ML20074A654

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Monthly Operating Rept for Apr 1983
ML20074A654
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 05/02/1983
From: Ruiter G
WISCONSIN PUBLIC SERVICE CORP.
To:
Shared Package
ML20074A653 List:
References
NUDOCS 8305130251
Download: ML20074A654 (5)


Text

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t DOCKET 50-305 KEW AUNEE NUCLEAR POWER PLA NT

SUMMARY

OF OPERATING EXPERIENCE April, 1983 CPERATIONS: The Cycle VIII-IX Refueling Cutage continued through April.

The core reload was completed on April 22.

MAINTENANCE: Refueling outage continued during the month.

Surveillance testing, as required by Tech. Spec.,

is in progress.

Ecplaced a faulty amplifier in Tavg summing circuit.

Replaced a de fective relay in Containment Spray control circuit.

Replaced de f ectiv e resistors in Engineered Safeguards test lamp circuit.

Replaced a defective relay in Reactor Control &

Protection circuit.

Ecplaced and/or repaired several defective valves in RCS.

Repaired several limitorque valve operators.

Installed equipment and rerouted cable for Appendix E modifications.

Inspected and replaced, as required, seals on both ECPs.

Installed Charging Pump suction stabilizers.

8305130251 830510 PDR ADOCK 05000305 R PDR i

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PAGE 2 3

Eebuilt a EUR Pump.

Repaired several defective breakers.

F AV ERAGE DAILY UNI T POW ER LEVEL DOCEET NO- 50-305 UNIT- KEWAUNEE COEPLETED BY- G. H. RUITER TELEPHONE- 414-388-2560 X225 REPORT HCNTH APEIL, 1983 AVERAGE DAILY DAY POWER LEVEL (MW E-N ET) 1 0 2 0 3 0 4 0 5 0 6 0 7 0 8 0 9 0 10 0 11 0 12 0 13 0 14 0 15 0 16 0 17 0 18 0 19 0 20 0 21 0 22 0 23 0 24 0 25 0 .

26 0 27 0 28 0 7

29 0

30 0 s

.) .

U N IT SHUTD0W N S A ND POW EB EEDUCTIONS

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DOCKET NO: 50-305 UNIT N AME: Kewaunce DATE: flay 2, 1983 COMPLETED Br: G. H. Ruiter  %>

T ELEP110N E: 414-388-2560 x 225

- C BEPORT MONTil - APEIL, 1983 I

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i NO. I DATE iTTPE lDURATIONiREASONl5ETHOD} LEE NUMBER ]SYS l COMPONENT} COMMENTS l I I t  :  : I  : 1  :  : 4 ,

~ 1 1 I i 1 1 1 1 1 I I e

l 1 14/ 1/831 S I 719.0 i C i 1 i N/A I ZZ l 22222: I 1. Continued Cycle VIII-II refueling outage. I  ;

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TYPE EE AS O N ftETHOD SYSTEM S COMPONENT CODES l F: Forced A-Equipment Failure (Explain) 1-Sanual Fron*NUREG-0161 l* S: Scheduled B-saintenance or Test 2-Manual Scras g C-Befueling 3-Automatic Scram l

D-Bequlatory Bestriction 4-Continuations i E-Operator Training & License Ezanination 5-Load Reductions  !

F- Ad ministra tive 9-Other C 1

. G-operational Error (Explain!

l . b-Other (Explaint g l

l l

l a

  • OPERATI NG D ATA REPO2T ^

e DOCKET NO- 50-305 - l COMPLETED BY- G. H. RUITER w

OPER ATI NG S T A T 't S TELEPHONE- 414-388-2560 1225 1 UNIT NAME KEWAUNEE **********************************************

e e t) 2 REPORTING PERIOD APRIL, 1983

  • NOTES
  • 3 LICENSED THEEM AL POWER (MWT) 1650
  • Schedaled refueling outage continued * (
  • through this entire reporting period.
  • 4 N AMEPLATE R ATING (GROSS MWE) 560 *
  • j 5 DESIGN ELECTRICAL RATING (NET MWE) 535 *
  • 6 MAXIMUM DEPENDABLE CAPACITY (GROSS MW E) 542 * '

, 7 MAKIM'JM DEPENDABLE CAPACITY (NET MWE) 514 ***?******************************************

d IF CHANG ES CCCUB IN CAPACITY RATINGS (ITEMS NUMDER 3 THROUGH 7) SINCE LAST REPOET, GIVE REASONS

, None

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, 9 POWER LEVEL To kHICH RESTRICTED, IF ANY (NET MWE) None 10 REASCNS FOR EESTRICTIONS, IF ANY a

J THIS MONTH YR-TC-DATE CUMULATIVE g

11 HOURS IN REPORIING PERIOD 719 2879 77784 12 NUMBER OF HOURS REACTOR WAS CRITICAL 0.0 1838.7 65590.4 b

, 13 REACTOR RESERVE SHUTDOWN HOURS 0.0 0. 0 2330.5 14 HOURS GENERATOR ON-LINE O.0 1822.9 64299.5 15 ULIT RESERVE SUIDOWN HOURS 0. 0 0. 0 10.0 l

, 16 GROSS THEEMAL EbERGY GENERATED (MWH) 0 2970698 100070699 J

17 Gl.0SS ELECTRICAL ENERGY GENERATED ( M W H) 0 968100 32935700 18 NET ELECTRICAL ENERGY GENERATED (MWH) 0 924039 31349147 /

19 UNIT SERVICE FACTOR 0.0 63.3 82.7 a

20 UNIT AVAILABILITY FACTOR 0.0 63.3 82.7

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21 UNIT CAPACITY FACTOR (USING MDC NET) 0.0 62.4 77.3 >

, 22 UNIT C AP ACITY F ACTOR (USING DER NET) 0.0 60.0 75.3 g,

23 UNIT FORCED OUT AGE R ATE 0.0 0. 0 4.2 24 SHUIDOWNS SCHEDULED OVER NEIT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)

None 1

25 IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP - May 10, 1983 II

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