IR 05000293/2006002

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IR 05000293-06-002 on 01/01/2006 - 03/31/2006 for Pilgrim Nuclear Power Station. Personnel Performance During Non-routine Plant Evolutions
ML061320564
Person / Time
Site: Pilgrim
Issue date: 05/12/2006
From: Anderson C
NRC/RGN-I/DRP/PB5
To: Balduzzi M
Entergy Nuclear Operations
References
IR-06-002
Download: ML061320564 (34)


Text

SUBJECT:

PILGRIM NUCLEAR POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000293/2006002

Dear Mr. Balduzzi:

On March 31, 2006, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Pilgrim reactor facility. The enclosed integrated inspection report documents the inspection findings, which were discussed on April 6, 2006, with Mr. Dietrich and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents one finding of very low safety significance (Green), which involved a violation of NRC requirements. However, because of the very low safety significance and because the issue has been entered into your corrective action program, the NRC is treating the issue as a non-cited violation (NCV), in accordance with Section VI.A.1 of the NRC's Enforcement Policy. Additionally, a licensee-identified violation that was determined to be of very low safety significance is listed in Section 4OA7 of this report. If you contest any NCV in this report, you should provide a response with the basis for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at Pilgrim.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosures will be available electronically for public inspection in the NRC Public Document

Michael Balduzzi 2 Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA by Tracy Walker for Clifford Anderson/

Clifford Anderson, Chief Projects Branch 5 Division of Reactor Projects Docket No. 50-293 License No. DPR-35

Enclosure:

Inspection Report 50-293/06-02 w/Attachment: Supplemental Information

REGION I==

Docket No: 50-293 License No: DPR-35 Report No: 05000293/2006002 Licensee: Entergy Nuclear Operations, Inc.

Facility: Pilgrim Nuclear Power Station Location: 600 Rocky Hill Road Plymouth, MA 02360 Inspection Period: January 1, 2006 through March 31, 2006 Inspectors: W. Raymond, Senior Resident Inspector C. Welch, Resident Inspector J. McFadden, Senior Health Physicist K. Diederich, Reactor Engineer J. DAntonio, Operator Licensing D. Silk, Senior Emergency Planning Inspector Approved By: Clifford Anderson, Chief Projects Branch 5 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000293/2006-002 ; 01/01/2006 - 03/31/2006; Pilgrim Nuclear Power Station. Personnel

Performance During Non-routine Plant Evolutions The report covered a 13-week period of inspection by resident inspectors and announced inspections by regional specialists in health physics and engineering as well as an in-office review of emergency plan changes. One Green finding, which was a non-cited violation (NCV),

was identified. The significance of most findings is indicated by their color (Green, White,

Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A. Inspector Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green.

The inspectors identified a non-cited violation (NCV) of Technical Specifications for failure to evaluate the impact of an inoperable manual bypass valve (1-HO-154) in the augmented off-gas (AOG) system. Specifically, on January 12 and March 12, 2006, when the bypass valve could not be opened, plant personnel did not initiate a condition report, evaluate the impact on plant operations, and consider the need to establish compensatory measures, contrary to corrective action process procedure requirements.

As a result, opportunities to repair the valve were missed and the valves inoperable condition was not communicated effectively to station management and within operations. Consequently, on March 13 the operating crew was unaware the bypass valve was inoperable and attempted to use the bypass valve to restore dilution steam flow to the recombiner when the controller failed. The inability to restore dilution steam flow led to an increase in recombiner temperature which required the operating crew to initiate a manual reactor scram in accordance with procedure 2.4.141, Abnormal Recombiner Operation. Corrective actions, immediate and long-term, are provided for in the root cause evaluation for condition report (CR) 20060977 and CR 20061024.

The finding was determined to be of very low safety significance (Green), when evaluated per the significance determination process of MC-0609, Appendix A. The finding is more than minor because it led to a plant transient. The findings significance however, was not greater than Green because it did not contribute to both a reactor trip and the likelihood that mitigation equipment or functions would not be available. This finding has a cross cutting aspect in problem identification and resolution which significantly contributed to the performance deficiency because Entergy did not thoroughly evaluate the degraded condition of the manual bypass valve for impact on the plant or appropriate compensatory measures. (Section 1R14)iii

Summary of Findings (contd)

Licensee Identified Violations

A violation of very low safety significance, which was identified by the licensee, has been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. The violation and corrective actions are listed in Section 4OA7 of this report.

iv

REPORT DETAILS

Summary of Plant Status

Pilgrim Nuclear Power Station operated for the majority of the period at 100 percent (%) core thermal power. The Unit was brought off-line for planned outages on January 11-12 and March 10-13 to support repair of the Unit Auxiliary Transformer (UAT) and thermal backwash of the main condenser. On March 13, 2006, while restoring the Unit to full power, the control room operators inserted a manual reactor scram at 49% power at 6:10 p.m. as required by station procedure 2.4.141, Abnormal Recombiner Operation; due to a high recombiner temperature

(> 1000EF). Following repair of the failed 300 psi pressure reducing valve, a startup was initiated on March 13. Criticality was achieved on March 15 at 8:07 a.m. and the Unit placed onto the grid at 3:14 p.m. full power (100% ) was achieved on March 20,

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity and Emergency Preparedness

1R01 Adverse Weather Protection

.1 Adverse (Cold) Weather Preparations

a.

Inspection Scope (1 sample)

The inspector performed walkdowns of plant systems during periods of cold weather in February 2006, and reviewed the site preparations for adverse weather (storms). The inspector assessed Entergys cold weather preparations and protection to verify that the adverse weather did not render key safety systems inoperable. The safety systems reviewed during the inspection included the emergency diesel generators, the salt service water system, and the blackout diesel generator. Completed copies of station procedure 8.C.40, Cold Weather Surveillance, were reviewed for February 2006. The Updated Final Safety Analysis Report section 10.9.3 and Table 10.9-1, Design Temperatures (Winter), were used as references during the inspection.

The inspector confirmed that Entergy was identifying cold weather related issues and had entered them into the corrective action program. The inspector reviewed the corrective actions to verify they were appropriate to resolve the issues. The references used in this review are listed in the attachment to this report. This activity represented one inspection sample.

b. Findings

No findings of significance were identified.

.2 Site Specific Adverse Weather Events

a. Inspection Scope

(2 samples)

The inspector reviewed licensee activities to protect plant systems during adverse winter weather conditions during the periods of February 9-13, 2006 (winter storm) and February 24-28 (cold temperatures). The inspector assessed Entergys adverse weather preparations and actions to mitigate the impact of the storms on the plant, plant personnel and key safety systems. The inspector reviewed the impact of the February 12 snow storm on the site, including the challenges to site access, security, resources, cooling water supplies, and the normal and emergency power supplies. The review of the impact of cold temperatures focused on systems in the intake house, emergency diesel generator building and station blackout diesel generator building.

The safety systems, structures, and components reviewed included the station security systems, the A and B emergency diesel generators, the station blackout diesel generator, the security diesel generator, the 23 KV and 345KV electrical systems and the salt service water system. The references used during this review are included in the attachment and included: station procedures 8.C.40, Cold Weather Surveillance, 2.1.37, Coastal Storm Preparations, 2.1.42, Operation During Severe Weather, and the Updated Final Safety Analysis Report Section 10.9.3.

The inspector confirmed that Entergy was identifying weather related issues and had entered them into the corrective action program. The inspector reviewed the corrective actions to verify they were appropriate to resolve the issues. This activity represented two inspection samples of specific events: one sample for a snow storm, and one sample for a period of cold temperatures.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial System Walkdowns

c. Inspection Scope

(4 samples)

The inspectors completed a partial system review of the risk significant systems listed below during periods when the redundant train or system was out-of-service for maintenance and/or testing or following restoration of the system or train from maintenance. The position of key valves, breakers, and control switches required for system operability were confirmed by field walkdown and/or review of the main control board indicators. To ascertain the required system configuration, the inspectors reviewed plant procedures, system drawings, the Updated Final Safety Analysis Report, and the Technical Specifications. The references used for this review are described in the attachment to this report. This inspection activity represented 4 samples.

  • B CRHEAFS lineup during alternate train work on 2/15/06
  • Technical Support Center Emergency Ventilation 3/01/06 The inspector confirmed that Entergy was identifying system alignment issues and had entered them into the corrective action program. The inspector reviewed the corrective actions to verify they were appropriate to resolve the issues.

b. Findings

No findings of significance were identified.

.2 Full System Walkdown

a. Inspection Scope

(1 sample)

The inspectors performed a full system review of the Residual Heat Removal (RHR)

System to verify the system was properly aligned and capable of performing its safety function. To ascertain the required system configuration, the inspectors reviewed plant procedures, system drawings, the Updated Final Safety Analysis Report, and the Technical Specifications. A walkdown of the accessible portions of the system was performed to assess the material condition of the system and the following attributes:

  • valves were correctly positioned and did not exhibit leakage that would impact the function(s) of any given valve;
  • electrical power was available and properly aligned;
  • major system components were properly labeled;
  • hangers and supports were correctly installed and functional;
  • ancillary equipment or debris did not interfere with system performance;
  • valves were locked as required by the locked valve program.

The systems material condition was further assessed based upon discussion with the system engineer and review of the following documents:

  • 2005 4rd quarter system health report;
  • condition reports for the RHR system issued in 2005; and
  • maintenance rule information.

Note: there were no open corrective maintenance work requests.

This activity represented one inspection sample.

1R05 Fire Protection

.1 Quarterly Fire Protection Inspection

a. Inspection Scope

(10 samples)

The inspector toured selected areas of the plant to observe conditions related to: (1)transient combustibles and ignition sources;

(2) fire detection systems;
(3) manual firefighting equipment and capability; and
(4) passive fire protection features. The inspector confirmed adequate material condition of active and passive fire protection systems features and the operational lineup and readiness. The inspector also reviewed the applicable fire hazard analysis fire zone data sheets and selected surveillance procedures to ensure that the specified fire suppression system surveillance criteria were met. This inspection activity represented 10 samples.
  • Fire Zone 1.9A A RHR Pipe Room
  • Fire Zone 1.11 EL 51" East Half Open Area and Rad Waste Cleanup Equipment
  • Fire Zone 1.6 CRD Pump Quad
  • Fire Zone 1.8 CRD Quad Mezzanine
  • Fire Zone 1.5 RCIC Pump Quad
  • Fire Zone 1.7 RCIC Quad Mezzanine
  • Fire Zone 2.5 Clean and Dirty Lube Oil Storage
  • Fire Zone 2.7 Turbine Lube Oil Reservoir
  • Fire Zone 3.2 Cable Spreading Room
  • Fire Zone 1.28 Reactor Recirculation Pump Motor Generator Set Room The inspector reviewed CR-2006-00415 concerning the discovery that the fire detectors in Fire Zone 2B, RBCCW Loop B Aux Bay, were inoperable. The Zone 2B control switch on Fire Panel C222 was inadvertently left disabled for approximately 2 weeks in January 2006. The systems in the B Aux Bay are required for safe plant shutdown. The references used for this review are described in the attachment to this report.

b. Findings

A licensee identified finding is described in Section 4OA7 of this report. No other findings of significance were identified.

.2 Annual Fire Drill Observation

a. Inspection Scope

(1 sample)

The inspector monitored performance of the fire brigade during a training drill conducted on January 18, 2006 per procedure1.4.23. The drill involved a simulated fire in the Machine Shop, Operations & Maintenance Building 23's elevation. The inspector observed fire brigade personnel performance, and confirmed that the licensees fire fighting pre-plan strategies per procedure 5.5.2 were utilized, the pre-planned drill scenario was followed, and that the drill objectives were met. The inspector confirmed that proper protective clothing and breathing apparatus were donned; that sufficient fire fighting equipment was brought to the scene; the fire brigade leaders fire fighting directions were clear; and communications with the plant operators and between fire brigade members were effective. The inspector confirmed the drill critique identified areas to enhance fire brigade performance. This activity represented one inspection sample.

b. Findings

No findings of significance were identified.

1R06 Flood Protection Measures

.1 Internal Flooding

a.

Inspection Scope (1 sample)

The inspector reviewed protective measures in-place to protect against internal flooding of the auxiliary bay compartments housing the reactor building component cooling water (RBCCW) pumps, heat exchangers, and electrical switchgear. The inspection was performed during maintenance on the B turbine building component cooling water (TBCCW) heat exchanger, which required the salt service water piping in the B aux bay be opened. The inspector performed visual inspections of the water tight door separating the A and B compartments, curbing around switchgear, and the de-watering lines from each compartment to the torus room. Isolation of the salt service water system, established in accordance with protective tag out 30B-0006-E-122B, was confirmed by walkdown and review of station drawings. Operability of the A and B aux bay flooding alarms was confirmed by review of completed surveillance 8.E.30.1, Closed Cooling Water System (CCWS) Instrumentation Calibration and Functional Test.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance (IP 71111.07B)

a. Inspection Scope

(4 samples)

Based on a plant specific risk assessment, past inspection results, and recent operational experience, the inspectors selected a sample of four safety-related heat exchangers (HXs) for review: the B Reactor Building Closed Cooling Water (RBCCW)

HX, the B Residual Heat Removal (RHR) room cooler, the High Pressure Coolant Injection (HPCI) room cooler, and the Reactor Core Isolation Cooling (RCIC) room cooler. The Salt Service Water (SSW) system, which provides cooling to the RBCCW HXs, was also reviewed, as was the RBCCW system, which provides cooling to the safety-related room cooler heat exchangers.

The inspector reviewed performance tests, periodic cleaning, eddy current inspections, chemical control methods, tube leak monitoring, the extent of tube plugging, potential water hammer analysis, operating procedures, maintenance practices. The inspector also confirmed that controls for the selected components conformed to Entergys commitments to Generic Letter 89-13, Service Water System Problems Affecting Safety-Related Equipment. The inspector compared the inspection results to the established acceptance criteria to verify that the results were acceptable and that the HXs operated in accordance with design. The inspector walked down the systems, structures, and components, and monitored a performance test of the B RBCCW HX. The inspectors reviewed system health reports and interviewed applicable system engineers.

The inspector confirmed that potential common cause heat sink performance problems that had the potential to increase risk were identified and corrected by Entergy. The inspector closely examined potential macro fouling (silt, debris, etc.) and biotic fouling issues. The inspector walked down the Salt Service Water intake, chlorination system, and other support and sub components of the Salt Service Water system to assess the material condition of these systems and components.

The inspector reviewed a sample of condition reports (CRs) related to the RBCCW HXs, the safety-related room coolers, and the SSW system to ensure that Entergy was appropriately identifying, characterizing, and correcting problems related to these systems and components. The documents that were reviewed are listed in the attachment to the report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Licensed Operator Simulator Training

a. Inspection Scope

(1 sample)

The inspector observed an evaluated licensed operator simulator training exercise on January 23, 2006. The training was performed using scenarios SES-148 and involved both operational transients and design basis events. The inspector evaluated both the crews performance and evaluators assessments in-terms of the crew meeting the scenario objectives, accomplishing the critical tasks, proper use of abnormal and emergency operating procedures, command and control, effective communication, and the crews ability to implement the emergency plan in-terms of event classification and notification. The inspector reviewed the post-scenario critique and confirmed lessons learned and items for improvement were discussed with the crew to enhance future performance.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule

a. Inspection Scope

(2 samples)

The inspector reviewed follow-up actions and the past performance history for the system, structure, and component(s) (SSC) listed below to assess the effectiveness of Entergys maintenance activities, problem identification and resolution actions, and implementation of the requirements of 10 CFR 50.65(a)(1) and (a)(2), Requirements for Monitoring the Effectiveness of Maintenance. Review of the systems (a)(1) or (a)(2)classification, performance monitoring criteria and goals, and applicable functional failure (FF) determinations, including categorization as maintenance preventable (MPFF) or repetitive maintenance preventable (RMPFF), was also accomplished. References used for the review are listed in the attachment to this report. This activity represents 2 samples.

  • Reactor Building Component Cooling Water (RBCCW) pump P-202F high vibration, CR 200600464: The inspector reviewed condition report 200600464, the fourth quarter 2005 system health report for RBCCW (System 30), and the current maintenance rule (a)(1) status (System Health Report Executive Summary).
  • Heating, Ventilation, and Air Conditioning (HVAC) system review, for both the safety and non-safety related HVAC systems: Specific issues reviewed included thrown fan belts, loss of reactor building and retention building differential pressure, building/compartment temperature concerns, habitability concerns; and deficiencies in the technical support center ventilation. The inspection covered the period of January 2001 through February 2006. Greater focus was placed on the more recent period including the current maintenance rule (a)(1) action plan and Top Ten Equipment Reliability Issues Action Plan for HVAC Maintenance Backlogs. In addition to references listed in the attachment to this report, the inspector interviewed the system engineers and walked down various portions of the HVAC systems.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

(6 samples)

The inspector evaluated on-line risk management for planned and emergent work. The inspector reviewed maintenance risk evaluations, work schedules, recent corrective actions, and control room logs to verify that other concurrent planned and emergent maintenance or surveillance activities did not adversely affect the plant risk already incurred with the out-of-service components. The inspector evaluated whether Entergy took the necessary steps to control work activities, took actions to minimize the probability of initiating events and maintained the functional capability of mitigating systems. The inspector assessed Pilgrims risk management actions during plant walkdowns. The inspector also discussed the risk management with maintenance, engineering and operations personnel as applicable for the activities. References used for the inspection are identified in the attachment to this report. The inspection covered the following six samples:

  • The elevated risk condition (Yellow) on January 30 during removal of salt service water piping in the auxiliary bay in support of MR 02104136;
  • MR 06101532, Cable Spreading Room Fire Barrier Repair for TA-06-1-07 (CR

===20060562) on February 9, 2006;

  • MR 02104136, Hot Work (CR 200600415) in the B auxiliary Bay;
  • The elevated risk condition (Yellow ) on February 21 for various planned maintenance activities on the High Pressure Core Injection system; and

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-routine Plant Evolutions (71111.14, 71153)

a. Inspection Scope

=

.1 The inspectors assessed the control room operators performance during the following

planned and unplanned, non-routine evolutions. The inspectors evaluated personnel performance during the power maneuvers (i.e., adequacy of personnel performance, procedure compliance, use of the corrective action process, etc.) against the requirements contained in station procedures. The inspectors evaluated personnel performance based on observations, reviews of operator logs, alarm response procedures, operating procedures, and interviews. This review covered three inspection samples.

a) The plant power reduction to 15% full power on January 11-12 per procedure 2.1.14 to perform a control rod pattern exchange and disconnect the unit auxiliary transformer. The inspector also used power maneuvering plan MAN.C16-18R1 as a reference for this review.

b) The operator response per procedures 2.4.A.23 and 2.2.135 following the loss of the 23 KV line #72 for about 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> on January 18 and the problems with the technical support system uninterruptible power supply and network servers. (CR

===20060241, 20060242 and 20060243).

c) The plant power reduction to 15% full power on March 10-11 per procedure 2.1.14 to perform a condenser thermal backwash and to recover the repaired unit auxiliary transformer. The inspector used power maneuvering plan MAN.C16-27 as a reference for this review.

.2 The inspector observed the operating crew respond to a manual reactor scram; initiated

per the requirements of procedure 2.4.141, Abnormal Recombiner Operation, on March 13, 2006, due to elevated temperature in the augmented off gas recombiner.

Control room observation focused on operator response, communications, command and control, and procedure usage and adherence. A review of the Post Trip Report, operator logs, and plant computer alarm and data printouts, was performed to determine if the operators responded in accordance with station procedures and training. Preceding events that led to the unplanned manual reactor scram were reviewed to assess what role, if any, personnel error contributed to the event.

b. Findings

Introduction:

Green. A finding of very low safety significance, that constituted a non-cited violation of Technical Specification 5.4, Procedures, was identified by the inspector. Operations personnel did not initiate a condition report, and did not evaluate the impact on the plant or potential need for compensatory measures for an inoperable manual bypass valve (1-HO-154) in the augmented off-gas (AOG) system. The failure to enter the degraded condition into the corrective action program resulted in missed opportunities to repair the inoperable valve and to effectively communicate the valves inoperable condition to station management and operations personnel. As a result, operators were unable to restore dilution steam to the recombiner which led to the March 13 manual reactor scram.

Description:

On Monday, March 13, unaware of the inoperable condition of the manual bypass valve (1-HO-154), the operating crew attempted to manually adjust the controller for the 300 psi AOG reducing station. The controller was operating in manual, due to erratic operation while in automatic. However, output steam pressure had drifted low. The controller failed while attempting to manually raise the set point to increase output steam pressure. As a result, the regulating valve closed interrupting dilution steam flow to the recombiner. The control room supervisors order to promptly restore dilution steam flow by opening bypass valve 1-HO-154 could not be implemented and recombiner temperature rose above 1000EF due to the loss of dilution steam flow. Upon exceeding 1000EF, the shift initiated a manual reactor scram in accordance with the requirements of procedure 2.4.141, Abnormal Recombiner Operation.

The ensuing reactor scram was uncomplicated and all safety systems responded appropriately per design for the conditions encountered. Operator performance was in accordance with station procedures and the crew exhibited good command and control, communications, and procedure usage.

The manual bypass valve (1-HO-154) for the AOG 300 psi reducing station was identified as inoperable on January 13, 2006, while restoring the system to service per procedure 2.2.106, Augmented Off-Gas System. The valve was frozen/stuck in the closed position. A condition report was not generated for the inoperable valve, as required by procedure EN-LI-102, Corrective Action Process. The failed component was also not evaluated for plant impact or the need to establish a compensatory measure, as required by procedure 1.3.34.4, Compensatory Measures.

The 1-HO-154 was again found stuck closed during AOG restoration on March 12. A condition report was generated, though not until the morning of March 13. The failed component, however, was again not evaluated for plant impact or the need to establish a compensatory measure in accordance with procedure 1.3.34.4.

A performance deficiency was identified in that Entergy did not follow station procedures, implement the corrective action program, or evaluate the impact on the plant and need for compensatory measures for the failed valve. The failure to enter the valves inoperable condition into the corrective action program resulted in missed opportunities to: 1) repair the inoperable valve prior to March 13 and 2) to effectively communicate the degraded condition to station management and operations personnel, in particular to the March 13 operating crew; who were unaware the valve was stuck in the closed position and therefore did not have all the necessary information prior to attempting to manually adjust the controller for the 300 psi reducing station on March 13.

Analysis:

The finding, evaluated in accordance with the significance determination process, MC-0609, Appendix A, was determined to be of very low safety significance (Green). The finding is more than minor because it led to a plant transient (MC-0612, Appendix E, example 4.b). The findings significance is not greater than Green because it did not contribute to both a reactor trip and the likelihood that mitigation equipment or functions would not be available.

This finding has a cross cutting aspect in problem identification and resolution which significantly contributed to the performance deficiency because Entergy did not thoroughly evaluate the degraded condition of the manual bypass valve for impact on the plant or appropriate compensatory measures.

Enforcement:

Technical Specification 5.4.1.a, requires in part written procedures be established and implemented covering the activities in Regulatory Guide (RG)1.33, which includes Entergy administrative procedures EN-LI-102, Corrective Action Process, and 1.3.34.4, Compensatory Measures. Contrary to the above, on January 12 and again on March 12, 2006, operators did not follow station procedures and initiate a condition report for an inoperable valve in the augmented off-gas system (1-HO-154), nor did they evaluate the failed components impact on the plant or potential need to establish compensatory measures. Because the finding is of very low safety significance and has been entered into Entergys Corrective Action Program (CR 20060977, 200601154), this violation is being treated as a Non-Cited Violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy. NCV 0500293/2006002-001, Failure to evaluate failed AOG bypass valve contributes to manual reactor scram.

1R15 Operability Evaluations

a. Inspection Scope

=

The inspector reviewed selected operability determinations to assess the adequacy of the evaluations, the use and control of compensatory measures, compliance with the Technical Specifications, and the risk significance of the issues. The inspector used the Technical Specifications, Final Safety Analysis Report, associated design basis documents, Procedure ENN-OP-104 Operability Determinations, and the additional references listed in the attachment to this report for Section 1R15. This review covered three inspection samples.

  • CR 200600254, General Electric Safety Communication 2006-001 reports a new worst case single active failure may impact torus peak temperature analysis
  • CR 200600354, Intermittent Alarm Squib Valve Continuity Failure (C905R-A9)
  • CR 200600464, RBCCW Pump P-202F high vibration

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

(6 samples)

The inspector reviewed post-maintenance test activities on risk significant systems to verify that the effect of the test on the plant had been evaluated adequately, the test was properly performed in accordance with procedures, the test data met the required acceptance criteria, and the test activity was adequate to verify system operability and functional capability following maintenance. The inspector confirmed that systems were properly restored following testing and that discrepancies were appropriately documented in the corrective action process. The inspection activity represents six samples:

  • MR 02116598, Inspect/Replace CRD Pump B Lube Oil Cooler Zinc Anodes
  • MR 05116880, Replace Control Power Fuse for C7 Dry Well Vent SV-5043B
  • MR 05116878, Replace Control Power Fuse for C7 Torus Vent SV-5041B
  • MR 02116596, CRD flow control valve
  • MR 06103985, RMCS Timer Replacement
  • MR 06104291, RMCS Timer Replacement (CR 200601037)

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

(6 samples)

The inspector reviewed and/or observed surveillance testing to verify that the test acceptance criteria were consistent with Technical Specifications, ASME Code inservice test requirements, and Updated Final Safety Analysis Report requirements, and to confirm that the components were capable of performing their intended safety functions. The inspector also confirmed that the test was performed in accordance with the written procedure, the test data was complete and met procedural requirements, and the system was properly returned to service following testing. The inspector observed pre-job briefs for the test activities. The inspection activity represented six inspection samples:

  • 8.5.2.2.1, LPCI System Loop A Operability - Pump Quarterly and Biennial (Comprehensive) Flow Rate Tests and Valve Tests
  • 8.5.2.3, LPCI and Containment Cooling Motor-Operated Valve Operability Tests
  • 8.M.2-2.10.8.2, Diesel Generator B Initiation by RHR Logic
  • 8.5.1.1, Core Spray System Operability - Pump Quarterly and Biennial Comprehensive Flow Rate Tests and Valve Tests (Attachment 2B)

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

(1 sample)

The inspector reviewed the temporary modification identified below to verify that the licensing bases and performance capability of the associated risk significant system had not been degraded through the modification. The references used for this review are listed in the attachment to this report. This inspection activity represented one sample.

  • Temporary Alteration 06-1-07 to install temporary power to EPIC modules from power panel Y2 in the cable spreading room on February 8-10, 2006. The temporary alteration was developed after the Technical Support Center UPS supply became unreliable as a power supply to power panel 48L which powers the plant computer. The EPIC modules provide the 3D Monicor program used by the plant operators to evaluate reactor core operating conditions. The licensee provided an analysis as part of the technical justification for TA 06-1-07. The inspector reviewed the design drawings and specifications, and discussed the temporary alteration with licensee personnel. The inspector reviewed the controls used by the licensee to assure the fire protection features of the cable spreading room were maintained. The inspector reviewed the changes to applicable plant drawings and confirmed the modification was installed per TA 06-1-07.

b. Findings

No findings of significance were identified

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

(1 sample)

An in-office inspection that reviewed recent changes to the Pilgrim emergency plan and implementing procedures was conducted on February 2 and March 27, 2006. Entergy made the changes in accordance with 10 CFR 50.54(q). Entergy determined that the changes did not decrease effectiveness of the Plan and concluded that the changes continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR 50.

During this inspection, the inspector conducted a sampling review of the changes which could potentially result in a decrease in effectiveness. This review does not constitute an approval of the changes and, as such, the changes are subject to future NRC inspection.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 4, and the applicable requirements in 10 CFR 50.54(q) were used as reference criteria.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

b. Inspection Scope

(1 sample)

The inspector observed an evaluated licensed operator simulator training exercise on January 23, 2006 and evaluated the crews ability to implement the emergency plan.

Specifically, the inspector confirmed the crew properly classified the event, activated the notification system, and appropriately completed and transmitted the event notification forms in a timely manner.

c. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a. Inspection Scope

(7 samples)

The inspector reviewed radiological work activities and practices and procedural implementation during observations and tours of the facilities, and inspected procedures, records, and other program documents to evaluate the effectiveness of Pilgrims access controls to radiologically significant areas. During this inspection, the inspector observed pre-job radiological briefings for the examination of fuel assemblies in the spent fuel pool and for the transfer of a radioactive waste liner from an on-site storage container to a shipping cask. Also, the inspector discussed aspects of a near-term spent fuel pool radioactive waste clean-up project with cognizant licensee and contracted personnel. The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) to evaluate the adequacy of radiological controls. The review in this area was against criteria contained in 10 CFR 19.12, 10 CFR 20 (Subparts D, F, G, H, I, and J), Technical Specifications, and licensee procedures. This inspection activity represents the completion of seven samples relative to this inspection area (i.e.,

inspection procedure sections 02.01, 02.02.f, 02.03.b and d, and 02.05.a thru c) in partial fulfillment of the annual inspection requirements.

Planning (02.01)

The inspector confirmed that there were no licensee Performance Indicator (PI) events for the Occupational Exposure Cornerstone which required follow-up. During this inspection, the inspector reviewed issues identified in the corrective action program (CAP) and discussed selected occurrences related to this PI with radiation protection personnel.

Also, during this inspection, the inspector met with the radiation protection person who was responsible for tracking and reporting the status of this PI within the site organization.

Plant Walk Downs and Radiation Work Permit (RWP) Reviews (02.02.f)

During this inspection, the inspector examined the licensees physical and programmatic controls for highly activated or contaminated materials (non-fuel) stored within the spent fuel pool. The licensee had incorporated procedural controls in several procedures (i.e.,

procedures 1.16.1 and 6.1-009 which are listed in the List of Documents Reviewed section). Also, the inspector observed the implementation of these controls during fuel examinations which were being performed in the spent fuel pool during this inspection.

Problem Identification and Resolution (02.03.b and d)

The inspector reviewed selected corrective action reports related to access controls. This review included one radiological incident in a high radiation area measuring less than 1 Roentgen/hour that occurred since the last inspection in this area. The inspector interviewed staff and reviewed documents to determine if the follow-up activities were being conducted in an effective and timely manner commensurate with their importance to safety and risk. As stated previously, the inspector confirmed that there were no licensee PI events for the Occupational Exposure Cornerstone which would require review of the documentation packages for same.

High Risk Significant, High Dose Rate High Radiation Area (HDR-HRA) and Very High Radiation Area (VHRA) Controls (02.05.a thru c)

The inspector focused on verifying aspects of the licensees performance indicator activities for high risk, high dose rate, high radiation areas and for very high radiation areas. The inspector discussed the licensees controls and procedures for these types of areas with the Radiation Protection Manager (RPM). The RPM reported that the primary procedure for control of these areas (i.e., procedure 6.1-014) had not been changed since the last inspection. The inspector also discussed the controls and procedures with a health physics supervisor and another cognizant licensee health physicist. Also, during this inspection, the inspector confirmed the adequate posting and locking of all reasonably accessible entrances to HDR-HRAs and VHRAs. The inspector reviewed the status board list of current locations posted as VHRAs, locked high radiation areas (LHRAs), and high radiation areas (HRAs). Using this list, the inspector physically toured and examined reasonably accessible postings and physical controls in the reactor building, the turbine building, and the radioactive waste areas.

b. Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

a. Inspection Scope

(4 samples)

The inspector reviewed the effectiveness of the licensees program to maintain occupational radiation exposure as low as is reasonably achievable (ALARA). During this inspection, the inspector observed a Site ALARA Committee meeting and examined a post-work ALARA review record (review no.05-013) for work on reactor water clean-up piping. The inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and for adequacy of control of radiation exposure. The review was against criteria contained in 10 CFR 20.1101 (Radiation protection programs), 10 CFR 20.1701 (Use of process or other engineering controls), and licensee procedures. This inspection activity represents the completion of four samples relative to this inspection area (i.e., inspection procedure sections 02.01.a, c, and d and 02.03.a) in partial fulfillment of the biennial inspection requirements.

Planning (02.01.a, c, and d)

The inspector reviewed pertinent information regarding plant collective exposure history, current exposure trends, and ongoing or planned activities in order to assess current performance and exposure challenges. The licensee initiated depleted zinc injection in the past followed by hydrogen injection. The licensee has plans to initiate noble metals chemical addition during the next refueling outage in Spring 2007. The near-term spent fuel pool radioactive waste clean-up project is one of the exposure challenges for 2006.

The inspector determined the plants current 3-year rolling average collective exposure for 2002 through 2004 and assessed the effect of the collective exposure result for 2005 on this 3-year rolling average. The inspector reviewed the site specific trends in collective exposures and source-term. The inspector confirmed that the average contact dose rates with reactor coolant piping had not changed significantly over the last several refueling outages.

The inspector reviewed the site specific procedures associated with maintaining occupational exposures ALARA (i.e., procedures 6.1-031 and 6.10-020 through -023).

The inspector reviewed the processes used to estimate and track work activity specific exposures. These processes included those described in the previously-cited procedures, as well as two dose reports and a radiological engineering spreadsheet used to track work activity specific exposures, as listed in the List of Documents Reviewed section.

Verification of Dose Estimates and Exposure Tracking Systems (02.03.a)

The inspector reviewed the assumptions and basis for the current annual collective exposure estimate. The current annual collective exposure estimate for 2006 included routine work dose based on historical experience and six dose estimates for projects. The inspector confirmed that the dose estimates for the projects were reasonable with respect to both the dose rate and man-hour estimates.

b. Findings

No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation and Protective Equipment (71121.03)

a. Inspection Scope

(2 samples)

The inspector reviewed the program for health physics instrumentation to determine the accuracy and operability of the instrumentation. During the tours of the reactor building, the turbine building, and the radioactive waste areas conducted during this inspection week, the inspector examined the calibration status and operability of selected radiation protection equipment in use in the plant. Also, the inspector performed a selective examination of documents (as listed in the List of Documents Reviewed section) for regulatory compliance and adequacy in this area. The review was against criteria contained in 10 CFR 20.1501, 10 CFR 20 Subpart H, Technical Specifications, and licensee procedures. This inspection activity represents the completion of two samples relative to this inspection area (i.e., inspection procedure sections 02.01 and 02.02) in partial fulfillment of the biennial inspection requirements.

Inspection Planning (02.01)

During this inspection, the inspector reviewed the sites Updated Final Safety Analysis Report (UFSAR) to identify applicable radiation monitors associated with transient high and very high radiation areas including those used in remote emergency assessment.

This review included area radiation monitors associated with the feed water heaters, the radiological waste sump area, the transverse in-core probe room, and the condensate demineralizer regeneration room. Emergency assessment instrumentation included the main steam line monitors, the main stack high range monitors, and the drywell atmospheric high range radiation monitoring system. The inspector also reviewed the type of instrumentation available for continuous air monitoring and for portable alarming area radiation monitors that are used to identify changing radiological conditions such that actions to prevent an overexposure may be taken.

Identify Additional Radiation Monitoring Instrumentation (02.02)

During this inspection, the inspector identified the types of portable radiation detection and sampling instrumentation used for job coverage of high radiation area work. The inspector reviewed the radiation protection procedure listing for radiological instrumentation, discussed instrumentation issues with cognizant radiation protection personnel, and observed portable radiation detection and sampling instrumentation which was being used and/or was available for use in the radiologically controlled area. The inspector also identified the types of radiation detection instruments utilized for personnel release from the radiologically controlled area and for whole body counting.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

[OA]

4OA1 Performance Indicator Verification

c. Inspection Scope

(3 samples)

The initiating event cornerstone performance indicator (PI) data for unplanned scrams per 7,000 critical hours; unplanned scrams with loss of normal heat removal; and unplanned power changes per 7,000 critical hours were reviewed to assess the completeness and accuracy of the reported information. Specifically, PI data for the years 2004 and 2005 was reviewed and compared to information contained in NRC inspection reports, Licensee Event Reports, and operator logs. This inspection activity represented three samples.

d. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Reactor Safety Cornerstone

.1 Daily Review of Corrective Action Program Issues

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, the inspector performed a screening of each item entered into the licensees corrective action program. This review was accomplished by reviewing printouts of each condition report, attending daily screening meetings and/or accessing the licensees database. The purpose of this review was to identify conditions such as repetitive equipment failures or human performance issues that might warrant additional follow-up.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution In-Depth Sample(s)

Emergency Diesel Generators Inoperable due to High Ambient Temperatures

a. Inspection Scope

(1 PI&R sample)

The licensee declared both emergency diesel generators (EDGs) inoperable for brief periods during the summer of 2005 when ambient air temperatures went above the procedure limits of 95 degrees F and 93 degrees F for the A EDG and B EDG, respectively (reference Event Notification EN 41799). The licensee retracted EN 41799 on August 12, 2005, based on an interim operability determination. The EDG issues were documented in Condition Report 200503151 and in NRC Inspection Report 2005-04.

During this inspection, the inspector reviewed the licensee long term corrective actions and final engineering evaluations for the EDGs.

The inspector reviewed the evaluations documented in Engineering Request ER 05116734,"EDG X-107A/B Design Basis Thermal Operating Limits," issued on 10/27/05, that were completed to establish the current design basis for the EDG thermal limits of operation. The inspector reviewed the emergency diesel licensing and design bases, including Calculation M1276 which provided a new model and heat balance calculation for the diesel engine. The inspector reviewed the Operability Determination completed on October 27, 2005, which provided the analytical bases for the conclusion that the EDGs remained operable for the site extreme maximum temperatures as described in FSAR Section 2.3. The inspector reviewed test data for EDG operating parameters and ambient conditions during monthly tests conducted from 1999 to 2005. The inspector reviewed procedures affected by the engineering evaluation, including 2.1.12.1, 2.2.8, 8.9.1, 7.8.1, 2.1.35 and 2.2.108. The references used in this review are listed in the attachment to this report.

b. Findings and Observations

No findings of significance were identified. The licensee developed appropriate corrective actions to address the adverse condition and completed a thorough engineering evaluation to demonstrate the EDGs remained operable for the site extreme maximum temperatures described in FSAR Section 2.3. These actions restored the licensing design basis in FSAR Section 2.3. The ER which established the current design basis for the EDG thermal limits of operation was supported by calculations which included the results of past analyses and modifications and was appropriately benchmarked with actual test data. The ER provided appropriate justification that no operability limits were exceeded with ambient temperatures up to at least 105 degrees F. Procedures were changed to reflect the new design limits and operating parameters. The corrective actions were appropriate to address the root and contributing causes.

Radiation Safety Cornerstone

.3 Occupational Radiation Safety

a. Inspection Scope

(71121)

The inspector selected six issues/condition reports (CRs) identified in the CAP for detailed review (i.e., 2004-01824 and 2005-04635, -05066, -05085, -05200, and -05264).

The issues were associated with the following: dose of record exceeding electronic dosimeter dose; evaluation of a highly radioactive object; unplanned dose due to human performance; movement of a contaminated area boundary; missing LHRA keys; and noncompliance with a HRA RWP; respectively. The documented reports for the issues were reviewed to determine whether the full extent of the issues were identified, appropriate evaluations were performed, and appropriate corrective actions were specified and prioritized.

b. Findings

No findings of significance were identified.

.4 Cross-References to PI&R Findings Documented in the Report

Section 1R14 of this report describes a cross-cutting aspect in the area of problem identification and resolution involving failure to thoroughly evaluate a degraded condition.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On April 6, 2006, the inspectors presented the inspection results to members of Entergy management led by Mr. Pete Dietrich. The inspectors confirmed that there was no information that Entergy considered proprietary included in this report.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by Entergy and is a violation of NRC requirements which meets the criteria of Section VI of the NRC Enforcement Policy for being dispositioned as a Non-cited Violation.

.1 Technical Specification 5.4.1, Procedures, requires written procedures be established,

implemented, and maintained covering the activities in Regulatory Guide (RG) 1.33.

Procedures for Maintenance and Tagging Controls are required per Appendix A to RG-1.33. Entergy procedure 8.B.14 provides for the completion of hot work when appropriate compensatory measures are established, which was conducted per MR 02104136 in the B Reactor Building Closed Cooling Water (RBCCW) room on January 11, 2006. Fire detection for C222 Zone 2B was disabled during the hot work per tagout 33-0010-E122B.

Contrary to the above, plant operators failed to restore fire detection to C222 Zone 2B when compensatory measures were relaxed following the completion of hot work in the B RBCCW room on January 13, 2006. The B RBCCW room was without its primary means of fire detection for about 2 weeks until the fire zone protection was restored on January 31, 2006. The licensee corrective actions included a review to determine that other fire zones were adequately protected or compensatory measures were in place. The licensee also conducted a review to identify the cause of the human error and additional corrective actions. The licensee addressed this matter, along with actions to prevent recurrence, in Condition Report 200600415.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

P. Dietrich General Manager Plant Operations

D. Noyes Assistant Operations Manager

E. Olson Operations Manager

V. Fallacara Training Manager

T. Trask System Engineering Manager

B. Ford Licensing Manager

B. Grieves Quality Assurance Manager

W. Coady ALARA Specialist

L. Foreaker Radiological Support Supervisor

J. Gaedtke System Engineer

P. Harizi Design Engineer

J. Kalb Design Engineer

K. Lane Component Engineer

P. Leavitt Chemistry

W. Lobo Licensing Specialist

W. Mauro ALARA Supervisor

J. McClellan Quality Specialist-Quality Assessment

B. McDonald Radiation Protection Specialist (Support)

P. McNulty Radiation Protection Manager

F. Mulcahy System Engineer

A. Niederburger System Engineer

K. Sejkora Effluent Engineer

D. Selig Programs and Components Supervisor

P. Smalley Chemistry Specialist

D. Smith Mechanical Maintenance

D. Sukanek Waste Control Specialist

J. Taormina Work Control Supervisor

T. Tetzlaff Radiological Operations Supervisor

G. Zavaski Radiation Protection Specialist (Projects)

Other:

M. Hooper Senior Nuclear Engineer, WMG, Inc.

NRC personnel

W. Raymond, Senior Resident Inspector
C. Welch, Resident Inspector

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Open and

Closed

NCV 0500293/2006002-001, Failure to evaluate failed AOG bypass valve contributes to manual reactor scram.

LIST OF DOCUMENTS REVIEWED