05000296/LER-2005-001, Regarding Automatic Reactor Scram Due to False Main Transformer Differential Signal

From kanterella
(Redirected from 05000296/LER-2005-001)
Jump to navigation Jump to search
Regarding Automatic Reactor Scram Due to False Main Transformer Differential Signal
ML051030010
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 04/12/2005
From: Skaggs M
Tennessee Valley Authority
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 05-001-00
Download: ML051030010 (9)


LER-2005-001, Regarding Automatic Reactor Scram Due to False Main Transformer Differential Signal
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2962005001R00 - NRC Website

text

April 12, 2005 10 CFR 50.73 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop OWFN, P1-35 Washington, D.C. 20555-0001

Dear Sir:

TENNESSEE VALLEY AUTHORITY - BROWNS FERRY NUCLEAR PLANT (BFN) -

UNIT 3 - DOCKET 50-296 - FACILITY OPERATING LICENSE DPR LICENSEE EVENT REPORT (LER) 50-296/2005-001-00 The enclosed report provides details of an automatic reactor scram caused by a simultaneous false trip signal generated to the main generator circuit breaker, switchyard circuit breakers, and a main generator trip. This report is submitted in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in an automatic actuation of the systems listed in paragraph (a)(2)(iv)(B) (i.e., Reactor Protection System including: reactor scram or reactor trip, and general containment isolation signals affecting containment isolation valves in more than one system).

There are no commitments contained in this letter.

Sincerely, Original signed by:

M. D. Skaggs cc: See page 2

U.S. Nuclear Regulatory Commission Page 2 April 12, 2005 Enclosure cc (Enclosure):

(Via NRC Electronic Distribution)

Ms. Eva Brown, Project Manager U.S. Nuclear Regulatory Commission (MS 08G9)

One White Flint, North 11555 Rockville Pike Rockville, Maryland 20852-2739 Ms. Margaret Chernoff, Project Manager U.S. Nuclear Regulatory Commission One White Flint, North (MS 08G9) 11555 Rockville Pike Rockville, Maryland 20852-2739 Mr. Stephen J. Cahill, Branch Chief U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303-8931 NRC Resident Inspector Browns Ferry Nuclear Plant 10833 Shaw Road Athens, Alabama 35611-6970

U.S. Nuclear Regulatory Commission Page 3 April 12, 2005 TEA:DTL:JWD:BAB Enclosure cc (Enclosure):

A. S. Bhatnagar, LP 6A-C J. C. Fornicola, LP 6A-C R. G. Jones, NAB 1A-BFN K. L. Krueger, POB 2C-BFN R. F. Marks, PAB 1C-BFN F. C. Mashburn, BR 4X-C N. M. Moon, LP 6A-C J. R. Rupert, NAB 1A-BFN K. W. Singer, LP 6A-C M. D. Skaggs, PAB 1E-BFN E. J. Vigluicci, ET 11A-K NSRB Support, LP 5M-C EDMS WT CA - K LEREvents@inpo.org S:lic/submit/lers/U3 LER 2005-001.doc

NRC FORM 366 (7-2001)

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (6-2004)

LICENSEE EVENT REPORT (LER)

(See reverse for required number of digits/characters for each block)

APPROVED BY OMB NO. 3150-0104 EXPIRES 06/30/2007

, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

1. FACILITY NAME Browns Ferry Unit 3
2. DOCKET NUMBER 05000296
3. PAGE 1 OF 6
4. TITLE Automatic Reactor Scram Due to False Main Transformer Differential Signal
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL NUMBER REV NO.

MONTH DAY YEAR FACILITY NAME none DOCKET NUMBER N/A 02 11 2005 2005-001-00 04 12 2005 FACILITY NAME none DOCKET NUMBER N/A

11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §:(Check all that apply)
9. OPERATING MODE 1

20.2201(b) 20.2203(a)(3)(i) 50.73(a)(2)(i)(C) 50.73(a)(2)(vii) 20.2201(d) 20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A) 50.73(a)(2)(viii)(A) 20.2203(a)(1) 20.2203(a)(4) 50.73(a)(2)(ii)(B) 50.73(a)(2)(viii)(B) 20.2203(a)(2)(i) 50.36(c)(1)(i)(A) 50.73(a)(2)(iii) 50.73(a)(2)(ix)(A) 20.2203(a)(2)(ii) 50.36(c)(1)(ii)(A)

X 50.73(a)(2)(iv)(A) 50.73(a)(2)(x) 20.2203(a)(2)(iii) 50.36(c)(2) 50.73(a)(2)(v)(A) 73.71(a)(4) 20.2203(a)(2)(iv) 50.46(a)(3)(ii) 50.73(a)(2)(v)(B) 73.71(a)(5) 20.2203(a)(2)(v) 50.73(a)(2)(i)(A) 50.73(a)(2)(v)(C)

OTHER

10. POWER LEVEL 100 20.2203(a)(2)(vi) 50.73(a)(2)(i)(B) 50.73(a)(2)(v)(D) specify in Abstract below or in (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17) E.

Loss of Normal Heat Removal Consideration:

The condenser remained available, providing a normal heat removal path following the reactor scram. Accordingly, this event did not result in a Scram with a loss of Normal Heat Removal as defined in NEI 99-02.

VIII.COMMITMENTS None