ML20097H932

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Monthly Operating Rept for Aug 1984
ML20097H932
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 08/31/1984
From: Hintz D, Ruiter G
WISCONSIN PUBLIC SERVICE CORP.
To:
NRC OFFICE OF ADMINISTRATION (ADM), NRC OFFICE OF INSPECTION & ENFORCEMENT (IE)
References
CON-NRC-84-150 NUDOCS 8409210048
Download: ML20097H932 (5)


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DCCEET 50-205 KEWAUNEE KUCLEAE POWEF PLANT SUMBABY CF OPERATING IIPERIENCE August, 1984 OPIPATIONS: Unit Icad has reduced on August 5, 1984 for performance of the monthly Turbine Stop Valve test. The unit was returned to full power operation the same day.

h AINT EN ANCE: Beplaced a defective Voltage regulator for the FPI rack.

Installed new check valves in the Diesel Generator air start syster. . _

, Peplaced a defective Steam Generator icw pressure histable unit. -

8409210048 840831 g PDR ADOCK 05000305 PDR 1 4e R

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. - ATEBAGI DAILY UN I.T POW EF L EVEL DCCKET NC- 50-305 UNIT- KEWAUNEE CCMPLETEC BY- G. B. EDITER TELEPHONE- 414-38E-2560 X225 PEPOET MONTH AUGUSI, 1SE4 AVERAGE DAILY DAY ECWEB IEVEI

( M W E-NE T) 1 520 2 515 3 520 4 515 5 491 6 516 7 515 8 515 9 520 10 515

,. 11 507 12 511 13 507 14 507 15 507 16 507 17 507 .

18 507 -

19 507 20 511 21 507 22 520 23 515 24 511 25 511 26 515 27 519 28 519 29 520 30 520 31 524 h

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UN 2T H E1D0W 5S AND PO8 IE BIEUCTIONS

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%. j CCCFZT 3C: SC-3C5 DNIT BARI: Revannee 6,

, EATE: September 4, 1984 V

'CCEPIE1ED BY: G. H. Buiter TILIPHONE: 414-328-2560 m225 L SEPORT MONT8 - AUGUST, 1984 .

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. I NC. I DATE ITYPE lE05A11CNIFIf!ONIMITECDI IER NUEBES ISTS I CCFFONENT l CCMMENTS I 1 6  :  :  :  :  :  :  :  :  : 4

! L I i i i I I I I I I I J l I I I I I I I I I to shutdowns or power reducticas in August. I i i i i I I I i 1 1 I

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I. I. I. . I. I. .I I Ls TYPI 523 SON METHCD SYSTER & COMPONINT CCDES  %)

F: Forced A-Iquipment railure (Esplais) 1-Manual Frca NUREG-0161

%, S: Scheduled I-Eaintenance cr Test 2-Manual Scran (J C-fef ueling 3-Automatic Screa C-Segulatcry factriction 4-Continuations L +

I-CFerator Training s License Examination 5-toad seductions G F-fdainistrative 9-Other G-Cperaticaal Irror (Esplais) 4 B-Cther (Isplain)

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. @ PI3ATING~ D 1.T A 5E50B1 . -

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d C35PLETED B1- G. H. EDITEP .

OPER ATIN G S 1 A T U -S TILIPECNI- 414-386-2560 1225

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1 UNIT NAME REWAOBEE **********************************************

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  • J 2 I!!CETING PIRIOC AUGUST, 1924
  • 3C1ES
  • e
  • b 3 LICINSID THEP5AL EOHIR (MWT) 1E50
  • Normal power operation continued through
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  • this reportlag period. *
  • 4 NAMIELATE BATING (GBCSS mRE) 560 *
  • g:

5 tISIGN ELICTBICAL PATING (MIT RWE) 535 *

  • b
  • 6 PAI1505 DYPINEAELI CAPACITY (GECSS RnE) 529 , '* d 7 PAIIMOM DEPENCAELI CAPACITY (BET EEE) 503 **'******************************************

8 IF CHANGES CCCUF IN CAIACITY TATI5GS (1715! NUMBIS 3 TERCOGB 7) SINCE LAST BEFOBT, GIVE BEASONS Meme g.

9 FCWIP LEVEL 70 EBICH BI!1BICTID, IF ABY (NIT RWE) lone ,

10 BEA!ONS FCB BES1PICTICIS, IF l>Y J

TBIS MONTE IB-70-DATE CURULATIVI 11 HCUIS IN IFPCBTIBG IIFICE 744 5855 89520 12 EDMEIf 0F HCOBS BIAC1CR NAS CFITICAL 744.0 4641.6 ,75821.5 ,

- 0 13 FIACTCP BISIRVI SIOTC0hp BOURS 0.0 0.0 2330.5 g

14 HCUPS GENEFA1CR r!-LI5t 744.0 4599.3 74411.7 15 UNI 1 BESEFV! SuitCNN BCOSS 0.0 0.0 10.0 d 16 GE0!S THEBMAL INIfGY GINIPATEC (MEB) 1222297 7301828 116272914 17 GFOSS ELECTBICAL INIBGY GENEBATED (Mau) 401200 2408600 38266700 IE NET ELECTFICAL INIFGY GINIPATID (REB) 381602 2293515 36425551 s 15 UNI 1 S!RVICE FAC1C5 100.0 78.6 83.1 J

20 0511 AVAII4EILI11 FACTCf 100.0 78.6 E3.1 21 UNIT CAPACITY FAC10B (OSING ECC NET) 102.0 77.9 78.3 J 22 UNIT CAPACITY FACTOR (OSING DIS NET) 95.9 73.2 16.1 G

23 UNI 1 F05CID 00TAGI BATI 0.0 0.3 3.7 b

24 SH41DCWNS SCHEDDIID CVII REIT 6 McNTBS (TYfE, DATE, AMC DURATION OF ERCH) O Befueling shutdova of E-veek duratica scheduled to start lettuary 15, 1985.

b 25 IF !HUI DCWN AT 15C,07 REPORT PERIOD, ESTIPAIED DA11 Cf ST AETOP - 5/ A I

. NRC-84-150 WISCONSIN PUBLIC SERVICE CORPORATION P.O. Box 1200, Green Bay, Wisconsin 54305 September 10, 1984 Director,

-Office of Inspection and Enforcement Attention Document Control Desk U. S. Nuclear Regulatory Commission Washington, D.C. 20555 Gentlemen:

Docket 50-305 Operating License DPR-43 Kewaunee Nuclear Power Plant Monthly Operating Report The narrative " Summary of Operating Experience" and completed forms covering plant and component availability for the Kewaunee Nuclear Power Plant for August 1984 are enclosed.

Very truly yours,

/N$

D. C. Hintz Manager - Nuclear Power JGT/js Enc.

cc - Mr. J. G. Keppler, Reg Adm US NRC - Region III Mr. Robert Nelson, NRC Sr Resident Inspector RR #1, Box 999, Kewaunee, WI 54216 Mr. S. A. Varga, Chief US NRC - Div. of Licensing INP0 Records Center, Suite 1500, 1100 Circle 75 Parkway, Atlanta, GA 30339 -

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