05000296/LER-2016-006, Regarding High Pressure Coolant Injection System Found to Be Inoperable During Testing

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Regarding High Pressure Coolant Injection System Found to Be Inoperable During Testing
ML16218A477
Person / Time
Site: Browns Ferry Tennessee Valley Authority icon.png
Issue date: 08/05/2016
From: Bono S
Tennessee Valley Authority
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
LER 16-006-00
Download: ML16218A477 (10)


LER-2016-006, Regarding High Pressure Coolant Injection System Found to Be Inoperable During Testing
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v), Loss of Safety Function
2962016006R00 - NRC Website

text

Tennessee Valley Authority, Post Office Box 2000, Decatur, Alabama 35609-2000 August 5, 2016 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001

Subject:

Browns Ferry Nuclear Plant, Unit 3 Renewed Facility Operating License No. DPR-68 NRC Docket No. 50-296 Licensee Event Report 50-296/2016-006-00 10 CFR 50.73 The Tennessee Valley Authority is submitting this report in accordance with Title 10 of the Code of Federal Regulations 50. 73(a)(2)(v)(D), as an event or condition that could have prevented the fulfillment of the safety function of structures or systems which are needed to mitigate the consequences of an accident.

There are no new regulatory commitments contained in this letter. Should you have any questions concerning this submittal, please contact J. L. Paul, Nuclear Site Licensing Manager, at (256) 729-2636.

Enclosure: Licensee Event Report 50-296/2016-006 High Pressure Coolant Injection System Found to be Inoperable During Testing.

cc (w/ Enclosure):

NRC Regional Administrator - Region II NRC Senior Resident Inspector - Browns Ferry Nuclear Plant

ENCLOSURE Browns Ferry Nuclear Plant Unit 3 Licensee Event Report 50-296/2016-006-00 High Pressure Coolant Injection System Found to be Inoperable During Testing See Enclosed

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 (11 -2015)

..,~..:J..~- REC <t.t.,>

the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE Browns Ferry Nuclear Plant, Unit 3 05000296 1 OF8
4. TITLE High Pressure Coolant Injection System Found to be Inoperable During Testing
5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED I

SEQUENTIAL I REV FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR NUMBER NO.

MONTH DAY YEAR N/A N/A FACILITY NAME DOCKET NUMBER 06 08 2016 2016 -

006 00 08 05 2016 N/A N/A

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)

D 20.2201

D 20.2203<a><3Hi>

D 50. 73(a)(2)(ii)(A)

D 50. 73(a)(2)(viii)(A) 1 D 20.2201 <d>

D 20.2203(a)(3)(ii)

D 50. 73(a)(2)(ii)(B)

D 50. 73(a)(2)(viii)(B)

D 20.2203(a)(1 >

D 20.2203<a><4>

D 50. 73(a)(2)(iii)

D 50. 73(a)(2)(ix)(A)

D 20.2203(a)(2)(i)

D 50.36(c)(1 )(i)(A)

D 50. 73(a)(2)(iv)(A)

D 50.73(a)(2)(x)

10. POWER LEVEL D 20.2203(a)(2)(ii)

D 50.36(c)(1 )(ii)(A)

D 50. 73( a)(2)(v)(A)

D 73.71 <a><4>

D 20.2203(a)(2)(iii)

D 50.36(c)(2)

D 50. 73(a)(2)(v)(B)

D 73. 71 (a)(5)

D 20.2203(a)(2)(iv)

D 5o.4s(a)(3)(ii)

D 50.73(a)(2)(v)(C)

D 73.77(a)(1) 100 D 20.2203(a)(2)(v)

D 50. 73(a)(2)(i)(A)

[gl 50. 73(a)(2)(v)(D)

D 73. 77(a)(2)(i)

D 20.2203(a)(2)(vi)

D 50. 73( a)(2)(i)(B)

D 50. 73(a)(2)(vii)

D 73. 77(a)(2)(ii)

D 50. 73(a)(2)(i)(C)

D OTHER Specify in Abstract below or in

3. LER NUMBER SEQUENTIAL NUMBER 006 REV NO.

00 B. Status of structures, components, or systems that were inoperable at the start of the event and that contributed to the event:

There were no structures, systems, or components (SSCs) whose inoperability contributed to this event.

C. Dates and approximate times of occurrences

Dates and Approximate Times June 8, 2016 at 0925 CDT June 8, 2016 at 1013 CDT June 8, 2016 at 1026 CDT June 8, 2016 at 1037 CDT June 8, 2016 at 1500 CDT June 9, 2016 at 0130 CDT June 10, 2016 at 0555 CDT Occurrence Unit 3 HPCI was declared inoperable for a planned surveillance test.

Pre-startup trip tests were completed.

Unit 3 HPCI turbine was given an initiation signal in accordance with the surveillance procedure, but the system failed to start properly.

HPCI turbine was manually tripped and returned to standby readiness following erratic operation upon turbine start.

HPCI surveillance test completed with an unsatisfactory (UNSAT) result.

Mechanical Maintenance Group performed a HPCI oil system check as a part of troubleshooting activities, which revealed that the failure of the Mechanical Trip Valve reset spring caused the event, and not air in the oil system.

Unit 3 HPCI system is declared Operable.

D. Manufacturer and model number (or other identification) of each component that failed during the event:

The inoperable valve was a Terry Steam Turbine Company mechanical trip valve, model CCS.

E. Other systems or secondary functions affected

No other systems or secondary functions were affected by this event.

F. Method of discovery of each component or system failure or procedural error

Valve inoperability was discovered during the scheduled performance of 3-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure, when the turbine steam supply valve was opened to supply steam to the turbine. The control room observed erratic turbine operation, and the turbine was manually tripped shortly thereafter.

G. The failure mode, mechanism, and effect of each failed component, if known:

The HPCI mechanical trip valve failed due to insufficient Reset Spring force, caused by end-of-life failure. The spring was permanently deformed by continual compression, and it was 3/16 inches shorter than its replacement. The failed spring also lacked resiliency when compressed; the specification for the trip force is 2-5 pounds (lbs), but post-event maintenance found that the trip force was less than 1 lb. There is no documented history of this spring having ever been replaced on Unit 3 HPCI; although the tappet had been damaged and replaced, the old spring was reinstalled.

H. Operator actions

The event began when the Unit 3 HPCI system was manually tripped following erratic operation upon turbine start. In accordance with the surveillance procedure, the turbine steam supply valve was opened to supply steam to the turbine. Operators in the Unit 3 Control Room noted that the turbine showed no immediate response followed by a turbine tripped alarm, and that both the HPCI stop valve and the HPCI control valve operated slowly and erratically.

I. Automatically and manually initiated safety system responses

There were no automatic or manual safety system responses associated with this event.

Ill.

Cause of the event

A. The cause of each component or system failure or personnel error, if known:

The HPCI mechanical trip valve failed due to insufficient Reset Spring force, caused by end-of-life failure. The spring was permanently deformed by continual compression.

B. The cause(s) and circumstances for each human performance related root cause:

The preventive maintenance (PM) that implements procedure MCl-0-073-TRB001, HPCI Turbine

- Terry Turbine CCS - Disassembly, Inspection, Rework and Reassembly, did not contain a requirement to specify that the trip tappet, spring, and piston require replacement as part of the valve's 10 year overhaul.

IV.

Analysis of the event

SEQUENTIAL NUMBER 006 REV NO.

00 The Tennessee Valley Authority (TVA) is submitting this report in accordance with Title 10 of the Code of Federal Regulations 50. 73(a)(2)(v)(D), as an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. It was determined that the HPCI mechanical trip valve was inoperable due to the end-of-life failure of the valve's reset spring, which caused it to generate insufficient force.

The condition was discovered on June 8, 2016, during a planned surveillance. While the HPCI system was already declared inoperable to perform the surveillance, the discovery of a condition that could have led to the system being declared inoperable in a Mode where Operability is required is considered a reportable event, in accordance with NUREG-1022.

System availability was impacted by this event, since HPCI is a single-train system. The HPCI Turbine Stop Valve Mechanical Trip Valve (i.e. "HPCI mechanical trip valve") functions as part of the HPCI OS trip sequence, to trip the turbine and allow it to automatically re-start. Final Safety Analysis Report (FSAR) Section 7.4, Emergency Core Cooling Control, states that the only protection devices that can act to interrupt planned Emergency Core Cooling System (ECCS) operation are those which must act to prevent complete component or system failure; the HPCI turbine OS trip is one such protection device. The HPCI mechanical trip valve may also be used locally to trip the turbine.

Turbine OS protection and local manual trip capability are not specified safety functions of the HPCI system, since these functions do not contribute to the system's core cooling function. However, the HPCI mechanical trip valve must remain in its normal "stand-by" position during HPCI operation to allow the HPCI stop valve to remain open. If the HPCI mechanical trip valve is re-positioned, either by manually lifting its reset knob, or by the OS trip weight striking the bottom of the tappet assembly, then the control oil to the HPCI stop valve is dumped, closing the HPCI stop valve under spring pressure. The reset spring failure resulted in erratic HPCI stop valve operation during the system start on June 8, 2016. Because of this degradation in system reliability, Operations declared the HPCI system inoperable.

V.

Assessment of Safety Consequences

This event resulted in inoperability of the single train of the BFN, Unit 3, HPCI system, resulting in the inability of the HPCI system to perform its required safety function to mitigate the consequences of an accident.

Several alternate methods were available to Operations personnel in the event of an emergency to provide core cooling, safe and sustainable shutdown of the reactor, residual heat removal, and mitigation of accident consequences. For Design Basis Accidents, adequate core cooling was ensured by the operability of the other low pressure ECCS injection/spray subsystems in conjunction with the Automatic Depressurization System (ADS). All ADS valves were operable during the time period and ADS initiation capability was maintained during this time period. Additionally, two Core Spray [BM] subsystems and two Low Pressure Coolant Injection [BO] subsystems, all low pressure ECCS subsystems, and their initiation capability, remained operable. While this even caused a YEAR 2016

3. LER NUMBER SEQUENTIAL NUMBER 006 REV NO.

00 Reactor Core Isolation Cooling (RCIC) suction pressure alarm, this transient was very brief and RCIC remained operable and able to perform its required function as an alternate high pressure injection system through the duration of this event.

This event was resolved within the 14 day completion time required by TS LCO 3.5.1, Condition C.

Therefore, BFN Unit 3 remained in an analyzed safe condition throughout this event.

The initial system response on June 8, 2016, during the HPCI pre-startup trip checks, was that the HPCI stop valve operated normally. Therefore, it is reasonable to conclude that if a valid HPCI initiation signal was given prior to the performance of the HPCI pre-startup check, that the HPCI system would have started normally and provided the design flow rate to the reactor vessel. This operation would not have been challenged by the insufficient force on the Reset Spring unless the HPCI system was tripped by overspeed, by locally by manual operation of the HPCI stop valve.

However, overspeed trip and manual trip functionality are not specified safety functions of the HPCI system.

Based on the above, during the time period that the HPCI system was inoperable, TVA has concluded that sufficient systems were available to provide the required safety functions needed to protect the health and safety of the public.

A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event:

While this event caused the RCIC Turbine Suction Pressure Low alarm to annunciate, RCIC was verified to be operable by Operations personnel. During this event, all other Emergency Core Cooling Systems, including the Automatic Depressurization System, were available to mitigate abnormal and accident conditions.

B. For events that occurred when the reactor was shut down, availability of systems or components needed to shut down the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident:

This event did not occur when the reactor was shutdown.

C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:

Approximately two days elapsed between the time of discovery and returning the train to service.

VI.

Corrective Actions

Corrective Actions are being managed by TVA's corrective action program under Condition Report (CR) 1179483.

A. Immediate Corrective Actions

A troubleshooting work order was initiated, which found the HPCI Turbine Step Valve Mechanical Trip Valve Reset Spring was deformed and weakened from years of continuous compression.

The spring was replaced and HPCI was returned to service.

8. Corrective Actions to Prevent Recurrence Corrective actions to prevent recurrence include revising procedures to:

Specify replacement of the Trip Tappet, Piston, and Reset Spring on a defined periodicity.

Require recording the as-left breakaway force a minimum of three times, and selecting the lowest value as the most accurate. To ensure repeatability, additional tests shall be performed if the lowest two recorded values are not within 0.5 lb of each other.

Clarify that the performance of the lift force check after adjusting the spring compression shall be conducted with the aux oil pump running.

VII. Additional Information

A. Previous Similar Events

A similar event occurred on February 11, 2012, when the HPCI Stop Valve failed to open following a simulated HPCI Turbine Overspeed (OS) Trip. During a BFN, Unit 3, HPCI System quarterly surveillance, personnel verified the proper operation of the HPCI Turbine Mechanical trip valve. During the event in question, when personnel lifted the trip tappet, it never fell to reset the system; the stop valve remained closed instead of opening again. During troubleshooting personnel mechanically agitated the trip tappet by stroking it up and down while rotating the assembly, with the auxiliary oil pump running, until the tappet began operating correctly. The tappet was then rotated to various positions and repeatedly pulled to verify its repeatability over all angles. The trip tappet was able to fall, reset, and fulfill surveillance conditions. Later investigations found metal shavings the area, and the event was attributed to debris blocking the piston port. The mechanical agitation removed the debris, correcting the problem. The duplex oil filters should prevent debris from traveling from the tank to the piston. Additionally, the oil tank was drained and cleaned.

These conditions will also be addressed by the corrective actions (CAs) for the event described in this report, by making changes to the PM and the maintenance procedures to clean the HPCI 2016 006 00 Turbine Overspeed OS Trip valve internals every 10 years, as part of periodic tappet, piston, and spring replacement.

B. Additional Information

There is no additional information.

C. Safety System Functional Failure Consideration:

In accordance with NUREG-1022, this event is considered a safety system functional failure.

HPCI pre-startup trip checks on June 8, 2016 verified normal operation of the HPCI stop valve trip function. These checks included a manual trip of the HPCI stop valve, which demonstrated proper operation of the Reset Spring, at 0954 CDT. Operators declared HPCI inoperable due to erratic indications during surveillance testing at 1026 CDT. Valve troubleshooting and the replacement of the Reset Spring were not part of pre-planned maintenance, causing a period of unplanned operability which lasted until June 10, 2016 at 0555 CDT. HPCI was then inoperable for an unexpected condition that could have prevented HPCI from performing its safety function for approximately two days, while in a Mode where HPCI Operability was required.

D. Scram with Complications Consideration:

This event did not result in a reactor scram.

VIII. COMMITMENTS

There are no new commitments.