IR 05000395/1982037

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IE Insp Rept 50-395/82-37 on 820607-09.No Noncompliance Noted.Major Areas Inspected:Startup Test Program Procedure Review
ML20054M953
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 06/17/1982
From: Jape F, Taylor P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20054M946 List:
References
50-395-82-37, NUDOCS 8207150185
Download: ML20054M953 (3)


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UNITED STATES

! ff'(** "%<,),, - NUCLEAR REGULATORY COMMISSION ,A

{ g REGION 11 101 MAFilETT A ST., N.W.. SUIT E 3100

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5 :s j 'N 0, g AT LANT A. GEORGI A 30303 -

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l Report No. 50-395/82-37 i

! Licensee: South Carolina Electric and Gas Company P. O. Box 764 (Mail Code F-04)

Columbus, SC 29218 ~

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! Facility Name: V. C. Summer -

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l Docket No. 50-395

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License No. CPPR-94 Inspection at V. C. Summer site near Jenkinsville, South Carolina '

Inspector: axM , ~

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pt P. A. Tay16r [/ / Date Signed Approved by: .g qq b C

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G/ / 7/[u F. Jape, 'Section Chief F N '

^Date' Signed Engineering Inspection Branch s_,

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Division of Engineering and Technical Programs Ns s

. SUMMARY ,

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Inspection on June 7-9, 1982 '

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s Areas Inspected ~

This routine, unannounced inspection involved 16 inspector-hours on sit in the

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area of start-up test program procedure review.

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Results 1 Within the areas inspected, no violations or deviations were identifie ,

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t 8207150185 820618 i PDR ADOCK 05000395 '

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REPORT DETAILS Person s Co'etacted Licensee Employees

  • W. A. Williams Jr, General Manager Nuclear Operations
  • 0. S. Bradham, Station Manager
  • A. R. Koon, Technical Services Cordinator
  • S. S. Howre, Nuclear Licensing Engineer G. Taylor, Station Nuclear Engineer NRC Resident Inspector
  • J. Skolds, Senior Resident Inspector
  • Attended exit interview Exit Interview The inspection scope and findings were summarized on June 9, 1982, with those persons indicated in paragraph 1 abov Licensee management acknowledged the inspection finding without significant commen , Licensee Action on Previous Inspection Findings Not inspecte . vnresolved Items Unresolved items were not identified during this inspectio Procedure Review Startup Test Program The inspector reviewed the following Power Operations Test Procedures:

POT-10 Shutdown From Outside the Control Room POT-11 Station Electrical Blackout POT-14 Plant Trip From 100*. Power These procedures were reviewed to verify that they were consistant with technical specification requirements, FSAR Charter 14.1 and Regulatory Guide 1.68 Commitments and that the procedure contains the required prerequisites, precautions, plant conditions and acceptance criteri Within the areas inspected no violations or deviations were identified. The inspector did note certain deficiencies with two of the procedures as follows:

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POT-10 Shutdown From Outside The Control Roo FSAR Chapter 14.1, Table 14.1.79 describes the test methods, objec-tives, prerequisites and acceptance criteria for conducting the tes Test step 3.1 of Table 14.1.79 specifies that the plant be tripped from outside the contro POT-10 test step 6.4 requires initiations of a manual trip from the control room utilizing Emergency Operating Procedure E0P-8, which is contrary to that as specified in the FSA POT-10 test steps 6.5.1 and 6.5.2 requires boration using E0P-8 step The correct step in E0P-8 for boration is POT-10 test step 6.6.1 indicates maintaining the plant in " Hot Shut-down" This should be changed to " Hot Standby" as this is the plant conditions to be demonstrated as a result of performing the tes The license indicated that the procedure would be reviewed and corrective measures taken. This area will remain open (395/82-37-01) and reviewed at a subsequent inspectio POT-11 Station Electrical Blackout POT-11 steps 6.13, 6.15, and 6.16 specify " Hot Shutdown" plant condition This should be changed to " Hot Standby" as the purpose of the test is to achieve and maintain hot standby conditions for 30 minute The license indicated that the procedures would be reviewed and corrective measures taken. This area will remain open (395/82-37-02) and reviewed at a subsequent inspectio _ _ _ _ _ _ _