IR 05000261/2014004

From kanterella
Revision as of 16:42, 10 January 2025 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
IR 05000261/2014004, on July 1, 2014 Through September 30, 2014; H. B. Robinson Steam Electric Plant, Unit 2; Integrated Inspection Report
ML14301A011
Person / Time
Site: Robinson 
Issue date: 10/28/2014
From: Hopper G
Reactor Projects Region 3 Branch 4
To: Glover M
Duke Energy Progress
References
IR 2014004
Download: ML14301A011 (33)


Text

October 28, 2014

SUBJECT:

H.B. ROBINSON STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT 05000261/2014004

Dear Mr. Glover:

On September 30, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your H. B. Robinson Steam Electric Plant, Unit 2. On October 16, 2014, the NRC inspectors discussed the results of this inspection with you and other members of your staff.

Inspectors documented the results of this inspection in the enclosed inspection report.

No NRC-identified or self-revealing findings were identified during this inspection. However, inspectors documented a licensee-identified violation which was determined to be of very low safety significance in this report. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II, the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at H. B. Robinson Steam Electric Plant, Unit 2. In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publically Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

George T. Hopper, Chief Reactor Projects Branch 4 Division of Reactor Projects

Docket No.:

50-261 License No.: DPR-23

Enclosure:

Inspection Report 05000261/2014004 w/Attachment: Supplemental Information

REGION II==

Docket Nos.:

50-261

License Nos.:

DPR-23

Report No.:

05000261/2014004

Licensee:

Duke Energy Progress, Inc.

Facility:

H. B. Robinson Steam Electric Plant, Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

July 1, 2014 through September 30, 2014

Inspectors:

K. Ellis, Senior Resident Inspector

C. Scott, Resident Inspector

M. Riches, Resident Inspector (Acting)

A. Nielson, Senior Health Physicist, 2RS8 R. Hamilton, Senior Health Physicist, 2RS7 J. Rivera, Health Physicist, 2RS1, 4OA1 R. Kellner, Health Physicist, 2RS6, 4OA1

Approved by:

George T. Hopper, Chief Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000261/2014004, July 1, 2014 through September 30, 2014; H. B. Robinson Steam

Electric Plant, Unit 2; Integrated Inspection Report.

The report covered a three-month period of inspection by resident inspectors and announced inspections by reactor inspectors. One licensee-identified violation of very low safety significance (Green) was identified. The significance of inspection findings are indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP) dated June 02, 2011.

The NRCs program for overseeing the safe operations of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been reviewed by the NRC. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and corrective action tracking number is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

The unit began the inspection at 100 percent power and remained there through the end of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

a. Inspection Scope

Partial Walkdown

The inspectors verified that critical portions of the selected systems were correctly aligned by performing partial walkdowns. The inspectors selected systems for assessment because they were a redundant or backup system or train, were important for mitigating risk for the current plant conditions, had been recently realigned, or were a single-train system. The inspectors determined the correct system lineup by reviewing plant procedures and drawings. Documents reviewed are listed in the Attachment.

The inspectors selected the following three systems or trains to inspect:

  • Dedicated Shutdown Diesel Generator (DSDG)

Complete Walkdown

The inspectors verified the alignment of the Unit 2 Service Water system. The inspectors selected this system for assessment because it is a risk-significant mitigating system. The inspectors determined the correct system lineup by reviewing plant procedures, drawings, the updated final safety analysis report, and other documents.

The inspectors reviewed records related to the system outstanding design issues, maintenance work requests, and deficiencies. The inspectors verified that the selected system was correctly aligned by performing a complete walkdown of accessible components.

To verify the licensee was identifying and resolving equipment alignment discrepancies, the inspectors reviewed corrective action documents, including condition reports and outstanding work orders. The inspectors also reviewed periodic reports containing information on the status of risk-significant systems, including maintenance rule reports and system health reports. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R05 Fire Protection

a. Inspection Scope

Quarterly Inspection

The inspectors evaluated the adequacy of selected fire plans by comparing the fire plans to the defined hazards and defense-in-depth features specified in the fire protection program. In evaluating the fire plan, the inspectors assessed the following items:

  • control of transient combustibles and ignition sources
  • fire detection systems
  • water-based fire suppression systems
  • gaseous fire suppression systems
  • manual firefighting equipment and capability
  • passive fire protection features
  • compensatory measures and fire watches
  • issues related to fire protection contained in the licensees corrective action program

The inspectors toured the following four fire areas to assess material condition and operational status of fire protection equipment. Documents reviewed are listed in the

.

  • Rod Control Room
  • 4160 Switchgear Room
  • Mezzanine deck of the Turbine Building

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

Internal Flooding

The inspectors reviewed related flood analysis documents and walked down the area listed below containing risk-significant structures, systems, and components susceptible to flooding. The inspectors verified that plant design features and plant procedures for flood mitigation were consistent with design requirements and internal flooding analysis assumptions. The inspectors also assessed the condition of flood protection barriers and drain systems. In addition, the inspectors verified the licensee was identifying and properly addressing issues using the corrective action program. Documents reviewed are listed in the Attachment.

  • Component Cooling Water Pump Room

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

a. Inspection Scope

Routine Operator Requalification Review: On August 26, 2014, the inspectors observed operators in the plants simulator during licensed operator requalification training to verify that the operator performance was adequate, evaluators were identifying and documenting crew performance issues and training was being conducted in accordance with station procedures. The inspectors observed a shift crews response to the scenario listed below. Documents reviewed are listed in the Attachment.

Operators were required to perform a rapid depressurization of the reactor coolant system to limit the radioactive release to the environment through the ruptured steam generator tube and out the unisolable steam line break. The inspectors assessed the following:

  • licensed operator performance
  • the ability of the licensee to administer the scenario and evaluate the operators
  • the quality of the post-scenario critique
  • simulator performance

Review of Licensed Operator Performance: The inspectors observed licensed operator performance in the main control room during a downpower to 98% from 100% to support testing on the Auxiliary Feedwater system and the Rod Control system.

The inspectors assessed the following:

  • use of plant procedures
  • control board manipulations
  • communications between crew members
  • use and interpretation of instruments, indications, and alarms
  • use of human error prevention techniques
  • documentation of activities
  • management and supervision

Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors assessed the licensees treatment of the two issues listed below to verify the licensee appropriately addressed equipment problems within the scope of the maintenance rule (10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants). The inspectors reviewed procedures and records to evaluate the licensees identification, assessment, and characterization of the problems as well as their corrective actions for returning the equipment to a satisfactory condition. The inspectors also interviewed system engineers and the maintenance rule coordinator to assess the accuracy of performance deficiencies and extent of condition.

Documents reviewed are listed in the Attachment.

  • AR 492296492296 Engine Driven Fire Pump Maintenance Rule Concerns not visible in decision making
  • AR 699900699900 Trip of Water Cooled Condensing Unit (WCCU) 1B

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the four maintenance activities listed below to verify that the licensee assessed and managed plant risk as required by 10 CFR 50.65(a)(4) and licensee procedures. The inspectors assessed the adequacy of the licensees risk assessments and implementation of risk management actions. The inspectors also verified that the licensee was identifying and resolving problems with assessing and managing maintenance-related risk using the corrective action program. Additionally, for maintenance resulting from unforeseen situations, the inspectors assessed the effectiveness of the licensees planning and control of emergent work activities.

Documents reviewed are listed in the Attachment.

  • Reviewed the weekly Risk Mitigation Plan for 9/8 to 9/15
  • Reviewed the Critical Activity Plan and associated protected equipment during removal of the A EDG for testing
  • Reviewed the protected equipment while the engine driven fire pump was out of service for maintenance
  • Reviewed the protected equipment during A Safety Injection Pump and HVH-6A out of service for maintenance

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors selected the six operability determinations or functionality evaluations listed below for review based on the risk-significance of the associated components and systems. The inspectors reviewed the technical adequacy of the determinations to ensure that technical specification operability was properly justified and the components or systems remained capable of performing their design functions. To verify whether components or systems were operable, the inspectors compared the operability and design criteria in the appropriate sections of the technical specification and updated final safety analysis report to the licensees evaluations. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the attachment.

  • AR 695891695891 C Component Cooling Water (CCW) Pump Outboard seal leakage high
  • AR 705419705419 Removal of A and F flow elements from averaging circuit for R-14, Plant Stack Radiation Monitor
  • AR 699365699365 AFW-33 failed as-found lift test
  • AR 700539700539 Motor-operated potentiometer failure on the manual voltage regulator for the Dedicated Shutdown Diesel Generator
  • AR 704902704902 EDG jacket water cooling system seismic concerns

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

The inspectors verified that the plant modification listed below did not affect the safety functions of important safety systems. The inspectors confirmed the modifications did not degrade the design bases, licensing bases, and performance capability of risk significant structures, systems and components. The inspectors also verified modifications performed during plant configurations involving increased risk did not place the plant in an unsafe condition. Additionally, the inspectors evaluated whether system operability and availability, configuration control, post-installation test activities, and changes to documents, such as drawings, procedures, and operator training materials, complied with licensee standards and NRC requirements. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with modifications. Documents reviewed are listed in the Attachment.

  • EC 91633, Diesel Fire Pump Engine Replacement

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors either observed post-maintenance testing or reviewed the test results for the six maintenance activities listed below to verify the work performed was completed correctly and the test activities were adequate to verify system operability and functional capability.

  • WO 13316129, Post Maintenance EDG Ventilation Exhaust (HVE-17), Operability Check, July, 21, 2014
  • WO 13354016, OST-251-2 B RHR Pump and Components Test following breaker replacement, July 31, 2014
  • WO 02180018, PM-124, Perform Thermal Overload Testing on Breaker 2M (V6-33E, Containment Recirculation Cooler [HVH-4] Selective Service Water Inlet Valve) on MCC-5, September 15, 2014
  • Acceptance criteria were clear and demonstrated operational readiness.
  • Effects of testing on the plant were adequately addressed.
  • Test instrumentation was appropriate.
  • Tests were performed in accordance with approved procedures.
  • Equipment was returned to its operational status following testing.
  • Test documentation was properly evaluated.

Additionally, the inspectors reviewed a sample of corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with post-maintenance testing. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the six surveillance tests listed below and either observed the test or reviewed test results to verify testing adequately demonstrated equipment operability and met technical specification and licensee procedural requirements. The inspectors evaluated the test activities to assess for preconditioning of equipment, procedure adherence, and equipment alignment following completion of the surveillance.

Additionally, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with surveillance testing. Documents reviewed are listed in the attachment.

Routine Surveillance Tests

  • OST-401-1, EDG A Slow Speed Start, Rev. 61
  • OST-908-3, Component Cooling Water Pump B Test, Rev. 3
  • MST-021, Reactor Protection Logic Train B at Power, Rev. 37
  • MST-022, Safeguard Relay Rack Train A, Rev. 22

In-Service Tests (IST)

Reactor Coolant System Leak Detection

  • OST-051, Reactor Coolant System Leakage Evaluation (Every 72 Hours during Steady State Operation and within 12 Hours after Reaching Steady State Operation),

Rev. 47

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed the emergency preparedness drill conducted on July 9, 2014.

The inspectors observed licensee activities in the simulator and/or technical support center to evaluate implementation of the emergency plan, including event classification, notification, and protective action recommendations. The inspectors evaluated the licensees performance against criteria established in the licensees procedures.

Additionally, the inspectors attended the post-exercise critique to assess the licensees effectiveness in identifying emergency preparedness weaknesses and verified the identified weaknesses were entered in the corrective action program. Documents reviewed are listed in the attachment.

b. Findings

No findings were identified.

RADIATION SAFETY

2RS1 Radiological Hazard Assessment and Exposure Controls

a. Inspection Scope

Hazard Assessment and Instructions to workers: During facility tours, the inspectors directly observed labeling of radioactive material and postings for radiation areas, High Radiation Areas (HRAs), and Locked High Radiation Areas (LHRAs) established within the Radiologically Controlled Area (RCA) of the auxiliary building and radioactive waste (radwaste) processing and storage locations. The inspectors independently measured radiation dose rates or directly observed conduct of licensee radiation surveys for selected RCA areas. The inspectors reviewed survey records for several plant areas including surveys for airborne radioactivity, gamma surveys with a range of dose rate gradients, and pre-job surveys for Forced Outage (FO) R229F3. The inspectors also discussed changes to plant operations that could contribute to changing radiological conditions since the last inspection. The inspectors observed radiological briefings by Health Physics (HP) personnel and reviewed Radiation Work Permit details to assess communication of radiological control requirements and current radiological conditions to workers.

Hazard Control and Work Practices: The inspectors evaluated access barrier effectiveness for selected LHRA locations. Changes to procedural guidance for LHRA and Very High Radiation Area (VHRA) controls were discussed with HP supervisors.

Controls and their implementation for storage of irradiated material within the spent fuel pool were reviewed and discussed in detail. Established radiological controls (including airborne controls) were evaluated for selected FO R229F3 work, including reactor cavity decontamination, steam generator (SG) manway removal, and seal table incore detector replacement. In addition, licensee controls for areas where dose rates could change significantly as a result of plant shutdown and refueling operations were reviewed and discussed.

The inspectors observed HP technician proficiency during the surveying and downposting of a LHRA in the radwaste building. Electronic dosimeter (ED) alarm set points and worker stay times were evaluated against area radiation survey results for FO R229F3 reactor cavity decontamination, SG manway removal, and seal table incore detector replacement. Procedures for the use of personnel dosimetry (ED alarms, extremity dosimetry, multibadging in high dose rate gradients, etc.) as well as worker response to dose and dose rate alarms were reviewed.

Control of Radioactive Material: The inspectors observed surveys of material and personnel being released from the RCA using small article monitor, personnel contamination monitor, and portal monitor instruments. The inspectors discussed equipment sensitivity, alarm setpoints, and release program guidance with licensee staff.

The inspectors also observed the daily source check of a personnel contamination monitor. The inspectors also reviewed records of leak tests on selected sealed sources and discussed nationally tracked source transactions with licensee staff.

Problem Identification and Resolution: Nuclear Condition Reports (NCRs) associated with radiological hazard assessment and control were reviewed and assessed. The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures.

Radiation protection activities were evaluated against the requirements of Updated Final Safety Analysis Report (UFSAR) Section 12; Technical Specifications (TS) Sections 5.4 and 5.7; 10 CFR Parts 19 and 20; and approved licensee procedures. Licensee programs for monitoring materials and personnel released from the RCA were evaluated against 10 CFR Part 20 and IE Circular 81-07, Control of Radioactively Contaminated Material. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

2RS6 Radioactive Gaseous and Liquid Effluent Treatment

a. Inspection Scope

Program Reviews: The inspectors reviewed the 2013 Annual Radioactive Effluent Release Report for consistency with the requirements in the Offsite Dose Calculation Manual (ODCM) and Technical Specifications. Radioactive effluent monitor inoperability periods and compensatory sampling were reviewed and discussed with plant staff. No changes have been made to the ODCM since the last inspection. Planned 2015 ODCM changes were discussed with licensee staff.

Walk-Downs and Observations: The inspectors walked-down selected components of the gaseous and liquid discharge systems to ascertain material condition, configuration and alignment. To the extent practical, the inspectors observed the material condition of abandoned in place liquid waste processing equipment for indications of degradation or leakage that could constitute a possible release pathway to the environment. The inspectors observed collection and analysis of gaseous effluent samples (noble gas, iodine, particulates) from two release points and preparation of gaseous effluent release permits. The inspectors walked-down portions of the containment and auxiliary building ventilation systems, to ascertain material condition, configuration, and alignment. In addition, the inspectors reviewed the most recent air cleaning surveillance testing results for the auxiliary building ventilation system.

Sampling and Analyses: In addition to observing collection of gaseous effluent samples, the inspectors observed a chemistry technician verifying plant stack flow rates and performing daily verification checks of effluent radiation monitors. The inspectors reviewed analysis results and release reports generated during a recent SG tube leak and discussed how the results will be reported in the 2014 annual report. The results of the chemistry count rooms inter-laboratory comparison program were reviewed and discussed with cognizant licensee personnel.

Dose Calculations: The inspectors reviewed several liquid and gaseous release permits, and monthly gaseous/liquid effluent dose calculation summaries. The inspectors reviewed the contributions to public dose from reported abnormal releases. The sites 10 CFR 61 analysis was reviewed for expected nuclide distribution from the aspects of quantifying effluents, the treatment of hard to detect nuclides, and determining appropriate calibration nuclides for instrument counting libraries. The inspectors also reviewed the licensees most recent Land Use Census results.

Ground Water Protection: The inspectors reviewed the licensees continued implementation of the industrys Ground Water Protection Initiative (Nuclear Energy Institute 07-07) as part of Inspection Procedure 71124.07.

Problem Identification and Resolution: Selected corrective action program documents associated with the effluent monitoring and control program, including NCRs and audits, were reviewed and assessed. The inspectors verified that problems were being identified at an appropriate threshold and resolved in accordance with licensee procedures. Documents reviewed are listed in the report Attachment.

b. Findings

No findings were identified.

2RS7 Radiological Environmental Monitoring Program (REMP)

a. Inspection Scope

REMP Implementation: The inspectors observed routine sample collection and surveillance activities as required by the licensees environmental monitoring program.

The inspectors noted the material condition and operability of airborne particulate filter and iodine cartridge sample stations and observed collection of weekly air samples at selected monitoring locations. The inspectors checked environmental thermoluminescent dosimeters for material condition at 10 monitoring sites including several indicator locations and a control location that was greater than 10 miles away.

The inspectors also observed collection of surface water samples at 4 locations including Black Creek and the ash basin. The inspectors observed the collection of composite water samples at the east and west retention ponds. In addition, the inspectors reviewed and evaluated land use census results, changes to the ODCM, monitoring for hard-to-detect radionuclides, and sample collection/processing activities.

The inspectors reviewed the last two calibration records for selected environmental air samplers. The inspectors also reviewed the 2013 Radiological Environmental Operating Report and the 2013 Annual Radioactive Effluent Report. The inspectors reviewed the 2014 Accreditation Reports for the vendor labs used to process environmental samples.

The inspectors reviewed the interlaboratory comparison results for all 4 quarters of 2013 and the first quarter of 2014. Selected environmental measurements were reviewed for consistency with licensee effluent data, evaluated for radionuclide concentration trends, and compared with detection level sensitivity requirements.

Ground Water Protection: The inspectors discussed program guidance for spills, leaks, and unexpected discharges with licensee staff and reviewed recent entries into the 10 CFR 50.75(g) decommissioning file. The inspectors reviewed and discussed the licensees program for monitoring of structures, systems, and components with the potential to release radioactive material to the environment. Potential effluent release points due to onsite surface water bodies were also evaluated. In addition, the inspectors reviewed recent groundwater sampling results.

Meteorological Monitoring Program: The inspectors observed the physical condition of the tower and its instrumentation and discussed equipment operability and maintenance history with licensee staff. The inspectors evaluated transmission of locally generated meteorological data to other licensee groups such as main control room operators. For the meteorological measurements of wind speed, wind direction, and temperature, the inspectors reviewed the last two calibration records for applicable tower instrumentation.

The inspectors also evaluated measurement data recovery for 2013.

Problem Identification and Resolution: The inspectors reviewed selected NCRs in the areas of radiological environmental monitoring and meteorological tower maintenance.

The inspectors evaluated the licensees ability to identify and resolve the issues in accordance with licensee procedures. The inspectors also evaluated the scope of the licensees internal audit program and reviewed recent assessment results.

REMP implementation, meteorological monitoring, and groundwater protection activities were reviewed against the guidance and requirements of 10 CFR Part 20; Appendices E and I to 10 CFR Part 50; TS Section 5.0; UFSAR Chapter 2; ODCM; Regulatory Guide 4.15, Quality Assurance for Radiological Monitoring Programs (Normal Operation) -

Effluent Streams and the Environment; Safety Guide 23, Onsite Meteorological Programs; Branch Technical Position, An Acceptable Radiological Environmental Monitoring Program - 1979; and approved licensee procedures. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and

Transportation

a. Inspection Scope

Waste Processing and Characterization: During inspector walk-downs, accessible sections of the liquid and solid radwaste processing systems were assessed for material condition and conformance with system design diagrams. Inspected equipment included storage tanks, transfer piping, resin dewatering and packaging components, and abandoned radwaste processing equipment. The inspectors discussed component function, processing system changes, and radwaste program implementation with licensee staff.

The inspectors reviewed the 2013 Annual Radioactive Effluent Report and radionuclide characterizations from 2013 - 2014 for each major waste stream. For Spent Resin Storage Tank resin and Dry Active Waste, the inspectors evaluated analyses for hard-to-detect nuclides, reviewed the use of scaling factors, and examined quality assurance comparison results between licensee waste stream characterizations and outside laboratory data. Waste stream mixing and concentration averaging methodology for resin and filter waste streams were evaluated and discussed with radwaste staff. The inspectors also reviewed the licensees procedural guidance for monitoring changes in waste stream isotopic mixtures.

Radioactive Material Storage: During walk-downs of indoor and outdoor radioactive material storage areas, the inspectors observed the physical condition and labeling of storage containers and the posting of Radioactive Material Areas. The inspectors also reviewed licensee procedural guidance for storage and monitoring of radioactive material.

Transportation: The inspectors evaluated shipping records for consistency with licensee procedures and compliance with NRC and Department of Transportation (DOT)regulations. The inspectors reviewed emergency response information, DOT shipping package classification, waste classification, and radiation survey results. Licensee procedures for opening and closing Type B shipping casks were compared to Certificate of Compliance requirements. Since there were no shipments available for observation during the week of inspection, the inspectors reviewed qualification records for radworkers who perform shipping preparation activities.

Problem Identification and Resolution: The inspectors reviewed NCRs in the areas of shipping and radwaste processing. The inspectors evaluated the licensees ability to identify and resolve the issues.

Radwaste processing, radioactive material handling, and transportation activities were reviewed against the guidance and requirements contained in the licensees Process Control Program, UFSAR Chapter 11, 10 CFR Part 20, 10 CFR Part 61, 10 CFR Part 71, the Branch Technical Position on Waste Classification (1983), and NUREG-1608.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed a sample of the performance indicator (PI) data, submitted by the licensee, for the Unit 2 PIs listed below. The inspectors reviewed plant records compiled between July 2013 and June 2014 to verify the accuracy and completeness of the data reported for the station. The inspectors verified that the PI data complied with guidance contained in Nuclear Energy Institute 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedures. The inspectors verified the accuracy of reported data that were used to calculate the value of each PI. In addition, the inspectors reviewed a sample of related corrective action documents to verify the licensee was identifying and correcting any deficiencies associated with PI data.

Documents reviewed are listed in the Attachment.

Cornerstone: Initiating Events

  • SCRAMS with complications

Cornerstone: Mitigating Systems

  • Heat removal system Occupational Radiation Safety Cornerstone: The inspectors reviewed the Occupational Exposure Control Effectiveness PI results for the Occupational Radiation Safety Cornerstone from December 2013 through July 2014. For the assessment period, the inspectors reviewed ED alarm logs and NCRs related to controls for exposure significant areas. Documents reviewed are listed in the Attachment.

Public Radiation Safety Cornerstone: The inspectors reviewed the Radiological Control Effluent Release Occurrences PI results for the Public Radiation Safety Cornerstone from May, 2013 through June, 2014. For the assessment period, the inspectors reviewed cumulative and projected doses to the public contained in liquid and gaseous release permits and corrective actions related to Radiological Effluent Technical Specifications/ODCM issues. The inspectors also reviewed licensee procedural guidance for collecting and documenting PI data. Documents reviewed are listed in the

.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

The inspectors screened items entered into the licensees corrective action program in order to identify repetitive equipment failures or specific human performance issues for follow-up. The inspectors reviewed condition reports, attended screening meetings, or accessed the licensees computerized corrective action database.

.2 Operator Work-Around Annual Review

a. Inspection Scope

The inspectors performed a detailed review of the licensees operator work-around, operator burden, and control room deficiency lists for the station in effect on July 21, 2014 to verify that the licensee identified operator workarounds at an appropriate threshold and entered them in the corrective action program. The inspectors verified that the licensee identified the full extent of issues, performed appropriate evaluations, and planned appropriate corrective actions. The inspectors also reviewed compensatory actions and their cumulative effects on plant operation. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion

(Closed) LER 2013-001-01, Non-Environmentally-Qualified Splice Rendered Post Accident Monitoring (PAM) Instrumentation Channel Inoperable

On October 6, 2013, during work to replace the limit switches of the CVC-204B, Letdown Line Isolation Valve, the licensee discovered that a non-environmentally qualified butt splice was installed on a wire for the closed limit switch. The improper wiring for the limit switch did not meet environmental qualification (EQ) requirements and rendered the Post-Accident Monitoring (PAM) Instrumentation function of containment isolation valve position indication inoperable. The licensees cause investigation determined that the improper splice was installed in 1992 and that on multiple occasions the function was inoperable for a period of time greater than allowed by technical specifications TS 3.3.3, PAM Instrumentation Limiting Condition of Operation (LCO). The licensee determined that the cause of this event was a human performance event in which a technician failed to use the proper heat shrink insulators as directed by CM-309. The licensee entered this issue in the corrective action program as NCR 640902 and replaced the improper splice with the appropriate material. The inspectors reviewed the corrective actions and determined that they were adequate. Revision 1 was issued to include the system/component failure codes. The enforcement aspects of this Licensee Event Report (LER) were documented in IR 05000261/2014003 Section 4OA3.1 Follow-up of Events and Notices of Enforcement Discretion. Revision 1 of the LER was reviewed and no additional findings were identified and no additional violation of NRC requirements occurred. This LER is closed.

(Closed) LER 2014-001-01, Reactor Trip Due to a Two-Out-of-Three Logic Signal from Steam Generator Water Level Protection Train B Logic Matrix

On January 9, 2014, with the unit in Mode 1 at 100 percent power, a turbine trip and an automatic reactor trip occurred during the performance of surveillance test procedure MST-013, Steam Generator Water Level Protection Channel Testing. The reactor trip occurred during Step 8.2.85 of MST-013, when the bistable switch was placed in the test position (opens the two LC-494A1-X contacts). One channel contact (contact 2-6 on relay LC-496A1-X(B)) was unknowingly open due to foreign material lodged between the contact faces. This half-trip condition did not show on the control room annunciator panel. When the two LC-494A1-X contacts opened, the two-out-of-three logic was completed. For corrective actions, the licensee inspected both trains of relay racks to identify and remove any potential foreign material. The licensee also tested both trains of reactor protection relays to verify no foreign material was present. Additionally, the licensee plans to replace the wire labels in the reactor protection and safeguards relay racks during the next two refueling outages. The inspectors also reviewed post-trip activities to verify that the licensee identified and resolved event-related issues prior to restarting the plant. Revision 1 was issued to include the System/Component codes, add Energy Industry Identification System (EIIS) functional identifiers to the narrative and describe the half trip condition. The enforcement aspects of this LER were document in IR 05000261/2014003 Section 4OA3.1 Follow-up of Events and Notices of Enforcement Discretion. Revision 1 of the LER was reviewed and no additional findings were identified and no additional violation of NRC requirements occurred. This LER is closed.

(Closed) LER 2013-003-01, Reactor Trip on 4KV Bus Undervoltage during Load Transfer

On November 5, 2013, with the unit at 19 percent power, an automatic reactor trip occurred due to a loss of voltage on 4kv Buses 1 and 2. The reactor trip occurred while operators were transferring loads from the Start-up transformer to the Auxiliary transformer as part of power ascension, following refueling outage 28. During the breaker operation, a broken operating rod on breaker 52/7 prevented the breaker from closing and resulted in a momentary loss of power to 4KV Bus 2 and 4KV Bus 1. For corrective actions, the licensee replaced the operating rod for the failed breaker and performed post maintenance testing to verify operation, prior to returning the unit to service. The inspectors reviewed the corrective actions and determined that they were adequate. The inspectors also reviewed post-trip activities to verify that the licensee identified and resolved event-related issues prior to restarting the plant. Revision 1 was issued to add the system/component identifiers, include EIIS codes to the narrative and add additional description of the failure. The enforcement aspects of this LER were document in IR 05000261/2014002 Section 1R12 Maintenance Effectiveness. Revision 1 of the LER was reviewed and no additional findings were identified and no additional violation of NRC requirements occurred. This LER is closed.

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

On October 16, 2014, the resident inspectors presented the inspection results to Mr.

Glover and other members of the licensees staff. The inspectors verified that no proprietary information was retained by the inspectors or documented in this report.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and is a violation of NRC requirements which met the criteria of the NRC Enforcement Policy, for being dispositioned as a Non-Cited Violation.

  • 10 CFR 26.205(d)(7), Work Hour Controls, requires, in part that the licensee shall control the work hours of individuals to less than a weekly average of 54 hours6.25e-4 days <br />0.015 hours <br />8.928571e-5 weeks <br />2.0547e-5 months <br />, calculated using an average period of six weeks. Contrary to this requirement, seven covered workers violated the work hour limits on thirteen occasions.

Specifically, following the Spring 2014 forced outage, the licensee failed to recode all covered workers to an on-line status. This finding was more than minor because if left uncorrected, the failure to change the individual coding from off-line to on-line status would have allowed all covered workers onsite to exceed work hour limits, and could lead to a more significant safety concern. This violation was determined to be of very low safety significance because no significant events or human performance issues were directly linked to personnel fatigue as a result of the hours worked. The licensee entered this issue into their CAP as CR 698782.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

T. Cosgrove, Plant General Manager
S. Connelly, Licensing
H. Curry, Training Manager
D. Douglas, Maintenance Manager
R. Gideon, Vice President
M. Glover, Director - Site Operations
R. Hightower, Licensing/Reg. Programs Supervisor
D. Hoffman, Nuclear Oversight Manager
K. Holbrook, Operations Manager
C. Sherman, Radiation Protection Superintendent
L. Martin, Engineering Director
K. Moser, Outage & Scheduling Manager
S. Williams, Chemistry Manager
C. Spencer, Supervisor - Chemistry

NRC personnel

G. Hopper, Chief, Reactor Projects Branch 4

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Closed

05000261/2013-001-01 LER Non-Environmentally-Qualified Splice Rendered Post Accident Monitoring (PAM) Instrumentation Channel Inoperable
05000261/2014-001-01

LER Reactor Trip Due to a Two-Out-of-Three Logic Signal from Steam Generator Water Level Protection Train B Logic Matrix

05000261/2013-003-01

LER Reactor Trip on 4KV Bus Undervoltage during Load Transfer

LIST OF DOCUMENTS REVIEWED