ML20050F831

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Monthly Operating Rept for Oct 1981
ML20050F831
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 11/02/1981
From: Ruiter G
WISCONSIN PUBLIC SERVICE CORP.
To:
Shared Package
ML20050F776 List:
References
NUDOCS 8204130384
Download: ML20050F831 (4)


Text

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s C 1 GI OuIT S5UTD0W B $ A 5 D PO8 IE 5 ID0CTIO55

  • O PJ g 20 BCCEET no: 50-305

[,' UBIT NAME: Kemannee

  • O L) DATE: November 2, 1981 t 01 C05PLETED BY: G. H. Reiter TELIFBCat: 414-388-2560 m225 k O A b"

or REPORT SCETH - OCTCBER, 1981 4 O*

T tJw C00 g D l 30. l DATE lTIPE lDURATICElREA50Nl5ftHCDj LEB EU5BER lSYS lCCFFCNENTl C055ESTS l

! l l l l l l l  ? l 4 1 I I I 1 1 1 1 1 I i g I 9 110/ J/831 F 1 0. 0 1 B 1 5 i s/A 1 HF 1 HTEICH I 9. A load reduction to 425 povec was required to 1 1 1 I I I I I l I s I permit inspection of the Sain Condenser I i I I i I i I I i 1 waterboxes and the plugging of two condenser i g i I i 1 I i 1 1 I I tubes due to circulating water leakage into I i 1 1 1 1 I I 1 1 I the condenser. I I i 1 1 I I I I I I i y 3 10 11C/31/81) F I 0.0 1 8 3 5 1 3/A I HF I HTEICH I 10. A load reduction to 425 power was required to 3 i i 1 I I I i i 1 A permit laspection of the Rain Condenser I I I I I I I I I I I waterboxes and the plujiing of one condenser i y 1 3 1 1 I i 1 1 1 I tube due to circulating water leakage into the i I I I I i 1 1 I i 1 condenser. 1 1 I I i 1 I A I I i 1 y i 1 1 I I I i 1 1 I I I I I i i i i I i 1 1 1 I I I J 3 I I I 3 I g, I I I I I I 3 3 I I I I I I i I i i I J a l -

1 i i i i I I i i  ! i g, I i 1 1 I I I I J l I I i i I I I I I 1 1 1 1 I I I 1 i I I i 1 1 y i I I I I I I I i 3 I I i 1 I I I I I I I I -

1 I I i 1 1 1 I i 1 1 y i I I I I i I I i 1 1 1 I I I I I I I I I 1 e i I I I i 1 1 I I I I y i I I I I 'I I I I I I I I I I I I i 1 1 I I -

,1 .I I I I

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.I . - - .

s TIFE BEASCM R ETHCD SYSTER G COMPONENT CODES F: Forced A-Equipment Failure (Explain) 1-Manual From NOREG-0161 +

S: Scheduled 2-Eaintenance or Test 2-nanual Scras y C-Befueling J-Automatic Scram D-6eg ula tory Bestriction 4-Continuations s E-Operator Training & License Emanimation 5-Load Beauctions C F- A d min is tra tive 9-Other G-operaticnal Error (Esplain) /

Il-Ct her (Explain) v a

h,

DOCKET 50-305 a

KEWAUNEE NUCLEAR PCWEB PLANT

SUMMARY

OF OPEBATING EXPERIENCE October, 1981 u

OPERATIONS: Cn October 3, the unit load was reduced to 225 MW to check for condenser leakage. The sonthly turbine stop valve test was completed during the power reduction. The unit was returned to full load on October 4.

On October a:, the unit load was reduced to 225 EU to check for condenser leakagr. The November turbine stop valve test was also completed during the power reduction.

M A INT EN A NCE: Beplaced a leaking scienoid valve in a diesel generator air starting system.

Replaced a faulty controller fcr a SBV damper contrclier.

Replaced a faulty static trip device on a containment spray pump circuit brcaker.

Febuilt a charging pump.

Replaced a diesel generator startup air compressor motor.

Replaced a defective coil for a SEY exhaust fan damper solenoid valve.

l l

LEVEL A V ER AG E DAILY UNIT POW ER DOC KET EO- 50-305 UNIT- KEW AUNEE COMPLETED BY- G. H. RUITEB TELEPHONE- 414-388-2560 X225 DEPORT MCETH OCTOBER, 1981 AVERAGE CAILY DAY PCWER LEVEL (MW E-N ET) 1 512 2 508 y 3 234 ,

4 275 5 503 6 512 7

  • 512 8 512 9 512 10 512 11 512 12 512 13 512 14 512 15 508 16 532 17 512 38 512 19 516 20 512 21 512 22 513 23 512 24 512 25 511 26 512 27 512 28 512 29 512 30 512 31 230

b

@ PE B ATING DATA aEPOR 1 g, CCCEET 30- 53-305 C*EPLETED BI- G. B. BOITER .

OP ER ATI 5G STAT 35 TELEPhost- 414-386-2560 3225 s 4

1 UNIT BASE EEWA05EE e**ee*****************eeeeeeeeeeeeeeeeeeeeeees

(, e e 2 REPORTING PEaIOC OCTOBER, 1981

  • NOIES The unit has teen on line for
  • e 1s6 consecutive days. *

(, 3 LICEuSED TEERSIL FOWER (531) 1650 * * ;

4 s&MIELATE BATING (GROSS 5WE) 560 e *

(, *

  • 5 DESIGu ELECTRICAL B ATIE0 (BET SS E) 535 *
  • e .

(, 6 5&II535 DEPERCAELE CAPACITY (CEOSS BWE) 545

  • e e a 7 5AIIM35 DEPENCABLE CAPACITY (5ET BEE) 512 ese*****ese*************************eeeeeeeeee 4,

8 IF CH& uGES OCCUR Ib CAPACITY EATIECS (ITE85 EUMBER 3 THECUGH 7) SINCE LAST BEPOBT, GIVE REASONS The aarinum Dependable Capacity was updated to 512 ewe based on the fourth

(, guarter capacity test.

9 POW ER LEVEL TO kHICS B E ST BICT E D, IF Auf (5ET BWE) None 4

10 REASCNS FOR SESTRICTIONS, IF ABT L

THIS 50518 YR-TC-DATE CUMULATIVE L

11 HOUSS 15 RBf08715G PERIOD 745 7296 64681 g, 12 NJ55E8 0F HOURS EIACTOR BAS CBITICAL 745.0 6215.3 54537.9 13 BEACTOR BESERVE SHOTDOBE B00BS 0.0 0.0 2330.5

~

14 HOURS GEutRATOR OD-LINE 745.0 6133.9 53342.8 g, 15 UNIT BEStaVE SUTDous 8008S 0.0 0.0 10.0 16 GROSS THERRAL EBEBGY GEBEB ATED (nWM) 1870754 9752247 82439471 17 GROSS ELECTRICAL ENERGY GENERATED (SEH) 380600 3185000 27179200 -

g, 18 NEY ELECTRICAL EMIEGT CENESATED ( 5W H) 361946 30J1737 25862707 19 UNIT SERVICE FACTOR 100.0 84.1 82.5 20 UNIT AFAILABILITY FACTOR 100.0 84.1 82.5 s g, 21 UNIT CAPACITY FACTOR (USING 5tc NET) 94.9 80.4 76.4 a

22 UNIT CAPACITT FACTOR (OSING DES NET) 90.8 17.7 74.7 6

23 OMIT FOBCED OUTAGE BATE 0.0 0.8 4.9 /

gy 24 SHUTDOWNS SCHEDULED CV EB NEIT 6 BONTHS (T YP E, DATE, AND DURATIOE OF ZACH)

/

No ne

- (, 25 IF SHOT DOWN AT END OF BLPOST PERIOD, ESTIM ATED D ATE OF . ST ARTOP - 5/ A e

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