Reactor Vessel Head, 5/6/03

Radiation Survey Report 050703-1, Reactor Vessel Head, 5/6/03

ALARA Briefing Packages for Radiation Work Permits 6375, 6376, 6377, 6378, 6379,

and 6380

Daily Exposure reports for 5/6 & 7/03

Radiation Work Permits (RWPs)

RWP 6375, U3 Rx Bldg - RHRP - Install and Remove Scaffolding, Rev. 0, 02/06/03

RWP 6376, U3 Rx Bldg - RHRP - Install Shielding, Encapsulate Rx Head, and Decon

Activities, Rev. 0, 02/06/03

RWP 6377, U3 Rx Bldg - RHRP - Remove and Install Interferences in the Equipment

Chase Area, Rev. 0, 02/06/03

RWP 6378, U3 Rx Bldg - RHRP - Remove and Install Rx Head Interferrences, Piping, and

all CRDM Work, Rev. 0, 02/06/03

RWP 6379, U3 Rx Bldg - RHRP - Install and Remove Lifting Equipment, Remove Original

Reactor Head Assembly (RHA) and Install Replacement RHA, Rev. 0, 02/06/03

RWP 6380, U3 Rx Bldg - RHRP - Load, Transport and Store Original RHA, Incluses All

Outside Work, Rev. 0, 02/06/03

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LIST OF ACRONYMS

ADAMS - Agencywide Documents Access and Management System

ALARA - As Low As Reasonably Achievable

ASME - American Society of Mechanical Engineers

BCM - Boiler/Condenser Mode

BWST - Borated Water Storage Tanks

CC - Component Cooling

CFR - Code of Federal Regulations

COLR - Core Operating Limits Report

CRDM - Control Rod Drive Mechanism

DEC - Duke Energy Corporation

DPC - Duke Power Company

EFW - Emergency Feedwater

EHC - Electro-Hydraulic Control

EOC - End of Cycle

ES - Engineered Safeguards

ESI - Engine Systems, Inc

ET - Eddy Current Testing

FSAR - Final Safety Analysis Report

HELB - High Energy Line Break

HPI - High Pressure Injection

HPT - Health Physics Technician

INPO - Institute of Nuclear Power Operations

IR - Inspection Report

IST - Inservice Testing

LBLOCA - Large Break Loss of Coolant Accident

LCO - Limiting Condition for Operation

LLRT - Local Leak Rate Test

LPI - Low Pressure Injection

LPSW - Low Pressure Service Water

NCV - Non-Cited Violation

NDE - Non-Destructive Examination

NRC - Nuclear Regulatory Commission

NRR - Nuclear Reactor Regulation

NSM - Nuclear Station Modification

OFD - Oconee Flow Diagram

ONOE - Minor Modification

ONS - Oconee Nuclear Station

OTSG - Once-Through Steam Generator

PI - Performance Indicators

PIP - Problem Investigation Process (report)

PT - Performance Test

PMT - Post-Maintenance Testing

PORV - Power Operated Relief Valve

QA - Quality Assurance

QC - Quality Control

RBCU - Reactor Building Cooling Unit

RBS - Reactor Building Spray

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RCP - Reactor Coolant Pump

RCS - Reactor Coolant System

RFO - Refueling Outage

RTP - Rated Thermal Power

RVHRP - Reactor Vessel Head Replacement Project

RWP - Radiation Work Permit

SBLOCA - Small Break Loss of Coolant Accident

SDP - Significance Determination Process

SG - Steam Generator

SR - Surveillance Requirement

SSC - Structure, System and Component

SSF - Standby Shutdown Facility

TDEFW - Turbine Driven Emergency Feedwater

TS - Technical Specification

UFSAR - Updated Final Safety Analysis Report

URI - Unresolved Item

UT - Ultrasonic Testing