ML20125C742
ML20125C742 | |
Person / Time | |
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Site: | Brunswick |
Issue date: | 11/18/1992 |
From: | Christensen H, Prevatte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
To: | |
Shared Package | |
ML20125C668 | List: |
References | |
50-324-92-34, 50-325-92-34, NUDOCS 9212140056 | |
Download: ML20125C742 (18) | |
See also: IR 05000324/1992034
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g UNITED ST ATES
,f g NUCLEAR REGULATORY COMMISslO96
[ 'g' g RErlON11
g, nt 101 M ARIETT A ST RE ET. N W.
o '$ ATL ANTA, GEORGI A 30323
%s, p#
.....
Report Nos.: 50-325/34 and 50 324/34
Licensee: Carolina Pnwer and Light Company
P, 9. Box 1551
Rtleigh, NC 27602
Docket Nos.: 50 325 and 50-324 ticense Nos.: OPR-71 and DPR-62
Facility Name: Brunswick 1 and 2
Inspection Conducted: October 3 - October 31, 1992'
Lead Inspector: 4 cc3 % 4Senig[r Res' ent inspector
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R. L. Prevatre, ~
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Date Signed
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Other inspectors: D. J. Nelson, Resident Inspector f
P. M. Byron Resident Inspactor
Approved By: k[
H. Chri~ stensen, Chief
D- Il f13 7L
Date Signed
Reactor Projects Section lA
Division of Reactor Projects
SUMMARY
Scope:
This rcutine safety inspection by the resident inspectors invo'Jved the areas of
maintenance observation, surveillance observation., operational safety verification,
licensee self-assessment, outage activities, organizational changes and quality
control inspections.
Results:
In the areas inspected, one violation was identified involving a reactor operator
with an inactive license standing watches (paragraph 4). Additionally, further
examples of Violation 325,324/92-28-02 were identified for failure to maintain g
positive control of visitors (paragraph 4).
Within the area of outage work activities some progress was noted in completing work
requests / job orders (WR/J0s). However, identification of new work negated progress
in backlog reduction of WR/J0s. A reduction in operator work arounds was noted
(paragraph 5).
Units 1 and 2 were in cold shutdown for the entire reporting period. The outage
that started on April 2), 1992, continuad with no announced startup date.
)- 9212140056 921127
PDR ADOCK 05000324
G PDR
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REPORT DETAILS
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1 Persons Contacted
- Licensee Employees
K. Ahern, Manager - Operations Unit 2
M. Bradley, Manager - Brunswick Project Assessment
M. Brown, Plant Manager - Unit 2
, *S. Callis, On-Site Licensing Engineer
J. Cowan, Manager - Technical and Regulatory Support
J. Dobbs Assistant to Site Vice President
- *S. Floyd, Manager - RegJlator.y Compliance
, *R. Godley, Supervisor - Regulatory Compliance
R. Helme, Manager - Technical Support
J. Holder, Manager - Outage Management & Modifications (0M&M)
- M Jackson, Manager - Maintenance Unit 2
M. Jones, Manager - Training
- P. Leslie, Manager - Security
D. Moore, Manager - Maintenance Unit 1
R. Morgan, Plant Manager - Unit 1
R. Richey, Vice-President - Biunswick Nuclear Project
C. Robertson, Manager - Envirnneental & Radiological Control
- J. Simon, Manager - Operations Unit 1
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- R. Tart, Manager Operations Unit 2
- J, Titrington, Manager - Operations Unit 1
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C. Warriner, Manager - Contract and Administration
- E. Willett, Manager - Planning and Scheduling
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Other licensee employees contacted included construction craf tsmen,
engineers, technicians, operators, office personnel and security force
members.
l * Attended the exit interview.
Acronyms and initiailsms used in the report are listed in the last
l paragraph.
2. Maintenance Observation (62703)
The inspectors observed maintenance activities, interviewed personnel
and reviewad records to verify that work was conducted in accordance
- with approved precedures, Technical Specificat-ions and applicable
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industry codes and. standards. The inspectors also verified that:
redundant components were operable; administrative controls were
followed; tagouts were adequate; personnel were qualified; correct
replacement parts were used; radiological controls were proper; fire
protection was adequate; quality control hold points were adequate and
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observed; adequate post-maintenance testing was performed; and
independent verification requirements were implemented. The inspectors
. independently verified that selected equipment was properly returned to
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service.
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. Outstanding work requests were reviewed to ensure that the licensee gave
priority to safety related maintenance. The inspectors ,
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observed / reviewed portions of the following maintenance activities:
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WR/JO 92 ABBR 1 thru 8 Bearing replacement and other outage
- work activities on DG No. 1
Diesel Generator No. 1
.
- DG No. 1 inspections and maintenance activities discussed in the
previous report continued. The licensee identified additional problems
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with this DG. The damaged first idler gear and the broken teeth
- (Inspection Report 325,324/92-28) were sent to CP&L's Harris
Environmental & Energy (E&E) Center and the consultant for failure
analysis. This analysis has not been completed.
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The four connecting rod bearings adjacent to bearings 6 and 9 were
disa m mbled and inspected. Even though no damage was observed, they
were reassembled with new bearings. Vendor services were obtained to
repair the minor scoring previously identified on the Number 9 bearing
j ourr.al . During the journal repair, the contractor identified that the
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crankshaf t was bowed approximately 0.002 inches.
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As part of the bowed crankshaft investigation, the generator stator
dowel pins were removed. The dowels were found to be slightly bent.
The inspector observed that the stator had shifted outward approximately
1/64 - 1/32 inches. However, it was also found that the stator base
paint was not disturbed, indicating that the stator movement was not
- recent. The licensee is still investigating the cause of this movement.
The dowel pins were sent to the Harris E&E Center to determine the force
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required to bend them. This analysis had not been completed at the end
, of the reporting period.
On October 8,1992, cold crankshaft web deflection readings were taken,
lhese readings exceeded the allowable band of .002 inches. After
consultations witn former Nordberg engineers, the licensee decided to
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realign the crankshaft. This was accomplished by adding a 0.020 inch
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shim under the generator pedestal bearing to raise the crankshaft. This
4 returried the deflection readings to within specifications. Reassembly
of the engine was completed on October 13 and break in runs commenced.
The engine was run for 5, 15 and 30 minutes with no load and inspections
were performed after each run. On October 14, the unit was run for one
hour with a 900kw load. Post run inspections found thrust collar
- temperatures above normal. Investigation revealed that the thrust
collars had experienced severe thermal stress. Metal displacement was
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i found on the bearing surfaces and radial cracking was identified at
several points on the outer edge of the generator side thrust collar.
The inspector observed that the radial cracking was more significant at '
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the top of the collar. He also noted some pitting of the lower shell of
the No. 9 bearing and that there were slight deposits of aluminu:n
bearing material on the thrust collars. The licensee subsequently found
i brass from the thrust collar embedded in the crankshaft thrust surface.
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On October 16, the licensee removed the oil seal assembly from the
generator end of the engine and found signs of excessive heating on the
upper assembly. The heat stress zone extended from about 280 degrees to
i 100 degrees of the radial area and was approximately 1/2 inch wide on
the inner radius. The inspector noted that the first of four labyrinth
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rings showed signs of heat stress. The housing and first two labyrinth
rings had rolled edges. The crankshaft at a corresponding axial
position was gouged approximately seven to eight inches long,1/2 inch
wide and several mils deep. Because of the above damage, the No. 9
. bearing journal and the No. 8 R and No. 8 L connecting rod bearing
journals were dye-penetrant tested. No damage was found.
l The licensee requested on site assistance from NAK Engineering Company.
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This company is composed of the former chief service engineer and other
former Nordberg engineers. They also held the engine _ design drawings,
- The NAK representative has previously assisted the licensee in trouble
. shooting and identifying the causes of previous engine problems.
. The licensee took additional crankshaft measurements on October 17 and
j 18 and concluded that the crankshaft was bowed approximately 0.003
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inches. A marine engineering consultant was contracted to provide a
- second opinion and assist in straightening the crankshaft. This
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consultant, after inspecting the crankshaft, determined that it had a
- kink instead of a bow. The kink resulted in the No.10 journal being
! offset 4 mils from the No. 9 journal. The marine engineering consultant
believed that the damage was caused by high heat stress which had
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resulted from overheating of the thrust collars. He believed that the
crankshaft could be straightened by using a peening process to relieve
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the induced stresses. He also concluded that the damage in the area of
, the oil seal was caused by the crankshaft jumping. The licensee
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disagreed with his conclusion and believed the damage was caused by 4
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wobbling crankshaft. Neither party has been able to explain the cause
i of the phenomenon which they believed to have caused the damage. Two
representatives from the NRR staff were onsite October 21 and 22, and
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reviewed the problems associated with this engine.
On October 31, the inspector observed the crankshaft peening process. A
hand held pneumatic hammer was used to peen a point predetermined by
- rotational clearance measurements on the engine side radius of No. 9
i- journal. The crankshaft straightened approximately .0005 inches. The
l Nos. 6 and 9 journals were then polished by the consultant to remove any
damage that resulted from the previously described failed bearings. A
! second peening operation took place November 2. The licensee then had
difficulty obtaining repetitive measurements while measuring to
determine the amount that the crankshaft had straightened. While
- troubleshooting the cause of these inconsistent readings, the licensee
. discovered damage to the flexible drive gear located at the opposite end
(front) of the engine from the generator. The drive gear is attached to
the crankshaft and drives the engine driven lube oil pump. The
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inspector observed that damage occurred on the face of the gear teeth
- for approximately 300 degrees The damage was about 1/4 to 3/4 inches
j in length and varied in height on the tooth face. It was noted that as
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the damage approached the root it occurred on both faces and appeared to
have been caused by impact. The licensee observed that approximately
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one-half of the lthe oil pump gear showed signs of thermal stress.
These gears had been previously inspected during the current outage. -It
was therefore apparent that this damage had occurred during the pest .
maintenance runs.
The licensee's diesel consultant, NAK, believed that the gear damage may
have been caused by movement of the diesel ard suggested that the
collision blocks be inspected. Collision blocks are steel blocks
attached to the engine skid by 1-inch steel dowel pins and 3/4-inch
bolts. There are two collision blocks on each side and ends of the
engine. They are used primarily in mobile and marine installations to
restrict engine movement in the event of a vehicle or ship _ collision.
The blocks can be used to determine if there has been any movement of
the engine block relative to the skid. An inspection' revealed that both-
collision blocks at the rear of the engine (generator end) were missing.
The collision blocks were found under the generator mounting . rails.
Investigation revealed that both the dowels and bolts were sheared at
the foundation surface and the bolts were missing. The inspector
observed thht the dowels remaining in the blocks were deformed. The
licensee calculated that the engine had moved approximately 1/4 inch
toward the rear, or generator _end. At the end of this reporting period -
the licensee was attempting to determine the cause(s) of all damage
sustained to DG No. 1. The inspector will follow the licensee's
investigations, inspections and repairs, and rrovide additional
information in the next monthly report.
On October 6, 1992, while observing maintenance on DG No. 1, the
inspector observed that material was improperly stored in an adjacent -
"Q" Temporary Storage Area. The storage area contained material with
unprotected threads and valves which did not have the openings covered
and were not tagged. The inspector -informed maintenance and QC of this
concern. The maintenance foreman stated that the untagged material was
to be scrapped. The scrap material ~ was immediately removed and placed
in a trash container.
Violations and deviations were not identified.
3. Surveillance Observation (61726)
The inspectors observed surveillance testing required by Technical
Specifications. -Through observation, interviews, and records review,
the inspectors verified that: tests conformed to Technical
Specification requirements; administrative controls were followed;
personnel were qualified; instrumentation was calibrated; and data was
accurate and complete.- The inspectors independently verified selected
test results and proper return to _ service of equipment.
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- The inspectors-witnessed / reviewed portions of the following test
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! OMST DG-50lR3 54 month inspection on~DG No. 3
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j PT 12.2 B DG No. 2 Monthly t.oad Test
j PT 12.2 0 DG No. 4 Monthly Load Test
' These above tests and inspections were well planned and managed with
j adequate supervisory and technical oversite.-
l Violations and deviations were not identified.
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4. Operational Safety Verification (71707)
The inspectors verified that Unit I and Unit 2 were operated in
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compliance with Technical Specifications and other regulatory
i requirements by direct observations of activities, facility tours,
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C.:;cussions with personnel, reviewing records and independent
l verification of safety _ system status.
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! The inspectors verified that control room manning requirements of 10 CFR
- 50.54 and the Technical Specifications were met.- Control operator,
shift supervisor, clearance, STA, daily and standing instructions and
- jumper / bypass logs were reviewed to obtain information concerning
i operating trends and out of service safety systems to ensure that there
. were.no conflicts with Technical Specification Limiting Conditions for
- Operations. Direct observations of control room panels, instrumentation
and recorder traces important to safety were conducted to verify
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operability and that operating parameters were within Technical
Specification limits. The inspectors observed shift turnovers to verify
l that system status continuity was maintained. -The inspectors also
- verified the status of selected control room annunciators.
The inspectors verified the system alignment and operability of .
! equipment used for the normal and backup means for shutdown cooling on
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each unit. They additionally verified that there was no leakage of
major components; that proper lubrication and cooling water _was
j available; and conditions did not exist- which could prevent. fulfillment
!- of each system's functional- requirements. Instrumentation essential to
system actuation or performance was verified operable by observing on-
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scale indication and proper instrument valve lineup, if accessible.
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The inspectors verified that the licensee's HP policies and procedures-
were followed. This included observation of HP practices _and a review
-of area surveys, radiation work permits, posting and_ instrument
! calibration.
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The inspectors verified by general observations that: the secur_ity
l organization was properly manned and security personnel were capable of
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performing their assigned functions; persons and packages were checked.
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prior to entry into the PA; vehicles were properly authorized, searched
and escorted within the PA; persons within the PA displayed photo
identification badges; personnel in vital areas were authorized;
effective compensatory measures were employed when required; and
security's response to threats or alarms was adequate.
Three occurrences of failure to maintain positive control of visitors
were identified by the licensee during the assessment period. On
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October 2, 1992, an escort attempted to leave the protected area while
his visitor remained in the protected area eating lunch. This is
documented in ACR 92-793. On October 21, an escort was relieved t.t the
i end of his shift, but failed to notify security of the transfer to a new
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escort. This was detected by security when the escort attempted to
leave the protected area without his assigned visitor. This is
documented in ACR 92-847. The next day a security officer observed two
visitors without an escort. It was determined that the escort was in an -
adjacent area and did not have positive control of his visitors. This
is documented in ACR 92-846. These findings indicate that security
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office alertness has increased; however, it appears that other plant
personnel are not adequately trained in escort duties or that additional
. emphasis and oversite by supervisory personnel is necoed. The licensee
received a violation (Inspection Report 325,324/92-28) for failure to
maintain positive control of visitors on September 15, 1992. The
licensee's investigation of that event has not been completed and all
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corrective actions have not been identified. Therefore, the above
deficiencies will be identified as additional examples of Violation
. 325,324/92-28-02. In response to Violation 325,32/,92-28-02, the
licensee agreed to provide any additional correcth e action that is
being taken to address the above events.
The inspectors also observed plant housekeeping controls, verified
i position of certain containment isolation valves, checked clearances and
verified the operability of onsite and offsite emergency power sources.
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In early July 1992, a licensed reactor operator was removed from
licensed duties and placed in a rehabilitation program cfter his
admission of using a controlled substance contrary-to the requirements
, of 10 CFR 26 and subsequent positive testing. The individual completed
a rehabilitation program and his facility unescorted access was restored
on September 8. After a period of observation in unlicensed activities
he was returned to licensed duties on October 3, 1992. He was assigned
and assumed the licensed duties of Reactor Operator, Balance of Plant
(B0P), at approximately 7:00 a.m., on October 3, 1992. At approximately
9:00 a.m., while updating the accumulated watchstanding hours log for
licensed operators, the Operations Shift Supervisor discovered that the
subject operator had not completed the required 60 hours6.944444e-4 days <br />0.0167 hours <br />9.920635e-5 weeks <br />2.283e-5 months <br /> (five-12 h:.ur
shifts) of watchstanding in the previous quarter (i.e., July, Augusi. and
September). Upon discovery, the Shift Supervisor relieved this
individual of his assigned duties and placed him on watch in a training
status to begin license reactivation.
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10 CFR 55.53.e requires that in order to maintain an active license, the
licensee shall actively perform the function of an operator or senior
operator for a minimum of seven 8-hour or five 12-hour shifts per
calendar quarter. This requirement is implemented ii) the licensing
training instruction, NRC Licensee Operator / Quarterly Reporting
Requirements, TI-208, Volume 1, Rev 6. A review of the licensee's
accumulated watchstanding hour log by the resident inspector showed that
the individual did not stand any licensed watches during the July,
. August and September quarter.
Technical Specification 6.2.2.a and Table 6.2.2.1 list the minuum shift
composition for Unit conditions. The requirements spe.ify that for both
units in Condition 4, a minimum of two Reactor Operators shall be in the
control room. The licensee appears to have met this requirement.
However, the inactive operatnr was the only reactor operator at the
controls for Unit 2. The licensee states that the condition existed for
a very short period. A review of the SCO and C0 logs could neither
substantiate nor disprove that fact. However, the inspector noted that
he entered the control room on October 3 at approximately 9:00 a.m.,
reviewed the operating logs for both units and held a conversation with
the operator concerning his return to duty. At that time he and the
Senior Control Operator were the only licensed reactor operators on
Unit 2 and he was the only individual monitnring the Unit 2 Reactor
Control Board.
On Thursday, October 1, the Unit 2 Manager of Operations informed the
Senior Resident Inspector that the subject operator was being returned
to duty. At the time, he indicated that everything had been checked and
that a letter was being sent to inform the Regional Office that the
individual was being returned to a full duty status. However, a review
after this event reveals that when the individual was returned to an
l active status and reassigned to a shift on September 25, he met the
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requirements of 10 CFR 55.53e since he had stood more than five-12 hour
watches in the preceding quarter of April, May and June 1992. Based on
interviews with affected personnel, it appears that they did not realize
that the quarter would change prior to the individual being returned to
duty and did not perform an actual record review for the second or third
quarter of 1992. The review was accomplished by asking the operator if
he was current in his watch-standing. At the time he was questioned, he
was satisfactory.
The licensea, upon identification of this event, appears to have taken
the correct action of relieving the individual and reassigning his
duties to an active licensed person. The licensee initiated ACR 92-797
to document this event and determine the cause and required corrective
actions. The ACR stated that the immediate corrective action was to
summon a second R0 to the Unit 2 control room to assume the B0? operator
duties and place the above individual in a training status for license
re stora ti'"1. A review of the SCO and C0 logs does not confirm this
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action. Neither log shows that a new reactor operator assumed the watch
I after this event. The log does show that the involved B0P operator
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lined through his duty as B0P operator and changed it to Reactor
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Operator Trainee (ROT) with a date of October 3, 1992. Discussion with
the involved individuals indicated that the Plant Monitor Reactor
Operator was summoned back to the control room to assume the Reactor
, Operator watch. However, this was not documented in either the Reactor
Operator or Senior Reactor Operator log. This weakness and
inconsistency in the amount of information placed in Control Room logs
has been previously identified. Although improvement has been made,
logkeeping is still inconsistent between shifts and generally does not
contain adequate detail to document all significar,t shift occurrences or
allow recreation of events at a later date.
The inspectors became aware of the above event during a routine rev1ew
of ACRs the week of October 19, 1992. Inspection revealed the event and
4 the actions taken to restore the operator to an active status were
incomplete. 10 CFR 55.53(f) states that if the requirements of
10 CFR 55.53(e) are not met, then the licensee operator must complete a
minimum of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of on-shift functions under the direction of an
operator or senior operator as appropriate and in the position to which
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the individual will be assigned. The 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> must have included a
complete tour of the plant and all required turnover procedures.
The inspectors interviewed the operator involved in the event and
reviewed the reactor operator logs for documentation of the required
training. This review revealed that the operator had used the hours of
watch he stood on October 3 as an unqualified B0P operator as a credit
i toward his required 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> for retraining after disqualification on
October 3.
The inspector then questioned the operator about when he completed the
requirements to return to active status and was told that he had
finished these on October 6. At this time he offered as evidence a
completed Form TI-208-5 used to certify completion of action required to
return to active status. The inspector noted that this form showed 40.5
hours which included the time in question on October 3, 1992. At that
time the inspector requested that security provide a security access
printout for this operator for the period of September 15 to October 27.
A review of this record determined that the operator did not complete a
tour of the plant between his removal from watch on October 3 and his
return to an active status on October 6. The Shift Supervisor signed
him off as completing the tour on October 4, but the inspector
determined that he toured only a few areas of the plant between October
3 and 4.
Questioning of this operator and the Shift Supervisor by Operations
Management revealed that the Shift Supervisor and operator thought that
they could take credit for a period of Auxiliary Operator watches the
individual had stood between October 15 and October 27 as adequate for
the plant tour and that he could take credit for the hours on watch as
an unqualified Reactor Operator on October 3 to meet the requirements.
A further review of the security access logs by the inspector and-
Operations Management determined that the individual had not toured all
plant areas during the Auxiliary Operator watch standing time. It also
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' revealed that the individual had not stood a complete four hour watch
thut he took credit for on October 6. He had credited 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> on
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Octobee 6, but had left the control room and the protected area of the
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- ' ant prior to completing those 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />. In both instances, October 3
u i 00.tober 9, 1992, the operator was returned to an active status
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thout completing the requirements of 10 CFR 55.53. This is a
j ,iolation: Watchstanding With An Inactive License (325,324/92-34-01).
1 The licensee, upon becoming aware of the first event, removed the
! individual from an active licensed status and placed him in a training
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status. After the second event the watchstander was removed from
licensed duties until an investigation could be completed. The
j licensee's corrective actions to_date include: retraining and
- recertification of the affected operator, personnel actions for the
Reactor Operator and Shift' Supervisor and improvements in the
! computerized scheduling system _to track watchstanding hours and posting
- of all inactive licensed operators in the Shift Supervisor's office.
, This action will be completed by November 24.
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- The licensee had prior notification that it might be susceptible to an
event of this nature. In 1989, an event occurred at a nuclear plant:
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where a senior reactor operator with an inactive license assumed the
- ' watch as operator at the controls. As a result of that event, an
inspection was conducted at Brunswick and other' plants in Region Il to
, determine the administrative controls in place to prevent an occurrence
j of this nature. Inspection Report 325,324/ 89-34_ determined that "no
- program or administrative safety net existed to prevent unintentional or
a willful assumption of licensed duties by an unqualified licensed
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operator." That-report also stated the on-shift operations management
had no means in the control room to independently verify that on-watch
personnel are duly licensed. The report noted that no violations had
- been identified concerning unqualified personnel performing licensed
duties ~since 1984.
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As a result of the above inspection, the licensee initiated a procedure
change to Licensee Watch Standing Log Operating _ Instruction 01-49,
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Volume VII, Rev. 3, Step 6.2.3, to require that the Day Shift Production
Assistant on the first Saturday of March, June, September and December,
forward a list to the Operations Manager of all personnel whose license
will become inactive at the end of the calendar quarter. This step
i provided approximately one month early notification to-allow remedial
l action before a license became inactive._ This step was deleted when the
above 01-49 procedure was revised on August 1, 1991, to clarify the
I- duties of the production assistant.
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Service Water Pioino
Through wall piping leaks have occurred frequently in the service water
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system. Through wall leaks are significant because, if not corrected,
L they could progress to failures rendering safety systems inoperable. On l
October 19, 1992, a through wall leak occurred in an 18-inch service '
water line running through the Diesel Generator No. 4, four day fuel oil
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- tank room. This line is a branch from the Unit 2 Nuclear Service Water
Diesels No. 3 and No. 4 rely on this source as their primary heat sink
, with the Unit I source as an automatic backup. The opposite
. configuration exists for DGs No. I and No. 2. The one to two gallon per
i minute leak was temporarily repaired. Code repair will be affected '
i before restart. No adverse effects occurred. ,
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The leak occurred in a non-welded, straight run section of the pipe just
- downstream from a flanged connection. The carbon steel pipe is cement
! lined. The cement lining is intended to prevent corrosive brackish
water from contacting the carbon steel. This material- combir:atibn was
! prevalent in the service water system a: originally constructed, but
- most is being gradually replaced with corrosion resistant copper-nickel
j or stainless steel. The leaking section was replaced in 1985 in
- conjunction with changing the upstream piping to co)per-nickel due to
- underground leaks. The flanged connection became tie boundary between
, the new copper-nickel and existing carbon steel. This necessitated.
. replacing a short section of carbon steel with new carbon steel to
a accommodate the new flange connection.
Almost all leaks in service water piping occur at weld joints, including
1 some in copper-nickel. Since April 1989, 24 service water. leaks due to
! internal erosion / corrosion have been identified. Only three of these,
( including the one described above, have occurred in non-weld areas; but
i these represent three of the total seven leaks in cement lined carbon
. steel. In all cases, leaks in cement lined carbon steel are the result
of water penetrating the cement lining through cracks or seams. ,
l The remaining cement lined carbon steel pipe in safety significant
l applications is either scheduled to be replaced or visually inspected.
- Inspected portions are large diameter pipe sizes that permit entry by
! personnel or remote controlled cameras. No other non-destructive
l- examination methods are routinely included, but in--progress corrosion
i areas are easily identified by the characteristic " rust plume" on the
cement lined internal surface.
No routine internal inspections or non-destructive examinations occur on
i carbon-steel piping that is scheduled for replacement. The current
i schedule, which extends into late 1995, includes all piping downstream
! of the leak described above that supplies the DGs and all Unit 1 DG
- supply piping from its branch connection with the Unit.1 nuclear service
j water header. This includes hundreds of feet of-piping and many weld
j -joints. Of the-seven safety significant portions of cement lined carbon
- steel pipe that developed leaks, four have occurred in these areas of DG
. service water piping.
i Two of these DG service water leaks occurred at 6 X 8 inch reducers near
L the connections to the DG jacket water coolers. These may be more
,
susceptible to erosion / corrosion due to the flow turbulence induced by
I the : mall-to-large diameter change. However, the inspector concludad ,
l that many other susceptible leak locations exist in the DG service water
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supply lines. Most of this piping is too small for internal inspection;
therefore no surveillance is performed to assess the condition of the
piping and hence the failure potential. The majority of this is 6-inch,
non-insulated piping accessible within the DG building and therefore,
could be easily tested by ultrasonic methods.
'
The service water system engineers are aware of the vulnerability to
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leaks in these areas and routinely walkdown accessible portions of this
piping specifically to locate leaks. The inspector concluded that while
- this is prudent, more evaluation may be warranted in consideration of
the large portion of the system not inspected and the high safety
, significance of Failures in this ara.. URI 92-34-02; Service Water
q
Leaks.
Violations and deviations were not identified.
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5. Outage Work Activities (62703)(37828)
DGB & CB Walls
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Designs are issued on 59 of 61 walls that require repair or
modification. The two remaining designs involve DGB wall modifications
for tornado venting. The repair activities are approximately 75 percent
complete. It is anticipated that the remaining designs will be
completed in early November and work will be completed in December.
Engineering design and design changes have caused the majority of delays
- in completing this project.
fWE/SW Booster luni
The 2A and 2C pum) motors have been inspected and refurbished. New pump
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motor baseplates iave been installed. The pumps have been mcdified with
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new pullout pump assemblies and supports have been added to the
discharge piping. Check valve slam tests were performed to verify that
check valve operation will not affect alignment. Extensive vibration
and thermal growth testing / analysis was performed to determine their
effect on alignment. Correct torque values and torquing sequences of
bolts have been determined and incorporated into procedures. The above
activities resulted in reduced vibration levels, lower bearing
temperatures and significant improvements in performance of the pump
motors. Additional work is currently being planned for Unit 1.
Double-D_isc Gate Valy35
Due to concerns noted by the BNP Motor-Operated Valve Task Group in 1988
in19ving the potential for thermal binding and/or bonnet
oveipressurization in certain flex-wedge gate valve applications, the
licensee embarked on a program to replace the valves with a valve type
which would prove to be less susceptible to these phenomena. Plant
modifications were developed to replace 22 flex-wedge gate valves in
both units, 20 of which were in 11RT applications. The applicable plant
systems include HPCI, RCIC, RUCU and Main Steam.
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Over the past several refueling outages,: the valves were replaced with
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Anchor Darling double-disc gate valves. Since the valves have been
- installed, the plant has experienced an unusually high LLRT failure rate
- of these valves. Eight failures have been identified in this outage. !
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Several of the failures have ultimately been discovered to be.the result
- of poor quality and workmanship during the valve manufacturing ~ process.
ACR 892-782 was generated to investigate the root cause of the failures.
! and to look into commonalities in the failures. The inspector will
! follow licensee activities on this item.-
1
1 Reactor Recirculation System Rina Header Supports
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l This work activity is essentially complete except for shielding removal,
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insulation and grating replacement, turnover, and operability testing,
j Maintenance W3/JO Status
!, The current status of the backlog is as follows:
i
- Completed Remaining
,
Pre 4/21/92 Post 4/21 Since 4/21 In Backlog
- . Mnit 1
i Outage 783 -962 858 887
Non-outage 993 3002 2291 1704
hiLZ
. Outage 673 1451 1202 922
Non-Outage 1582- 4319 3772 2129
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l The corrective maintenance backlog was reduced by approximately 200
i items during October. This progress has been very slow. Approxihiately
i
5900 corrective maintenance items remained open at the end of October.
The pre-April' 21 backlog has been. reduced from 4465 to 1673 during the
- outage. The initia1 ' screening of the overall backlog on a system
! priority basis was essentially-completed for 79 systems as of
i October 27. -Management review of the planned work on items to be
! excepted is still ongoing. Revision 0 of the startup schedule was
! completed, but is under further review and refinement. -The united
l schedule contained several unresolved issues and assumptions that must
be resolved or clarified to improve the schedule accuracy. -The licensee
- has committed to providing. a copy of the Integrated Startup Schedule for
! Unit 2 to NRC by November 30, 1992.
!' Structural Steel
l- A summary and status of this item is contained in Inspection Report
325,324/92-27.
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Instrument Racks
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Work on rack replacement on Unit _2 is approx'W.ely 85 percent complete.
Three of three replacement racks are installed. All designs on Unit 2
are completed. This project is behind schedule with an_ anticipated
.
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completion in late January. Work on Unit 1.is approximately 45 percent
com)lete. The estimated completion date of January may be extended as
wor ( activities and focus are redirected to completing viork and
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restarting Unit 2.
Operator Work-Arounds
Add'd emphasis and focus by the licensee has improved progress on this
item. There were 66 o)en operator work-arounds on Unit 1 and 117 on
. Unit 2 at the end of tie reporting period. The licensee now tracks
these items on a daily basis and provides a report on additions, _
-completions and items not completed on schedule in the daily p.lan of the
-
day meeting. Accountability is assigned _for each item. This added
emphasis . appeared to be improving the completion rate of open items in
this area.
Plant Material Condition
Work continues in this area with emphasis in the condenser pits and
intake structure areas. Severely corroded ccmponents are being replaced
and painting / preservation work occurred on the SW/CW intake areas and-
crane, the CB crane, condenser pits, reactor feedpumps, turbine building
" breezeways" and other plant areas. The licensee has developed a plan
and schedule for these activities. A significant amount of work remains
around the SW/CW intake screens.
Turbine 2A low PreswIg Rotor-
The ten year Unit 2 low pressure A turbine ultrasonic inspection
recommended by General Electric was completed. Several indications were
located during the process. Many of the crack indications found in the
1982 inspection have grown in size. Several new crack indications were
discoverad in the dovetails, keyways and hubs.
The recommended fix is to first remove the buckets around the notch on
the fourth stage, turbine end. Depending on the severity of.the cracks
found, options are_ available. One option is to remove the buckets at
the notch and replace the notch buckets with titanium blocks, keyed in
place. Blades. at 180 degrees would be removed. to counterbalance. If 1
the cracks are deep and extensive enough on the wheel, the' buckets or
the entire wheel will be removed and replaced with pressure plate. The-
turbine could then be run, but at reduced efficiency. As the cracks are
being ground out, they will be magnetic particle inspected to check for
crack removal. The keyway cracks will not prevent the unit-from '
starting up but several recommendations _on inspection intervals have
been provided by GE. %s licensee is currently-studying the available l
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options which may include rotor replacement. The inspector will follow .
actions taken on this item.
6. Licensee Celf-Assessment (40500)
l
- The inspectors attended selected Plant Nuclear Safety Committee meetings
L conducted during the period. A significant number of ' hose meetings
involved system review of planned and exempted systems ark backlogs.
.
The inspectors verified that the meetings were conducted in accordance
- with Technical Specification requirements regarding quorum membership,
.; review process, frequency and personnel qualifications. Meeting minutes
! were reviewed to confirm that decisions and recommendations were
i reflected in the minutes and followup of corrective actions was
1 completed. There were no ca.icerns identified relative to the PNSC
'
meetings attended. The ;esolution of safety issues presented during
these meetings was considered to be acceptable,
i In October, the Site Project Assessment Group of NAD loaned the manager
4
of the Management Assessment Section to Maintenance for a 90 day period
4 to assist in the training of new maintenance planners and implementation
of maintenance planning upgrades. To supplement.the loss, an engineer
from the corporate assessment section was sent to assume his duties
during this period. On October.23, the inspector was informed by the
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rianager of the Site Project Assessment that he was also -loaning two of
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the three Engineering / Technical Support Assessors to the Site Technical
Support Section to assist the Technical Support Managers from Nuclear
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and BOP areas in managing selected projects. This loan was to be for a
period of three weeks starting on October 26. The reason given for
these reassignments was that the managers of the Technical Support area
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were very involved in the review and prioritization of backlogs and in
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the development of the site restart and three year business plans, and
needed supervisory assistance. When informed of this decision, the
I inspector expressed a concern that this could result in a loss of
j independence from line functions by the assessors. The inspector asked
'
what measures had been established to prevent the assessors from later
evaluating activities they were involved in. No measures had been
. established, but after being questioned, the licensee took steps to
address this concern. After lengthy discussions with the licensee, the
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inspector was convinced that these personnel were needed to assist the
i Technical Support and Maintenance areas for a short duration project.
- During these conversations the inspector received assurances from the
l Manager of NAD that his organization would not be used in the future as
j a source of personnel for line organizations.
'
7. Organizational Changes
On October 6,1992, Mr. J. W. Spencer resigned as Plant General Manager.
_
4 The licensee implemented a unitized organizational structure with Mr. R.
. E. Morgan and Mr. J. M. Brown named as temporary Unit .1 and Unit 2
i
Managers, respectively. Mr. J. G. Titrington and Mr. K. J. Ahern were
named as Manager of Operations and Mr. D. E. Moore and Mr. M. E. Jackson
- - were named as Manager of Maintenance for Units 1 and 2, respectively.
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! The E&RC organization will now report to Mr. G. Warriner, Manager - '
! Contract and Ad.Wstration Section. On October 12. Mr. J. P. Cowan was
'
named Manager of rechnical and Regulatory Support reporting to Mr, R. B.
- Richey, Site Vice President. Mr. -Cowan is on loan from INPO to assist
-
in plant recovery operations. Mr. E. E. Willett from the Harris -)lant
was named Manager - Planning and Scheduling, reporting to Mr.- Ric.acy.
l This organization combines OM&M, Planning _and Scheduling, Maintenance
Planning and SWFCG. OM&M will continue to manage outages and implement ,
- modifications. The licensee stated that some of the above positions-are
j being filled on a temporary basis and additional changes may occur.
l 8. Quality Control (QC)
1
l Quality Control identified numerous welding deficiencies during the -
d
outage. These deficiencies included welders working to verbal
i instructions, inadequate welding controls, improper techniques and
i inadequate control of welding rod material. These findings were
3
documented in several QC assessment reports and indicated significant
i weaknesses with the site welding program.
2
The inspector discussed his concerns in this area with the Corporate
Manager of Quality Control. The QC manager decided to_obtain the
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services of an outside consultant to assess the site welding pr.ogram,
1
The assessment identified weaknesses in the areas of welder testing and
i training, procedures and control: of weld rod material. Many of the
-
findings were similar to those-previously' identified by QC. The
, assessment concluded that the large number of deficiencies indicated a
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weak welding program. An ACR was written to determine the rov cause
and. corrective actions needed. -The NRC ins)ector noted that this
i assessment focused on the overall program, aut did not contain extsnsive
j field observations.
<
j The inspector reviewed the licensee's corrective actions for the
L findings to date. The corrective actions were found to address
[ individual findings, but did not appear to address overall welding
i program weaknesses.
- -
- QC has in the past been successful in effecting corrective actions on
i- individual problems as they are identified; however, it appears that QC
- does not have the authority to require progran,matic changes. In
addition, CP&L Quality Verification Procedure,-QVS-202, Support of Self-
i Assessment and Field Surveillance Programs, Revision 0, limits the
'
. activities of the QC organization. It-allows QC to stop work on
individual jobs if a hold point exists. The above procedure requires
that QC pass their observations and finding:. to-the line organization
who will take corrective action as they deem _necessary. QC does not
l have an input in determining if corrective action is appropriate cr
adequate to correct the QC 1dentified deficiency. The authority to
assess programs is the responsibility of NAD. KAD has the'expertisc to
assess this area,.but has not performed any assessments of the welding
2
program. When questioned on this matter by the NRC inspector, the
,
Manager of NAD and the Project Assessment Manager stated-that they did ..
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not look into this item as yet. The inspector will continue to follow
actions teken by the licensee to address the welding program problems.
URI 92-34-03, Welding Program.
9. Exit Interview (30703)
The inspection scope and findings were summarized or, November 6,1992,
with those persons indicated in paragraph 1. The inspectors described
the areas inspected and discussed in detail the inspection findings
listed beiow and in the summary. Dissenting comments were not received
from the licensee. Proprietary information is not contained in this
report.
ILVAlhimjaC OfjLqrJAt_ ion /RefertpstParaarRh
_
325,324/92-34-01 Violation - Watchstanding With An
inactive License (paragraph 4).
325,324/92-34-02 URI - Service Water Leaks
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3?5,324/92-34-03 URI - Welding Program
10. Acronyms and initialisms
ACR Adverse Condition Report
BNP Brunswick Nuclear Project
BOP Balance of Plant
BSEP Brunswick Steam Electric Plant
CB Control Building
C0 Control Operator
CP&L Carolina Power & Light Company
DC Diesel Generator
DGb Diesel Generator Building
E&RC Environment'.1 & Radiation Control
HP Health Physics
HPCI High Pressure Coolant injection
J LLRT Local Leak Rate Test
MOP E tor Operated Potentiometer
MST Maintenance Surveillance Test
NAD Nuclear Assessment Department
NDE Non-Destructive Examination
NRC Nuclear Regulatory Commission
OM&M Outage Management & Modification
PA Protected Area
PNSC Plant Nalear Safety Committee
QC Quality Control
RC Run Control
RCIC Reactor Core Isolatien Cooling
ROT Reactor Operator Trainee
4
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i 500 Senior Control Operator l
- SSTR Stop/ start Timing Relay
SW/CW Service Water / Cooling Water
, SWFCG Site Work Force Control Group
( WR/JO Work Request / Job Order ,
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