On February 23, 2017, radiography results for the Browns Ferry Nuclear Plant ( BFN), Unit 2, Reactor Core Isolation Cooling ( RCIC) system stop check valve, 2-HCV-071-0014 (71-14 valve), showed the valve to be in the fully open position.
In this position, the valve was incapable of performing its design function as a Primary Containment Isolation Valve (PCIV).
In order to isolate the affected primary containment penetration flowpath, the RCIC Steam Line Outboard Isolation Valve was closed and deactivated to secure flow through the adjacent PCIV check valve in the exhaust line in accordance with plant Technical Specifications (TS) Limiting Conditions for Operation (LCO) for Primary Containment Isolation.
It is assumed in the Past Operability Evaluation (POE) that the 71-14 valve had been inoperable from April 2015 to February 2017, in violation of TS LCO 3.6.1.3. During this time period, another check valve (upstream of the 71-14 valve) remained capable of isolating the affected penetration. The 71-14 valve was repaired during the BFN, Unit 2, Cycle 19 Refueling Outage which began on February 25, 2017.
The cause of this condition was determined to be inadequate minimum allowable internal clearances for the 71-14 valve.
The 71-14 valve internals were machined to minimum allowable material as an interim action to mitigate risks. The corrective action to prevent recurrence is to replace the 71-14 valve with a new valve design that is not susceptible to the same internal binding potential. |
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Category:Letter
MONTHYEARIR 05000259/20240032024-11-0404 November 2024 Integrated Inspection Report 05000259/2024003 and 05000260/2024003 and 05000296/2024003 CNL-24-043, Application for Subsequent Renewed Operating Licenses, Second Safety Supplement2024-11-0101 November 2024 Application for Subsequent Renewed Operating Licenses, Second Safety Supplement ML24305A1692024-10-31031 October 2024 Site Emergency Plan Implementing Procedure Revision 05000259/LER-2024-003, Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators2024-10-29029 October 2024 Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators 05000259/LER-2024-001-02, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-10-28028 October 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure ML24299A2632024-10-25025 October 2024 Response to Apparent Violation in NRC Inspection Report 05000260/2024090, EA-24-075 ML24289A1232024-10-24024 October 2024 Letter to James Barstow Re Environmental Scoping Summary Report for Browns Ferry CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24308A0042024-10-16016 October 2024 Ahc 24-1578 Environmental Review of the Browns Ferry Nuclear Plant, Units 1, 2 and 3 Subsequent License Renewal Application Limestone County CNL-24-077, Application for Subsequent Renewed Operating Licenses, Response to Request for Additional Information, Set 12024-10-0909 October 2024 Application for Subsequent Renewed Operating Licenses, Response to Request for Additional Information, Set 1 ML24270A2162024-09-27027 September 2024 Notice of Intentions Regarding Preliminary Finding from NRC Inspection Report 05000260/2024090, EA-24-075 CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A1502024-09-24024 September 2024 Requalification Program Inspection - Browns Ferry Nuclear Plant ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan ML24263A2952024-09-19019 September 2024 Site Emergency Plan Implementing Procedure Revision CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions IR 05000260/20240902024-09-17017 September 2024 NRC Inspection Report 05000260/2024090 and Preliminary White Finding and Apparent Violation - 1 CNL-24-062, Cycle 16 Reload Analysis Report2024-09-16016 September 2024 Cycle 16 Reload Analysis Report ML24255A8862024-09-10010 September 2024 Core Operating Limits Report for Cycle 16 Operation, Revision 0 IR 05000259/20244042024-09-0303 September 2024 Cyber Security Inspection Report 05000259/2024404 and 05000260-2024404 and 05000296/2024404-Cover Letter ML24239A3332024-09-0303 September 2024 Full Audit Plan IR 05000259/20240052024-08-26026 August 2024 Updated Inspection Plan for Browns Ferry Nuclear Plant, Units 1, 2 and 3 - Report 05000259/2024005, 05000260/2024005 and 05000296/2024005 ML24225A1682024-08-16016 August 2024 – Notification of Inspection and Request IR 05000259/20244022024-08-0606 August 2024 Security Baseline Inspection Report 05000259/2024402 and 05000260/2024402 and 05000296/2024402 ML24219A0272024-08-0606 August 2024 Response to NRC Regulatory Issue Summary 2024-01, Preparation and Scheduling of Operator Licensing Examinations IR 05000259/20240022024-08-0202 August 2024 Brown Ferry Nuclear Plant – Integrated Inspection Report05000259/2024002 and 05000260/2024002 and 05000296/2024002 ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter ML24183A4142024-07-10010 July 2024 – License Renewal Regulatory Limited Scope Audit Regarding the Environmental Review of the License Renewal Application (EPID Number: L-2024-SLE-0000) (Docket Numbers: 50-259, 50-260, and 50-296) 05000296/LER-2024-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2024-07-0808 July 2024 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2024-001-01, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-07-0303 July 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure ML24184A1142024-07-0202 July 2024 Site Emergency Plan Implementing Procedure Revision ML24183A3842024-07-0101 July 2024 Registration of Use of Cask to Store Spent Fuel (MPC-364, -365) ML24179A0282024-06-26026 June 2024 Evaluation of Effects of Out-of-Limits Condition as Described in IWB-3720(a) 05000259/LER-2024-002, Reactor Scram Due to Generator Step-Up Transformer Failure2024-06-24024 June 2024 Reactor Scram Due to Generator Step-Up Transformer Failure ML24176A1132024-06-23023 June 2024 American Society of Mechanical Engineers, Section XI, Fourth 10 Year Inspection Interval, Inservice Inspection, System Pressure Test, Containment Inspection, and Repair and Replacement Programs, Owner’S Activity Report Cycle 21 Oper ML24175A0042024-06-23023 June 2024 Interim Report of a Deviation or Failure to Comply Associated with a Valve in the Unit 3 High Pressure Coolant Injection System ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24155A0042024-06-18018 June 2024 Proposed Alternative to the Requirements of the ASME Code (Revised Alternative Request 0-ISI-47) ML24158A5312024-06-0606 June 2024 Registration of Use of Cask to Store Spent Fuel (MPC-361, -362, -363) ML24071A0292024-06-0505 June 2024 Subsequent License Renewal Application Enclosure 3 - Proprietary Determination Letter ML24068A2612024-06-0505 June 2024 SLRA Fluence Methodology Report - Proprietary Determination Letter IR 05000259/20244032024-05-22022 May 2024 – Security Baseline Report 05000259/2024403 and 05000260/2024403 and 05000296/2024403 05000260/LER-2024-002, High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation2024-05-20020 May 2024 High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24136A0702024-05-15015 May 2024 2023 Annual Radiological Environmental Operating Report IR 05000259/20240012024-05-14014 May 2024 Integrated Inspection Report 05000259/2024001, 05000260/2024001, and 05000296/2024001 CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24123A2012024-05-0202 May 2024 NRC Cybersecurity Baseline Inspection (NRC Inspection Report 05000259/2024404, 05000260-2024404, 05000296/2024404) and Request for Information ML24122A6852024-05-0101 May 2024 2023 Annual Radioactive Effluent Release Report and Offsite Dose Calculation Manual 2024-09-03
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000259/LER-2024-003, Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators2024-10-29029 October 2024 Valid Specified System Actuation Caused the Automatic Start of Emergency Diesel Generators 05000259/LER-2024-001-02, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-10-28028 October 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000296/LER-2024-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2024-07-0808 July 2024 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2024-001-01, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-07-0303 July 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure 05000259/LER-2024-002, Reactor Scram Due to Generator Step-Up Transformer Failure2024-06-24024 June 2024 Reactor Scram Due to Generator Step-Up Transformer Failure 05000260/LER-2024-002, High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation2024-05-20020 May 2024 High Pressure Coolant Injection Inoperable Due to Rupture Disc Failure and Resulting System Isolation 05000296/LER-2024-002, Breaker Trip Automatically Started an Emergency Diesel Generator2024-04-24024 April 2024 Breaker Trip Automatically Started an Emergency Diesel Generator 05000296/LER-2024-001, Primary Containment Isolation Valve Inoperable Due to Incorrect Motor Operated Valve Setup2024-04-22022 April 2024 Primary Containment Isolation Valve Inoperable Due to Incorrect Motor Operated Valve Setup 05000260/LER-2024-001-01, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-04-17017 April 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000259/LER-2024-001, Inoperability of Unit 3 Diesel Generator Due to Relay Failure2024-04-11011 April 2024 Inoperability of Unit 3 Diesel Generator Due to Relay Failure 05000260/LER-2024-001, Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure2024-02-16016 February 2024 Secondary Containment Isolation Valve Inoperable Due to Mechanical Failure 05000259/LER-2023-003, Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage2024-01-29029 January 2024 Standby Liquid Control Inoperable Due to Demineralized Water In-Leakage 05000259/LER-2022-002-01, High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator2023-10-12012 October 2023 High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator 05000260/LER-2023-001-01, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure2023-09-18018 September 2023 Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line Due to Fatigue Failure 05000260/LER-2023-002, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2023-08-0404 August 2023 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2022-003-01, Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line Due to Fatigue Failure2023-07-31031 July 2023 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line Due to Fatigue Failure 05000259/LER-2023-002, Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip2023-07-17017 July 2023 Full Reactor Scram Due to an Oscillation Power Range Monitor (OPRM) Confirmation Density Algorithm (CDA) Trip 05000259/LER-2023-001-01, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm2023-06-13013 June 2023 High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm 05000260/LER-2023-001, Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line2023-04-19019 April 2023 Pressure Boundary Leak on Recirculation Pump Discharge Isolation Valve Drain Line 05000259/LER-2023-001, High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm2023-03-27027 March 2023 High Pressure Coolant Injection System Inoperable Due to a Torn Valve Diaphragm 05000259/LER-1922-003, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2023-02-0606 February 2023 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2022-003, Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line2023-01-31031 January 2023 Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line 05000296/LER-2022-002, Both Standby Liquid Control Subsystems Inoperable Due to an Insufficient Boron Injection Rate2022-12-19019 December 2022 Both Standby Liquid Control Subsystems Inoperable Due to an Insufficient Boron Injection Rate 05000259/LER-2022-002, High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator2022-09-12012 September 2022 High Pressure Coolant Injection System Declared Inoperable Due to a Corroded Actuator 05000296/LER-2022-001, Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints2022-07-11011 July 2022 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000259/LER-2021-001-01, Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay2022-07-0606 July 2022 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay 05000259/LER-2022-001, From Browns Ferry Nuclear Plant, Unit 1 Regarding Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line2022-03-16016 March 2022 From Browns Ferry Nuclear Plant, Unit 1 Regarding Pressure Boundary Leak on Residual Heat Removal System Low Pressure Coolant Injection Test Line 05000259/LER-2021-001, Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay2021-11-22022 November 2021 Volt Load Shed Logic Inoperable Longer than Allowed by Technical Specifications Due to Failed Relay 05000260/LER-2021-001-01, Inoperability of a TS-required Main Steam Isolation Valve2021-08-20020 August 2021 Inoperability of a TS-required Main Steam Isolation Valve ML20160A0232020-06-0404 June 2020 SR 2020-001-00 for Browns Ferry Nuclear Plant (Bfn),Inoperable Oscillating Power Range Monitor (OPRM) Instrumentation 05000296/LER-2017-0022017-12-29029 December 2017 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses, LER 17-002-00 for Browns Ferry Nuclear Plant, Unit 3 Regarding 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses 05000296/LER-2017-0012017-10-31031 October 2017 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications, LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications 05000260/LER-2017-0042017-07-0707 July 2017 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 17-004-00 for Browns Ferry, Unit 2, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000260/LER-2017-0032017-05-30030 May 2017 Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting, LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting 05000259/LER-2017-0022017-04-27027 April 2017 Unauthorized Firearm Introduced into the Protected Area, LER 17-002-00 for Browns Ferry, Unit 1, Regarding Unauthorized Firearm Introduced into the Protected Area 05000260/LER-2017-0022017-04-24024 April 2017 Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications, LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications 05000260/LER-2017-0012017-04-14014 April 2017 High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse, LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse 05000259/LER-2016-0022016-09-19019 September 2016 High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve, LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve 05000260/LER-2016-0022016-09-13013 September 2016 High Pressure Coolant Injection System Failure Due To Stuck Contactor, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor 05000260/LER-2016-0012016-08-16016 August 2016 High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay, LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay 05000296/LER-2016-0062016-08-0505 August 2016 1 OF 8, LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing 05000259/LER-2016-0012016-06-21021 June 2016 Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves, LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves 05000296/LER-2016-0052016-06-17017 June 2016 Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits, LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits 05000296/LER-2016-0042016-06-0606 June 2016 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2016-0032016-04-25025 April 2016 Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements, LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements 05000296/LER-2016-0022016-04-22022 April 2016 Improperly Installed Switch Results in Condition Prohibited by Technical Specifications, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications 05000296/LER-2016-0012016-03-21021 March 2016 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure, LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure 05000260/LER-2015-0022016-03-17017 March 2016 High Pressure Coolant Injection System Inoperable due to Manual Isolation of Steam Leak I, LER 15-002-01 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection System Inoperable Due to Manual Isolation of Steam Leak ML1108400352011-03-22022 March 2011 Letter Re Licensee Event Report Which Occurred on December 22, 2010, Concerning Low Pressure Coolant Injection Operability, TVA Expects to Submit a Revised LER by April 15, 2011 ML1015505752010-04-0707 April 2010 Event Notification for Browns Ferry on Spill of Water Containing Tritium 2024-07-08
[Table view] |
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
I. Plant Operating Conditions Before the Event
At the time of discovery, Browns Ferry Nuclear Plant (BFN), Unit 2, was in Mode 1 at approximately 74 percent rated thermal power.
II. Description of Event
A. Event Summary:
On February 23, 2017, at approximately 2239 Central Standard Time (CST), radiography results for BFN, Unit 2, Reactor Core Isolation Cooling (RCIC) [BN] system stop check valve [ISV], 2-HCV-071-0014 (71-14 valve), was discovered to be in the fully open position, thereby not meeting the acceptance criteria of Surveillance Instruction 2-Sl-3.2.3, Testing ASME OM Code and Augmented IST Check Valves (Internal Inspection). This valve is the RCIC turbine exhaust stop check valve and is one of two Primary Containment Isolation Valves (PCIVs) connecting the RCIC exhaust directly to primary containment. The acceptance criteria is for the valve to be fully closed to satisfy the containment isolation function. A Past Operability Evaluation (POE) determined that the 71-14 valve was inoperable from April 3, 2015, at 2356 Central Daylight Time (CDT), until Unit 2 was placed in Mode 4 on February 25, 2017, at 0506 CST.
BFN, Unit 2, Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.6.1.3 requires each PCIV, except reactor building-to-suppression chamber vacuum breakers, to be Operable in Modes 1, 2, and 3, and when associated instrumentation is required to be Operable per LCO 3.3.6.1, “Primary Containment Isolation Instrumentation”. In response to this event, on February 23, 2017, at 2250 CST, Operations personnel entered TS 3.6.1.3 Required Action A.1 which required the RCIC system to be isolated within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> to prevent flow through the RCIC Turbine Exhaust check valve, 2-CKV-071-0580 (71-580 valve). Based on the results from the POE, the 71-14 valve was inoperable longer than allowed by the TS. On February 24, 2017, at 0018 CST, Operations personnel isolated the RCIC system in accordance with plant TS by closing the RCIC Steam Line Outboard Isolation Valve 2-FCV-071-0003 (71-3 valve).
On February 25, 2017, the scheduled Unit 2 refueling outage commenced.
On March 24, 2017 at 1641 CDT, BFN completed repairs to the 71-14 valve and restored the RCIC penetration flowpath.
B. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event The 71-14 valve was unable to perform its function as a PCIV because it was stuck in the open position.
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
C. Dates and approximate times of occurrences
Dates & Approximate Times Occurrence April 3, 2015, at 2356 CDT It is assumed in the POE that the 71-14 valve bound open immediately after the start of the RCIC Turbine during performance of 2-SR-3.5.3.4, RCIC System Rated Flow at Low RPV Pressure.
February 23, 2017, at 2239 CST Radiography results for the 71-14 valve showed the valve to be in the fully open position.
February 23, 2017, at 2250 CST Operations declared 71-14 valve inoperable and entered TS Action 3.6.1.3.A to secure flow through check valve 71-580.
February 24, 2017, at 0018 CST Valve 71-3 was closed to secure flow through check valve 71-580 which also removed the RCIC system from service.
February 25, 2017, at 0001 CST Unit 2 inserted a manual reactor scram and entered Mode 3 for the previously scheduled Unit 2 refueling outage.
February 25, 2017, at 0506 CST Unit 2 entered Mode 4 where operability of the 71-14 valve was no longer required.
March 24, 2017, at 1641 CDT Operations personnel restored the RCIC penetration flowpath following completion of repairs to the 71-14 valve.
D. Manufacturer and model number of each component that failed during the event The failed component was the 71-14 valve. The component was model 5312WE, manufactured by the Walworth Company.
E. Other systems or secondary functions affected
The 71-14 valve is one of two PCIVs connecting the RCIC exhaust directly to primary containment.
Containment was isolated by closing the 71-580 valve resulting in the RCIC system being unable to perform its design function.
III. Cause of the event
A. Cause of each component or system failure or personnel error The root cause of this condition was inadequate minimum allowable clearances for the 71-14 valve.
There were two direct causes identified for the valve's failure:
F. Method of discovery of each component or system failure or procedural error On February 23, 2017, radiography results for the BFN, Unit 2, 71-14 valve showed the valve to be in the fully open position.
G. The failure mode, mechanism, and effect of each failed component The disc of the 71-14 valve was stuck in the fully open position due to internal binding. Three factors aligned to cause the internal binding of the valve: limited internal clearance for moving parts, corrosion debris from the RCIC piping was deposited into the valve, and the valve bonnet was not centered on the body. This configuration resulted in the 71-14 valve being unable to perform its safety function as a PCIV.
H. Operator actions
Operations personnel declared the 71-14 valve inoperable. The Primary Containment flowpath was isolated by securing the 71-580 valve. The 71-3 valve was closed, resulting in the RCIC system becoming inoperable.
I. Automatically and manually initiated safety system responses
2. The 71-14 valve was mechanically bound, preventing the valve disc from returning to the closed position.
B. Cause(s) and circumstances for each human performance related root cause There were no human performance root causes.
1. The Corrective Action to Prevent Recurrence developed for a similar 2013 valve failure, which was to submit a Preventive Maintenance Change Request to open, inspect, clean, and replace valve disc, dashpot and stem as necessary for Units 1, 2, and 3 71-14 valves, did not prevent recurrence of future similar events.
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3. LER NUMBER
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05000-260
IV. Analysis of the event
The Tennessee Valley Authority (TVA) is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the plant's TS.
The 71-14 valve is one of two PCIVs connecting the RCIC exhaust directly to primary containment through penetration X-212. This 71-14 valve has a safety-related function in the closed position and a quality-related, important to safety function, in the open position. According to TS Bases 3.6.1.3 for PCIVs, PCIVs form a part of the primary containment boundary. The PCIV safety function is related to minimizing the loss of reactor coolant inventory and establishing the primary containment boundary during a Design Basis Accident. PCIV operability supports leak tightness of primary containment.
The 71-14 valve is normally closed to provide its safety-related function as containment isolation. The valve opens from its normally closed position to allow a flow path from the RCIC Turbine Exhaust to the Pressure Suppression Chamber (PSC). The 71-14 valve closes when the RCIC system is shut down due to the weight of the valve disc. The exhaust header is designed to contain a check valve and a stop check valve to prevent backflow of Suppression Pool water into the RCIC exhaust line.
TS LCO 3.6.1.3 for PCIVs requires each PCIV, except reactor building-to-suppression chamber vacuum breakers, to be Operable in Modes 1, 2, and 3. However, on February 23, 2017, the 71-14 valve was found failed open during surveillance testing. At the time of discovery, Unit 2 was in Mode 1. As a result of the 71-14 valve being declared inoperable, Operations personnel entered TS 3.6.1.3 required actions to isolate the RCIC system preventing flow through the 71-580 valve which is the upstream RCIC turbine exhaust line PCIV. The 71-14 valve was determined to have been inoperable longer than allowed by TS resulting in a condition prohibited by the plant's TS.
V. Assessment of Safety Consequences
The ability of the Primary Containment penetration X-212 to perform its design function was not adversely affected by the 71-14 valve being bound in the open position due to the 71-580 valve remaining capable of isolating the penetration.
Additionally, the ability of the 71-14 valve to fulfill its function of providing a flow path for RCIC Turbine Exhaust Steam was not adversely affected by it being bound in the open position. Since the 71-14 valve must be in the open position to operate RCIC, the RCIC System injection function was not affected when this valve was bound open; therefore, the RCIC System was capable of injecting water into the reactor vessel and would have met its mission time.
Therefore, the RCIC system was still capable of performing its required safety functions to protect the comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
health and safety of the public.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event With the 71-14 valve being bound in the open position, this valve could not perform its design function as a PCIV. However, the 71-580 valve remained capable of isolating the penetration.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident This event did not occur when Unit 2 reactor was shutdown.
C. For failure that rendered a train of a safety system inoperable, estimate of the elapsed time from discovery of the failure until the train was returned to service It is assumed in the POE that the 71-14 valve was inoperable from April 3, 2015, at 2356 CDT, until Unit 2 was placed in Mode 4 on February 25, 2017, at 0506 CST.
VI. Corrective Actions
Corrective Actions are being managed by TVA's corrective action program under Condition Report (CR) 1265552.
A. Immediate Corrective Actions
The 71-14 valve was repaired.
B. Corrective Actions to Prevent Recurrence or to reduce the probability of similar events occurring in the future The root cause of this event will be addressed by replacing the Unit 2 71-14 valve with a new valve design that is not susceptible to the same internal binding potential as the existing valve.
VII. Previous Similar Events at the Same Site Previous similar events at BFN include failure of the Unit 2 71-14 valve. On March 2, 2013, radiography results for the Unit 2 71-14 valve displayed the valve bound in the fully open position. This event was reportable, and LER 50-260/2013-001-00, Inoperable Stop Check Valve Results in Condition Prohibited by Technical Specifications and Reactor Shutdown Required by Technical Specifications, was submitted to the Nuclear Regulatory Commission on May 1, 2013.
A search was performed of CRs relating to the 71-14 valve. CRs related to the condition reported in the
VIII. Additional Information
There is no additional information.
IX. Commitments There are no new commitments.
comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
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