ML20211A087

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Notice of Violation from Insp on 870105-08
ML20211A087
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 02/03/1987
From: Reyes L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20211A067 List:
References
50-269-87-01, 50-269-87-1, 50-270-87-01, 50-270-87-1, 50-287-87-01, 50-287-87-1, NUDOCS 8702190087
Download: ML20211A087 (1)


Text

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ENCLOSURE 1 NOTICE OF VIOLATION Duke Power Company Docket Nos. 50-269, 270, 287 Oconee License Nos. DPR-38, 47, 55 During the Nuclear Regulatory Commission (NRC) inspection conducted on January 5-8, 1987, a violation of NRC requirements was identified. The violation involved . failure to provide pipe erection procedure with acceptance criteria for cold springing of pipe. In accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1986), the violation is listed below:

10 CFR 50, Appendix B, Criterion V, as implemented by Topical Report Duke 1-A, Section 17.2.5, requires in part, that instructions, procedures, or drawings shall include appropriate quantitative or qualitative acceptance criteria for determining that important activities have been satisfactorily accom-plished.

Contrary to the above, on January 8,1987, the licensee failed to provide procedures with appropriate qualitative or quantitative acceptance criteria for activities important to safety in that the Oconee Pipe Specification used to erect safety related field fabricated piping provided no acceptance criteria for cold springing during installation.

This is a Severity Level IV Violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Duke Power Company is hereby required to submit to this Office within 30 days of the date of the letter transmitting this Notice a written statement or explanation in reply including (for each violation): (1) admission or denial of the violation, (2) the reason for the violation if admitted, (3) the corrective steps which have been taken and the results achieved, (4) the corrective steps which will be taken to avoid further violations, and (5) the date when full compliance will be achieved. Where good cause is shown, consideration will be given to extending the response time.

FOR THE NUCLEAR REGU'." TORY COMMISSION Original. Signed by Luis A. Reyes 87021}Q@y $o$$!69 Luis A. Reyes, Acting Director ppR Division of Reactor Projects

$DR Dated at Atlanta, Georgia this34d ay of g 1987