03-21-2016 | At 0313 on January 25, 2016, Operators initiated a manual reactor trip on Unit 1 due to high levels of sodium in the Feedwater and Condensate systems that exceeded the threshold levels in Abnormal Operating Procedure 10, Abnormal Secondary Chemistry Conditions. Subsequent investigation determined the high sodium levels were due to a condenser tube leak located in 13A Condenser. The failed condenser tube and several adjacent tubes were plugged and refueling outage eddy current testing confirmed a circumferential crack on the failed condenser tube. The apparent cause is that the condenser tube failure was vibration induced. Radial stakes were installed to help limit future vibration. A causal analysis will be completed following the Unit 1 refueling outage. |
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Category:Letter
MONTHYEARIR 05000336/20240032024-11-0707 November 2024 Integrated Inspection Report 05000336/2024003 and 05000423/2024003 and Apparent Violation and Independent Spent Fuel Storage Installation Inspection Report 07200008/2024001 IR 05000318/20240072024-11-0606 November 2024 Assessment Follow-Up Letter for Calvert Cliffs Nuclear Power Plant, Unit 2 (Report 05000318/2024007) ML24317A1432024-11-0404 November 2024 Constellation Energy Generation, LLC, 2024 Annual Report - Guarantees of Payment of Deferred Premiums IR 05000317/20240032024-10-22022 October 2024 Integrated Inspection Report 05000317/2024003, 05000318/2024003, and Independent Spent Fuel Storage Installation Report 07200008/2024001 RS-24-093, Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-10-10010 October 2024 Response to Request for Additional Information - Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests ML24283A0012024-10-0909 October 2024 Senior Reactor and Reactor Operator Initial License Examinations IR 05000317/20245012024-10-0707 October 2024 Emergency Preparedness Biennial Exercise Inspection Report 05000317/2024501 and 05000318/2024501 ML24275A2442024-10-0303 October 2024 Reassignment of the U.S. Nuclear Regulatory Commission Branch Chief, Division of Operating Reactor Licensing ML24255A8642024-09-0606 September 2024 Rscc Wire & Cable LLC Dba Marmon Industrial Energy & Infrastructure - Part 21 Retraction of Final Notification IR 05000317/20240052024-08-29029 August 2024 Updated Inspection Plan for Calvert Cliffs Nuclear Power Plant, Units 1 and 2 (Report 05000317/2024005 and 05000318/2024005) ML24240A1112024-08-27027 August 2024 Registration of Use of Casks to Store Spent Fuel ML24240A2462024-08-27027 August 2024 Submittal of the Reactor Vessel Material Surveillance Program Capsule Technical Report ML24222A6772024-08-0909 August 2024 Response to Request for Additional Information for Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition IR 05000317/20240022024-08-0606 August 2024 Integrated Inspection Report 05000317/2024002 and 05000318/2024002 IR 05000317/20240102024-07-31031 July 2024 Age-Related Degradation Inspection Report 05000317/2024010 and 05000318/2024010 ML24179A3262024-07-23023 July 2024 LTR - Constellation - SG Welds and Nozzles (L-2023-LLR-0053, L-2023-LLR-0054, L-2023-LLR-0055, L-2023-LLR-0056) ML24198A0442024-07-16016 July 2024 Inservice Inspection Report IR 05000317/20244012024-07-0909 July 2024 Security Baseline Inspection Report 05000317/2024401 and 05000318/2024401 ML24177A1832024-06-25025 June 2024 Inservice Inspection Report RS-24-061, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations2024-06-14014 June 2024 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations ML24161A0012024-06-0909 June 2024 Independent Spent Fuel Storage Installation, Annual Radioactive Effluent Release Report ML24150A0522024-05-29029 May 2024 Operator Licensing Examination Approval ML24079A0762024-05-23023 May 2024 Issuance of Amendments to Adopt TSTF 264 ML24136A1962024-05-15015 May 2024 Independent Spent Fuel Storage Installation - Annual Radiological Environmental Operating Report IR 05000317/20240012024-05-0707 May 2024 Integrated Inspection Report 05000317/2024001 and 05000318/2024001 RS-24-041, Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests2024-04-30030 April 2024 Alternative Request to Utilize Code Case OMN-32, Alternative Requirements for Range and Accuracy of Pressure, Flow, and Differential Pressure Instruments Used in Pump Tests 05000317/LER-2024-002, Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus2024-04-29029 April 2024 Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus 05000318/LER-2024-001, Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip2024-04-24024 April 2024 Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip ML24101A1942024-04-22022 April 2024 Closeout Letter for GL 2004-02 ML24114A0182024-04-18018 April 2024 Electronic Reporting of Occupational Exposure Reporting ML24103A2042024-04-12012 April 2024 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-591-A, Revise Risk Informed Completion Time (RICT) Program Revision 0 and Revise 10 CFR 50.69 License Condition 05000318/LER-2023-004-01, Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer2024-04-12012 April 2024 Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer IR 05000317/20240402024-04-11011 April 2024 95001 Supplemental Inspection Report 05000317/2024040 and Follow-Up Assessment Letter RS-24-002, Constellation Energy Generation, LLC - Annual Property Insurance Status Report2024-04-0101 April 2024 Constellation Energy Generation, LLC - Annual Property Insurance Status Report ML24082A0082024-03-22022 March 2024 Request for Exemption from Certain Requirements of 10 CFR 72.212 and 10 CFR 72.214 ML24078A1152024-03-18018 March 2024 10 CFR 50.46 Annual Report ML24059A0632024-03-15015 March 2024 Authorization and Safety Evaluation for Alternative Request ISI-05-021 (EPID L-2023-LLR-0006) - Non-Proprietary IR 05000317/20230062024-02-28028 February 2024 Annual Assessment Letter for Calvert Cliffs Nuclear Power Plant, Units 1 and 2, (Reports 05000317/2023006 and 05000318/2023006 ML24052A0072024-02-14014 February 2024 Core Operating Limits Report for Unit 1, Cycle 27, Revision 0 ML24040A0962024-02-0909 February 2024 Notification of Readiness for NRC 95001 Inspection ML24040A1492024-02-0909 February 2024 Response to NRC Request for Additional Information Regarding Final Response to Generic Letter 2004-02 IR 05000317/20230042024-02-0101 February 2024 Integrated Inspection Report 05000317/2023004 and 05000318/2023004 ML24029A0102024-01-29029 January 2024 Request for Information and Notification of Conduct of IP 71111.21.N.04, Age-Related Degradation, Reference Inspection Report 05000317/2024010 and 05000318/2024010 ML24003A8872024-01-19019 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0033 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24011A0732024-01-11011 January 2024 Proposed Alternative to the Requirements for Repair/Replacement of Saltwater (SW) System Buried Piping 05000318/LER-2023-003, Forward LER 2023-003-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Manual Actuation of Auxiliary Feedwater System Due to 22 Steam Generator Feedwater Pump Trip2024-01-0808 January 2024 Forward LER 2023-003-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Manual Actuation of Auxiliary Feedwater System Due to 22 Steam Generator Feedwater Pump Trip ML24005A0222024-01-0505 January 2024 Revised Steam Generator Tube Inspection Reports ML23304A0642024-01-0202 January 2024 Issuance of Amendment No. 349 to Modify the Long-Term Coupon Surveillance Program RS-23-125, Request for Exemption from 10 CFR 2.109(b)2023-12-0707 December 2023 Request for Exemption from 10 CFR 2.109(b) ML23331A2992023-11-27027 November 2023 Submittal of Condition Prohibited by Technical Specifications Due to Failure to Sample Diesel Generator Fuel Oil Storage Tank 2024-09-06
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000318/LER-2024-002, Automatic Reactor Trip Due to Main Turbine Loss of Load2024-09-16016 September 2024 Automatic Reactor Trip Due to Main Turbine Loss of Load 05000317/LER-2024-003, A Diesel Generator Inoperable Due to Potential Transformer Failure2024-09-0606 September 2024 A Diesel Generator Inoperable Due to Potential Transformer Failure 05000318/LER-2024-001-01, Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip2024-08-20020 August 2024 Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip 05000317/LER-2024-001-01, Condition Prohibited by Technical Specifications Due to Safety Injection Check Valve Not Full Closed2024-07-0202 July 2024 Condition Prohibited by Technical Specifications Due to Safety Injection Check Valve Not Full Closed 05000317/LER-2024-002, Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus2024-04-29029 April 2024 Emergency Diesel Generators Automatic Start Due to Loss of a 13kV Bus 05000318/LER-2024-001, Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip2024-04-24024 April 2024 Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip 05000318/LER-2023-004-01, Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer2024-04-12012 April 2024 Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer 05000317/LER-2024-001, Condition Prohibited by Technical Specifications Due to Safety Injection Check Valve Not Full Closed2024-03-13013 March 2024 Condition Prohibited by Technical Specifications Due to Safety Injection Check Valve Not Full Closed 05000318/LER-2023-004, Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer2024-01-16016 January 2024 Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer 05000318/LER-2023-002, Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer2024-01-0808 January 2024 Automatic Reactor Trip from Reactor Protection System Actuation Due to Loss of Unit Service Transformer ML23331A2992023-11-27027 November 2023 Submittal of Condition Prohibited by Technical Specifications Due to Failure to Sample Diesel Generator Fuel Oil Storage Tank 05000317/LER-2023-001, Condition Prohibited by Technical Specifications Due to Failure to Sample Diesel Generator Fuel Oil Storage Tank2023-11-27027 November 2023 Condition Prohibited by Technical Specifications Due to Failure to Sample Diesel Generator Fuel Oil Storage Tank 05000318/LER-2023-001-01, Condition Prohibited by Technical Specifications Due to Inoperable Nuclear Instrumentation at Very Low Power2023-09-29029 September 2023 Condition Prohibited by Technical Specifications Due to Inoperable Nuclear Instrumentation at Very Low Power 05000318/LER-1923-001, Condition Prohibited by Technical Specifications Due to Inoperable Nuclear Instrumentation at Very Low Power2023-05-11011 May 2023 Condition Prohibited by Technical Specifications Due to Inoperable Nuclear Instrumentation at Very Low Power 05000318/LER-2022-003, Pressurizer Safety Valve As-Found Settings (Low) Outside Technical Specification Limits Due to Setpoint Drift2022-11-21021 November 2022 Pressurizer Safety Valve As-Found Settings (Low) Outside Technical Specification Limits Due to Setpoint Drift 05000318/LER-2022-002, Unplanned Safety Injection Actuation Signal Due to Human Error2022-11-11011 November 2022 Unplanned Safety Injection Actuation Signal Due to Human Error ML22063A7032022-03-0303 March 2022 Automatic Reactor Trip Due to High Reactor Coolant System 05000318/LER-2022-001, Forwards LER 2022-001-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Automatic Reactor Trip Due to High Reactor Coolant System Pressure2022-03-0303 March 2022 Forwards LER 2022-001-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Automatic Reactor Trip Due to High Reactor Coolant System Pressure 05000318/LER-2021-004, Manual Reactor Trip Due to Lowering Steam Generator Levels2022-01-18018 January 2022 Manual Reactor Trip Due to Lowering Steam Generator Levels 05000318/LER-2021-003, Auxiliary Feedwater Pump Inoperable Due to Improper Reset of Trip Throttle Valve2021-09-23023 September 2021 Auxiliary Feedwater Pump Inoperable Due to Improper Reset of Trip Throttle Valve 05000318/LER-2002-002, Manual Reactor Trip Due to Lowering Steam Generator Level Following Main Feedwater Regulating Valve Going Shut2021-05-19019 May 2021 Manual Reactor Trip Due to Lowering Steam Generator Level Following Main Feedwater Regulating Valve Going Shut 05000318/LER-2021-001, Calvert Cliff Nuclear Power Plant Unit No. 2, Pressure Heater Sleeve Weld Pressure Boundary Leakage Caused by Primary Water Stress Corrosion Cracking2021-04-21021 April 2021 Calvert Cliff Nuclear Power Plant Unit No. 2, Pressure Heater Sleeve Weld Pressure Boundary Leakage Caused by Primary Water Stress Corrosion Cracking 05000317/LER-2020-001, Regarding Undervoltage Condition on 4.16kV Electrical Bus 11 Resulted in Actuation of Emergency Diesel Generator 1 a2021-01-27027 January 2021 Regarding Undervoltage Condition on 4.16kV Electrical Bus 11 Resulted in Actuation of Emergency Diesel Generator 1 a ML19169A0592019-06-13013 June 2019 Reactor Vessel Level Monitoring System Special Report, Rev. 1 05000318/LER-2017-0012017-04-19019 April 2017 Pressurizer Safety Valve As-Found Settings Outside Technical Specification Limits Due To Setpoint Drift, LER 17-001-00 For Calvert Cliffs, Unit 2 re: Pressurizer Safety Valve As-Found Settings Outside Technical Specification Limits Due to Setpoint Drift 05000318/LER-2016-0012017-01-24024 January 2017 Automatic Reactor Trip Due to Main Turbine Electro-Hydraulic Control Fluid Leak, LER 16-001-00 for Calvert Cliffs Nuclear Power Plant, Unit No. 2 Regarding Automatic Reactor Trip Due to Main Turbine Electro-Hydraulic Control Fluid Leak 05000317/LER-2016-0032016-07-29029 July 2016 Unit 1 Automatic Trip on Loss of Load due to Spurious Steam Generator High Level Turbine Trip, LER 16-003-00 for Calvert Cliffs Nuclear Power Plant, Unit No. 1 Regarding Automatic Trip on Loss of Load due to Spurious Steam Generator High Level Turbine Trip 05000317/LER-2016-0042016-07-20020 July 2016 High Energy Line Break Barrier Breeched Due to Human Performance Error Causing Both Service Water Trains to be Inoperable, LER 16-004-00 for Calvert Cliffs, Unit 1 Regarding High Energy Line Break Barrier Breeched Due to Human Performance Error Causing Both Service Water Trains to be Inoperable 05000317/LER-2016-0022016-04-14014 April 2016 Pressurizer Safety Relief Nozzle Dissimilar Metal Weld Flaw Exceeded American Society of Mechanical Engineers Code Allowable Limit, LER 16-002-00 for Calvert Cliffs, Unit 1, Regarding Pressurizer Safety Relief Nozzle Dissimilar Metal Weld Flaw Exceeded American Society of Mechanical Engineers Code Allowable Limit 05000317/LER-2016-0012016-03-21021 March 2016 Manual Reactor Trip Due to High Secondary Side Sodium Levels Due to a Condenser Tube Leak, LER 16-001-00 for Calvert Cliffs Nuclear Power Plant Unit 1, Regarding Manual Reactor Trip Due to High Secondary Side Sodium Levels Due to a Condenser Tube Leak 05000318/LER-2015-0012016-01-27027 January 2016 Manual Reactor Trip Due to 22 Steam Generator Feed Pump Trip, LER 15-001-00 for Calvert Cliffs, Unit 2, Regarding Manual Reactor Trip Due to Steam Generator Feed Pump 22 Trip ML0319504602003-07-0303 July 2003 Special Report: National Pollution Discharge Elimination System Permit # MD0002399 Violation 2024-09-06
[Table view] |
I. DESCRIPTION OF EVENT:
Energy. Industry Identification System (EIIS) codes are identified in the text as [XX].
A. INITIAL CONDITIONS:
Unit 1 was operating in Mode 1 at 10 percent power with the Main Turbine [TA] offline on January 25, 2016 prior to the event.
B. EVENT:
At 0235 on January 25, 2016 Operators received a Condensate [SD] Conductivity high level alarm. Chemistry was notified and began to investigate the cause of the alarm. The Chemistry Technician reported that the Condensate Conductivity levels were rising. Concurrently Operators placed the condensate demineralizers [FDM] in service in attempt to reduce conductivity. Operators entered Abnormal Operating Procedure (AOP)-10, Abnormal Secondary Chemistry Conditions. Operators secured the circulating water pump in the when Feedwater [FJ] and Condensate sodium sample levels exceeded AOP-10 threshold limits that required a reactor trip. Following verification that Emergency Operating Procedure (EOP)-0, Post Trip Immediate Actions, safety functions were met, EOP-1, Reactor Trip, was entered for an uncomplicated reactor trip.
Subsequent investigation detdrmined there was a condenser tube leak on one of the condenser tubes in 13A Condenser [COND] Waterbox. The cracked condenser tube and several surrounding condenser tubes were plugged and the site began preparations to start-up the unit.
Unit 1 was returned to Mode 1 at 2220 on January 25, 2016 and the unit returned to full power at 2310 on January 26, 2016.
During the 2016 Unit 1 refueling outage, eddy current testing confirmed a circumferential crack on the affected tube. The apparent cause was that the crack was vibration induced.
C. INOPERABLE STRUCTURES, COMPONENTS, OR SYSTEMS THAT CONTRIBUTED TO
THE EVENT:
There were no structures, systems or components inoperable at the start of the event that contributed to the event.
D. DATES AND APPROXIMATE TIMES OF MAJOR OCCURRENCES:
January 25, 2016 0235 Received alarm in Control Room for high level of Condensate Conductivity.
0240 Chemistry Technician reported Condensate Conductivity level rising.
0255 Entered AOP-10.
0312 Chemistry Technician reported Condensate sodium of 432 ppb; Feedwater sodium of 232 ppb.
0313 Unit 1 Manual reactor trip due to exceeding AOP-10 trip criteria.
0318 EOP-0 safety functions verified met.
0331 Implemented EOP-1 for uncomplicated reactor trip.
0429 Exited EOP-1 and implemented Operating Procedure OP-4, Plant Shutdown from Power Operation to Hot Standby.
2220 Unit 1 entered Mode 1.
January 26, 2016 2310 Unit 1 returned to full power.
E. FAILURE MODES:
The failed 13A Condenser tube is a titanium tube that was installed during the 2012 refueling outage. During initial installation of the titanium condenser tubes, vertical stakes were installed to reduce vibration of the condenser tubes however the vertical stakes do not prevent vibration in the vertical direction.
Eddy current testing during the 2016 refueling outage identified that the affected condenser tube experienced a circumferential crack around approximately 180 degrees. The apparent cause for the tube leak is that the failure was vibration induced in the unrestrained direction.
F. METHOD OF DISCOVERY:
The condenser tube leak in 13A Condenser Hotwell was self-revealing. This event is documented in the site's Corrective Action Program under IR02616491.
IJ
II. CAUSE OF EVENT
A. SAFETY CONSEQUENCES:
The Reactor Protection System [JD] was manually initiated in response to the condenser tube leak in 13A Condenser Hotwell in accordance with AOP-10. During performance of AOP-10, Operators started 13 Auxiliary Feedwater [BA] Pump [P] and secured both Steam Generator Feed Pumps. Although both Steam Generator [SG] Feed Pumps were secured to reduce sodium buildup in the steam generators, the Main Feedwater system remained functional.
Additionally, Operators shut the Main Steam [SB] Isolation Valves [ISV] to protect the condenser from overpressure. This step, although listed in the abnormal operating procedure, was not required as sufficient condenser vacuum was still being maintained by the remaining Circulating Water [KE] Pumps. The Main Steam Isolation Valves were subsequently re-opened.
The safety consequence of this event was the introduction of sodium into the Condensate and Feedwater systems and ultimately into the Steam Generator. If left uncorrected, the high sodium conditions would have a detrimental effect on steam generator tube integrity. The condenser tube leak resulted in a manual reactor trip to be initiated once sodium levels exceeded AOP-10 allowed levels. Operators continued actions to restore steam generator secondary side water chemistry to acceptable levels.
This event satisfies the criteria in NUREG-1022, Revision 3, for system actuations of the Reactor Protection system and the Auxiliary Feedwater system. Therefore, this event is reportable pursuant to 10 CFR 50.73(a)(2)(iv)(A). An immediate event notification report (51683) was also made pursuant to 10 CFR 50.72(b)(2)(iv)(B) for reactor protection system actuation while critical and 10 CFR 50.72(b)(3)(iv)(A) for the manual actuation of the auxiliary feedwater system.
B. CORRECTIVE ACTIONS:
The failed condenser tube and several adjacent tubes were plugged prior to returning the unit to power operations.
During Unit l's 2016 refueling outage eddy current testing confirmed a through-wall circumferential crack of around 180 degrees on the affected condenser tube. The apparent cause is that the condenser tube failure was vibration induced. As part of the extent of condition investigation the normal number of condenser tubes that were eddy current tested in 13A Condenser during a refueling outage was expanded. As a result four other condenser tubes in 13A Condenser were found to have indications of wear at tube stake locations and were subsequently plugged. Radial stakes were then installed during the refueling outage to reduce movement in the x and y direction. The site conducted the normal amount of eddy current testing on the remaining Unit 1 condensers with no similar issues detected.
Following the refueling outage, a causal analysis will be performed to determine the cause of the tube leak. If additional information is subsequently developed that would significantly affect the understanding of this event, a supplemental licensee event report will be submitted.
III. PREVIOUS SIMILAR EVENTS:
A review of Calvert Cliffs' events over the past several years was performed and no similar instance was found.
A. COMPONENT INFORMATION:
COMPONENT IEEE 803 IEEE 805
FUNCTION ID SYSTEM ID
13A Condenser Tube COND SG The 13A Condenser tubes were fabricated by Valtimet.
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05000318/LER-2016-001 | Automatic Reactor Trip Due to Main Turbine Electro-Hydraulic Control Fluid Leak LER 16-001-00 for Calvert Cliffs Nuclear Power Plant, Unit No. 2 Regarding Automatic Reactor Trip Due to Main Turbine Electro-Hydraulic Control Fluid Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000317/LER-2016-001 | Manual Reactor Trip Due to High Secondary Side Sodium Levels Due to a Condenser Tube Leak LER 16-001-00 for Calvert Cliffs Nuclear Power Plant Unit 1, Regarding Manual Reactor Trip Due to High Secondary Side Sodium Levels Due to a Condenser Tube Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000317/LER-2016-002 | Pressurizer Safety Relief Nozzle Dissimilar Metal Weld Flaw Exceeded American Society of Mechanical Engineers Code Allowable Limit LER 16-002-00 for Calvert Cliffs, Unit 1, Regarding Pressurizer Safety Relief Nozzle Dissimilar Metal Weld Flaw Exceeded American Society of Mechanical Engineers Code Allowable Limit | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000317/LER-2016-003 | Unit 1 Automatic Trip on Loss of Load due to Spurious Steam Generator High Level Turbine Trip LER 16-003-00 for Calvert Cliffs Nuclear Power Plant, Unit No. 1 Regarding Automatic Trip on Loss of Load due to Spurious Steam Generator High Level Turbine Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000317/LER-2016-004 | High Energy Line Break Barrier Breeched Due to Human Performance Error Causing Both Service Water Trains to be Inoperable LER 16-004-00 for Calvert Cliffs, Unit 1 Regarding High Energy Line Break Barrier Breeched Due to Human Performance Error Causing Both Service Water Trains to be Inoperable | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability |
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