05000260/LER-2078-003, Relief Valve 2-1-41 Opened and Failed to Reseat During Steady State Operation
ML18283A997 | |
Person / Time | |
---|---|
Site: | Browns Ferry ![]() |
Issue date: | 02/15/1978 |
From: | Fox H Tennessee Valley Authority |
To: | O'Reilly J NRC/IE, NRC/RGN-II |
References | |
LER 1978-003-00 | |
Download: ML18283A997 (6) | |
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Declared Inoperable Due to Steam Supply Isolation 05000260/LER-2019-002, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2019-07-18018 July 2019 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 2025-01-10 |
Event date: | |
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Report date: | |
2602078003R00 - NRC Website | |
text
REGULATORY INFORMATION DISTRIBUTION SYSTEM (BIDS)
DISTRIBUTION FOR INCOMING MATERIAL 50-260 t
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OREXLI Y J F'RG:
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S DOCDATE: 02/i5/78 NRC TN VALLEY AUTH DATE RCVD: 02/22/78
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DOCTYPE:
LETTER NOTARIZED:
NO COPIES RECEIVED
SUBJECT:
LTR i ENCL LICENSEE EVENT REPT.
NO.- 50-260/783 CONCERNING RELIEF VALVE 2-1-41 OPENING 8( FAILING TO RESEAT DURING STEADY STATE OPERATION...
PLANT NAME:BROWNS FERRY UNIT 2
'EVIEWER INITIAL:
XRL DISTRIBUTOR INITIAL:
t DISTRIBUTION QF THIS MATERIAL IS AS FOLLOWS INCIDENT REPORTS (DISTRIBUTION CODE A002>
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FEB 1< ]9IB TENNESSEE VALLEY'AUTHORITY
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'Reilly, Director U.S. Nuclea Regulatory Commission Office of spection and Enforcement Region II 1217 Dear Mr. O'Reilly's ESSEE ALLEY AUTHORITY BROWNS PERRY NUCLEAR PLANT UNIT 2 Very truly yours, TENNESSEE VALLEY AUTHORITY TENN DOCKET NO. 50>>260 - PACILXTY OPERATING LICENSE DPR-52 REPORTABLE OCCURRENCE REPORT BFRO-50-260/783 The enclosed report provides details concerning relief valve 2-1-41 which opened and failed to reseat during steady state operation.
This report is submitted in accordance with Browne Perry unit 2 Technical Specifications, Sectiom 6.7.2.a.(2) and 6.7.2.a.(9).
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