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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000317/LER-1999-006, :on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With1999-10-22022 October 1999
- on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With
05000317/LER-1998-011, :on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With1999-09-20020 September 1999
- on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With
05000317/LER-1999-005, :on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With1999-08-23023 August 1999
- on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With
05000317/LER-1999-003, :on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With1999-07-30030 July 1999
- on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With
05000317/LER-1999-002, :on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With1999-05-25025 May 1999
- on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With
05000317/LER-1997-010, :on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With1999-01-29029 January 1999
- on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With
05000317/LER-1998-009, :on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With1999-01-0808 January 1999
- on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With
05000317/LER-1998-008, :on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With1998-11-11011 November 1998
- on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With
05000318/LER-1998-005-01, :on 980725,initiated Plant Cooldown Due to RCS Pressure Boundary Leakage.Caused by Crack in Inconel Alloy 600-type Weld Filler Matl of Nozzle.Leaking Penetration Was Repaired from Outside of Pressurizer1998-08-24024 August 1998
- on 980725,initiated Plant Cooldown Due to RCS Pressure Boundary Leakage.Caused by Crack in Inconel Alloy 600-type Weld Filler Matl of Nozzle.Leaking Penetration Was Repaired from Outside of Pressurizer
05000318/LER-1998-004-01, :on 980723,manual Plant Trip Occurred Due to Moisture Separator Reheater Vent Line Rupture.Caused by Flow Accelerated Corrosion.Replaced Ruptured Pipe & Completed Insp of Other Small Bore high-energy Piping1998-08-24024 August 1998
- on 980723,manual Plant Trip Occurred Due to Moisture Separator Reheater Vent Line Rupture.Caused by Flow Accelerated Corrosion.Replaced Ruptured Pipe & Completed Insp of Other Small Bore high-energy Piping
05000318/LER-1998-003-01, :on 980507,relays out-of-calibration Were Noted Due to Bumped Dial & Actions Not Taken.Caused by Improperly Installed Cover.Technicians Will Be Trained on Event & Protective Covers Will Be Clearly Marked1998-06-0404 June 1998
- on 980507,relays out-of-calibration Were Noted Due to Bumped Dial & Actions Not Taken.Caused by Improperly Installed Cover.Technicians Will Be Trained on Event & Protective Covers Will Be Clearly Marked
05000317/LER-1998-007, :on 980404,eight of Sixteen MSSVs on Unit 1 Lifted at Pressure Above Setpoint Required in Tech Specs During as-found Lift Test.Cause of Event Currently Under Investigation.Reset Failed Valves1998-05-0404 May 1998
- on 980404,eight of Sixteen MSSVs on Unit 1 Lifted at Pressure Above Setpoint Required in Tech Specs During as-found Lift Test.Cause of Event Currently Under Investigation.Reset Failed Valves
05000317/LER-1998-006, :on 980325,1B DG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Nylon in Governors Shutdown Solenoid Valve.Conducted Review1998-04-21021 April 1998
- on 980325,1B DG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Nylon in Governors Shutdown Solenoid Valve.Conducted Review
05000317/LER-1998-005, :on 980312,spare Reactor Trip Breaker Did Not Meet TS Requirements.Caused by Inadequate Procedures.Revised Procedures to Include Testing Requirements for Spare Breaker1998-04-13013 April 1998
- on 980312,spare Reactor Trip Breaker Did Not Meet TS Requirements.Caused by Inadequate Procedures.Revised Procedures to Include Testing Requirements for Spare Breaker
05000318/LER-1998-002-01, :on 980305,failure of Handswitch Passive Contact to Close Occurred.Caused by Contacts in Lower Contact Block of Handswitch Did Not Close as Designed. Handswitch Replaced1998-04-0707 April 1998
- on 980305,failure of Handswitch Passive Contact to Close Occurred.Caused by Contacts in Lower Contact Block of Handswitch Did Not Close as Designed. Handswitch Replaced
05000317/LER-1998-004, :on 980303,battery Charger Circuit Breakers Were Noted Missing from Seismic Positioner.Caused by Quality Issue Related to Vendor.All safety-related 480-volt Circuit Breakers Have Been Inspected1998-04-0101 April 1998
- on 980303,battery Charger Circuit Breakers Were Noted Missing from Seismic Positioner.Caused by Quality Issue Related to Vendor.All safety-related 480-volt Circuit Breakers Have Been Inspected
05000318/LER-1998-001-01, :on 980113,unit 2B EDG Had Been Inoperable for 15 Days.Caused by Speed Switch Adapter Failure.Inspected/ Replaced Other Diesel Speed Switch Adapters to Ensure Spring Clips Are Not Degraded1998-02-12012 February 1998
- on 980113,unit 2B EDG Had Been Inoperable for 15 Days.Caused by Speed Switch Adapter Failure.Inspected/ Replaced Other Diesel Speed Switch Adapters to Ensure Spring Clips Are Not Degraded
05000317/LER-1998-002, :on 980107,fire Hose Station & Room Sprinkler Sys Were Noted out-of-service.Caused by Operating Mislabeled Valve.Correct Tagout Boundary Was Established & Verified by Addl Complete Walkdown of Tagout1998-02-0909 February 1998
- on 980107,fire Hose Station & Room Sprinkler Sys Were Noted out-of-service.Caused by Operating Mislabeled Valve.Correct Tagout Boundary Was Established & Verified by Addl Complete Walkdown of Tagout
05000317/LER-1998-003, :on 980113,damage Was Found on Stanchion & Restraining Steel of Unit 1 LPSI Sys Pipe Support Location on Common Discharge Line.Caused by LPSI Pump Discharge Check Valve Slam(S).Pipe Support Was Removed1998-02-0606 February 1998
- on 980113,damage Was Found on Stanchion & Restraining Steel of Unit 1 LPSI Sys Pipe Support Location on Common Discharge Line.Caused by LPSI Pump Discharge Check Valve Slam(S).Pipe Support Was Removed
05000317/LER-1998-001, :on 980104,Unit 1 Entered Condition Outside of Tech Specs Due to Having Both Secondary Control Element Assembly Position Indications out-of-svc.Caused by Position Indication Being Inoperable.Procedure Revised1998-02-0303 February 1998
- on 980104,Unit 1 Entered Condition Outside of Tech Specs Due to Having Both Secondary Control Element Assembly Position Indications out-of-svc.Caused by Position Indication Being Inoperable.Procedure Revised
05000317/LER-1997-007, :on 971029,discovered That Three Surveillance Test Procedures Were Not Completed within Test Interval. Caused by Excessive Use of 25% Grace Period Allowed for Completion of Surveillance.Revised Procedures1997-12-0101 December 1997
- on 971029,discovered That Three Surveillance Test Procedures Were Not Completed within Test Interval. Caused by Excessive Use of 25% Grace Period Allowed for Completion of Surveillance.Revised Procedures
05000317/LER-1997-009, :on 971024,automatic Reactor Trip Occurred. Caused by Failure to Properly Terminate Electrical Lead on Condenser Vacuum Breaker Handswitch During Prior Handswitch Maintenance.Over 200 Similar Connection Insp1997-11-20020 November 1997
- on 971024,automatic Reactor Trip Occurred. Caused by Failure to Properly Terminate Electrical Lead on Condenser Vacuum Breaker Handswitch During Prior Handswitch Maintenance.Over 200 Similar Connection Insp
05000317/LER-1997-008, :on 971017,two Reactor Protective Sys Channels Were OOS During Test.Caused by Significant Variations in Power Supply Voltages.Requested Maint to Back Out of Calibr of Channel C & Return Channel to Svc1997-11-12012 November 1997
- on 971017,two Reactor Protective Sys Channels Were OOS During Test.Caused by Significant Variations in Power Supply Voltages.Requested Maint to Back Out of Calibr of Channel C & Return Channel to Svc
05000317/LER-1996-001, :on 960117,SRW Heat Exchanger Microfouling High than Assumed in Design Basis Occurred.Caused by Original Design Calculations for SRW Heat Exchangers Assumed Min SRW Flow.New Operability Limits Implemented1997-10-21021 October 1997
- on 960117,SRW Heat Exchanger Microfouling High than Assumed in Design Basis Occurred.Caused by Original Design Calculations for SRW Heat Exchangers Assumed Min SRW Flow.New Operability Limits Implemented
05000317/LER-1997-006, :on 970722,cable Spreading Room Halon Sys Was Inoperable.Caused by Personnel Error.Operations Personnel Reminded of Possibility of Inoperable Dampers Affecting Halon Sys Operability1997-08-21021 August 1997
- on 970722,cable Spreading Room Halon Sys Was Inoperable.Caused by Personnel Error.Operations Personnel Reminded of Possibility of Inoperable Dampers Affecting Halon Sys Operability
05000317/LER-1997-004, :on 970602,trip Bypasses Were Not Removed When Thermal Power Was Increased Above 15%.Caused by Failure to Recognize Difference Between Nuclear Instrument & Delta-T. Revised Plant Procedures1997-07-0202 July 1997
- on 970602,trip Bypasses Were Not Removed When Thermal Power Was Increased Above 15%.Caused by Failure to Recognize Difference Between Nuclear Instrument & Delta-T. Revised Plant Procedures
05000317/LER-1997-005, :on 970529,reactor Coolant Sys Leak Occurred. Caused by Failed Compression Fitting.Conducted Review of Compression Fitting Maint Performed on High Pressure Systems & Completed Insps of Compression Fittings1997-06-30030 June 1997
- on 970529,reactor Coolant Sys Leak Occurred. Caused by Failed Compression Fitting.Conducted Review of Compression Fitting Maint Performed on High Pressure Systems & Completed Insps of Compression Fittings
05000317/LER-1997-003-01, :on 970424,fuel Moved in Spent Fuel Pool Without Charcoal Absorber Banks Being in Svc.Caused by Personnel Error.Fuel Movement Suspended Until All Appropriate Personnel Could Be Trained1997-05-23023 May 1997
- on 970424,fuel Moved in Spent Fuel Pool Without Charcoal Absorber Banks Being in Svc.Caused by Personnel Error.Fuel Movement Suspended Until All Appropriate Personnel Could Be Trained
05000318/LER-1997-003, :on 970423,chemistry Sampling Was Not Performed as Required by TS 3.4.7 Due to Insufficient Consideration of Precise Wording of TS on Part of Chemistry Personnel.Ts Will Be Clarified When Improved TS Are Implemented1997-05-21021 May 1997
- on 970423,chemistry Sampling Was Not Performed as Required by TS 3.4.7 Due to Insufficient Consideration of Precise Wording of TS on Part of Chemistry Personnel.Ts Will Be Clarified When Improved TS Are Implemented
05000318/LER-1997-002-01, :on 970405,containment Purge Valve Isolation Sys TS Violation Occurred.Caused by Inaccurate Implementation of TS 3.9.9.Personnel Air Lock Interlocks Restored1997-05-0505 May 1997
- on 970405,containment Purge Valve Isolation Sys TS Violation Occurred.Caused by Inaccurate Implementation of TS 3.9.9.Personnel Air Lock Interlocks Restored
05000318/LER-1997-001-01, :on 970401,refueling Machine Overload Protective Circuitry Was Inoperable Due to Failure to Correctly Translate Refueling Machine Circuitry Design Into Ts.Mod to Overload Bypass Was Installed1997-04-30030 April 1997
- on 970401,refueling Machine Overload Protective Circuitry Was Inoperable Due to Failure to Correctly Translate Refueling Machine Circuitry Design Into Ts.Mod to Overload Bypass Was Installed
05000317/LER-1997-002, :on 970220,misread TS Requirements Resulted in Inadequate Test.Caused by Lack of Strict Adherence to Wording of Plants TS Requirements.Edgs 1B,2A & 2B Were Successfully Tested & Returned to Svc1997-03-24024 March 1997
- on 970220,misread TS Requirements Resulted in Inadequate Test.Caused by Lack of Strict Adherence to Wording of Plants TS Requirements.Edgs 1B,2A & 2B Were Successfully Tested & Returned to Svc
05000317/LER-1997-001, :on 970110,spent Fuel Moved W/Ventilation Sys Inoperable & Missed Surveillance Occurred.Cause Analysis Being Performed to Determined Casual Factors & Generic Implications for Event.Surveillance Performed1997-02-10010 February 1997
- on 970110,spent Fuel Moved W/Ventilation Sys Inoperable & Missed Surveillance Occurred.Cause Analysis Being Performed to Determined Casual Factors & Generic Implications for Event.Surveillance Performed
05000318/LER-1996-006, :on 961210,discovered EDG Had Been Inoperable for Six Days.Caused by Personnel Error.Checked Fuse Holder Covers,Conducted Tailgate Training & Revised Procedure Re Installation of Fuse Holder Covers1997-01-10010 January 1997
- on 961210,discovered EDG Had Been Inoperable for Six Days.Caused by Personnel Error.Checked Fuse Holder Covers,Conducted Tailgate Training & Revised Procedure Re Installation of Fuse Holder Covers
05000318/LER-1996-002, :on 960522,missed Fire Watch Occurred Due to Personnel Error.Root Cause Analysis Has Been Completed. Plant Mgt Reemphasized to Site Personnel Importance of & Requirements for Fire Watches1996-12-31031 December 1996
- on 960522,missed Fire Watch Occurred Due to Personnel Error.Root Cause Analysis Has Been Completed. Plant Mgt Reemphasized to Site Personnel Importance of & Requirements for Fire Watches
05000318/LER-1996-005, :on 961117,automatic Reactor Trip Occurred Due to Closure of Feedwater Regulating Valve.Magnetic Particle Examination Was Conducted on New,Replacement Spring Retainers.No Indications Were Found1996-12-17017 December 1996
- on 961117,automatic Reactor Trip Occurred Due to Closure of Feedwater Regulating Valve.Magnetic Particle Examination Was Conducted on New,Replacement Spring Retainers.No Indications Were Found
05000318/LER-1996-004-01, :on 960926,missed Surveillance Occurred Due to Less than Adequate Technical Review of Stp.Procedures Revised1996-10-28028 October 1996
- on 960926,missed Surveillance Occurred Due to Less than Adequate Technical Review of Stp.Procedures Revised
05000317/LER-1995-005, :on 951109,manual Reactor Trip Occurred.Caused by Failure of Digital Feedwater Control Module FIC-1111. Reviewed Design Engineering Standards & Existing FP 2000 Digital Controllers Are Being Replaced1996-10-10010 October 1996
- on 951109,manual Reactor Trip Occurred.Caused by Failure of Digital Feedwater Control Module FIC-1111. Reviewed Design Engineering Standards & Existing FP 2000 Digital Controllers Are Being Replaced
05000317/LER-1996-004, :on 960802,two Asi Channels OOS Due to Reversed Nuclear Instrumentation Leads.Leads Were Correctly Reconnected When Plant Was Brought Down on 9608021996-09-0303 September 1996
- on 960802,two Asi Channels OOS Due to Reversed Nuclear Instrumentation Leads.Leads Were Correctly Reconnected When Plant Was Brought Down on 960802
05000318/LER-1996-003-01, :on 960619,discovered Missed Fire Protection Compensatory Action.Caused by Personnel Error.Provided Awareness Training to Personnel Re Fire Protection Compensatory Actions Expectations1996-07-17017 July 1996
- on 960619,discovered Missed Fire Protection Compensatory Action.Caused by Personnel Error.Provided Awareness Training to Personnel Re Fire Protection Compensatory Actions Expectations
05000318/LER-1996-002-01, :on 960522,fire Watch Missed.Caused by Personnel Error.Counseled Personnel Re Event1996-06-21021 June 1996
- on 960522,fire Watch Missed.Caused by Personnel Error.Counseled Personnel Re Event
05000317/LER-1996-003, :on 960423,discovered Holes in Containment Sump Screen Larger than Described in Ufsar.Holes Most Likely Installed During Plant Const.Sump Screens Visually Inspected & Repaired1996-05-24024 May 1996
- on 960423,discovered Holes in Containment Sump Screen Larger than Described in Ufsar.Holes Most Likely Installed During Plant Const.Sump Screens Visually Inspected & Repaired
05000317/LER-1996-002, :on 960410,required Fire Watch Missed.Caused by Lack of Fire Watch Ownership.Circumstances of Event Will Be Reviewed W/Appropriate Groups1996-05-14014 May 1996
- on 960410,required Fire Watch Missed.Caused by Lack of Fire Watch Ownership.Circumstances of Event Will Be Reviewed W/Appropriate Groups
05000318/LER-1996-001-01, :on 960227,breakers 552-41,552-21 & 552-61 Tripped Open in Plant Switchyard.Caused by Failure of Auxiliary Relay Card in Breaker 552-41.Failed Relay Card Replaced1996-03-28028 March 1996
- on 960227,breakers 552-41,552-21 & 552-61 Tripped Open in Plant Switchyard.Caused by Failure of Auxiliary Relay Card in Breaker 552-41.Failed Relay Card Replaced
05000317/LER-1996-001, :on 960117,determined That SW HX Microfouling Higher than Assumed in Design Basis.Caused by Design Deficiency.Conservative Operability Limits Established & Bay Temp & SW HXs Being Monitored1996-02-16016 February 1996
- on 960117,determined That SW HX Microfouling Higher than Assumed in Design Basis.Caused by Design Deficiency.Conservative Operability Limits Established & Bay Temp & SW HXs Being Monitored
05000317/LER-1995-006, :on 951116,manual Reactor Trip Occurred Due to Loss of 12 SG Feed Pump.Caused Oil Losses Allowing Pressure to Drop Before Standby Pump Could Restore Pressure.Trip Mechanism & Thrust Cleaned & Adjusted1995-12-13013 December 1995
- on 951116,manual Reactor Trip Occurred Due to Loss of 12 SG Feed Pump.Caused Oil Losses Allowing Pressure to Drop Before Standby Pump Could Restore Pressure.Trip Mechanism & Thrust Cleaned & Adjusted
05000317/LER-1995-005-01, :on 951109,manual Reactor Trip Occurred Due to Increasing SG 11 Water Level.Caused by Failure of Digital Control Module FIC-1111.Controller Sent to Vendor for Troubleshooting & Root Cause Analysis1995-12-11011 December 1995
- on 951109,manual Reactor Trip Occurred Due to Increasing SG 11 Water Level.Caused by Failure of Digital Control Module FIC-1111.Controller Sent to Vendor for Troubleshooting & Root Cause Analysis
05000317/LER-1995-004-01, :on 950816,inoperable Fire Barrier Penetration Seal Was Discovered.Caused by Inadequate Engineering Oversight & Less than Adequate Surveillance Procedure.Sealed Penetration Seal1995-09-15015 September 1995
- on 950816,inoperable Fire Barrier Penetration Seal Was Discovered.Caused by Inadequate Engineering Oversight & Less than Adequate Surveillance Procedure.Sealed Penetration Seal
05000317/LER-1995-003-01, :on 950730 & 31,entered TS 3.0.3 Due to High Bay Water Temps.Administration Limit for Bay Water Temp Raised & Current Unit 1 & Unit 2 SW Tube Type HXs Will Be Replaced1995-08-28028 August 1995
- on 950730 & 31,entered TS 3.0.3 Due to High Bay Water Temps.Administration Limit for Bay Water Temp Raised & Current Unit 1 & Unit 2 SW Tube Type HXs Will Be Replaced
05000317/LER-1995-002-01, :on 950616,manual Trip Occurred Due to Loss of 12 SG Feed Pump.Repaired Overspeed Trip Mechanism & Restarted Unit 11995-07-14014 July 1995
- on 950616,manual Trip Occurred Due to Loss of 12 SG Feed Pump.Repaired Overspeed Trip Mechanism & Restarted Unit 1
1999-09-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEAR05000317/LER-1999-006, :on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With1999-10-22022 October 1999
- on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With
ML20217G6971999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Calvert Cliffs Npp,Units 1 & 2.With 05000317/LER-1998-011, :on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With1999-09-20020 September 1999
- on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With
ML20216J8731999-09-10010 September 1999 Rev 52 to QA Policy for Calvert Cliffs Nuclear Power Plant ML20211J3531999-09-0101 September 1999 Safety Evaluation Supporting Amends 231 & 207 to Licenses DPR-53 & DPR-69,respectively ML20212A4441999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Ccnpp,Units 1 & 2. with ML17326A2011999-08-23023 August 1999 LER 99-004-00:on 990724,reactor Tripped Due to Main Transformer Bushing Flashover.Plant Was Brought to SS & Components Were Tested & Performed Satisfactorily.With 990823 Ltr 05000317/LER-1999-005, :on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With1999-08-23023 August 1999
- on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With
ML20210S6091999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-003, :on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With1999-07-30030 July 1999
- on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With
ML20210N6001999-07-27027 July 1999 ISI Summary Rept for Calvert Cliffs Unit 2. Page 2 of 3 in Encl 1 of Incoming Submittal Not Included ML20210B7941999-07-15015 July 1999 SER Denying Licensee Request for Changes to Current Ts,Re Deletion of Tendon Surveillance Requirements for Calvert Cliffs LD-99-039, Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified1999-06-30030 June 1999 Part 21 Rept Re Defect of ABB 1200A 4kV Vacuum Breakers. Initially Reported on 990625.Defect Results in Breaker Failing to Remain in Closed Position.Root Cause Evaluation & Corrective Action Plan Being Developed.Licensee Notified ML20209F1721999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Calvert Cliffs Npp.With LD-99-035, Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed1999-06-25025 June 1999 Part 21 Rept Re ABB 1200A 4KV Vacuum Breakers Performing Trip Free Operation When Close Signal Received by Breaker. Defect Results in Breaker Failing to Remain in Closed Position.Root Cause & CAP Being Developed ML20196C6981999-06-21021 June 1999 Safety Evaluation Concluding That Use of ASME Section XI Code Including Summer 1983 Addenda as Interim Code for Third 10-year Insp Interval at Calvert Cliffs Units 1 & 2 Until Review of 1998 Code Completed,Would Be Acceptable ML20195K2811999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Ccnpp,Units 1 & 2. with 05000317/LER-1999-002, :on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With1999-05-25025 May 1999
- on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With
ML20206U7031999-05-18018 May 1999 Rev 1 to Ran 97-031, Main CR Fire Analysis for IPEEE Section 4-1 ML20206R5871999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Ccnpp,Units 1 & 2. with ML20195B3891999-04-30030 April 1999 0 to CENPD-279, Annual Rept on ABB CE ECCS Performance Evaluation Models ML20205N2951999-04-13013 April 1999 Special Rept:On 990314,fire Detection Sys Was Removed from Svc to Support Mod to Replace SRW Heat Exchangers in Unit 2 SRW Room During Unit 2 Refueling Outage.Contingency Measure 15.3.5.A.1 Will Continue Until Fire Detection Sys Restored ML20205J8331999-04-0707 April 1999 Safety Evaluation Concluding That Security Lighting,Portable Lighting & Helmet Lights,As Described by Licensee Satisfies Underlying Purpose of 10CFR50,App R,Section Iii.J.Grants Licensee Request for Exemption ML20210T5211999-04-0101 April 1999 Rev 0 to Ccnpp COLR for Unit 2,Cycle 13 ML20205P5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20204H6471999-03-21021 March 1999 SER Re License Renewal of Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20204B5961999-03-17017 March 1999 Corrected Page 7 to SER for Amend 205 for License DPR-69. Staff Deleted Word Not on Line One of Page 7 ML20207L2991999-03-0808 March 1999 Safety Evaluation Supporting Amend 205 to License DPR-69 ML20207M8321999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Calvert Cliffs Nuclear Power Plant.With ML20203D4311999-02-0505 February 1999 Safety Evaluation Accepting Procedure Established for long-term Corrective Action Plan Related to Containment Vertical Tendons 05000317/LER-1997-010, :on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With1999-01-29029 January 1999
- on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With
ML20199G4671999-01-20020 January 1999 SER Accepting USI A-46 Implementation for Plant ML20206Q3221999-01-11011 January 1999 Special Rept:On 981226,wide Range Noble Gas Effluent RM Was Removed from Operable Status.Caused by Failure of mid-range Checksource to Properly Reseat.Completed Maint & post-maint Testing & RM Was Returned to Operable Status on 990104 ML20207L0451999-01-0808 January 1999 Cost-Benefit Risk Analyses:Radwaste Sys for Light Water Reactors ML20199F4781999-01-0808 January 1999 Safety Evaluation Concluding That Bg&E Performed Appropriate Evaluations of Operational Configurations of safety-related power-operated Gate Valves to Identify Valves Susceptible to Pressure Locking.Concludes GL 95-07 Actions Were Addressed 05000317/LER-1998-009, :on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With1999-01-0808 January 1999
- on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With
ML20198S7591999-01-0707 January 1999 SER Accepting Quality Assurance Program Description Change for Calvert Cliffs Nuclear Power Plant,Units 1 & 2 ML20199E2931998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Calvert Cliffs Npp. with ML20207M2281998-12-31031 December 1998 1998 Annual Rept for Bg&E. with ML20206R9911998-12-0808 December 1998 Rept of Changes,Tests & Experiments (10CFR50.59(b)(2)). with ML20198B2631998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Calvert Cliffs Nuclear Power Plant,Units 1 & 2.With ML20195H1001998-11-16016 November 1998 Safety Evaluation of First Containment Insp Interval Iwe/Iwl Program Alternative 05000317/LER-1998-008, :on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With1998-11-11011 November 1998
- on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With
ML20195E5281998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Calvert Cliffs Nuclear Power Station,Units 1 & 2.With ML20196E2211998-10-31031 October 1998 Non-proprietary Rev 03-NP to CEN-633-NP, SG Tube Repair for Combustion Engineering Designed Plant with 3/4 - .048 Wall Inconel 600 Tubes Using Leak Limiting Alloy 800 Sleeves ML20154Q7191998-10-21021 October 1998 Special Rept:On 980923,unit 1 Wrngm Was Removed from Operable Status.Caused by Failure of Process Flow Transducer.Completed Maint to Remove Process Flow Transducer Input to Wrngm Microprocessor & Completed Formal Evaluation ML20154G3931998-10-0505 October 1998 Safety Evaluation Concluding That Flaw Tolerance Evaluation for Assumed Flaw in Inboard Instrument Weld of Pressurizer Meets Rules of ASME Code ML20154M5841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Calvert Cliffs Nuclear Plant,Units 1 & 2.With ML20153C1091998-09-18018 September 1998 Part 21 Rept Re Defective Capacity Control Valves.Trentec Personnel Have Been in Contact with Bg&E Personnel Re Condition & Have Requested Potentially Defective Valves ML20153C2571998-09-18018 September 1998 Special Rept:On 980830,wide Range Noble Gas Monitor (Wrngm) Channel Was Removed from Operable Status.Caused by Need to Support Performance of Required 18-month Channel Calibr.Will Return Wrngm to Operable Status by 980925 1999-09-30
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seRC P.rne 308 UK NUCLEAR REO'JLATORY _
M AP0flOVE3 Oese eso. 3190 E104 LICENSEE EVENT REPORT (LER)
PACILITY esAaBE (11 DOCRET NURSER (3)
PRUE W Calvert Cliffs. Unit 1 o Is l o lo l o l3 l117 1 lor l014 TITLE 14)
EVENT DATE 106 LER NUnsgER del R5POstT DATE m OTHER PACILITIES INVOLVED 18) sag MONTH DAY YEAR P AcaLITY NAuss DOCKET NUGAGERIS) i 5'
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LICCNSEE CONTACT POft TH0S LER (131 NAME TELEPHONE NUMBE1 AREA CODE Brian E. Holian, Engineer 31011 21610 l-1413 1814 COMPLETE ONE LINE FOR EACH CORMOfeE887 FAILURE DESCRt350 IN THIS ItEPORT (13)
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At 1416 on January 16, 1985 a ten minute Safety Injection Tank (SIT) check valve inleakage test was conpleted.
Initial results indicated excessive inleakage into two SITS. The results were presented to the Plant Operations and Safety Review Omni ttee (IOSRC).
It was decided that the high pressure Safety Injection flow rate l
specified in the Technical Specifications could not be assured. Additionally, under l
certain ciretsnstances, the SIT inleakage could render the tanks inoperable. Based on this information the POSRC reccmnended that both Unit 1 High Pressure Safety l
Injection headers be declared inoperable. Reactor shutdown was conpleted at 1845.
'IWo SIT outlet check valves were overhauled on January 17, 1985. Each valve's seating surface o-ring was found g roximately one-third degraded. The Ethylene Prepylene o-rings had been upgraded previously due to their inability to withstand the tenperature environment in which these valves operate. Both o-rings were replaced with a more heat resistant o-ring. Both check valves were subsequently satisfactorily leak tested.
The following corrective actions will be taken as a result of this event:
(1) All SIT outlet check valves will be leak tested quarterly.
(2) 'Ihe renaining six SIT outlet chec* valves will be overhauled during their respective 1985 refueling outage. The Ethylene Propylene o-rings will be replaced by the higher talperature resistant Dupont Kalrez caTpound.
(3) A change to the Technical Specifications justifying a more flexible mininun conbined flow rate for the lowest three High Pressure Safety Injection leg flows will continue to be pursued.
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NRC Penn 3BSA LICEN!EE EVENT REPORT (LER) TEXT CONTINUATION aPPaovEo one No. sm-eion EXPtIES. 8/31/95 FACIL3Tv NAmet II)
DOCKET NUMBER (2)
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On the afternoon of January 15,1985, a leak test was performed on Unit 1 and Unit 2-Safety Injection Tank (SIT) (EIIS BP-TK) Outlet Check Valves (EIIS BP-V). This test was performed to obtain backgrour.d data necessary for a revision to Surveillance Test Procedure (STP) 0-65, " Quarterly Valve Operability Verification". The test consisted e
of pressurizing the High Pressure Safety Injection (HPSI). (EIIS BQ) Header for ten minutes, simultaneously monitoring SIT inleakage. There are two possible leakage paths.- The first path is through two 1" Isolation Valves (EIIS BP-ISV): the SIT " Check Valve Leakage Drain Valve" and the " Fill Valve". The second path is simply reverse flow through the SIT outlet check valve. Unit 2 results were considered negligible whereas Unit i results warranted further investigation to more accurately verify and quantify SIT check valve inleakage.
At 1406 on January 16,1985, with Unit 1 in MODE 1, Number 13 High Pressure Safety Injection Pump (EIIS BQ-P) was started commencing a second inleakage test. This test was. patterned after the Calvert Cliffs' Opcrating Instruction for leak testing SIT fill, drain and tank outlet check valves. Prior to starting the HPSI pump, one potential leakage path was isolated by closing the manual isolation valves for the SIT fill header. At 1416 the HPSI pump was secured. A marked rise was noted in #11A SIT during the ten minute pump run. (This identical tank also had the highest indicated inleakage on the previous day's test.) The following rates of volume change were calculated:
SIT INLEAKAGE (GPM) 11A 27.2 11B 7.6 12A 1.6 12B 2.0 All applicable data was assembled and presented to the Plant Operations and Safety Review Committee (POSRC).
The unsuing discussion centered on the safety consequences of this inleakage. Two over-riding concerns dominated the discussion.
First, the HPSI flow rate specified in the Technical Specifications could not be assured, thereby potentially worsening the consequences of the limiting small break Loss of Coolant Accident (LOCA). Secondly, during prolonged operation of HPSI, the SIT inleakage could cause the tank's relief valve (EIIS BP-RV) to lift (250 t 8 psig setpoint), reducing the nitrogen inventory and thereby rendering the tanks inoperable.
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asRC Feren 3e6A U 5. NUCLEAR LESULATORY COMMIS$10N LICENSEE EVENT REPORT (LER) TEXT CONTINUATION AreRovfo oms No mo-om EMPIRES 8/31/85 F ACILITY NAMS (1p DOCKET NUMSER (2)
LER NUMBER (S)
PAGE (33
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= =.m vs*a Calvert Cliffs, Unit 1 olsjololol3l1l7 8l 5 0l0l1 0l0 0 l3 oF 0 l4 TEXT Mmere esos e auguset use esWeenaf NAC Fonn JE4W $1D Based on this information the POSRC recommended that both Unit 1 HPSI Headers be declared inoperable. At 1600 on January 16,1985, the Plant Superintendent ordered a Unit 1 shutdown in accordance with the requirements of Technical Specification 3.0.3. Operators commenced reducing reactor power at 1640 and declared an Unusual Event due to Unit 1 shutdown. At 1835 the Main Turbine (EIIS SB-TRB) was taken off-line. Reactor (EIIS AC) shutdown was completed at 1845.
At 0340 on January 17,1985, Unit 1 entered MODE 4, thereby downgrading from the Emergency Action Level " Unusual Event". Preparations were made for draining and venting 11A and 11B SITS. Work packages were prepared for overhauling both of these tanks' outlet check valves. These valves are 12" - 1500#, swinging disc check valves with an inclined, " soft" seat. They provide pressure isolation for the tanks from both primary coolant pressure and HPSI pump discharge pressure. An Ethylene Propylene o-ring (Type E-832-9)(EUS BP-SEAL) is utilized at the seating surface. This material has bean found to deteriorate at a rate greater than that specified by the manufacturer. Three different types of ethylene propylene have been used since initial operation. Although successive o-ring materials have had better temperature and radiation resistant qualities, each type has experienced degradation. A facility modification was approved in December 1983 to allow for the use of Dupont Kalrez 4079 as replacement o-ring material.
Kalrez, a perfluoroelastomer, will better withstand the temperature environment in which these valves operate.
This modification had been scheduled for completion during 1985 on both units.
Repairs commenced concurrently on both SIT outlet check valves at approximately 1200 on January 17, 1985. The valves were disassembled and valve internals were cleaned and inspected.
Approximately one-third of the o-ring seats were found degraded. Both o-rings were replaced with Kalrez Compound 4079. Valve repairs took approximately 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br />. Both SITS were filled by 1556 on January 18, 1985. Both check valves were subsequently satisfactorily tested for zero leakage. Unit 1 was taken critical at 1825 on January 19,1985. At 2258 Unit 1 was paralleled to the grid.
The following corrective actions will be taken as a result of this event:
1.
All SIT outlet check valves will be leak tested quarterly.
2.
The remaining six SIT outlet check valves will be overhauled during their respective 1985 refueling outage.
The Ethylene Propylene o-rings will be replaced by the higher temperature resistant Kalrez compound.
3.
A change to tne Technical Specifications justifying a more flexible minimum combined flow rate for the lowest three High Pressure Safety Injection leg flows will continue to be pursued.
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maC Poem atWa UL 88UCLEIA REGULATony C LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
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mo, nvi ASSESSMENT OF SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT f
Concerning the safety implications of this event, given the limiting small break Loss of Coolant Accident (LOCA), assuming the worst single failure and the lowest combination of three injection leg flows, and crediting no flow from the Chemical Volume and Control System (CVCS) (EIIS CB), the flow reaching the core could have fallen'short of the value assumed in the small break LOCA analysis. However, the hot full power moderator temperature coefficient, the peak linear heat rate, and the axial shape index have been significantly less adverse than those assumed in the accident analysis. It is also likely that some CVCS flow would exist. A specific small break LOCA calculation using the most adverse conditions that existed throughout cycle life (in conjunction with modeling the pressure dependent SIT inleakage) might, therefore, show acceptable results for peak clad temperature.
Such a calculation was not performed. Finally, NRC test programs bsve shown that significant conservatism exists in the mandated LOCA methodology.
Besides degraded HPSI flow concerns, the consequences of SIT inoperability must be
. addressed. SIT inleakage could cause a situation whereby one or more SITS may become inoperable. Substantial inleakage could pressurize a tank sufficiently to lift its relief valve, thereby reducing the nitrogen inventory. This consequence would not precent a concern in the large break LOCA analyses where SIT discharge occurs prior to the commencement of HPSI flow. Additionally, our most limiting small break, i
LOCA shows clad' temperature peaking prior to SIT discharge. SIT water in this case-is not required to limit peak clad temperature, although it may accelerate the rate o'f subsequent cooldown.
Thre.e additional Safety Implications were considered. The first, the possibility of the overpressurization of a SIT, was discounted due to the capability of the associated relief valve to adequately pass at least twice the amount of this event's measured l
inleakage. The second, possible HPSI pump run out, is not possible in this case due to l
the presence of preset throttled HPSI flow valves in the discharge piping of the HPSI pumps. Lastly, the effect of degraded HPSI flow was evaluated for the main steam line break event analysis. In this event steam generator blowdown is complete, and peak reactivity and return to power occur prior to boration from HPSI reaching the core. Therefore, the minor diversion to the SITS has no impact.
1 An examination of previous LER's dealing with Safety Injection System problems revealed the following similar Events: 82-033, and 78-031.
The contact person for this Event is B. E. Holian (301) 260-4384.
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.J B ALTIMORE G AS AND' ELECTRIC COMPANY P.O. B O X 14 7 5 '
B ALTIM OR E M A R YL AN D 21203 NUCLEAR POWER DEPARTMENT '
' CALVERT CLIFFS NUCLEAR POWER PL ANT LUSBY. M ARYLAND 20657 February _8, 1985 U. S. Nuclear Regulatory Comission Docket No.
50-317 Document Control Desk License No. DPR 53 Washington, D. C.
20555
Dear Sirs:
'Ihe attached LER 85 ')1 is being sent to you as required by 10 CFR 50.73.
Should you have any questions regarding this report, we would be pleased to discuss them with you.
Very truly yours, 1SLA' L. B. Russell Plant Superintendent M
LBR/BEH/pah cc: Dr. 'Ihomas E. Murley Director, Office of Management Information and Program Control Messrs:
A. E. Lundvall, Jr.
J. A. Tiernan i
i l
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05000317/LER-1985-001, :on 850116,leakage Discovered in Two Safety Injection Tank Check Valves Necessitating Reactor Shutdown. Caused by Degraded O Rings.O Rings to Be Replaced & Tech Specs Changed |
- on 850116,leakage Discovered in Two Safety Injection Tank Check Valves Necessitating Reactor Shutdown. Caused by Degraded O Rings.O Rings to Be Replaced & Tech Specs Changed
| | 05000317/LER-1985-001-01, :on 850116,reactor Shut Down.Caused by Excessive Inleakage Into Two HPCI Safety Injection Tanks.Two Outlet Check Valves Overhauled |
- on 850116,reactor Shut Down.Caused by Excessive Inleakage Into Two HPCI Safety Injection Tanks.Two Outlet Check Valves Overhauled
| | 05000318/LER-1985-001-02, :on 850423,manual Trip Occurred as Result of Degradation of Reactor Coolant Pump 21A Shaft Seal. Degradation Caused by Temp Fluctuations Resulting in Pressure Oscillations Between Stages of Seal |
- on 850423,manual Trip Occurred as Result of Degradation of Reactor Coolant Pump 21A Shaft Seal. Degradation Caused by Temp Fluctuations Resulting in Pressure Oscillations Between Stages of Seal
| | 05000317/LER-1985-002, :on 850205,reactor Tripped on Low Steam Generator Water Level Condition.Caused by Personnel Error. Event Reviewed & Training Will Be Revised If Necessary |
- on 850205,reactor Tripped on Low Steam Generator Water Level Condition.Caused by Personnel Error. Event Reviewed & Training Will Be Revised If Necessary
| | 05000318/LER-1985-002-01, :on 850506,automatic Trip Occurred Due to Low Reactor Coolant Flow Condition Resulting from Loss of Reactor Coolant Pump 21A.Caused by Jarring of Auxiliary Cubicle Door Housing 251 Overcurrent Device |
- on 850506,automatic Trip Occurred Due to Low Reactor Coolant Flow Condition Resulting from Loss of Reactor Coolant Pump 21A.Caused by Jarring of Auxiliary Cubicle Door Housing 251 Overcurrent Device
| | 05000317/LER-1985-003, :on 850405,7 of 16 Main Steam Valves Found to Be Out of Tolerance.Caused by Measurement Technique & Room Equilibrium Temp.Main Steam Safety Valves Reset Prior to Completion of Test |
- on 850405,7 of 16 Main Steam Valves Found to Be Out of Tolerance.Caused by Measurement Technique & Room Equilibrium Temp.Main Steam Safety Valves Reset Prior to Completion of Test
| | 05000318/LER-1985-003-01, :on 850518,incorrect Stud Matl & Cracked Studs Identified in Pressurizer Spray Valves & Bypass Valves. Problems Initially Identified on 850425 Following Reactor Trip.Studs Replaced W/Approved Matl |
- on 850518,incorrect Stud Matl & Cracked Studs Identified in Pressurizer Spray Valves & Bypass Valves. Problems Initially Identified on 850425 Following Reactor Trip.Studs Replaced W/Approved Matl
| | 05000317/LER-1985-004, :on 850406,inadvertent ESF Actuation Occurred During Surveillance Testing While Facility in Mode 4.Caused by Inadequacy of Test Procedure.Esf Procedures Associated W/Blocked Signals Revised |
- on 850406,inadvertent ESF Actuation Occurred During Surveillance Testing While Facility in Mode 4.Caused by Inadequacy of Test Procedure.Esf Procedures Associated W/Blocked Signals Revised
| | 05000318/LER-1985-004-01, :on 850518,surveillance Testing Determined That Control Room post-loss of Coolant Incident Filter Sys Did Not Meet Limits for Flow Rate,Pressure Drop & Efficiency. Caused by Accumulation of Dust & Dirt |
- on 850518,surveillance Testing Determined That Control Room post-loss of Coolant Incident Filter Sys Did Not Meet Limits for Flow Rate,Pressure Drop & Efficiency. Caused by Accumulation of Dust & Dirt
| | 05000317/LER-1985-005-01, :on 850406,inadvertent Initiation of Steam Generator Isolation Signal Occurred.Caused by Failure to Insert Keys Necessary to Block Signal in Keyswitches Prior to Cooldown Procedure.Procedure Modified |
- on 850406,inadvertent Initiation of Steam Generator Isolation Signal Occurred.Caused by Failure to Insert Keys Necessary to Block Signal in Keyswitches Prior to Cooldown Procedure.Procedure Modified
| | 05000318/LER-1985-005, :on 850523,recirculation Actuation Signal Inadvertently Initiated.Caused by Technician Violating Procedure,Which Stipulates That Only One Channel Can Be Tested at Time.Technicians Counseled |
- on 850523,recirculation Actuation Signal Inadvertently Initiated.Caused by Technician Violating Procedure,Which Stipulates That Only One Channel Can Be Tested at Time.Technicians Counseled
| | 05000318/LER-1985-006-01, :on 850526,both Emergency Diesel Generators Declared Inoperable Due to Cracks in Interpolar Connections of Damper Windings on Rotor Poles of Generator.Interpolar Connections Removed |
- on 850526,both Emergency Diesel Generators Declared Inoperable Due to Cracks in Interpolar Connections of Damper Windings on Rotor Poles of Generator.Interpolar Connections Removed
| | 05000317/LER-1985-006, :on 850418,maint Personnel Removed Upper Guide Structure from Reactor Vessel W/O Fuel Handling Supervisor. Cause Not Stated.Procedures Revised to Require Fuel Handling Supervisor to Sign Off on Procedure |
- on 850418,maint Personnel Removed Upper Guide Structure from Reactor Vessel W/O Fuel Handling Supervisor. Cause Not Stated.Procedures Revised to Require Fuel Handling Supervisor to Sign Off on Procedure
| | 05000317/LER-1985-007, :on 850415,HPSI Sys Injection Leg Flow Rates Outside Tech Specs.Cause Not Stated.Tech Spec Changes Implemented |
- on 850415,HPSI Sys Injection Leg Flow Rates Outside Tech Specs.Cause Not Stated.Tech Spec Changes Implemented
| | 05000318/LER-1985-007-01, :on 850626,main Vent Noble Gas Monitor Iodine & Particulate Samplers Declared Out of Svc Due to Surveillance Test Not Being Performed.Caused by Personnel Error.Site Procedures Revised |
- on 850626,main Vent Noble Gas Monitor Iodine & Particulate Samplers Declared Out of Svc Due to Surveillance Test Not Being Performed.Caused by Personnel Error.Site Procedures Revised
| | 05000318/LER-1985-008-01, :on 850724,MSIV Failed to Fully Close & Declared Inoperable.Caused by Oil Deficiency Due to Gas Bubble in Hydraulic Fluid Header & Addl Component Malfunctions.Suppressor Bladders Replaced |
- on 850724,MSIV Failed to Fully Close & Declared Inoperable.Caused by Oil Deficiency Due to Gas Bubble in Hydraulic Fluid Header & Addl Component Malfunctions.Suppressor Bladders Replaced
| | 05000317/LER-1985-008, :on 850806,main Turbine Tripped on High Moisture Separator Reheater Level.Caused by High Level Dump Manual Isolation Valve Being Left in Shut Position After Maint Performed.Work Forms Modified |
- on 850806,main Turbine Tripped on High Moisture Separator Reheater Level.Caused by High Level Dump Manual Isolation Valve Being Left in Shut Position After Maint Performed.Work Forms Modified
| | 05000317/LER-1985-009, :on 850806,reactor Tripped on Low Steam Generator Water Level Due to Insufficient Feed Pump Speed. Caused by Personnel Error.Evaluation Will Be Performed Frequently on Plant Simulator |
- on 850806,reactor Tripped on Low Steam Generator Water Level Due to Insufficient Feed Pump Speed. Caused by Personnel Error.Evaluation Will Be Performed Frequently on Plant Simulator
| | 05000318/LER-1985-009-01, :on 851015,svc Water Subsystem 21 Declared Inoperable.Caused by Partial Blockage of Saltwater Sys Flow Through Svc Water HX 21.HX Cleaned & Returned to Svc |
- on 851015,svc Water Subsystem 21 Declared Inoperable.Caused by Partial Blockage of Saltwater Sys Flow Through Svc Water HX 21.HX Cleaned & Returned to Svc
| | 05000317/LER-1985-010, :on 850807,reactor Trip Occurred Due to Main Turbine Trip.Caused by Improperly Set Thrust Bearing Wear Detector Device Trip Settings.Detector Removed for Maint & Investigation.Detector Readings Increased |
- on 850807,reactor Trip Occurred Due to Main Turbine Trip.Caused by Improperly Set Thrust Bearing Wear Detector Device Trip Settings.Detector Removed for Maint & Investigation.Detector Readings Increased
| | 05000318/LER-1985-010-01, :on 851019,during Surveillance Test,Determined That Pressurizer Safety Valve 2-RC-201-RV Lift Setpoint Out of Spec.Setpoint Reset |
- on 851019,during Surveillance Test,Determined That Pressurizer Safety Valve 2-RC-201-RV Lift Setpoint Out of Spec.Setpoint Reset
| | 05000318/LER-1985-010, :on 851019,determined That Pressurizer Safety Valve 2-RC-201-RV Lift Setpoint Out of Spec.Cause Undetermined.Setpoint Reset.Setpoint Rechecked on 851201 & Found to Be within 2 Psi |
- on 851019,determined That Pressurizer Safety Valve 2-RC-201-RV Lift Setpoint Out of Spec.Cause Undetermined.Setpoint Reset.Setpoint Rechecked on 851201 & Found to Be within 2 Psi
| | 05000318/LER-1985-011, :on 851019,11 of 16 Main Steam Safety Valve (MSSV) Setpoints Out of Tech Spec Range.Valves Reset & Procedures Revised.On 860123,one MSSV Outside Tech Specs. Caused by Measuring Technique |
- on 851019,11 of 16 Main Steam Safety Valve (MSSV) Setpoints Out of Tech Spec Range.Valves Reset & Procedures Revised.On 860123,one MSSV Outside Tech Specs. Caused by Measuring Technique
| | 05000318/LER-1985-011-01, :on 851019,while in Mode 3 Shutdown, Surveillance Test Procedure Determined 11 of 16 Main Steam Safety Valve (MSSV) Setpoints Out of Spec.Valve Setpoints Reset & Hydroset Sent to Vendor |
- on 851019,while in Mode 3 Shutdown, Surveillance Test Procedure Determined 11 of 16 Main Steam Safety Valve (MSSV) Setpoints Out of Spec.Valve Setpoints Reset & Hydroset Sent to Vendor
| | 05000317/LER-1985-011, :on 850930,reactor Automatically Tripped on Loss of Load Due to Main Turbine Loss.Caused by Intermittent Ground or High Level Alarm in Circuitry Actuating Feedwater Heater |
- on 850930,reactor Automatically Tripped on Loss of Load Due to Main Turbine Loss.Caused by Intermittent Ground or High Level Alarm in Circuitry Actuating Feedwater Heater
| | 05000318/LER-1985-012-01, :on 851212,during Mode 1,reactor Tripped on Low Steam Generator Water Due to Loss of Steam Generator Feed Pump 21.Caused by Defective High Signal Selector.Selector Replaced |
- on 851212,during Mode 1,reactor Tripped on Low Steam Generator Water Due to Loss of Steam Generator Feed Pump 21.Caused by Defective High Signal Selector.Selector Replaced
| | 05000317/LER-1985-012, :on 851002,main Turbine Tripped on Erroneous Feedwater Heater 12C hi-hi Signal to Turbine Trip Circuit. Caused by Grounded Feedwater Heater Level Control Switch. Ground Control Switch Repaired |
- on 851002,main Turbine Tripped on Erroneous Feedwater Heater 12C hi-hi Signal to Turbine Trip Circuit. Caused by Grounded Feedwater Heater Level Control Switch. Ground Control Switch Repaired
| | 05000318/LER-1985-013-01, :on 851111,operator Inadvertently Initiated Safety Injection Actuation & Steam Generator Isolation Signal While Energizing Esfas.Caused by Failure of Generator to Use Correct Section of Instruction |
- on 851111,operator Inadvertently Initiated Safety Injection Actuation & Steam Generator Isolation Signal While Energizing Esfas.Caused by Failure of Generator to Use Correct Section of Instruction
| | 05000317/LER-1985-013, :on 851009,unidentified RCS Leakage Determined to Be Greater than 1.0 Gpm.Caused by Cracked Weld Between Reactor Coolant Pump Shaft Seal & Control Bleedoff Line.Line & Flanges Replaced.Design Mod Implemented |
- on 851009,unidentified RCS Leakage Determined to Be Greater than 1.0 Gpm.Caused by Cracked Weld Between Reactor Coolant Pump Shaft Seal & Control Bleedoff Line.Line & Flanges Replaced.Design Mod Implemented
| | 05000317/LER-1985-014, :on 851120,discovered One Isolation Damper in Each of Two Control Room HVAC Inlet Ducts Inoperable.Caused by Improper Adjustment of Damper Linkages.Blade Brackets Replaced & Procedure Changed |
- on 851120,discovered One Isolation Damper in Each of Two Control Room HVAC Inlet Ducts Inoperable.Caused by Improper Adjustment of Damper Linkages.Blade Brackets Replaced & Procedure Changed
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