ML021230646
ML021230646 | |
Person / Time | |
---|---|
Site: | Comanche Peak |
Issue date: | 05/03/2002 |
From: | Howell A Division of Reactor Safety IV |
To: | Terry C TXU Generation Co, LP |
References | |
IR-01-007, IR-02-003 | |
Download: ML021230646 (13) | |
See also: IR 05000445/2002003
Text
May 3, 2002
Mr. C. L. Terry
Senior Vice President & Principal Nuclear Officer of
TXU Generation Management Company LCC,
Managing General Partner for
TXU Generation Company LP
ATTN: Regulatory Affairs Department
P.O. Box 1002
Glen Rose, Texas 76043
SUBJECT: COMANCHE PEAK STEAM ELECTRIC STATION - NRC SUPPLEMENTAL
INSPECTION REPORT 50-445/02-03; 50-446/02-03
Dear Mr. Terry:
On April 25, 2002, the NRC completed a supplemental inspection at your Comanche Peak
Steam Electric Station. The enclosed report documents the inspection findings which were
discussed with you and other members of your staff at the completion of the inspection.
NRC Inspection Report 50-445/01-07; 50-446/01-07 documented a preliminary White finding
and apparent violation that involved 11 examples in which radiological surveys to detect
radioactivity required by Technical Specification procedures were not adequate. On February
21, 2002, the NRC issued its Final Significance Determination and Notice of Violation for NRC
Inspection Report 50-445/01-07; 50-446/01-07. The significance of the violation was
determined to have low to moderate (White) importance to safety when processed through
public radiation safety significance determination process.
This supplemental inspection was conducted to provide assurance that the root causes and
contributing causes of the White finding were understood, the extent of condition was identified,
and the corrective actions for risk significant performance issues were sufficient to address the
causes and prevent recurrence. To accomplish these objectives, the inspector reviewed your
root cause analysis, evaluation of extent of condition, and proposed corrective actions.
Based on the results of this inspection, the NRC determined that the identification of the root
causes, contributing causes, and corrective actions associated with the White finding were
comprehensive and broad-based. Implementation of the corrective actions should correct the
subject radioactive material control issue.
TXU Generation Company LP -2-
In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter, its
enclosure, and your response will be made available electronically for public inspection in the
NRC Public Document Room or from the Publicly Available Records (PARS) component of
NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/ADAMS.html (the Public Electronic Reading Room).
Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
Sincerely,
/RA/
Arthur T. Howell lll, Director
Division of Reactor Safety
Dockets: 50-445
50-446
Licenses: NPF-87
Enclosure:
NRC Inspection Report
50-445/02-03; 50-446/02-03
cc w/enclosure:
Roger D. Walker
Regulatory Affairs Manager
TXU Generation Company LP
P.O. Box 1002
Glen Rose, Texas 76043
George L. Edgar, Esq.
1800 M. Street, NW
Washington, D.C. 20036
G. R. Bynog, Program Manager/
Chief Inspector
Texas Department of Licensing & Regulation
Boiler Division
P.O. Box 12157, Capitol Station
TXU Generation Company LP -3-
County Judge
P.O. Box 851
Glen Rose, Texas 76043
Chief, Bureau of Radiation Control
Texas Department of Health
1100 West 49th Street
Environmental and Natural
Resources Policy Director
Office of the Governor
P.O. Box 12428
Brian Almon
Public Utility Commission
William B. Travis Building
P.O. Box 13326
1701 North Congress Avenue
Susan M. Jablonski
Office of Permitting, Remediation and Registration
Texas Natural Resource Conservation Commission
MC-122
P.O. Box 13087
Austin, TX 78711-3087
TXU Generation Company LP -4-
Electronic distribution by RIV:
Regional Administrator (EWM)
DRP Director (KEB)
DRS Director (ATH)
Senior Resident Inspector (DBA)
Branch Chief, DRP/A (DNG)
Senior Project Engineer, DRP/A (CJP)
Staff Chief, DRP/TSS (PHH)
RITS Coordinator (NBH)
Only inspection reports to the following:
Scott Morris (SAM1)
CP Site Secretary (LCA)
DOCUMENT NAME: R:\DRS\REPORTS\CP2002-03RP-MPS.WPD
RIV:DRS/PSB PEER REVIEW C:PSB C:DRP/A D:DRS
MPShannon GMGood WDJohnson AHowell
/RA/ /RA/ /RA/ /RA/ /RA/
4/ 29 /02 4/29 /02 5/01 /02 5/02 /02 5/03/02
OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax
ENCLOSURE
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Docket No(s).: 50-445; 50-446
License No(s).: NPF-87; NPF-89
Report No: 2002-03
Licensee: TXU
Facility: Comanche Peak
Location: Glen Rose, Texas
Dates: April 23-25, 2002
Inspector: Michael P. Shannon, Senior Health Physicist
Gail M. Good, Chief, Plant Support Branch
Division of Reactor Safety
-2-
SUMMARY OF FINDINGS
Comanche Peak
NRC Inspection Report No. 50- 445-02-03; 50-446-02-03
IR 05000445-02-03; IR 05000446-02-03; on 04/23-25/2002; TXU Energy; Comanche Peak
Steam Electric Station; Units 1 and 2. Regional Report.
The inspection was conducted by a regional office inspector. The inspection identified no
findings of significance. The significance of issues is indicated by their color (Green, White,
Yellow, or Red) and was determined by the Significance Determination Process in Inspection
Manual Chapter 0609. The NRCs program for overseeing the safe operation of commercial
nuclear power reactors is described at its Reactor Oversight Process website at
http://www.nrc.gov/NRR/OVERSIGHT/index.html.
Cornerstone: Public Radiation Safety
- This supplemental inspection was performed by the NRC to assess the licensees
evaluation of the control of radioactive material. A finding previously characterized as
having low to moderate safety significance (White) was documented in the Final
Significance Determination for NRC Inspection Report 50-445/01-07; 50-446/01-07.
During this supplemental inspection performed in accordance with Inspection Procedure
95001, the inspector determined that the licensee performed a thorough, broad-based
evaluation of the causes of the radioactive material control issue and correctly identified
the extent of the conditions that led to the control problems. The licensees evaluation
identified 17 root causes. Corrective actions included: (1) conducting a pre-outage
stand-down with all station work groups to discuss the past associated problems and the
importance for control of radioactive material; (2) procedural revisions that clarified
radioactive material control expectations and identification programs; (3) improved
Radiation Worker Training lesson plans that stressed the need for and the controls in-
place for handling radioactive material; and, (4) increased staffing for monitoring and
controlling the release of radioactive material during outages. An effectiveness
evaluation of radiation protection activities, to include the control of radioactive material,
will be documented in Nuclear Oversight Department Evaluation 2002-015, at the
completion of refueling outage 2RFO6.
Because of the licensees acceptable performance in addressing the control of
radioactive material, the White finding associated with this issue will only be considered
in assessing plant performance for a total of four quarters, in accordance with the
guidance in IMC 0305, Operating Reactor Assessment Program.
Report Details
01 Inspection Scope
This supplemental inspection was performed to assess the licensees evaluation of the
root causes, contributing causes, and corrective actions associated with the White
radioactive material control finding. This performance issue was previously
characterized as White in NRC Inspection Report 50-445/01-07; 50-446/01-07 and is
related to the public radiation safety cornerstone in the radiation safety strategic
performance area.
The inspector interviewed radiation workers and reviewed the following documents:
- Smart Form 2001-2621 and the associated root cause evaluation which
documented the control of radioactive material issue identified in NRC inspection
report 50-445/01-07; 50-446/01-07,
- Nuclear Overview Department Draft Evaluation 2002-015; Station Procedure
STA-652, Radioactive Material Control, Revision 11; Nuclear Procurement
Services Procedure NPS-4.13, Control of Tools in the Radiologically Controlled
Area, Revision 3; Radiation Protection Instructions RPI-213, Survey and
Release of Material and Personnel, Revision 8; RPI-602, Radiological
Surveillance and Posting, Revision 20; and RPI-802, Performance of Source
Checks, Revision 6; Radiation Protection Guideline 2-1, RMC Activities,
Revision 0; Security Instruction 3.3, Vehicle/Material Delivery Access Control,
Revision 10, and
- Radiation Worker Training lesson plans dated March 11, 2002.
02 Evaluation of Inspection Requirements
02.01 Problem Identification
a. Determine that the evaluation identifies who (i.e. licensee, self revealing, or
NRC), and under what conditions the issue was identified.
There were 11 events associated with the White finding. The details of the 11 events
are documented in NRC Inspection Report 50-445/01-07; 50-446/01-07. The licensee
documented all the events; however, two of these events were self revealing (Protected
area egress radiation portal monitors alarmed.) The other nine events were identified by
the licensee.
b. Determine that the evaluation documents how long the issue existed, and prior
opportunities for identification.
The evaluation documented that the licensee identified issues with the control of
radioactive material as early as January 2000. Corrective actions implemented during
this time period included discontinued use of launderable glove liners and the phasing-
-2-
out of modesty garments with pockets. These actions were taken to help eliminate
contaminated glove liners from being removed from the radiologically controlled area.
c. Determine that the evaluation documents the plant specific risk consequences
(as applicable) and compliance concerns associated with the issue.
A plant specific probabilistic risk assessment is not applicable to this control of
radioactive material finding. However, the evaluation did identify that the continued
failure to properly control radioactive material may result in a loss of public confidence
with the safe operation of Comanche Peak Steam Electric Station.
02.02 Root Cause and Extent of Condition Evaluations
a. Determine that the problems were evaluated using a systematic method(s) to
identify root cause(s) and contributing cause(s).
The inspector concluded that the root cause analysis was performed in a systematic
manner which correctly and completely determined the root causes and contributing
factors. The evaluation team performed the root cause analysis using an industry
accepted methodology which employed the following techniques: records review,
personnel interviews, barrier analysis, and change analysis. The inspector determined
that the above root cause evaluation was performed in accordance with Station
Procedure STA-422, Processing Smart Forms, Revision 18. The licensee employed a
six-person root cause evaluation team led by a trained member of the licensee's staff.
b. Determine that the root cause evaluation was conducted to a level of detail
commensurate with the significance of the problem.
The licensees root cause evaluation identified 17 root causes. Recommended actions
fell into four general categories:
- Release of radioactive material to areas outside the protected and satellite
radiologically controlled areas.
- Plant wide communication to reinforce positive tool control practices.
- Improvement of the radiologically controlled area tool control and identification
programs.
- Facility changes to reduce the requirements for releasing large amounts of
material from the radiologically controlled area.
The inspector determined that each root cause evaluation focused on the overall events
and was conducted to the appropriate level of detail commensurate with the significance
of the problem. When combined, the evaluations were thorough, broad-based, and
conducted to a sufficient level of detail to enhance the program for the control of
radioactive material.
-3-
c. Determine that the root cause evaluation included a consideration of prior
occurrences of the problem and knowledge of prior operating experience.
The inspector concluded that the root cause evaluation considered similar events
associated with the problem of maintaining control of radioactive material for the past
two years. From discussions with the licensees staff, the inspector determined that
industry experience was reviewed to help improve their program.
d. Determine that the root cause evaluation included consideration of potential
common cause(s) and extent of condition of the problem.
The licensees evaluation considered the potential common causes and the extent of the
conditions associated with the control of radioactive material. Common causes included
procedure deficiencies and lack of ownership for the control of radioactive materials on
the part of radiation workers.
02.03 Corrective Actions
a. Determine that appropriate corrective action(s) are specified for each
root/contributing cause or that there is an evaluation that no actions are
necessary.
The inspector concluded that the corrective actions appropriately addressed the
associated root causes. The inspector found that licensee representatives had
identified specific corrective actions to address each of the documented 17 root causes.
Corrective actions included: (1) holding a pre-outage stand-down with all station work
groups to discuss the importance for the control of radioactive material and the past
associated problems; (2) procedural revisions that clarified radioactive material control
expectations and identification programs; (3) improved Radiation Worker Training
lesson plans that stressed the need for and the controls in-place for handling radioactive
material; and, (4) increased staffing for monitoring and controlling the release of
radioactive material during outages.
The inspector determined that the corrective actions appeared to be appropriate to
prevent similar occurrences.
b. Determine that the corrective actions have been prioritized with consideration of
the risk significance and regulatory compliance.
The inspector concluded that the corrective actions were properly prioritized. A
completion date and priority were assigned for each corrective action.
c. Determine that a schedule has been established for implementing and
completing the corrective actions.
From a review of the root cause evaluation, the inspector determined that a schedule
had been developed for the completion of each corrective action. As of April 19, 2002,
all corrective actions were completed.
-4-
d. Determine that quantitative or qualitative measures of success have been
developed for determining the effectiveness of the corrective actions to prevent
recurrence.
From a review of Draft Nuclear Oversight Department (NOD) Evaluation 2002-015 and
discussions with members of the NOD, the inspector concluded that NOD performed
observations of radiation protection activities during refueling outage 2RFO6. An
effectiveness evaluation of radiation protection activities, including the control of
radioactive material, will be documented, at the completion of refueling outage 2RFO6.
4. OTHER ACTIVITIES
4OA3 Event Followup
(Closed) Violation (VIO) 50-445/0107-01; 50-446/0107-01(EA-01-304)
The Final Significance Determination for NRC Inspection Report 50-445/01-07;
50-446/01-07, documented a violation that involved 11 examples in which radiological
surveys to detect radioactivity required by Technical Specification procedures were not
adequate. The inspector reviewed the licensees root cause determination and
associated corrective action document (Smart Form 2001-2621) pertaining to the
Technical Specification 5.4.1.a violation. The licensees evaluation identified corrective
actions that fell into four general categories: (1) Release of radioactive material to areas
outside the protected and satellite radiologically controlled areas, (2) Plant wide
communication to reinforce positive tool control practices, (3) Improvement of the
radiologically controlled area tool control and identification programs, and (4) Facility
changes to reduce the requirements for releasing large amounts of material from the
radiologically controlled area.
The inspector concluded that the licensees corrective actions adequately addressed the
root causes.
4OA6 Management Meetings
Exit Meeting Summary
The inspector presented the inspection results to Mr. L. Terry, Senior Vice-President
and Principal Nuclear Officer, and other members of licensee staff at the conclusion of
the inspection on April 25, 2002. The licensee acknowledged the findings presented.
This meeting constituted the regulatory performance meeting specified in the Inspection
Manual Chapter 0305 action matrix.
The inspector asked the licensee whether any materials examined during the inspection
should be considered proprietary. No proprietary information was identified.
Attachment 1
PARTIAL LIST OF PERSONS CONTACTED
Licensee
S. Bradley, Supervisor, Radiation Protection
J. Curtis, Manager, Radiation Protection
T. Hope, Manager, Regulatory Compliance
D. Kay, Supervisor, Radiation Protection
J. Kelly, Vice-President Engineering
M. Lucas, Manager, Nuclear Oversight Department
R. McGaughy, Engineer, Nuclear Oversight Department
C. Terry, Senior Vice-President and Principal Nuclear Officer
R. Walker, Manager, Regulatory Affairs
D. Wilder, Manager, Radiation and Industrial Safety
C. Wilkerson, Senior Engineer, Regulatory Affairs
NRC
G. Good, Chief, Plant Support Branch
ITEMS OPENED, CLOSED, AND DISCUSSED
Closed During this Inspection
50-445;446/0107-01 VIO Failure to survey (EA-01-304)
SUMMARY OF FINDINGS
Comanche Peak
NRC Inspection Report No. 50- 445; 50-446
INSPECTION PERIOD APRIL 23-25, 2002
IR 05000445-02-03; IR 05000446-02-03; on 04/23-25/2002; TXU Electric; Comanche Peak
Steam Electric Station; Units 1 and 2. Regional Report.
The inspection was conducted by a regional office inspector. The inspection identified no
findings of significance. The significance of issues is indicated by their color (Green, White,
Yellow, or Red) and was determined by the Significance Determination Process in Inspection
Manual Chapter 0609. The NRCs program for overseeing the safe operation of commercial
nuclear power reactors is described at its Reactor Oversight Process website at
http://www.nrc.gov/NRR/OVERSIGHT/index.html.
M. Shannon (4640)
Cornerstone: Public Radiation Safety
PIM NRC FIN PS April 25, 2002 95001
Supplemental inspection results
- A supplemental inspection was performed by the NRC to assess the licensees
evaluation of the control of radioactive material. A finding previously characterized as
having low to moderate safety significance (White) was documented in the Final
Significance Determination for NRC Inspection Report 50-445/01-07; 50-446/01-07.
During this supplemental inspection performed in accordance with Inspection Procedure
95001, the inspector determined that the licensee performed a thorough, broad-based
evaluation of the causes of the radioactive material control issue and correctly identified
the extent of the conditions that led to the control problems. The licensees evaluation
identified 17 root causes. Corrective actions included: (1) conducting a pre-outage
stand-down with all station work groups to discuss the past associated problems and the
importance for control of radioactive material; (2) procedural revisions that clarified
radioactive material control expectations and identification programs; (3) improved
Radiation Worker Training lesson plans that stressed the need for and the controls in-
place for handling radioactive material; and, (4) increased staffing for monitoring and
controlling the release of radioactive material during outages. An effectiveness
evaluation of radiation protection activities, to include the control of radioactive material
will be documented in Nuclear Oversight Department Evaluation 2002-015, at the
completion of refueling outage 2RFO6.
Because of the licensees acceptable performance in addressing the control of
radioactive material, the White finding associated with this issue will only be considered
in assessing plant performance for a total of four quarters, in accordance with the
guidance in IMC 0305, Operating Reactor Assessment Program.