09-19-2016 | On July 18, 2016, the Unit 1 High Pressure Coolant Injection ( HPCI) System was removed from service for a scheduled maintenance outage. In support of maintenance activities, the HPCI steam line inboard primary containment isolation valve ( PCIV) was placed in the closed position. Following the maintenance outage, warmup of the HPCI System commenced on July 20. During this evolution, unexpected system pressure conditions and responses were encountered that indicated the PCIV was not open. Failure to open the valve resulted in the inability to restore HPCI System operability and a reportable safety system functional failure. Because the valve is a PCIV located inside primary containment, the station planned and manually shutdown the reactor on July 26 for troubleshooting and corrective maintenance. A local leak rate test determined the PCIV function was ineffective, and disassembly of the valve found the valve stem severed. Following repair, the PCIV functions and HPCI System were declared operable on July 31 and August 1, respectively. Unit 1 was returned to full power on August 4.
The cause of this event was a tensile failure of the valve stem. The cause analysis concluded that the failure occurred on April 20, 2016, when the valve was stroked for in-service testing. Based on this the PCIV was inoperable longer than allowed by Technical Specifications. Corrective actions include valve repair, procedure revisions to provide additional margin to prevent back-seating, revision of guidance for high speed valve open limit switch settings, and evaluation of the extent of condition population. The safety significance of this event was determined to be low. |
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Category:Letter
MONTHYEARML24032A4762024-02-0101 February 2024 Final Report of a Part 21 Evaluation Associated with Starter Contactors for the BFN Unit 1 High Pressure Coolant Injection Suppression Pool Inboard Suction Valve ML24023A2802024-01-23023 January 2024 Final Report of a Deviation or Failure to Comply Associated with a Relay in the Reactor Core Isolation Cooling Condensate Pump CNL-24-017, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions2024-01-17017 January 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure and Emergency Preparedness Department Procedure Revisions ML24016A3042024-01-16016 January 2024 Final Report of a Part 21 Evaluation Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump CNL-23-071, Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-472024-01-11011 January 2024 Response to Request for Additional Information Regarding Browns Ferry Nuclear Plant, Units 1, 2, and 3, Inservice Inspection and Augmented Program Interval Revised Request for Alternative 0-ISI-47 ML24022A1732024-01-0303 January 2024 Receipt and Availability of the Subsequent License Renewal Application ML23319A1992024-01-0303 January 2024 Issuance of Amendment Nos. 333, 356, and 316 Regarding the Technical Specification Surveillance Requirements 3.4.3.2 and 3.5.1.11 Regarding Safety Relief Valves ML23355A2062023-12-21021 December 2023 Request for Exemption from Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Implementation ML23348A3942023-12-14014 December 2023 Interim Part 21 Report of a Potential Deviation or Failure to Comply Associated with Starter Contactors for the High Pressure Coolant Injection Suppression Pool Inboard Suction Valve IR 05000259/20230102023-12-11011 December 2023 Commercial Grade Dedication Inspection Report 05000259/2023010 and 05000260/2023010 and 05000296/2023010 ML23335A0722023-12-0101 December 2023 Interim Report of a Deviation or Failure to Comply Associated with a Relay in the Unit 2 Reactor Core Isolation Cooling Condensate Pump ML23334A2492023-11-30030 November 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-070, Submittal of Fifth 10-Year Interval Inservice Testing Program Plan2023-11-29029 November 2023 Submittal of Fifth 10-Year Interval Inservice Testing Program Plan ML23331A2532023-11-27027 November 2023 Summary Report for 10 CFR 50.9 Evaluations, Technical Specifications Bases Changes, Technical Requirement Manual Changes, and NRC Commitment Revisions CNL-23-067, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2023-11-27027 November 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML23325A1102023-11-21021 November 2023 Anchor Darling Double Disc Gate Valve Commitment Revision ML23320A2542023-11-16016 November 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump IR 05000259/20230032023-11-13013 November 2023 Integrated Inspection Report 05000259/2023003, 05000260/2023003 and 05000296/2023003 IR 05000259/20230402023-11-0202 November 2023 Supplemental Inspection Supplemental Report 05000259 2023040 and Follow-Up Assessment Letter ML23292A2532023-10-18018 October 2023 BFN 2024-301, Corporate Notification Letter (210-day Ltr) ML23282A0022023-10-0606 October 2023 Interim Part 21 Report of a Deviation or Failure to Comply Associated with Check Valve 0-CKV-023-0565 for D1 Residual Heat Removal Service Water Pump ML23278A0122023-10-0505 October 2023 Updated Final Safety Analysis Report, Amendment 30 ML23271A1702023-09-28028 September 2023 Site Emergency Plan Implementing Procedure Revision ML23270A0702023-09-26026 September 2023 SLRA Pre-Application Meeting Summary 09-13-2023 ML23257A1232023-09-22022 September 2023 Administrative Changes to Technical Specification Pages Issued for License Amendment Nos. 332, 355, and 315 CNL-23-061, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision2023-09-20020 September 2023 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML23263B1042023-09-20020 September 2023 Special Report 260/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation ML23205A2132023-09-0808 September 2023 Issuance of Amendment Nos. 332, 355, and 315 Regarding the Revision of Technical Specifications to Adopt TSTF-566-A and TSTF-580-A, Rev. 1 CNL-23-057, Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 642023-09-0505 September 2023 Central Emergency Control Center Emergency Plan Implementing Procedure Revisions. Includes CECC-EPIP-1, Revision 76 and CECC-EPIP-9, Revision 64 IR 05000259/20230052023-08-29029 August 2023 Updated Inspection Plan for Browns Ferry Nuclear Plant, Units 1, 2 and 3 - Report 05000259/2023005, 05000260/2023005 and 05000296/2023005 ML23233A0432023-08-18018 August 2023 Enforcement Action EA-22-122 Inspection Readiness Notification ML23219A1542023-08-17017 August 2023 Request to Use Later Edition of ASME Code for Operation and Maintenance and Alternative Requests BFN-IST-01 Through 05 for the Fifth 10-Year Interval Inservice Testing Program ML23228A1642023-08-16016 August 2023 Site Emergency Plan Implementing Procedure Revision ML23228A0202023-08-15015 August 2023 (BFN) Unit 1 - Special Report 259/2023-001 for Inoperable Post Accident Monitoring (PAM) Instrumentation IR 05000259/20230022023-08-10010 August 2023 Integrated Inspection Report 05000259/2023002, 05000260/2023002, 05000296/2023002 and 07200052/2023001 ML23192A4472023-07-31031 July 2023 Staff Assessment of Updated Seismic Hazards at TVA Sites Following the NRC Process for the Ongoing Assessment of Natural Hazards Information CNL-23-055, Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills2023-07-25025 July 2023 Tennessee Valley Authority - Emergency Preparedness Department Procedure Revision. Includes EPDP-3, Revision 3, Emergency Plan Exercises and Preparedness Drills ML23171A8862023-07-24024 July 2023 Issuance of Amend. Nos. 331, 354, and 314; 365 and 359 Regarding Adoption of TSTF-541-A, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated Position ML23201A2182023-07-20020 July 2023 Registration of Use of Cask to Store Spent Fuel (MPC-298 and -299) ML23159A2552023-07-20020 July 2023 Proposed Alternative to the Requirements of the ASME Code Regarding Volumetric Inspection of Standby Liquid Control Nozzles ML23199A3072023-07-18018 July 2023 Site Emergency Plan Implementing Procedure Revision CNL-23-053, Tennessee Valley Authority - Radiological Emergency Plan Revisions2023-07-18018 July 2023 Tennessee Valley Authority - Radiological Emergency Plan Revisions IR 05000259/20233012023-07-18018 July 2023 NRC Operator License Examination Report Nos. 05000259/2023301, 05000260/2023301, and 05000296/2023301 2024-02-01
[Table view] Category:Licensee Event Report (LER)
MONTHYEARML20160A0232020-06-0404 June 2020 SR 2020-001-00 for Browns Ferry Nuclear Plant (Bfn),Inoperable Oscillating Power Range Monitor (OPRM) Instrumentation 05000296/LER-2017-0022017-12-29029 December 2017 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses, LER 17-002-00 for Browns Ferry Nuclear Plant, Unit 3 Regarding 4kV Shutdown Board Potential Transformer Primary Fuses Do Not Coordinate with Secondary Fuses 05000296/LER-2017-0012017-10-31031 October 2017 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications, LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications 05000260/LER-2017-0042017-07-0707 July 2017 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 17-004-00 for Browns Ferry, Unit 2, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000260/LER-2017-0032017-05-30030 May 2017 Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting, LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting 05000259/LER-2017-0022017-04-27027 April 2017 Unauthorized Firearm Introduced into the Protected Area, LER 17-002-00 for Browns Ferry, Unit 1, Regarding Unauthorized Firearm Introduced into the Protected Area 05000260/LER-2017-0022017-04-24024 April 2017 Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications, LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications 05000260/LER-2017-0012017-04-14014 April 2017 High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse, LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse 05000259/LER-2016-0022016-09-19019 September 2016 High Pressure Coolant Injection Safety System Functional Failure due to Inoperability of Primary Containment Isolation Valve, LER 16-002-00 for Browns Ferry, Unit 1, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to Inoperability of Primary Containment Isolation Valve 05000260/LER-2016-0022016-09-13013 September 2016 High Pressure Coolant Injection System Failure Due To Stuck Contactor, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor 05000260/LER-2016-0012016-08-16016 August 2016 High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay, LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay 05000296/LER-2016-0062016-08-0505 August 2016 1 OF 8, LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing 05000259/LER-2016-0012016-06-21021 June 2016 Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves, LER 16-001-00 for Browns Ferry, Unit 1, Regarding Failure of 4kV Shutdown Board Normal Feeder Breaker Results in Actuations of Emergency Diesel Generators and Containment Isolation Valves 05000296/LER-2016-0052016-06-17017 June 2016 Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits, LER 16-005-00 for Browns Ferry, Unit 3, Regarding Automatic Depressurization System Valve Inoperability Exceeded Technical Specification Limits 05000296/LER-2016-0042016-06-0606 June 2016 Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints, LER 16-004-00 for Browns Ferry, Unit 3, Regarding Main Steam Relief Valves Lift Settings Outside of Technical Specifications Required Setpoints 05000296/LER-2016-0032016-04-25025 April 2016 Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements, LER 16-003-00 for Browns Ferry Nuclear Plant Unit 3 Regarding Main Steam Isolation Valve Leaking in Excess of Technical Specification Requirements 05000296/LER-2016-0022016-04-22022 April 2016 Improperly Installed Switch Results in Condition Prohibited by Technical Specifications, LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Improperly Installed Switch Results in Condition Prohibited by Technical Specifications 05000296/LER-2016-0012016-03-21021 March 2016 Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure, LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure 05000260/LER-2015-0022016-03-17017 March 2016 High Pressure Coolant Injection System Inoperable due to Manual Isolation of Steam Leak I, LER 15-002-01 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection System Inoperable Due to Manual Isolation of Steam Leak ML1108400352011-03-22022 March 2011 Letter Re Licensee Event Report Which Occurred on December 22, 2010, Concerning Low Pressure Coolant Injection Operability, TVA Expects to Submit a Revised LER by April 15, 2011 ML1015505752010-04-0707 April 2010 Event Notification for Browns Ferry on Spill of Water Containing Tritium ML1015505632008-01-10010 January 2008 Event Notification for Browns Ferry on Offsite Notification - Spill of Water Containing Tritium ML18283B3261978-09-29029 September 1978 LER 1978-205-01 for Browns Ferry, Unit 3 Four Main Steam Isolation Valves Which Exceeded the Leakage Limits of Technical Specification 4.7.A.2.i While Performing Local Leak Rate Testing During Refueling ML18283B3391978-07-25025 July 1978 Licensee Event Report Concerning Excessive Drywell Floor Drain Leak Rate Observed During Normal Operation ML18283B3411978-07-18018 July 1978 Licensee Event Report Concerning an Abnormal Indication on a 4-kV Standby Power Circuit Breaker During Normal Operation ML18283B3401978-07-18018 July 1978 Licensee Event Report Concerning an Outboard Main Steam Isolation Valve, Which Closed Faster than Allowed by Technical Specifications ML18283B3421978-05-31031 May 1978 Licensee Event Report Concerning MSIV 1-38 Which Closed in 1 Second Exceeding Limiting Condition of Operation ML18283A9901978-05-30030 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve on Standby Liquid Control Pump B Opened at 900 Psig (Which Is Lower than Designed Setting of 1425 +/- 75 Psig as Designated by Tech Spec 4.4.A.2.A) During Surveillance Tes ML18283A9911978-05-0909 May 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Building Ventilation Radiation Monitoring Channel Failed During Refueling Outage ML18283A9941978-05-0505 May 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 2, Local Leak Rate Tests of All Containment Isolation Valves Where Leak Rate Exceeded Allowable Leak Rate of 60 Percent of La Per 24 Hours or 707.1 Scfh ML18283A9921978-05-0505 May 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 2, Check Valve 2-73-603 in High-Pressure Coolant Injection System Was Found in Open Position During Maintenance Inspection After Failing Local Leak Rate Test ML18283B4001978-05-0101 May 1978 LER 1978-010-00 for Browns Ferry Nuclear Plant, Unit 3, Both RBM Channels Which Became Continuously Bypassed During Power Ascension ML18283B4011978-04-28028 April 1978 LER 1978-009-00 for Browns Ferry Nuclear Plant, Unit 3, Smoke Alarm Which Would Not Clear & Was Received for Preaction Sprinkler Zone in Reactor Building During Normal Operation ML18283B4021978-04-28028 April 1978 LER 1978-008-00 for Browns Ferry Nuclear Plant, Unit 3, Relief Valve 3-1-31 Which Failed to Reseat Until Reactor Pressure Reached 280 Psig During Reactor Scram ML18283B4041978-04-24024 April 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42, Found to Be Erratic & Did Not Meet Requirements of Tech Spec 4.7.II During Normal Operation, Which Is Superseding Previous Letter of 2/8/1978 ML18283B4031978-04-24024 April 1978 LER 1978-006-00 for Browns Ferry Nuclear Plant, Unit 3, Electrical Connector Carrying Thermocouple Circuits Monitoring Primary Containment Atmospheric Temperature Not Included as Part of Modification Which Qualified Connector Assemblies for ML18283B4051978-04-0404 April 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 3, Six CRD Accumulator Level Switches Which Would Not Alarm with Level Increases During Plant Operation While Performing Electrical Maintenance Instruction 50 ML18283B4061978-03-30030 March 1978 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Which Were Experienced with Six Charcoal Adsorber Beds in Offgas System During Normal Operation, Which Is Supplementing Previous Letter of 7/29/1977 ML18283A9951978-03-29029 March 1978 LER 1978-005-00 for Browns Ferry Nuclear Plant, Unit 2, Unidentified Coolant Leakage in Drywall Was Found to Be 9.5 Gpm & Exceeded 5 Gpm Limit of Technical Specification 3.6.C.1. During Normal Operation ML18283B4091978-03-28028 March 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 3, Three of Five Test Specimens Failed During Simulated LOCA Conditions & During Qualification Testing of Bendix Electrical Connectors Identical to Those Used in Primary Containment ML18283B4101978-03-22022 March 1978 LER 1977-005-00 for Browns Ferry Nuclear Plant, Unit 3, RPS MG Set a Which Continued Running & MG Set B Output Breaker Which Did Not Trip During Startup Test STI-31, Which Is Supplementing Previous Letter of 3/24/1977 ML18283B4111978-03-10010 March 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 3, Valve FCV 3-74-52 Was Found Inoperable During Performance of Surveillance Instruction 4.5.B.1.C ML18283A9961978-02-28028 February 1978 LER 1978-004-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-5 Opened and Failed to Reseat During Steady State Operation ML18283B4141978-02-28028 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 3, Bendix Connectors of Type Used Inside Primary Containment Have Failed a Post-Aging Environmental Test at Wyle Laboratory Testing Facility ML18283A9971978-02-15015 February 1978 LER 1978-003-00 for Browns Ferry Nuclear Plant, Unit 2, Relief Valve 2-1-41 Opened and Failed to Reseat During Steady State Operation ML18283B0001978-02-13013 February 1978 LER 1978-002-00 for Browns Ferry Nuclear Plant, Unit 2, Reactor Pressure Switch PS-68-95 Not Functioning as Required by Tech Spec Table 4.2.B During Normal Operation While Performing Surveillance Instruction ST 4.2.B-7 ML18283A9991978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 2, Surveillance Samples Were Taken from Charcoal in Unit 2 Primary Containment Purge System Following Maintenance Outage ML18283B4161978-02-0606 February 1978 LER 1978-001-00 for Browns Ferry Nuclear Plant, Unit 3, Torus Oxygen Sensor O2M-76-42 Found to Be Erratic & Did Not Meet Requirements of Technical Specification 4.7.H During Normal Operation ML18283B4071977-10-0505 October 1977 LER 1977-012-00 for Browns Ferry Nuclear Plant, Unit 3, Temperature Transients Were Experienced with Six Charcoal Adsorber Beds in Offgas System ML18283B4171977-09-26026 September 1977 LER 1977-017-00 for Browns Ferry Nuclear Plant, Unit 3, Primary Containment Isolation Valve 3-FCV-77-2A on Drywell Floor Drain Sump Pump Discharge Line Would Not Operate as Required by Tech Spec 3.7.D.L During Routine Operability Checks 2020-06-04
[Table view] |
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
I. Plant Operating Conditions Before the Event
At the time of discovery, Browns Ferry Nuclear Plant (BFN), Unit 1, was operating in Mode 1 at approximately 100 percent rated thermal power. BFN, Units 2 and 3, were unaffected by this event.
A. Event:
On July 18, 2016, the Unit 1 High Pressure Coolant Injection (HPCI)[BJ] system was removed from service for scheduled maintenance. Unit 1 HPCI Steam Line Inboard Isolation Valve 1-FCV-073-0002 [FCV] was cycled closed and tagged for isolation on the HPCI System, and Technical Specification (TS) Limiting Conditions for Operation (LCO) 3.5.1 Condition C, HPCI System Inoperable, Required Actions were entered.
Following the maintenance activity, Operations personnel commenced the warm-up of the HPCI System at 0250 Central Daylight Time (CDT) on July 20, 2016. The HPCI Steam Line Bypass Valve (1-FCV-073-81) was cycled; however, there was no change in indicated steam pressure. When 1-FCV-073-0003, HPCI Steam Line Outboard Isolation Valve, was approximately 30 percent open, only 65 pounds per square inch gauge (psig) of steam pressure was present in the steam line as indicated on pressure indicator 1-PI-73-4A [PI].
The Integrated Computer System (ICS)[JA] indicated 49 psig during the same time period.
The lack of response in steam pressure with 1-FCV-073-0003 partially open was an indication that 1-FCV-073-0002 was not open. Based on this, the discovery date is July 20, 2016. 1-FCV-073-0002 was declared inoperable for its primary containment isolation valve function, and TS 3.6.1.3 LCO Condition A, one primary containment isolation valve (PCIV) inoperable, Required Actions, were entered.
In response to the inability of the 1-FCV-073-0002 valve to open, Unit 1 was shutdown on July 26, 2016, for a Maintenance Outage. There were no TS LCO Condition Required Actions that required a reactor shutdown. Initial troubleshooting was conducted by attempting to operate the valve manually. During this troubleshooting effort, it was identified that the stem was rotating. Stem rotation is indicative of a valve internal failure.
Disassembly of the valve was performed, and it was determined that the stem was severed at a location just above the stem back-seat. The disc was located in the seat area and appeared to be fully seated. Although the disc was fully seated, the as-found local leak rate test (LLRT) determined valve leakage exceeded equipment capability prior to valve disassembly.
On July 31, 2016, at 1948, following verification that all maintenance activities were complete and all post maintenance tests were satisfied for 1-FCV-073-0002, Operations personnel declared the PCIV function for 1-FCV-73-0002 operable and exited TS LCO 3.6.1.3 Condition A.
On August 1, 2016, at 0010, following completion of warming the Unit 1 HPCI steam lines, verification of no leaks and all maintenance complete, and verification that Unit 1 HPCI surveillances were within periodicity, Operations personnel declared HPCI operable and exited TS LCO 3.5.1 Condition C.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 Rinegteurnlaettorye-mAilailirsto IFn5f0c3),011 cSt.s .NRuecsloeuarceIgnurclatgooryv , CaondmtmoisthseileWskasohffingronoffiDcCe 0f 20555-0001,Informato Information used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
...___ 2016 - 002 - 00 II.
On August 4, 2016, at 0418, BFN Unit 1 was returned to 100 percent power.
The event date was determined in the cause analysis, which concluded that the valve stem severed on April 20, 2016, when the valve was stroked for in-service test (IST) timing.
Description of Events
A. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event:
No inoperable systems, structures, or components contributed to this event.
B. Dates and approximate times of occurrences:
April 20, 2016 at 0104 CDT 1-FCV-073-0002 was cycled closed and opened per 1-SR-3.6.1.3.5(HPCI) for quarterly 1ST stroke time testing. Subsequent investigation determined failure of the PCIV occurred during this testing.
July 18, 2016, at 0300 CDT Unit 1 HPCI System 1-FCV-073-002 was cycled closed and tagged for scheduled maintenance on the HPCI System. Entered TS 3.5.1 LCO Condition C, HPCI System Inoperable, Required Actions.
July 20, 2016, at 1245 CDT During HPCI System restoration, steam line pressure could not be attained, and 1-FCV-073-0002 was declared inoperable for its primary containment isolation valve function. Entered TS 3.6.1.3 LCO Condition A, one PCIV inoperable, Required Actions.
July 20, 2016, at 1933 CDT Completed NRC 8-hr notification EN 52113 in accordance with 10 CFR 50.72(b)(3)(v)(D), Accident Mitigation.
July 26, 2016, at 0800 CDT Unit 1 Operations personnel inserted a Manual Reactor Scram due to planned maintenance outage. All systems responded as expected.
July 31, 2016, at 1948 CDT Verified all maintenance complete and PMTs satisfied for 1-FCV-073-0002.
Declared PCIV function for 1-FCV-73-0002 operable and exited TS LCO 3.6.1.3 Condition A.
August 1, 2016, 0010 CDT Completed warming U1 HPCI steam lines. Verified no leaks and verified all maintenance complete. Verified U1 HPCI surveillances are within periodicity. Declared HPCI operable and exited TS LCO 3.5.1 Condition C.
August 4, 2016, 0414 CDT Unit 1 returned to 100 percent power.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.Resource@nrc.goy, and to the Desk Officer, Office of Information and Regulatory Affairs, used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
2016 002 00 C. Manufacturer and model number (or other identification) of each component that failed during the event:
The 1-FCV-073-0002, HPCI steam line inboard isolation valve, is a 10 inch, Anchor/Darling (A/D), Class 900, pressure seal, double disc gate valve. The manufacturer part number is 900C WEOS. The vendor part number is FCV23-15.
D. Other systems or secondary functions affected:
There were no other systems or secondary systems affected.
E. Method of discovery of each component or system failure or procedural error:
On July, 20 2016, when 1-FCV-073-0003 was approximately 30 percent open, only 65 psig of steam pressure was present in the steam line as indicated on pressure indicator 1-PI-73-4A. ICS indicated 49 psig steam pressure during the same time period. The lack of response in steam pressure with 1-FCV-073-0003 partially open was an indication that 1-FCV-073-0002 had failed closed.
F. The failure mode, mechanism, and effect of each failed component, if known:
The failure mode identified for the 1-FCV-073-0002, HPCI Steam Line Inboard Isolation Valve, is a tensile failure of the valve stem during loading from the back-seat.
The cause analysis concluded that the valve stem severed on April 20, 2016, during opening of the valve. The location of the crack, the strong evidence of back-seating damage on the stem, and the apparent misalignment of the stem with the bonnet backseat indicate that the fracture was caused by a high peak tensile stress due to tension and bending when the stem was inadvertently back-seated.
G. Operator actions:
In response to the inability of Operations personnel to open and restore a steam flow path to HPCI following a maintenance outage on July 20, 2016, a troubleshooting/corrective maintenance outage was planned. Unit 1 Operations personnel inserted a manual reactor scram, and Unit 1 was shutdown on July 26, 2016, for this outage.
H. Automatically and manually initiated safety system responses:
There were no automatic safety system responses associated with this event. Because the HPCI System was inoperable at the time of discovery and primary containment isolation had been established, there were no manual safety system responses associated with this event.
III. Cause of the event
A. The cause of each component or system failure or personnel error, if known:
The direct cause of this event was a tensile failure of the HPCI Steam Line Inboard Isolation Valve stem.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
The root cause was determined to be associated with the design change process. The guidance in NPG-SPP-09.3.1, Guidelines for Preparation of Design Inputs and Change Impact Screen, was inadequate to ensure that the 1-FCV-073-0002 valve could be operated from the Main Control Room under all plant operating conditions without the valve stem interacting with the back-seat.
Three contributing causes were as follows:
1. Inadequate guidance was provided in General Specification G-50 for setting open limit switch on high speed valves.
2. Mechanical Design Standard DS-M18.2.21 does not consider potential for bending stresses in the valve stem induced by back-seating.
3. 1ST Program personnel elected not to incorporate guidelines from NUREG 1482 for deferral of testing to refuel outage.
B. The cause(s) and circumstances for each human performance related root cause:
No human performance related cause was identified.
IV. Analysis of the event:
The Tennessee Valley Authority (TVA) is submitting this report in accordance with Title 10 of the Code of Federal Regulations (10 CFR) 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the plant's Technical Specifications, and 10 CFR 50.73(a)(2)(v)(D), as any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.
An investigation determined that the valve stem failed in a single tensile failure mode. In order for this failure mode to occur, the valve stem had to fail in the open direction. Therefore, the failure could not have occurred in July as the last time the valve was operated in the open direction was on April 20, 2016, during performance of the HPCI system motor-operated valve (MOV) operability surveillance [1-SR-3.6.1.3.5(HPCI)]. Following completion of the surveillance, the HPCI main and booster pump set developed head and flow rate test at rated reactor pressure (1-SR-3.5.1.7) was performed. The valve was determined to have failed on April 20, 2016; however, due to valve conditions, including packing load and frictional forces induced from operating conditions, the 1-FCV-073-0002 partially closed when the demand to close was provided for maintenance on July 18, 2016. Because the PCIV was inoperable longer than required by TS, a violation of TS LCO 3.6.1.3 is reportable.
The safety function of HPCI is to assure that the reactor is adequately cooled to limit fuel cladding temperature in the event of a small break in the nuclear system and loss of coolant which does not result in rapid depressurization of the reactor vessel. The function of PCIVs, in combination with other accident mitigation systems is to limit fission product release during and following postulated Design Basis Accidents (DBAs) to within limits. Primary containment isolation within the time limits specified for those isolation valves designed to close automatically ensures that the release of radioactive material to the environment will be consistent with the assumptions used in the analyses for DBA. Because of the valve was unable to be opened, the HPCI System was inoperable in a mode of applicability, and a safety system functional failure is reportable.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
V. Assessment of Safety Consequences
This event resulted in additional, unplanned inoperability and unavailability of the single train of the BFN, Unit 1, HPCI system. This resulted in the inability of the HPCI system to perform its safety function, for mitigation of the consequences of an accident, longer than the planned system outage duration. In the event of an emergency, the RCIC system remained operable, and all other ECCS and ADS systems were available during this event to facilitate core cooling.
Therefore, during the time period that the HPCI system was inoperable, sufficient systems were available to provide the required safety function of accident mitigation. The preliminary risk evaluation results indicate that the safety significance of this event was low.
With respect to primary containment isolation requirements, the 1-FCV-073-0002 was not capable to perform its isolation function since April 20, 2016. During the time period that the valve was inoperable, 1-FCV-073-0003 and 1-FCV-073-0081 were available to provide the required safety functions of primary containment isolation. The preliminary risk evaluation results indicate that the safety significance of this event was low.
The risk evaluations are being finalized, and the LER will be revised if final results differ from preliminary results.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
During this event, RCIC was verified as operable by operations personnel. Additionally, all other ECCS and ADS systems remained operable. 1-FCV-073-0003 and 1-FCV-073-0081 were available to provide the required primary containment isolation safety functions.
B. For events that occurred when the reactor was shut down, availability of safety-related systems or components:
This event did not occur when the reactor was shut down.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
The Unit 1 HPCI system was declared inoperable due to placement of clearances to support scheduled maintenance on July 18, 2016, at 0300. On July 20 at 1245 1-FCV-073-0002, HPCI Steam Line Inboard Isolation Valve, was declared inoperable for its PCIV function and sustained HPCI inoperability. Because this valve is located inside primary containment and cannot be isolated at power, the reactor had to be shutdown to perform troubleshooting and corrective maintenance. Operations personnel inserted the manual reactor scram on July 26 at 0800. Once the PCIV function and HPCI System were restored, the HPCI System was declared operable on August 1 at 0010. From the time the HPCI System was declared inoperable until its return to service was approximately 13.88 days, which is less than the TS LCO 3.5.1 Condition C allowed outage time of 14 days.
comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
- 5 LICENSEE EVENT REPORT (LER) ....
CONTINUATION SHEET
3. LER NUMBER
2016 002 00
VI. Corrective Actions:
Corrective Actions (CA) are being managed by TVA's Corrective Action Program (CAP) under Condition Report (CR) 1193943.
The CAs described below address this condition:
1. Develop and implement guidance, for motor operated valves to accompany the Design Change process that requires consideration of operating conditions on valve coast including inertial and stem rejection forces, in Design Change Procedure NPG-SPP-09.3.1 Section 3.4.4 for valves.
2. Develop and implement modification for valves 1/2/3-FCV-073-0002 to provide additional margin to prevent back-seating.
3. Revise General Specification G-50 to provide guidance for high speed valve open limit switch settings.
4. Revise Mechanical Design Standard DS-M18.2.21 to require consideration for bending due to misalignment when evaluating back-seating.
5. Evaluate remaining extent of condition population: 2/3-FCV-073-0002, DC motor MOVs, non-IST, and 1ST valves not monitored in the closed direction.
The interim actions below were identified:
1. Adjust packing load on valve 1/2/3-FCV-073-0002 to compensate for coast effect.
2. Ensure 1/2/3-FCV-073-0002 are not electively closed for maintenance.
3. Implement administrative requirement to obtain program engineering and shift manager approval prior to stroking valves 1/2/3-FCV-073-0002 while associated reactor is NOT in Modes 4 or 5 with the exception of casualty response.
4. Modify the 1ST program to not require quarterly valve stroking of 1/2/3-FCV-073-0002.
VII. Additional Information:
A. Previous Similar Events:
A review of Condition Reports (CRs), Licensee Event Reports (LERs), BFN Self Assessments, INPO ICES database searches, and NRC website searches were conducted.
During the course of the investigation, a search of the CR database (Maximo) was conducted for similar and related issues, based on several different parameters. After reviewing the CRs, several BFN CRs were found to be similar to the issue found in CR 1193943, including two CRs (639155 and 658890) from a previous cause evaluation for a similar issue.
CR 639155 On 10/20/2012, the as-found local leak rate test (LLRT) for 1-FCV-073-0002, Unit 1 HPCI Inboard Steam Isolation Valve, significantly exceeded administrative limits. The measured leak rate was 599.8 standard cubic feet per hour (scfh) with an administrative limit of 30 scfh. 1-FCV-073-0002 was subsequently disassembled on 11/06/2012 to investigate the cause for the failure by work order 114039287. This investigation revealed that the valve comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
3. LER NUMBER
- 00 2016 002 stem to wedge anti-rotation pin (referred to as anti-rotation pin) had broken in several locations and the disc retainer had fallen from the wedge assembly and was found located between the valve discs.
CR 658890 This CR was initiated to document that the event identified by CR 639155 was OE preventable.
B. Additional Information:
There is no additional information.
C. Safety System Functional Failure Consideration:
The 1-FCV-73-0002 valve was not part of the planned maintenance being performed during the scheduled maintenance window on July 18, 2016. Due to additional, unplanned inoperability of the HPCI system resulting from the failure of the valve, this system was unable to perform its safety function while in a mode of applicability.
This event resulted in the inability of the BFN, Unit 1, HPCI system to perform its safety function for mitigation of the consequences of an accident. In accordance with NUREG-1022, this event is considered a safety system functional failure.
D. Scram with Complications Consideration:
Unit 1 was shut down manually by operations in order to correct the condition in a planned Maintenance Outage; however, this event did not result in an automatic reactor scram with complications.
VIII. COMMITMENTS
There are no new commitments.
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