IR 05000424/1988027

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Insp Repts 50-424/88-27 & 50-425/88-37 on 880627-30. Violation Noted.Major Areas inspected:as-built Verification of RCS Pressure Boundary Piping & safety-related Piping,Open Items & Activities Re NRC Bulletin 88-005
ML20153E993
Person / Time
Site: Vogtle  Southern Nuclear icon.png
Issue date: 08/18/1988
From: Blake J, Glasman M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20153E937 List:
References
50-424-88-27, 50-425-88-37, IEB-88-005, IEB-88-5, NUDOCS 8809070089
Download: ML20153E993 (6)


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UNITCD STATES

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, *j NUCLEAR REGULATORY COMMISSION o

REGION 11

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101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

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Report Nos.: 50-424/88-27 and 50-425/88-37

Licensee: Georgia Power Company P. O. Box 4545 Atlanta, GA 30302 Docket Nos.:

50-424 and 50-425 License Nos.: NPF-68 and CFPR-109

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Facility Name: Vogtle 1 and 2 Inspection Co

June 27-30, 1988

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Inspector: /%bb ttMm M. Glas~ man Date Signed

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Approved by:

c-i J. J Iake, Chief Date Signed Hat ri is and Processes

En in ering Branch j

Di ision of Reactor Safety j

i SUMMARY f

Scope:

This routine, unannounced inspection was in the areas of as-buil+

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verification of Reactor Coolant System (RCS) Prassure Boundary Piping

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and Safety-Related Piping.

Previously - identified open items were

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also reviewed, and licensee activities related to NRC Bulletin 88-05 t

were reviewed and observed.

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Results: In the areas inspected one violation, 425/88-37-01(paragraph 2c)was

identified.

This violation was in the area of RCS Work Observation

and involved the presence of Weld Spatter and gouges on the i

pressurizer surge line piping directly prior to application of

insolation.

Programatic strength was demonstrated by the rapid

evaluation and repair of the above mentioned damage.

However, the potential for weakness is indicated by conditions which allowed the

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weld spatter and gouges to remain on the Pressurizer Surge Line piping following at least two documented inspections of the RCS piping.

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l 8809070089 880823 i

PDR ADOCK V5000424

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REPORT DETAILS-i

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Persons Contacted

Licensee Employees

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  • A. Gallant, Project Compliance Coordinator

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  • J. Gilmartin, Mechanical Field Staff Engineer
  • E. Groover, Quality Assurance Site Manager
  • C. Hayes, Yogtle Quality Assurance Manager l
  • A. Pinson, Vice President t
  • K. Pointer, Senior Plant Engineer, NSAC
  • R. Pope, Mechanical Field Staff Engineer

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  • C. Rau, Mechanical Discipline Manager Other licensee eniployees contacted during this inspection included

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craftsmen, engineers, mechanics, technicians, and administrative

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personnel.

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Other Organizations

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  • J. Agold Supervisor, Pre-Service Inspection Southern Company Services i
  • D. Strohman, Project Quality Engineer, Bechtel

NRC Resident Inspector

  • R. Schepens, 5enior Resident Inspector (Construction)
  • Attended exit interview 2.

Work Observation and Verification of As-Built Reactor Coolant and Safety-RelatedPiping(37051,49053,49063)

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The inspector verified the as-build configuration of Reactor Coolant

System (RCS) piping and safety-related piping.

The applicable code for i

piping described herein is the ASME Boiler and Pressure Vessel Code,1974 Edition Sumer 1976 Addenda.

The piping and/or furnished spool pieces

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were installed by Pullman Power Products (PPP) or Georgia Power Company (GPC). With field welds performed by same.

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a.

Work Observation and Verification i

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Since the available window for work activities associated with installation of piping / components has passed, the inspector elected to complete a field examination of installed piping and associated i

valves, welds, and hangars.

Selected portions of piping and assemblies listed in Paragraph 2b were then compared against "as-built"

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design drawings and quality documentation.

The following was then determined:

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Piping, components / assemblies, and installed material meet

purchase specifications.

i Methods of assembly of piping and components / assemblies is

consistent with design drawings and work specifications.

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Measures exisc and are in force to protect installed piping and

components / assemblies from construction debris, physical damage, l

and hostile environments.

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Installation activities were conducted with reference to

specified procedures and by qualified personnel where required.

f Nondestructive Examination (NDE) was perfonned in accordance

with procedures, and examination personnel were qualified.

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t Inspection (QC) activities were performed as required by proper t

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procedures and by properly qualified personnel.

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f b.

Piping Systems Examined

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The following piping systems were examined in accordance with the

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above-Drawing or Fabrication System Line i

Isometric Description Number (s)

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2K4-1201-024-02 RCS-Resistance 1201-024-2" j

Temperature Detector 1201-186-186-2"

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Mainfold j

2K4-1208-047-02 Chemical and Volume 1208-047-1-1/2" i

Control System

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2K3-1205-003-02 Residual Heat Removal 1205-028-14" I

System

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2K3-1202-144-01 Nuclear Service 1202-321-1" Cooling Water 1202-035-10"

2J5-2403-051-01 Diesel Generator 2403-051-2" l

Fuel Oil System

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Train "A" j

2X40L4A17 Pressurizer Surge 1201-053-14" i

1.ine 1201-053-16" 2K4-1204-021-03 Safety Injection 1204-021-6" 2K4-1204-045-01 Safety Injection 1204-127-10"

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c.

Weld Spatter and Gouges on Pressurizer Surge Line A violation of failure to follow procedures was identified during the as-build verification inspection activities conducted on the pressurizer surge line.

The inspector discovered gouges and weld spatter on spool piece 053-S-03; The damage was on the 16" OD section of the pressurizer surge line; damage was located on the top surface of the surge line 22-1/4" from weld 053-W-03 and extending 19-1/4" long x 1-1/2" wide in an axial direction, and on the bottom surface of the surge line,10-1/2" from weld 053-W-03, 7 3/4" long x 1/2" wide, in an axial direction. The gouges were estimated at.015" deep.

The particular section of pipe on which the spatter and gouges were located had been prepared for insulation and was one of the last un-insulated portions on the pressurizer surge line.

This un-insulated portion of the surge line containing the damage was completely wrapped in plastic and according to licensta records, inspected for damage May 19,1988 (prior to primary hydro testing)

and for cleanliness on May 25-26, 1988.

GPC Procedure MD-T-19 Rev.

June 2,1988, "Insulation Installation Inspection" requires insulated piping to be checked for among other things"... are strikes, weld spatter and/or physical damage."

This procedure indicates that walkdown inspections are valid for a period not in excess of 60 days.

Following the inspector's discovery of the damage, a PPP QC inspector recorded the gouges and spatter on Deviation Report (DR) number PP-18142 dated June 29, 1988, for disposition by Westinghouse.

The PPP Inspector indicated that the damage was "As Supplied."

Their disposition was for removal of spatter and gouges by light i

buffing and blending, liquid penetrant te *.ing of the affected areas,

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and ultrasonic testing to ensure minimum wall requirements of the

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pipe were not violated.

The completed OR was received in the regional office immediately following this inspection.

Due to failure to identify this damage-especially due to its close proximity to a shop weld which required pre-service inspection, and

following walkdown inspections of the surge line, and failure to follow procedure this will be identified as Violation 425/88-37-01.

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Re:ords Reviews t

The inspec+or reviewed pertinent records associated with the piping and assemblies listed in Paragraph 2b to determine if materials used were in conformance with requirenents for naterial certification, installation, and testing per ASME Section II code.

This review included Non-destructive Examination (NDE) associated with the piping required by ASME Section II, certification of pipe utilized, and non-confortnance/ deviation reports.

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The following types of documentation were reviewed:

Certified mill test reports for pipe materials

Form NPP-1 Data Reports

NDE reports (Liquid Penetrant and Radiographic)

Weld History Records

Fabrication Sheets and Shop Travellers

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Yendor Certificates-of-Conformance for NDE material

No additional violations or deviations were identified within the scope of this inspection.

3.

Independent Inspection Effort Housekeeping (548348), Material Identification and Control (42902B), and Materials Control (429408)

The inspector conducted a general inspection of Unit 2 containment and auxiliary building to observe activities such as housekeeping, material identification and control; material control, and storage.

Within the scope of this inspection, no violations or deviations were found.

4.

Action on Previous Inspection Findings and NRC Bulletins (92701)

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(Closed) URI 425/88-33-01, Proper Incorporation of As-Built Corrections to Design Drawings.

A previous inspection identified discrepancies between identification data on penetrations in the Unit 2 containment and corresponding identified data on design drawings.

During this inspection, the inspector verified as-built conditions against design drawings 'in RCS pressure boundary and safety-related piping and no discrepancies were detected.

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(0 pen) NRC Bulletin 88-05 and NRC Bulletin 88-05, Supplement 1, Non-Conforming Materials Supplied by Piping Supplies, Inc. (PSI) at Folsom, NJ, and West Jersey Manufacturing Company (WJM) at Williamstown, NJ.

Licensee efforts to establish their actions and response to requirements of this bulletin were outlined by cognizant licensee personnel in a meeting held on June 28, 1988. The inspector, senior construction resident, and cognizant licensee personnel directly involved in planning the licensee response to NRCB 88-05 attended the meeting.

The inspector also witnessed hardness testing of a flange identified i

by Georgia Power Com;.any as having been suppled by WJM.

The flange

(8" blind flange, SA-105) was installed on a flushing tee adjacent

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to the discharge isolation valve on Train "A" CCW Pump No 5.

Results of the hardness test indicated the flange was 125 to 130 Brinnell.

This is contrary to ASME SA-105 which requires Brinnell 137 minimu __

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t The licensee's procedures for Equotip hardness testing are 252250 Revision 0, "Hardness Testing" and HD-A-08 revivision date June 27,

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1988. Equotip "Hardness Testing" for Units 1 and 2, respectively.

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c.

(0 pen) Unresolved Item 424/88-03-02; 425/88-02-02, Potential for Banded Microstructure in Cold leg Accumulator Piping The licensee furnished a sample measuring approximately 4-1/2" x 9"

of 10" Sch 140 pipe Type 316 SA-376 Class 1, heat 13-351 to the inspector for independent analysis by the NRC.

Cognizant licensee

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personnel indicated to the inspector that the sample p(rovided was of

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the same section analyzed by Law Engineering for GPC report dated March 15, 1988). Also relevant to this open item, cognizant licensee t

personnel in a telephone conversation following this inspection, have indicated Cortest of Columbus, OH will lie performing Corrosion and

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metallurgical evaluation of sample material per the plan outlined in i

NRC RI! Inspection Report Nos. 50-424/88-23 and 50-425/88-33.

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A final date for performance of this ' testing has not been set,

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i; however, GPC personnel have assured the inspector of their intention

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to keep the Region II office informed of changes in a timely manner.

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Exit Interview l

The inspection scope and results were sunnarized on June 30, 1988, with

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those person = indicated in paragraph 1.

The inspector described the areas

inspected and discussed in detail the inspection results listed below.

Although reviewed during this inspection, proprietary information is not

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contained in this report.

Dissenting connents were not received from the

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J licensee.

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(0 pen) Violation 425/88-37-01 Failure to Detect Damage on Pressurizer

j Surge Line l

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