03-21-2016 | On January 19, 2016, at approximately 1100 Central Standard Time ( CST), during troubleshooting of the Main Control Room ( MCR) green light indication on the 3A Residual Heat Removal ( RHR) Pump Motor Breaker Transfer Switch (MBTS), it was discovered that the 3A RHR Pump MBTS had malfunctioned, potentially preventing the pump from starting from the MCR. The 3A RHR Pump was declared inoperable.
On January 20, 2016, at approximately 0030 CST, the 3A RHR Pump was declared operable following replacement of the 3A RHR Pump MBTS.
A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from January 9 to January 20, 2016, exceeding the Technical Specification allowed outage time. During this time, the 3B and 3D RHR Pumps were also inoperable on January 14, 2016, from 0127 to 0215 CST, resulting in a Safety System Function Failure. A Probabilistic Risk Assessment determined there was a negligible increase in risk.
The cause of this event was failure of the transfer switch to fully latch due to binding resulting from the MBTS being installed greater than its twenty-one year service life with no Preventative Maintenance ( PM) performed. Corrective actions include verifying similar transfer switches are latched in the NORMAL positon on BFN, Units 1, 2, and 3, and creating a PM activity with a replacement schedule for these switches. |
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Category:Letter
MONTHYEARML24032A4762024-02-0101 February 2024 Final Report of a Part 21 Evaluation Associated with Starter Contactors for the BFN Unit 1 High Pressure Coolant Injection Suppression Pool Inboard Suction Valve ML24023A2802024-01-23023 January 2024 Final Report of a Deviation or Failure to Comply Associated with a Relay in the Reactor Core Isolation Cooling Condensate Pump CNL-24-017, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions2024-01-17017 January 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions ML24016A3042024-01-16016 January 2024 Final Report of a Part 21 Evaluation Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump CNL-23-071, Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-472024-01-11011 January 2024 Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-47 ML24022A1732024-01-0303 January 2024 Receipt and Availability of the Subsequent License Renewal Application ML23319A1992024-01-0303 January 2024 Issuance of Amendment Nos. 333, 356, and 316 Regarding the Technical Specification Surveillance Requirements 3.4.3.2 and 3.5.1.11 Regarding Safety Relief Valves ML23355A2062023-12-21021 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23348A3942023-12-14014 December 2023 Interim Part 21 Report of a Potential Deviation or Failure to Comply Associated with Starter Contactors for the High Pressure Coolant Injection Suppression Pool Inboard Suction Valve IR 05000259/20230102023-12-11011 December 2023 Commercial Grade Dedication Inspection Report 05000259/2023010 and 05000260/2023010 and 05000296/2023010 ML23335A0722023-12-0101 December 2023 Interim Report of a Deviation or Failure to Comply Associated with a Relay in the Unit 2 Reactor Core Isolation Cooling Condensate Pump ML23334A2492023-11-30030 November 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-070, Submittal of Fifth 10-Year Interval Inservice Testing Program Plan2023-11-29029 November 2023 Submittal of Fifth 10-Year Interval Inservice Testing Program Plan ML23331A2532023-11-27027 November 2023 Summary Report for 10 CFR 50.9 Evaluations, Technical Specifications Bases Changes, Technical Requirement Manual Changes, and NRC Commitment Revisions CNL-23-067, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-11-27027 November 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML23325A1102023-11-21021 November 2023 Anchor Darling Double Disc Gate Valve Commitment Revision ML23320A2542023-11-16016 November 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump IR 05000259/20230032023-11-13013 November 2023 Integrated Inspection Report 05000259/2023003, 05000260/2023003 and 05000296/2023003 IR 05000259/20230402023-11-0202 November 2023 Supplemental Inspection Supplemental Report 05000259 2023040 and Follow-Up Assessment Letter ML23292A2532023-10-18018 October 2023 BFN 2024-301, Corporate Notification Letter (210-day Ltr) ML23282A0022023-10-0606 October 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump ML23278A0122023-10-0505 October 2023 Updated Final Safety Analysis Report, Amendment 30 ML23271A1702023-09-28028 September 2023 Site Emergency Plan Implementing Procedure Revision ML23270A0702023-09-26026 September 2023 SLRA Pre-Application Meeting Summary 09-13-2023 ML23257A1232023-09-22022 September 2023 Administrative Changes to Technical Specification Pages Issued for License Amendment Nos. 332, 355, and 315 CNL-23-061, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision2023-09-20020 September 2023 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML23263B1042023-09-20020 September 2023 Special Report 260/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation ML23205A2132023-09-0808 September 2023 Issuance of Amendment Nos. 332, 355, and 315 Regarding the Revision of Technical Specifications to Adopt TSTF-566-A and TSTF-580-A, Rev. 1 CNL-23-057, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 642023-09-0505 September 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 64 IR 05000259/20230052023-08-29029 August 2023 Updated Inspection Plan for Browns Ferry Nuclear Plant, Units 1, 2 and 3 - Report 05000259/2023005, 05000260/2023005 and 05000296/2023005 ML23233A0432023-08-18018 August 2023 Enforcement Action EA-22-122 Inspection Readiness Notification ML23219A1542023-08-17017 August 2023 Request to Use Later Edition of ASME Code for Operation and Maintenance and Alternative Requests BFN-IST-01 Through 05 for the Fifth 10-Year Interval Inservice Testing Program ML23228A1642023-08-16016 August 2023 Site Emergency Plan Implementing Procedure Revision ML23228A0202023-08-15015 August 2023 (BFN) Unit 1 - Special Report 259/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation IR 05000259/20230022023-08-10010 August 2023 Integrated Inspection Report 05000259/2023002, 05000260/2023002, 05000296/2023002 and 07200052/2023001 ML23192A4472023-07-31031 July 2023 Staff Assessment of Updated Seismic Hazards at TVA Sites Following the NRC Process for the Ongoing Assessment of Natural Hazards Information CNL-23-055, Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills2023-07-25025 July 2023 Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills ML23171A8862023-07-24024 July 2023 Issuance of Amend. Nos. 331, 354, and 314; 365 and 359 Regarding Adoption of TSTF-541-A, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated Position ML23201A2182023-07-20020 July 2023 Registration of Use of Cask to Store Spent Fuel (MPC-298 and -299) ML23159A2552023-07-20020 July 2023 Proposed Alternative to the Requirements of the ASME Code Regarding Volumetric Inspection of Standby Liquid Control Nozzles ML23199A3072023-07-18018 July 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-053, Tennessee Valley Authority - Radiological Emergency Plan Revisions2023-07-18018 July 2023 Tennessee Valley Authority - Radiological Emergency Plan Revisions IR 05000259/20233012023-07-18018 July 2023 NRC Operator License Examination Report Nos. 05000259/2023301, 05000260/2023301, and 05000296/2023301 2024-02-01
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML20160A0232020-06-0404 June 2020 SR 2020-001-00 for Browns Ferry Nuclear Plant (Bfn),Inoperable Oscillating Power Range Monitor (OPRM) Instrumentation 05000296/LER-2017-0022017-12-29029 December 2017 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses, LER 17-002-00 for Browns Ferry Nuclear Plant, Unit 3 Regarding 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses 05000296/LER-2017-0012017-10-31031 October 2017 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications, LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications 05000260/LER-2017-0042017-07-0707 July 2017 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 17-004-00 for Browns Ferry, Unit 2, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000260/LER-2017-0032017-05-30030 May 2017 Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting, LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting 05000259/LER-2017-0022017-04-27027 April 2017 Unauthorized Firearm Introduced into the Protected Area, LER 17-002-00 for Browns Ferry, Unit 1, Regarding Unauthorized Firearm Introduced into the Protected Area 05000260/LER-2017-0022017-04-24024 April 2017 Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications, LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications 05000260/LER-2017-0012017-04-14014 April 2017 High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse, LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse 05000259/LER-2016-0022016-09-19019 September 2016 High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve, LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve 05000260/LER-2016-0022016-09-13013 September 2016 High Pressure Coolant Injection System Failure Due To Stuck Contactor, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor 05000260/LER-2016-0012016-08-16016 August 2016 High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay, LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay 05000296/LER-2016-0062016-08-0505 August 2016 1 OF 8, LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing 05000259/LER-2016-0012016-06-21021 June 2016 Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves, LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves 05000296/LER-2016-0052016-06-17017 June 2016 Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits, LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits 05000296/LER-2016-0042016-06-0606 June 2016 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2016-0032016-04-25025 April 2016 Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements, LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements 05000296/LER-2016-0022016-04-22022 April 2016 Improperly Installed Switch Results in Condition Prohibited by Technical Specifications, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications 05000296/LER-2016-0012016-03-21021 March 2016 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure, LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure 05000260/LER-2015-0022016-03-17017 March 2016 High Pressure Coolant Injection System Inoperable due to Manual Isolation of Steam Leak I, LER 15-002-01 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection System Inoperable Due to Manual Isolation of Steam Leak ML1108400352011-03-22022 March 2011 Letter Re Licensee Event Report Which Occurred on December 22, 2010, Concerning Low Pressure Coolant Injection Operability, TVA Expects to Submit a Revised LER by April 15, 2011 ML1015505752010-04-0707 April 2010 Event Notification for Browns Ferry on Spill of Water Containing Tritium ML1015505632008-01-10010 January 2008 Event Notification for Browns Ferry on Offsite Notification - Spill of Water Containing Tritium ML18283B3261978-09-29029 September 1978 LER 1978-205-01 for Browns Ferry, Unit 3 Four Main Steam Isolation Valves Which Exceeded the Leakage Limits of Technical Specification 4.7.A.2.i While Performing Local Leak Rate Testing During Refueling ML18283B3391978-07-25025 July 1978 Licensee Event Report Concerning Excessive Drywell Floor Drain Leak Rate Observed During Normal Operation ML18283B3411978-07-18018 July 1978 Licensee Event Report Concerning an Abnormal Indication on a 4-kV Standby Power Circuit Breaker During Normal Operation ML18283B3401978-07-18018 July 1978 Licensee Event Report Concerning an Outboard Main Steam Isolation Valve, Which Closed Faster than Allowed by Technical Specifications ML18283B3421978-05-31031 May 1978 Licensee Event Report Concerning MSIV 1-38 Which Closed in 1 Second Exceeding Limiting Condition of Operation ML18283A9901978-05-30030 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve on Standby Liquid Control Pump B Opened at 900 Psig (Which Is Lower than Designed Setting of 1425 +/- 75 Psig as Designated by Tech Spec 4.4.A.2.A) During Surveillance Tes ML18283A9911978-05-0909 May 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Building Ventilation Radiation Monitoring Channel Failed During Refueling Outage ML18283A9941978-05-0505 May 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 2, Local Leak Rate Tests of All Containment Isolation Valves Where Leak Rate Exceeded Allowable Leak Rate of 60 Percent of La Per 24 Hours or 707.1 Scfh ML18283A9921978-05-0505 May 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 2, Check Valve 2-73-603 in High-Pressure Coolant Injection System Was Found in Open Position During Maintenance Inspection After Failing Local Leak Rate Test ML18283B4001978-05-0101 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 3, Both RBM Channels Which Became Continuously Bypassed During Power Ascension ML18283B4011978-04-28028 April 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 3, Smoke Alarm Which Would Not Clear & Was Received for Preaction Sprinkler Zone in Reactor Building During Normal Operation ML18283B4021978-04-28028 April 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 3, Relief Valve 3-1-31 Which Failed to Reseat Until Reactor Pressure Reached 280 Psig During Reactor Scram ML18283B4041978-04-24024 April 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42, Found to Be Erratic & Did Not Meet Requirements of Tech Spec 4.7.II During Normal Operation, Which Is Superseding Previous Letter of 2/8/1978 ML18283B4031978-04-24024 April 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 3, Electrical Connector Carrying Thermocouple Circuits Monitoring Primary Containment Atmospheric Temperature Not Included as Part of Modification Which Qualified Connector Assemblies for ML18283B4051978-04-0404 April 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 3, Six CRD Accumulator Level Switches Which Would Not Alarm with Level Increases During Plant Operation While Performing Electrical Maintenance Instruction 50 ML18283B4061978-03-30030 March 1978 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Which Were Experienced with Six Charcoal Adsorber Beds in Offgas System During Normal Operation, Which Is Supplementing Previous Letter of 7/29/1977 ML18283A9951978-03-29029 March 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 2, Unidentified Coolant Leakage in Drywall Was Found to Be 9.5 Gpm & Exceeded 5 Gpm Limit of Technical Specification 3.6.C.1. During Normal Operation ML18283B4091978-03-28028 March 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 3, Three of Five Test Specimens Failed During Simulated LOCA Conditions & During Qualification Testing of Bendix Electrical Connectors Identical to Those Used in Primary Containment ML18283B4101978-03-22022 March 1978 LER 1977-005-00 for Browns Ferry Nuclear Plant, Unit 3, RPS MG Set a Which Continued Running & MG Set B Output Breaker Which Did Not Trip During Startup Test STI-31, Which Is Supplementing Previous Letter of 3/24/1977 ML18283B4111978-03-10010 March 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 3, Valve FCV 3-74-52 Was Found Inoperable During Performance of Surveillance Instruction 4.5.B.1.C ML18283A9961978-02-28028 February 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-5 Opened and Failed to Reseat During Steady State Operation ML18283B4141978-02-28028 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 3, Bendix Connectors of Type Used Inside Primary Containment Have Failed a Post-Aging Environmental Test at Wyle Laboratory Testing Facility ML18283A9971978-02-15015 February 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-41 Opened and Failed to Reseat During Steady State Operation ML18283B0001978-02-13013 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Pressure Switch PS-68-95 Not Functioning as Required by Tech Spec Table 4.2.B During Normal Operation While Performing Surveillance Instruction ST 4.2.B-7 ML18283A9991978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 2, Surveillance Samples Were Taken from Charcoal in Unit 2 Primary Containment Purge System Following Maintenance Outage ML18283B4161978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42 Found to Be Erratic & Did Not Meet Requirements of Technical Specification 4.7.H During Normal Operation ML18283B4071977-10-0505 October 1977 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Were Experienced with Six Charcoal Adsorber Beds in Offgas System ML18283B4171977-09-26026 September 1977 LER 1977-017-00 for Browns Ferry Nuclear Plant, Unit 3, Primary Containment Isolation Valve 3-FCV-77-2A on Drywell Floor Drain Sump Pump Discharge Line Would Not Operate as Required by Tech Spec 3.7.D.L During Routine Operability Checks 2020-06-04
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00
I. Plant Operating Conditions Before the Event
At the time of discovery, Browns Ferry Nuclear Plant (BFN), Unit 3, was operating in Mode 1 at approximately 79 percent rated thermal power. BFN, Units 1 and 2, were unaffected by this event.
II. Description of Events
A. Event:
On January 13, 2016, Operations personnel identified the MCR green light indication located above the 3A Residual Heat Removal (RHR)[BO] Pump handswitch was not illuminated. The light bulb was replaced but the light remained extinguished. A work order was initiated.
Operations verified correct light indications locally at the breaker.
On January 19, 2016, at approximately 1100 Central Standard Time (CST), during troubleshooting of the Main Control Room (MCR) green light indication on the 3A RHR Pump Motor Breaker [BKR] Transfer Switch (MBTS)[43], it was discovered that the 3A RHR Pump MBTS, 3-43-074-0005, had malfunctioned potentially preventing the pump from starting from the MCR. Contacts [CNTR] 4-4C in the MBTS were found to be open, creating an open circuit.
Operations personnel declared 3A RHR Pump inoperable.
On January 20, 2016, at approximately 0030 CST, Operations personnel declared 3A RHR Pump operable following replacement of 3A RHR Pump MBTS.
A Past Operability Evaluation (POE) was performed for the 3A RHR Pump. The POE concluded that the 3A RHR Pump was inoperable from January 9, 2016, to January 20, 2016, exceeding the Technical Specification allowed outage time. During this time, 3B and 3D RHR Pumps were inoperable on January 14, 2016, from 0127 to 0215 CST, resulting in a Safety System Functional Failure.
B. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event:
No inoperable systems, structures, or components contributed to this event.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 001 - 00
C. Dates and approximate times of occurrences:
January 9, 2016, at 1500 CST Operations personnel completed RHR System piping flushes. This was the last time the 3A RHR Pump MBTS was known to have been in the correct position.
January 14, 2016, at 0127 CST Operations personnel declared 3B and 3D RHR Pumps inoperable for planned system flush.
January 14, 2016, at 0215 CST Operations personnel declared 3B and 3D RHR Pumps operable.
January 19, 2016, at 1100 CST During troubleshooting of MCR green light indication, the 3EA 4kV Shutdown Board was inspected. It was identified that contacts 4-4C were not making good contact, creating an open circuit.
Operations personnel declared 3A RHR Pump inoperable.
January 20, 2016, at 0030 CST Operations personnel declared 3A RHR Pump operable following replacement of 3A RHR Pump MBTS.
D. Manufacturer and model number (or other identification) of each component that failed during the event:
The failed component during this event was a General Electric (GE) SB-1 switch. The part number is 16SB1RB2A11LSM2V.
E. Other systems or secondary functions affected:
There were no other systems or secondary systems affected.
F. Method of discovery of each component or system failure or procedural error:
On January 13, 2016, Operations personnel identified the MCR green light indication located above the 3A RHR pump handswitch was not illuminated. The light bulb was replaced but the light remained extinguished. A work order was initiated. Operations verified correct light indications locally at the breaker.
On January 19, 2016, Maintenance personnel discovered that Contacts 4-4C were open while troubleshooting MCR green light indication on the 3A RHR Pump MBTS.
G. The failure mode, mechanism, and effect of each failed component, if known:
This event was the result of age-related degradation of the MBTS, which rendered the switch unable to fully latch in the correct position.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00
H. Operator actions:
In response to indication that the 3A RHR Pump was not functional, Operations personnel took the following actions:
- Declared 3A RHR Pump operable following troubleshooting and replacement of switch by Electrical Maintenance Personnel, and exited TS LCOs
I. Automatically and manually initiated safety system responses:
No safety system responses resulted from this event.
Ill. Cause of the event A. The cause of each component or system failure or personnel error, if known:
The direct cause of this event was the opening of Contacts 4-4C in the 3A RHR Pump Motor Breaker MBTS. With the MBTS in the NORMAL position, Contacts 4-4C should be closed. Contacts 4-4C opened unexpectedly due to the MBTS not being placed in the fully latched condition when in the NORMAL position.
The apparent cause of this event was binding resulting from the MBTS being installed greater than its twenty-one year service life with no Preventative Maintenance (PM) performed.
B. The cause(s) and circumstances for each human performance related root cause:
At the time of the event, no PM tasks existed to periodically replace GE SB-1 switches that are classified as Critical/Non-Critical Components and are "maintained" type switches (i.e., not spring return type switches). Additionally, no PM was performed on the MBTS because vendor manual guidance cautions against the use of any lubricants and/or cleaning agents in any form (including aerosol sprays commonly available) for GE transfer switches.
IV. Analysis of the event:
The Tennessee Valley Authority (WA) is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(i)(B), as any event or condition which was prohibited by the plant's TS, and 10 CFR 50.73(a)(2)(v)(B) and (D), as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat and mitigate the consequences of an accident.
This event was the result of 3A RHR Pump Motor Breaker MBTS failing to latch in the NORMAL position due to binding in the ball detent and position sprocket mechanism. This binding resulted from the MBTS being installed greater than its twenty-one year service life with no preventive maintenance performed on the switch. This led to a situation where 3A RHR Pump was potentially comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 unable to automatically start, or manually start from the Control Room.
A POE determined that 3A RHR Pump was inoperable from January 9, 2016 at 1335 CST until January 20, 2016 at 0030 CST. TS LCO 3.5.1 requires that, in Modes 1, 2, and 3, each Emergency Core Cooling System (ECCS) injection/spray subsystem and the Automatic Depressurization System (ADS) function of six safety/relief valves shall be operable. High Pressure Coolant Injection (HPCI)[BJ] and ADS valves are not required to be operable with reactor steam dome pressure less than or equal to 150 pounds per square inch gauge (psig). Required Action A.1 requires, with one required ECCS injection/spray subsystem inoperable, that the required ECCS injection/spray subsystem be restored to operable status within seven days. Required Action B requires Unit 3 to be in Mode 3 within twelve hours and Mode 4 within thirty-six hours if the Required Actions and associated Completion Times of Condition A are not met. 3A RHR Pump, credited as a required low pressure ECCS injection/spray subsystem, was inoperable for approximately eleven days.
Therefore, BFN, Unit 3, was in violation of Required Actions A.1 and B.
The Low Pressure Coolant Injection (LPCI) function of RHR requires two operable pumps in order to fill the Reactor Vessel to at least two-thirds of its height during an accident. 3B and 3D RHR Pumps were inoperable on January 14, 2016, from 0127 to 0215 CST. During the time when 3B and 3D RHR pumps were inoperable concurrently with 3A, the BFN, Unit 3, Residual Heat Removal System (RHRS) would have been incapable of performing this safety function.
V. Assessment of Safety Consequences
This event resulted in BFN, Unit 3, 3A RHR Pump being inoperable for longer than allowed by the TS. The ability of the system to automatically start or manually start from the MCR was affected. At no time was the system known to have lost the capability to respond to a local manual start signal.
The safety objectives of the RHRS are as follows:
a. To restore and maintain the coolant inventory in the reactor vessel so that the core is adequately cooled after a loss-of-coolant accident. The RHRS also ensures cooling for the pressure suppression pool for condensation of steam resulting from the blowdown due to a design basis loss-of-coolant accident.
b. To further extend the redundancy of the Core Standby Cooling Systems by providing for containment cooling.
The Low Pressure Coolant Injection function of the RHRS is designed to reflood the reactor vessel to at least two-thirds core height and to maintain this level. During the period where 3A, 3B, and 3D RHR Pumps were inoperable, this function was not available.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 A Probabilistic Risk Assessment was performed during the period of 3A RHR inoperability, and found that the change in Incremental Core Damage Probability and the change in Incremental Large Early Release Probability for the time period that the system was inoperable correspond to a negligible increase in risk (2.69E-08 and 2.45E-09, respectively). Based on the above, WA has concluded that, during the time period that 3A RHR Pump was inoperable, there was no significant risk to the health and safety of the public or plant personnel for this event.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
During this event, 3A RHR Pump retained the ability to manually start from pump motor breaker 3-BKR-74-5, on 3EA 4KV Shutdown Board. Additionally, all required ADS valves and at least one Core Spray (CS)[BG] Loop remained operable at all times.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shut down the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident:
This event did not occur when the reactor was shut down.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
This event resulted in inoperability of the RHR Pump for approximately eleven days, from the last time the MBTS was known to have been in the correct position on January 9, 2016, until the time the pump was returned to service on January 20, 2016.
VI. Corrective Actions:
Corrective Actions (CA) are being managed by WA's Corrective Action Program (CAP) under Condition Report (CR) 1126697. The CAs addressing this condition are described below:
1. Verify similar SB-1 transfer switches are latched in the NORMAL positon on BFN, Units 1, 2, and 3.
2. Create a PM activity to periodically replace GE SB-1 transfer switches similar to the 3A RHR Pump MBTS on a 20 year frequency.
VII. Additional Information:
A. Previous Similar Events:
A review of the BFN CAP and Licensee Event Reports (LERs) for Units 1, 2, and 3 revealed two similar events over the last three years:
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 - 00 which was rendered inoperable for longer than allowed by TS due to improper landing of leads during PM. The event is similar because an improperly connected wire resulted in a long period of inoperability for a safety system. CAs were to develop and deliver a case study to the Maintenance, Modifications, and Operations departments based on the details of this event, and to inspect HFA relay terminations.
control room due to a loose terminal wire. The event is similar because an improperly latched hand switch resulted in a long period of inoperability for a safety system. Corrective Actions for this event were to discipline the individuals responsible, to tighten the loose fastener, and to revise maintenance instructions to reduce the probability of recurrence.
CAs from these LERs would not have prevented this event.
B. Additional Information:
There is no additional information.
C. Safety System Functional Failure Consideration:
The safety function of RHRS is to restore and maintain the coolant inventory in the reactor vessel so that the core is adequately cooled after a loss-of-coolant accident. During the concurrent inoperability of 3A, 3B, and 3D RHR Pumps, the BFN, Unit 3, RHRS was unable to perform its safety function to remove residual heat and mitigate the consequences of an accident. Therefore, in accordance with guidance in NUREG-1022, this event is considered a safety system functional failure.
D. Scram with Complications Consideration:
This event did not result in a reactor scram.
VIII. COMMITMENTS
There are no new commitments.
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05000296/LER-2016-001 | Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000260/LER-2016-001 | High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay | | 05000259/LER-2016-001 | Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000296/LER-2016-002 | Improperly Installed Switch Results in Condition Prohibited by Technical Specifications LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications | | 05000260/LER-2016-002 | High Pressure Coolant Injection System Failure Due To Stuck Contactor LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor | | 05000259/LER-2016-002 | High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000296/LER-2016-003 | Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000296/LER-2016-004 | Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints | | 05000296/LER-2016-005 | Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits | | 05000296/LER-2016-006 | 1 OF 8 LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing | |
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