IR 05000335/2004007
ML040890660 | |
Person / Time | |
---|---|
Site: | Saint Lucie |
Issue date: | 03/26/2004 |
From: | Joel Munday NRC/RGN-II/DRP/RPB3 |
To: | Stall J Florida Power & Light Co |
References | |
IR-04-007 | |
Download: ML040890660 (18) | |
Text
rch 26, 2004
SUBJECT:
ST. LUCIE NUCLEAR PLANT - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000335/2004007 AND 05000389/2004007
Dear Mr. Stall:
On February 27, 2004 the U. S. Nuclear Regulatory Commission (NRC) completed an inspection at your St. Lucie Nuclear Plant, Units 1 and 2. The enclosed inspection report documents the inspection findings, which were discussed on February 27, 2004 with Mr. William Jefferson and other members of your staff.
The inspection examined activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commissions rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, conducted plant observations, and interviewed personnel.
On the basis of the sample selected for review, there were no findings of significance identified during this inspection. The team concluded that, in general, problems were properly identified, evaluated, and resolved within the problem identification and resolution programs. However, during the inspection, several examples of minor problems were identified. The inspectors noted that your Quality Assurance department identified that not all self assessments or quarterly CR rollups scheduled for performance in 2003 were actually performed as required by plant procedures. Also, Quality Assurance identified that there has been a lack of emphasis on completing corrective actions as exemplified by an increasing backlog of overdue Plant Management Action Items (PMAIs). At the time of this inspection there was a backlog of 360 overdue PMAIs of varying importance.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's
FPL 2 document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Joel T. Munday, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16
Enclosure:
Inspection Report 05000335/2004007 and 05000389/2004007 w/Attachment - Supplemental Information
REGION II==
Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16 Report Nos.: 05000335/2004007, 05000389/2004007 Licensee: Florida Power & Light Company (FPL)
Facility: St. Lucie Nuclear Plant, Units 1 & 2 Location: 6351 South Ocean Drive Jensen Beach, FL 34957 Dates: February 9 - 27, 2004 Inspectors: C. Julian, Team Leader K. Green-Bates, Resident Inspector Turkey Point D. Mas-Penaranda, Nuclear Safety Intern S. Rudisail, Senior Project Engineer S. Sanchez, Resident Inspector St. Lucie Approved by: Joel Munday, Chief Reactor Projects Branch 3 Division of Reactor Projects Enclosure
SUMMARY OF FINDINGS
IR 05000335/2004007, 05000389/2004007; 02/09/2004 -02/27/2004; St. Lucie Nuclear Plant,
Units 1 & 2; Problem Identification and Resolution.
Identification and Resolution of Problems The inspectors determined that the licensee was generally effective in identifying problems and entering them into the Corrective Action Program. In general, the threshold for initiating Condition Reports (CRs) was low and employees were encouraged by management to initiate CRs.
The inspectors concluded that the Quality Assurance (QA) audits were comprehensive, were well conducted, and had identified numerous performance problems. For example, licensee Quality Assurance identified that not all self assessments or quarterly CR rollups scheduled for performance in 2003, were actually performed as required by plant procedures. Quality Assurance also identified that there has been a lack of emphasis on completing corrective actions as exemplified by an increasing backlog of overdue Plant Management Action Items (PMAIs). At the time of this inspection there was a backlog of 360 overdue PMAIs of varying importance. Additionally, the inspectors observed that a recent revision to procedure ADM-07.01, PMAI Corrective Action Tracking Program removed all time limits for closure of PMAIs.
The inspectors did not identify any reluctance by the plant staff to report safety concerns. The inspectors concluded that the employee concerns program, Speakout, was functioning well.
REPORT DETAILS
OTHER ACTIVITIES (OA)
4OA2 Problem Identification and Resolution
a.
Effectiveness of Problem Identification
- (1) Inspection Scope The inspectors reviewed procedures associated with the corrective action program (CAP) which described the administrative processes for identifying and resolving problems via Condition Reports (CRs). The inspectors also reviewed items selected across the seven cornerstones of safety and conducted interviews of station personnel to determine if problems were being properly identified, characterized, and entered into the licensee CAP. The inspectors specifically reviewed CRs initiated between May 1, 2002 and the end of year 2003 associated with the following plant systems: Intake Cooling Water, Low Head Safety Injection, Containment Spray, Fuel Pool Cooling, Emergency Diesel Generators, 4160 VAC electrical, 480V electrical, 125VDC, and 120V Vital AC. The inspectors discussed the resolution of a sample of those CRs with assigned system engineers. The inspectors reviewed all CRs associated with NRC findings and LERs for the period May 1, 2002 and the end of year 2003. The inspectors reviewed a sample of licensee audits and assessments, trending reports, system health reports, performance indicators, and various other documents related to problem identification and resolution. These reviews were conducted to determine if problems were being identified at an appropriate threshold, were accurately characterized, and entered into the CAP in accordance with licensee procedures.
The inspectors also conducted plant walkdowns of equipment associated with the selected systems to assess the material condition and to look for any deficiencies that had not been entered into the CAP. The inspectors reviewed CRs documenting selected industry operating experience items, including vendor CRs, 10 CFR Part 21 CRs, and NRC generic communications, to verify that these were appropriately evaluated for applicability.
Documents reviewed are listed in the Attachment.
- (2) Assessment The inspectors determined that the licensee was generally effective in identifying problems and entering them into the CAP. CRs normally provided complete and accurate characterization of the subject issues with only minor exceptions noted. In general, the threshold for initiating CRs was low and employees were encouraged by management to initiate CRs. The number of CRs issued in 2003 was 4601, which was a 42% increase over the previous year as a result of the lower threshold. Equipment performance issues were generally being identified and entered into the CAP.
Additionally the licensee was effective in evaluating internal and external industry operating experience items for applicability and entering issues into the CAP. No findings of significance were identified.
b.
Prioritization and Evaluation of Issues
- (1) Inspection Scope The inspectors reviewed corrective action documents including CRs, Plant Management Action Items (PMAIs), Management Action Items (MAIs), Procedure Change Requests (PCRs), and Work Orders (WOs) to determine if the licensee appropriately characterized problems for evaluation and resolution. Specifically, the inspectors review was to determine if the licensee correctly identified root and contributing causes for significant conditions adverse to quality, and where appropriate, adequately addressed operability, reportability, common cause, generic concerns, and extent of condition. The inspectors also reviewed corrective action documents to determine if issues were being correctly classified using the licensees definition of significance level with proper consideration of risk, operability, and reportability. The inspectors observed multiple meetings of the mini Condition Report Oversight Group (CROG), which screened newly written CRs to determine a proposed significance level and investigation type. The inspectors also observed meetings of the CROG which reviewed CRs to determine their final significance level and future disposition. The inspectors also reviewed the condition reports initiated by the licensee in response to NRC Non-Cited Violations (NCVs) and licensee event reports to verify that the licensee had appropriately addressed the associated issues.
- (2) Assessment The inspectors observed that the committees functioned satisfactorily. Site management was actively involved in the CAP process and focused appropriate attention on significant plant issues. The inspectors determined that the licensee properly prioritized issues entered into the CAP. Generally, the licensee performed adequate evaluations that were technically accurate and of sufficient depth. The inspectors noted, however, that although CRs might initially be given a high priority, implementation of the corrective action was often delayed due to lack of emphasis on completing PMAIs. No findings of significance were identified.
c.
Effectiveness of Corrective Actions
- (1) Inspection Scope The inspectors reviewed the corrective actions associated with condition reports to verify that the licensee had identified and implemented corrective actions commensurate with the safety-significance of the issue, and where appropriate, evaluated the effectiveness of the actions taken. The inspectors also checked if common causes and generic concerns were addressed when appropriate. The inspectors reviewed selected station internal performance indicators and reports, such as maintenance rule documents, and discussed safety system status with plant personnel to verify that deficiencies had been corrected. The inspectors confirmed implementation of selected PMAIs associated with CRs reviewed, along with the inspections discussed in Section 4OA2.a and b, to verify that the licensee had identified and implemented timely and appropriate corrective actions to address problems. The inspectors reviewed reports of Quality Assurance (QA) audits of Operations and Technical Specifications, Engineering, and Corrective Action Functional Area audits.
- (2) Assessment Corrective actions developed and implemented for plant equipment problems were generally effective in correcting the equipment deficiencies. The inspectors found that the scope and depth of corrective actions assigned by the licensee were appropriate for the severity and risk significance of the problem identified.
The inspectors conducted a focused review of corrective action documents for the 4160 Volt AC power system. Selection of these CRs and corrective action documents for review were directed towards circuit breaker and switchgear issues due to the increased number of past CRs initiated for these components. This system was also selected for a review of CRs generated over the last five years. The high number of CRs had been recognized and assessed by the licensee earlier and the system had been appropriately placed into Maintenance Rule (a)(1) status.
The inspectors observed that there were particular longstanding issues related to outdoor switchgear 2B-4. This switchgear is non-safety related equipment that is used to support maintenance with alternate electrical supplies for the startup transformers and can be used as an alternate means to restore power following a station blackout.
Problems with racking in and racking out these circuit breakers had been identified as far back as 1999. Despite this identification, corrective action to resolve the issue was still outstanding. The licensees most recent assessment concluded that the problem was a result of the switchgear floor settling and plans to implement a modification to the floor in 2004. Additional corrective actions to resolve overall circuit breaker reliability are planned and include replacement of 4KV and 6.9 KV breakers with ones of a new design which is scheduled to begin in April 2004. Because this equipment is non-safety related, no violation of regulatory requirements occurred.
The inspectors reviewed the majority of Significance Level 1 CRs that had been initiated since April 2002 at St. Lucie to assess the adequacy of the Root Cause Analyses. The inspectors determined that the Condition Reports reviewed had been thoroughly documented and the root cause analyses were comprehensive and appropriately focused. Corrective actions identified were appropriate and were being implemented.
The inspectors concluded that the QA audits were well conducted and identified numerous performance problems. QA identified that the past performances of quarterly CAP CR rollups were not being completed by all departments in 2003 as required by Procedure ADM-07.03, Condition Report Trending - step 6.2.8. QA also identified that not all self assessments scheduled for performance in 2003 were actually performed as required by Procedure ADM-11.05, Self Assessment. These procedures do not fulfill an NRC regulatory requirement and therefore no violation of NRC regulatory requirements occurred.
The inspectors reviewed a list of 360 overdue PMAIs to determine if there were significant issues that were not being addressed. The PMAIs contained a mix of corrective actions of varying importance resulting from CRs and desirable enhancements. This backlog had been previously identified by QA in an audit of the Corrective Action program. To correct this issue, CR 04-0217 was written which initiated seven additional CRs, 04-0283 through 04-0289, to individual departments for development of a prioritized workdown plan to eliminate the PMAI backlog. Those CRs were due to be completed on the day of the inspection exit. Inspectors subsequently learned that PMAI workdown plans had been developed and the seven CRs were closed. The inspectors concluded that the backlog of PMAIs will require aggressive action to resolve.
The inspectors observed that a January 21, 2004 revision 4 to procedure ADM-07.01, PMAI Corrective Action Tracking Program removed all time limit requirements for closure of PMAIs. A previous revision 2 contained the statement Due dates for non-outage PMAIs shall NOT EXCEED 12 months from the origination date without PGM approval. Plant staff stated that in June 2004 when an electronic CR system is scheduled to be implemented, PMAIs will no longer be used to track CR actions and CRs will stay open until all corrective actions are complete. The inspectors noted that during this interim period without goals or time limits for closing PMAIs, the potential to further increase the PMAI backlog exists which could delay corrective actions. No findings of significance were identified.
d.
Assessment of Safety-Conscious Work Environment
- (1) Inspection Scope During technical discussions with members of the plant staff the inspectors sought to develop a general perspective of the safety-conscious work environment at the site.
The discussions were also used to determine if any conditions existed that would cause employees to be reluctant to raise safety concerns.
The NRC previously reviewed Speakout (Employee Concerns Program) records for the period January 2001, through October 2003 and documented the results of that review in NRC integrated inspection report 05-335,389/2003007. During this PI&R inspection the inspectors reviewed all the case files generated by Speakout from November 2003 until February 2004.
- (2) Assessment Based on this inspection and the CR reviews, the inspectors concluded that licensee management emphasized the need for all employees to promptly identify and report problems using the appropriate methods established within the administrative programs.
The inspectors did not identify any reluctance by the plant staff to report safety concerns.
The inspectors also concluded that the Speakout files were complete and adequate.
No findings of significance were identified.
4OA6 Meetings
Exit Meeting Summary
On February 27, 2004 the inspectors presented the inspection results to Mr. W.
Jefferson, and other members of his staff who acknowledged the findings. The inspectors confirmed that proprietary information was not provided or examined during the inspection.
ATTACHMENT:
SUPPLEMENTARY INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
M. Alfonso Corrective Action Supervisor
W. Bryan Performance Improvement Department
C. Costanzo Operations Manager
R. De La Espriella Site Quality Manager
K. Frehafer Licensing Department
J. Gallagher Speakout Program
R. Hughes Site Engineering Manager
W. Jefferson Site Vice President
G. Johnston Plant General Manager
E. Katzman Performance Improvement Manager
J. Kirkpatrick Maintenance Manager
R. Leckey Speakout Program
T. Patterson Licensing Manager
M. Pearson Performance Improvement Department
J. Porter Inservice Engineering Manager
D. Whitwell Performance Improvement Department
S. Wisla Health Physics Manager
Other licensee employees contacted include office, operations, engineering, maintenance,
training, and corporate personnel.
NRC personnel
T. Ross Senior Resident Inspector