IR 05000327/1980049
| ML19350A227 | |
| Person / Time | |
|---|---|
| Site: | Sequoyah |
| Issue date: | 02/05/1981 |
| From: | Dance H, Ford E, Julian C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML19350A224 | List: |
| References | |
| 50-327-80-49, 50-328-80-27, NUDOCS 8103130155 | |
| Download: ML19350A227 (5) | |
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NUCLEAR REGULATORY COMN11SS!ON e
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REGION 11 A-y o, Y I.LH( / ;8,-
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Licensee: Tenne s see '! alley Authority 500A Chestnut Straet Chattanooga, TN 37401 Facility Name: Sequcyah Doc <et Nos. 50-327 and 50-325 L' cense Nos. CPR-77 ard CP R-73 Inscection at Secucyah site near Chattanooga, TN fs P
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C. J_u l i a n Cate Sigrea f'
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Approved by O
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H. C. Cance, Seccion Cnief Date Sigrec S U.'"'ARY Inspection on December 1-5, 1930 Areas Ins.ected This routine, unannounced inspection involved 46 inspector-hours on site in the areas of review of preoperational testing oeing conducted on Unit 2, pre-operational system walkdown on Unit 2, and a plant tour.
Results Of the 3 areas inspected, no violations or deviations.-<ere identified.
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8103130155
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DETAILS I
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Persons Contacted
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l Licensee Employees
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- J. M. Ballentine, Plant Manager I
W. F. Popp, Assistant Plant Manager C. E. Cantrell, Assistant Plant Manager
- W. T. Cottle, Cemoliance Supervi sor
"D. W. Mack, Assistart Construction Engineer
- W. E Andrews, Chief, Power QA Staff
- 0. O. McCloud, QA Supervi sor
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- E. A. Condon, Preoperational Test Supervisor
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"W. M. Hally, Preoperational Test Coordinator l
R. Ector, Assistant Outage Director
- L. G. Heoert, OEDC - QA i
- R. L. Moore, Power QA i
- W. J. Glasser, OPQA Coordinator Other-licensee employees contacted included numerous construction craf tsmen, technicians, operators, mechanics, security force members, and office personnel.
NRC Resident Inspector
- S. D. Butler
- Attended exit interview 2.
Exit Interview The inspection scope and findings were summarized v December 5,1980 with those persons indicated in paragraph 1 above.
The inspector restated the followup items included in the details.
Licensee representatives acknowl-edged their understanding of these items.
3.
Licensee Action on Previous Inspection Findings Not inspected.
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4.
Unresolved Items Unresolved items were not identifies during this inspection.
5.
Review of Preoperational Testing Reruits The inspector reviewed the documentation packages for the completed Unit 2 preoperational tests listed below and made the following comments. Licensee representatives stated that appropriate action will be taken to resolve each ite ?
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O a.
W12.2A Annunciator Equipment checkout, test completed 6/5/80.
(1) Page 62 states that annunciator 2-XA-55-63/30 ha- =. n apparent anomalous wiring condition and that this matter ne r. solution by TVA Engineering Design. (IFI 323/80-27-01).
(2) 'One page, Appendix F Temporary Condition Log, was missing from the test record.
Indications are that no temporary conditions were required during this test. (I F1 323/80-27-02).
The test record states that annunciator panel 2-M-21 needs to be
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ventilated anc dust protected.
Licensee representatives stated that an engineering change notice (ECN) has been issued to make the required modifications. (IFI 328/20-27-03)
-(4) The test record copy reviewed by the inspector had numerous missing and duplicate pages. Licensea representa:ives stated that they will c.nfirm that copies distributed for reviu are accurate.
(IFI 328/20-27-0?)
b.
TVA - 21A Containment Spray System (1) Step 5.1.21 contains a typographical error in a valve number yet
.was signed off as completed. Licensee representatives stated that a corrective memo will be added to the test record. (IFI 328/30-27-05)
(2) Test records show that the spray header piping was intentional 1" left water filled for an indeterminant period of time follcoing hydrostatic testing.
Licensee representatives stated they will investigate the ' potential for corrosion damage of this piping.
. (-IFI 323/80-2C-06)
c.
TVA - 8 Post-LOCA Hydrogen Recombiner, ' est completed 11/11/80 (1) A hot w:re anemometer used for air flow rate measurement exceeded its calibration due date during the test period.
The instrument was subsequantly checked and:found to be out of calibration. The test director stated-in the test package that the instrument was
reading low which would imply that. test results were still satis-
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. factory After re/iewing the calibration data, the inspector
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concluded. the opposite i.e.
that the instrument had been reading high ard that the apparent error was sufficient to possibly render the test.results ' unacceptable. 'After researching the matter,
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licensee representatives. stated that during test results review, TVA engineering design had also concluded that the test results were unacceptable and that the test will be repeated. (IFI 328/80-27-07)
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t (2) The. copy of the test package reviewed by the inspector was incomplete. in that the test log for 10/27/80 was missing.
Licensee representatives statec tna; they will confirm tna ccpies distributed for review are accurate. (IFI 323/53-27-03)
(3) The inspector noted that t e 22-3 recc=biner wcs initially en h
10/23/80 and after correction of wiring errors retested on
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10/27/80. Data sheet 5.1 reflects a large difference between :ne
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tro tests in the maximum power consumption of the recembiner.
Licensee representatives stated they sill investigate the cause.
(IFI 328/80-27-09)
No viclations or deviations were -identified in this area.
5.
Plant Tcur Tne inspector toured various portions of both units. Particular attention was given to unit 2 plant system status.
Major portions of tne Resicuai Heat Removal, Safety Injection, Chemical anc Volume Control System, and Contair. ment' Spray systans were examined c ccnfirm that piping c;nfiguraticn j
is accurately reflected by the piant drawings.
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l The inspector observed the folicwing apparent equipment inadequacies and
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pointed cut these items to plant management. Licensee representatives stated
that the items will be reviewed and appropriate action taken a.
Containment Spray systera motor operated valve 2-FCV-72-2'. was observed
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to have only two of the four required bolts present to a. tach the motor
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operator to the valve body.
Electrical conduits were not properly
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attached to the motor operator.
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ine eiectrical box JB758 containing local control switches for motor
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operated valves 2 HS-72-228 and 238 has attached an outdated construc-tien tag for valve 23 and.a nonconformance tag dated 7/11/79.
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The 2B-8 RHR pump seal appears to be leaking water.
d.
The Unit 2 RHR system contains numerous' construction tags from a ccid hydro test conducted during 10/80. The system has been transferred to
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Power Production and the tags should have been cleared at transfer-I according to the preoperational testing personnel.
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Valve 62-3468, the vent valve to flow transmitter 62-93, appears to
ha-a water leak in a weld.
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. Charging pump 2B-3 has been disassembled for repairs.
The system
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piping discenr.ected frca the pump. was observed to be cpen and a
unprotected fro't entry of foreign material.
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In the charging pun.,, 2A-A rocm, vent valve 62-512 was not capped as
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shown on the plant drawings. Also a wall nenetration to this rc:m did j
not appear to bc sealed.
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h In safety injection pump room 23-B, the room cooler was inoperaole with
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the ventilation fan belts removed.
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At the 2C charging pump, two bearing temperature sensors have exposed
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l wiring.
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In the penetration room, an air leak was observed or valve 2-FSV-
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At a pipe chase cooler en elevatten 669', instrument 2-FS-30-202 was
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cbserved to have exposec electrical wir ng.
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The inspectors discussed.with plant management that the majority of tnese
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inadequacies do not acoear on the Unit 2 Outstanding Work Items List (CWIL)
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or on the list of incomplete work iter-resulting from system wa.k down
during turnover from construction to pcwer proouction.
Licensee represen-l l
tatives stated that many of these type of items will be documented by
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Maintenance Request (MR) when identified by plant personnel and that the MR
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list will be merged with the OWIL list just prior to hot functional testing.
j This matter will be pursued further during a future inspection.
(IFI
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l-The inspectors s
'ed the need to obtain a firm control of system status now
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that' Unit 2 is i hot functional testing.
The Plant Manage
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this will be accomplished approximately one month before hot functional
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Unit 2 is placed under full security access control. The inspectors stated l
that the control of system status will be examined further during. future
inspection.
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l No violations or deviations were identified in this area.
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Previous Inspection Items
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(Closed) Open Item 328/80-04-02:
The ~ inspector examined the training
records of members of the preoperational test group. Satisfactory training f
frequency is being provided at this time.
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