05000317/LER-1999-006, :on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With1999-10-22022 October 1999
- on 990922,manual Reactor Trip Was Noted.Caused by Inadequate Electrical Current Determination.Evaluated Trip Risk Assessment Process for Enhancements.With
05000317/LER-1998-011, :on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With1999-09-20020 September 1999
- on 980428,prematurely Released Fire Watch Was Noted.Caused by Inadequate Cure Time Communications.Revised Configuration Control Documents.With
05000317/LER-1999-005, :on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With1999-08-23023 August 1999
- on 990720,corrosion Behavior & Onset of Oxide Spalling of High Duty Fuel Noted on Fuel Assemblies.Caused by Normal Phenomenon.Operability Evaluation for Current Cycle Operation Will Be Performed.With
05000317/LER-1999-003, :on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With1999-07-30030 July 1999
- on 990701,recognized That Unapproved Methodology Was Used to Allow CREVS to Remain Operable in accept-as-is Condition.Regulatory Notification Required in 10CFR50.72(b)(1)(ii)(A) Performed.With
05000317/LER-1999-002, :on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With1999-05-25025 May 1999
- on 990401,discovered That Radioactive Sources Were Lost.Caused by Inadequate Control.Searched Storage Locations on Three Separate Occasions,Including Document Storage Locations.With
05000317/LER-1997-010, :on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With1999-01-29029 January 1999
- on 971210,1B EDG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Stainless Steel Foreign Matl in Governor Hydraulic Boundaries.Stainless Steel Replaced.With
05000317/LER-1998-009, :on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With1999-01-0808 January 1999
- on 980408,required Hourly Fire Watch Missed, When Contractor Maint Worker Failed to Perform Fire Watch Patrol.Caused by Personnel Error.Plant Mgt Reiterated Expectation to Contractor Personnel.With
05000317/LER-1998-008, :on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With1998-11-11011 November 1998
- on 981020,reactor Protective Sys Instrumentation TS Error Was Noted.Caused by Incorrect Use of Thermal Power in Ts.Revised TSs 3.3.1 & 3.3.2.With
05000318/LER-1998-005-01, :on 980725,initiated Plant Cooldown Due to RCS Pressure Boundary Leakage.Caused by Crack in Inconel Alloy 600-type Weld Filler Matl of Nozzle.Leaking Penetration Was Repaired from Outside of Pressurizer1998-08-24024 August 1998
- on 980725,initiated Plant Cooldown Due to RCS Pressure Boundary Leakage.Caused by Crack in Inconel Alloy 600-type Weld Filler Matl of Nozzle.Leaking Penetration Was Repaired from Outside of Pressurizer
05000318/LER-1998-004-01, :on 980723,manual Plant Trip Occurred Due to Moisture Separator Reheater Vent Line Rupture.Caused by Flow Accelerated Corrosion.Replaced Ruptured Pipe & Completed Insp of Other Small Bore high-energy Piping1998-08-24024 August 1998
- on 980723,manual Plant Trip Occurred Due to Moisture Separator Reheater Vent Line Rupture.Caused by Flow Accelerated Corrosion.Replaced Ruptured Pipe & Completed Insp of Other Small Bore high-energy Piping
05000318/LER-1998-003-01, :on 980507,relays out-of-calibration Were Noted Due to Bumped Dial & Actions Not Taken.Caused by Improperly Installed Cover.Technicians Will Be Trained on Event & Protective Covers Will Be Clearly Marked1998-06-0404 June 1998
- on 980507,relays out-of-calibration Were Noted Due to Bumped Dial & Actions Not Taken.Caused by Improperly Installed Cover.Technicians Will Be Trained on Event & Protective Covers Will Be Clearly Marked
05000317/LER-1998-007, :on 980404,eight of Sixteen MSSVs on Unit 1 Lifted at Pressure Above Setpoint Required in Tech Specs During as-found Lift Test.Cause of Event Currently Under Investigation.Reset Failed Valves1998-05-0404 May 1998
- on 980404,eight of Sixteen MSSVs on Unit 1 Lifted at Pressure Above Setpoint Required in Tech Specs During as-found Lift Test.Cause of Event Currently Under Investigation.Reset Failed Valves
05000317/LER-1998-006, :on 980325,1B DG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Nylon in Governors Shutdown Solenoid Valve.Conducted Review1998-04-21021 April 1998
- on 980325,1B DG Failed to Start During Performance of Routine Surveillance Test.Caused by Piece of Nylon in Governors Shutdown Solenoid Valve.Conducted Review
05000317/LER-1998-005, :on 980312,spare Reactor Trip Breaker Did Not Meet TS Requirements.Caused by Inadequate Procedures.Revised Procedures to Include Testing Requirements for Spare Breaker1998-04-13013 April 1998
- on 980312,spare Reactor Trip Breaker Did Not Meet TS Requirements.Caused by Inadequate Procedures.Revised Procedures to Include Testing Requirements for Spare Breaker
05000318/LER-1998-002-01, :on 980305,failure of Handswitch Passive Contact to Close Occurred.Caused by Contacts in Lower Contact Block of Handswitch Did Not Close as Designed. Handswitch Replaced1998-04-0707 April 1998
- on 980305,failure of Handswitch Passive Contact to Close Occurred.Caused by Contacts in Lower Contact Block of Handswitch Did Not Close as Designed. Handswitch Replaced
05000317/LER-1998-004, :on 980303,battery Charger Circuit Breakers Were Noted Missing from Seismic Positioner.Caused by Quality Issue Related to Vendor.All safety-related 480-volt Circuit Breakers Have Been Inspected1998-04-0101 April 1998
- on 980303,battery Charger Circuit Breakers Were Noted Missing from Seismic Positioner.Caused by Quality Issue Related to Vendor.All safety-related 480-volt Circuit Breakers Have Been Inspected
05000318/LER-1998-001-01, :on 980113,unit 2B EDG Had Been Inoperable for 15 Days.Caused by Speed Switch Adapter Failure.Inspected/ Replaced Other Diesel Speed Switch Adapters to Ensure Spring Clips Are Not Degraded1998-02-12012 February 1998
- on 980113,unit 2B EDG Had Been Inoperable for 15 Days.Caused by Speed Switch Adapter Failure.Inspected/ Replaced Other Diesel Speed Switch Adapters to Ensure Spring Clips Are Not Degraded
05000317/LER-1998-002, :on 980107,fire Hose Station & Room Sprinkler Sys Were Noted out-of-service.Caused by Operating Mislabeled Valve.Correct Tagout Boundary Was Established & Verified by Addl Complete Walkdown of Tagout1998-02-0909 February 1998
- on 980107,fire Hose Station & Room Sprinkler Sys Were Noted out-of-service.Caused by Operating Mislabeled Valve.Correct Tagout Boundary Was Established & Verified by Addl Complete Walkdown of Tagout
05000317/LER-1998-003, :on 980113,damage Was Found on Stanchion & Restraining Steel of Unit 1 LPSI Sys Pipe Support Location on Common Discharge Line.Caused by LPSI Pump Discharge Check Valve Slam(S).Pipe Support Was Removed1998-02-0606 February 1998
- on 980113,damage Was Found on Stanchion & Restraining Steel of Unit 1 LPSI Sys Pipe Support Location on Common Discharge Line.Caused by LPSI Pump Discharge Check Valve Slam(S).Pipe Support Was Removed
05000317/LER-1998-001, :on 980104,Unit 1 Entered Condition Outside of Tech Specs Due to Having Both Secondary Control Element Assembly Position Indications out-of-svc.Caused by Position Indication Being Inoperable.Procedure Revised1998-02-0303 February 1998
- on 980104,Unit 1 Entered Condition Outside of Tech Specs Due to Having Both Secondary Control Element Assembly Position Indications out-of-svc.Caused by Position Indication Being Inoperable.Procedure Revised
05000317/LER-1997-007, :on 971029,discovered That Three Surveillance Test Procedures Were Not Completed within Test Interval. Caused by Excessive Use of 25% Grace Period Allowed for Completion of Surveillance.Revised Procedures1997-12-0101 December 1997
- on 971029,discovered That Three Surveillance Test Procedures Were Not Completed within Test Interval. Caused by Excessive Use of 25% Grace Period Allowed for Completion of Surveillance.Revised Procedures
05000317/LER-1997-009, :on 971024,automatic Reactor Trip Occurred. Caused by Failure to Properly Terminate Electrical Lead on Condenser Vacuum Breaker Handswitch During Prior Handswitch Maintenance.Over 200 Similar Connection Insp1997-11-20020 November 1997
- on 971024,automatic Reactor Trip Occurred. Caused by Failure to Properly Terminate Electrical Lead on Condenser Vacuum Breaker Handswitch During Prior Handswitch Maintenance.Over 200 Similar Connection Insp
05000317/LER-1997-008, :on 971017,two Reactor Protective Sys Channels Were OOS During Test.Caused by Significant Variations in Power Supply Voltages.Requested Maint to Back Out of Calibr of Channel C & Return Channel to Svc1997-11-12012 November 1997
- on 971017,two Reactor Protective Sys Channels Were OOS During Test.Caused by Significant Variations in Power Supply Voltages.Requested Maint to Back Out of Calibr of Channel C & Return Channel to Svc
05000317/LER-1996-001, :on 960117,SRW Heat Exchanger Microfouling High than Assumed in Design Basis Occurred.Caused by Original Design Calculations for SRW Heat Exchangers Assumed Min SRW Flow.New Operability Limits Implemented1997-10-21021 October 1997
- on 960117,SRW Heat Exchanger Microfouling High than Assumed in Design Basis Occurred.Caused by Original Design Calculations for SRW Heat Exchangers Assumed Min SRW Flow.New Operability Limits Implemented
05000317/LER-1997-006, :on 970722,cable Spreading Room Halon Sys Was Inoperable.Caused by Personnel Error.Operations Personnel Reminded of Possibility of Inoperable Dampers Affecting Halon Sys Operability1997-08-21021 August 1997
- on 970722,cable Spreading Room Halon Sys Was Inoperable.Caused by Personnel Error.Operations Personnel Reminded of Possibility of Inoperable Dampers Affecting Halon Sys Operability
05000317/LER-1997-004, :on 970602,trip Bypasses Were Not Removed When Thermal Power Was Increased Above 15%.Caused by Failure to Recognize Difference Between Nuclear Instrument & Delta-T. Revised Plant Procedures1997-07-0202 July 1997
- on 970602,trip Bypasses Were Not Removed When Thermal Power Was Increased Above 15%.Caused by Failure to Recognize Difference Between Nuclear Instrument & Delta-T. Revised Plant Procedures
05000317/LER-1997-005, :on 970529,reactor Coolant Sys Leak Occurred. Caused by Failed Compression Fitting.Conducted Review of Compression Fitting Maint Performed on High Pressure Systems & Completed Insps of Compression Fittings1997-06-30030 June 1997
- on 970529,reactor Coolant Sys Leak Occurred. Caused by Failed Compression Fitting.Conducted Review of Compression Fitting Maint Performed on High Pressure Systems & Completed Insps of Compression Fittings
05000317/LER-1997-003-01, :on 970424,fuel Moved in Spent Fuel Pool Without Charcoal Absorber Banks Being in Svc.Caused by Personnel Error.Fuel Movement Suspended Until All Appropriate Personnel Could Be Trained1997-05-23023 May 1997
- on 970424,fuel Moved in Spent Fuel Pool Without Charcoal Absorber Banks Being in Svc.Caused by Personnel Error.Fuel Movement Suspended Until All Appropriate Personnel Could Be Trained
05000318/LER-1997-003, :on 970423,chemistry Sampling Was Not Performed as Required by TS 3.4.7 Due to Insufficient Consideration of Precise Wording of TS on Part of Chemistry Personnel.Ts Will Be Clarified When Improved TS Are Implemented1997-05-21021 May 1997
- on 970423,chemistry Sampling Was Not Performed as Required by TS 3.4.7 Due to Insufficient Consideration of Precise Wording of TS on Part of Chemistry Personnel.Ts Will Be Clarified When Improved TS Are Implemented
05000318/LER-1997-002-01, :on 970405,containment Purge Valve Isolation Sys TS Violation Occurred.Caused by Inaccurate Implementation of TS 3.9.9.Personnel Air Lock Interlocks Restored1997-05-0505 May 1997
- on 970405,containment Purge Valve Isolation Sys TS Violation Occurred.Caused by Inaccurate Implementation of TS 3.9.9.Personnel Air Lock Interlocks Restored
05000318/LER-1997-001-01, :on 970401,refueling Machine Overload Protective Circuitry Was Inoperable Due to Failure to Correctly Translate Refueling Machine Circuitry Design Into Ts.Mod to Overload Bypass Was Installed1997-04-30030 April 1997
- on 970401,refueling Machine Overload Protective Circuitry Was Inoperable Due to Failure to Correctly Translate Refueling Machine Circuitry Design Into Ts.Mod to Overload Bypass Was Installed
05000317/LER-1997-002, :on 970220,misread TS Requirements Resulted in Inadequate Test.Caused by Lack of Strict Adherence to Wording of Plants TS Requirements.Edgs 1B,2A & 2B Were Successfully Tested & Returned to Svc1997-03-24024 March 1997
- on 970220,misread TS Requirements Resulted in Inadequate Test.Caused by Lack of Strict Adherence to Wording of Plants TS Requirements.Edgs 1B,2A & 2B Were Successfully Tested & Returned to Svc
05000317/LER-1997-001, :on 970110,spent Fuel Moved W/Ventilation Sys Inoperable & Missed Surveillance Occurred.Cause Analysis Being Performed to Determined Casual Factors & Generic Implications for Event.Surveillance Performed1997-02-10010 February 1997
- on 970110,spent Fuel Moved W/Ventilation Sys Inoperable & Missed Surveillance Occurred.Cause Analysis Being Performed to Determined Casual Factors & Generic Implications for Event.Surveillance Performed
05000318/LER-1996-006, :on 961210,discovered EDG Had Been Inoperable for Six Days.Caused by Personnel Error.Checked Fuse Holder Covers,Conducted Tailgate Training & Revised Procedure Re Installation of Fuse Holder Covers1997-01-10010 January 1997
- on 961210,discovered EDG Had Been Inoperable for Six Days.Caused by Personnel Error.Checked Fuse Holder Covers,Conducted Tailgate Training & Revised Procedure Re Installation of Fuse Holder Covers
05000318/LER-1996-002, :on 960522,missed Fire Watch Occurred Due to Personnel Error.Root Cause Analysis Has Been Completed. Plant Mgt Reemphasized to Site Personnel Importance of & Requirements for Fire Watches1996-12-31031 December 1996
- on 960522,missed Fire Watch Occurred Due to Personnel Error.Root Cause Analysis Has Been Completed. Plant Mgt Reemphasized to Site Personnel Importance of & Requirements for Fire Watches
05000318/LER-1996-005, :on 961117,automatic Reactor Trip Occurred Due to Closure of Feedwater Regulating Valve.Magnetic Particle Examination Was Conducted on New,Replacement Spring Retainers.No Indications Were Found1996-12-17017 December 1996
- on 961117,automatic Reactor Trip Occurred Due to Closure of Feedwater Regulating Valve.Magnetic Particle Examination Was Conducted on New,Replacement Spring Retainers.No Indications Were Found
05000318/LER-1996-004-01, :on 960926,missed Surveillance Occurred Due to Less than Adequate Technical Review of Stp.Procedures Revised1996-10-28028 October 1996
- on 960926,missed Surveillance Occurred Due to Less than Adequate Technical Review of Stp.Procedures Revised
05000317/LER-1995-005, :on 951109,manual Reactor Trip Occurred.Caused by Failure of Digital Feedwater Control Module FIC-1111. Reviewed Design Engineering Standards & Existing FP 2000 Digital Controllers Are Being Replaced1996-10-10010 October 1996
- on 951109,manual Reactor Trip Occurred.Caused by Failure of Digital Feedwater Control Module FIC-1111. Reviewed Design Engineering Standards & Existing FP 2000 Digital Controllers Are Being Replaced
05000317/LER-1996-004, :on 960802,two Asi Channels OOS Due to Reversed Nuclear Instrumentation Leads.Leads Were Correctly Reconnected When Plant Was Brought Down on 9608021996-09-0303 September 1996
- on 960802,two Asi Channels OOS Due to Reversed Nuclear Instrumentation Leads.Leads Were Correctly Reconnected When Plant Was Brought Down on 960802
05000318/LER-1996-003-01, :on 960619,discovered Missed Fire Protection Compensatory Action.Caused by Personnel Error.Provided Awareness Training to Personnel Re Fire Protection Compensatory Actions Expectations1996-07-17017 July 1996
- on 960619,discovered Missed Fire Protection Compensatory Action.Caused by Personnel Error.Provided Awareness Training to Personnel Re Fire Protection Compensatory Actions Expectations
05000318/LER-1996-002-01, :on 960522,fire Watch Missed.Caused by Personnel Error.Counseled Personnel Re Event1996-06-21021 June 1996
- on 960522,fire Watch Missed.Caused by Personnel Error.Counseled Personnel Re Event
05000317/LER-1996-003, :on 960423,discovered Holes in Containment Sump Screen Larger than Described in Ufsar.Holes Most Likely Installed During Plant Const.Sump Screens Visually Inspected & Repaired1996-05-24024 May 1996
- on 960423,discovered Holes in Containment Sump Screen Larger than Described in Ufsar.Holes Most Likely Installed During Plant Const.Sump Screens Visually Inspected & Repaired
05000317/LER-1996-002, :on 960410,required Fire Watch Missed.Caused by Lack of Fire Watch Ownership.Circumstances of Event Will Be Reviewed W/Appropriate Groups1996-05-14014 May 1996
- on 960410,required Fire Watch Missed.Caused by Lack of Fire Watch Ownership.Circumstances of Event Will Be Reviewed W/Appropriate Groups
05000318/LER-1996-001-01, :on 960227,breakers 552-41,552-21 & 552-61 Tripped Open in Plant Switchyard.Caused by Failure of Auxiliary Relay Card in Breaker 552-41.Failed Relay Card Replaced1996-03-28028 March 1996
- on 960227,breakers 552-41,552-21 & 552-61 Tripped Open in Plant Switchyard.Caused by Failure of Auxiliary Relay Card in Breaker 552-41.Failed Relay Card Replaced
05000317/LER-1996-001, :on 960117,determined That SW HX Microfouling Higher than Assumed in Design Basis.Caused by Design Deficiency.Conservative Operability Limits Established & Bay Temp & SW HXs Being Monitored1996-02-16016 February 1996
- on 960117,determined That SW HX Microfouling Higher than Assumed in Design Basis.Caused by Design Deficiency.Conservative Operability Limits Established & Bay Temp & SW HXs Being Monitored
05000317/LER-1995-006, :on 951116,manual Reactor Trip Occurred Due to Loss of 12 SG Feed Pump.Caused Oil Losses Allowing Pressure to Drop Before Standby Pump Could Restore Pressure.Trip Mechanism & Thrust Cleaned & Adjusted1995-12-13013 December 1995
- on 951116,manual Reactor Trip Occurred Due to Loss of 12 SG Feed Pump.Caused Oil Losses Allowing Pressure to Drop Before Standby Pump Could Restore Pressure.Trip Mechanism & Thrust Cleaned & Adjusted
05000317/LER-1995-005-01, :on 951109,manual Reactor Trip Occurred Due to Increasing SG 11 Water Level.Caused by Failure of Digital Control Module FIC-1111.Controller Sent to Vendor for Troubleshooting & Root Cause Analysis1995-12-11011 December 1995
- on 951109,manual Reactor Trip Occurred Due to Increasing SG 11 Water Level.Caused by Failure of Digital Control Module FIC-1111.Controller Sent to Vendor for Troubleshooting & Root Cause Analysis
05000317/LER-1995-004-01, :on 950816,inoperable Fire Barrier Penetration Seal Was Discovered.Caused by Inadequate Engineering Oversight & Less than Adequate Surveillance Procedure.Sealed Penetration Seal1995-09-15015 September 1995
- on 950816,inoperable Fire Barrier Penetration Seal Was Discovered.Caused by Inadequate Engineering Oversight & Less than Adequate Surveillance Procedure.Sealed Penetration Seal
05000317/LER-1995-003-01, :on 950730 & 31,entered TS 3.0.3 Due to High Bay Water Temps.Administration Limit for Bay Water Temp Raised & Current Unit 1 & Unit 2 SW Tube Type HXs Will Be Replaced1995-08-28028 August 1995
- on 950730 & 31,entered TS 3.0.3 Due to High Bay Water Temps.Administration Limit for Bay Water Temp Raised & Current Unit 1 & Unit 2 SW Tube Type HXs Will Be Replaced
05000317/LER-1995-002-01, :on 950616,manual Trip Occurred Due to Loss of 12 SG Feed Pump.Repaired Overspeed Trip Mechanism & Restarted Unit 11995-07-14014 July 1995
- on 950616,manual Trip Occurred Due to Loss of 12 SG Feed Pump.Repaired Overspeed Trip Mechanism & Restarted Unit 1