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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARBW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155C2601998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Braidwood Generating Station,Units 1 & 2 ML20151X6671998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Braidwood Generating Station,Units 1 & 2.With ML20237A1091998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Braidwood Generating Station,Unit 1 & 2 ML20236N7001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Braidwood Generating Station,Units 1 & 2 ML20249A5451998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Braidwood Generating Station Units 1 & 2 ML20247L7591998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Braidwood Generating Station,Units 1 & 2 ML20216C6621998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Braidwood Generating Station,Units 1 & 2 ML20217Q1951998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Braidwood Generating Station,Units 1 & 2 ML20202C6431998-01-31031 January 1998 Monthly Operating Repts for Jan 1998 for Braidwood Generating Station,Units 1 & 2 ML20198J7091997-12-31031 December 1997 Monthly Operating Repts for Dec 1997 for Braidwood Generating Station,Units 1 & 2 ML20202H6231997-11-30030 November 1997 Monthly Operating Repts for Nov 1997 for Braidwood Generating Station,Units 1 & 2 ML20199D0781997-10-31031 October 1997 Monthly Operating Repts for Oct 1997 for Braidwood Generating Station,Units 1 & 2 ML20217G1571997-09-30030 September 1997 Monthly Operating Repts for Sept 1997 for Braidwood Generating Station,Units 1 & 2,covering Period 970901-970930 ML20216C2931997-08-31031 August 1997 Monthly Operating Repts for Aug 1997 for Braidwood Generating Station,Units 1 & 2 ML20198F0321997-07-31031 July 1997 Monthly Operating Repts for Jul 1997 for Braidwood Generating Station,Units 1 & 2 ML20140C6271997-05-31031 May 1997 Monthly Operating Repts for May 1997 for Braidwood Generating Station,Units 1 & 2 ML20148B2411997-04-30030 April 1997 Monthly Operating Repts for Apr 1997 for Braidwood Nuclear Power Station,Units 1 & 2 ML20137N9971997-03-31031 March 1997 Monthly Operating Repts for Mar 1997 for Braidwood Nuclear Power Station,Units 1 & 2 ML20136B4371997-02-28028 February 1997 Monthly Operating Repts for Feb 1997 for Braidwood Nuclear Power Station,Units 1 & 2 ML20138J9891997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Braidwood Nuclear Power Station,Units 1 & 2 ML20133E1641996-12-31031 December 1996 Monthly Operating Repts for Dec 1996 for Braidwood Nuclear Power Station,Unit 1 & 2 ML20132B9511996-11-30030 November 1996 Monthly Operating Repts for Nov 1996 for Braidwood Nuclear Power Station,Unit 1 & 2 ML20134G8341996-10-31031 October 1996 Monthly Operating Repts for Oct 1996 for Braidwood Nuclear Power Station,Unit 1 & 2 ML20128K2631996-09-30030 September 1996 Monthly Operating Repts for Sept 1996 for Braidwood Nuclear Power Station Units 1 & 2 ML20117K7451996-08-31031 August 1996 Monthly Operating Repts for Aug 1996 for Braidwood Nuclear Power Station Unit 1 & 2 ML20116M6171996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Bs Nuclear Power Station,Units 1 & 2 ML20115B0731996-06-30030 June 1996 Monthly Operating Repts for June 1996 for Bs ML20117K4761996-05-31031 May 1996 Monthly Operating Repts for May 1996 for Braidwood Nuclear Power Station Units 1 & 2 ML20117D6991996-04-30030 April 1996 Monthly Operating Repts for Apr 1995 for Braidwood Nuclear Power Station Units 1 & 2 ML20101N8121996-03-31031 March 1996 Monthly Operating Repts for Mar 1996 for Braidwood Nuclear Power Station,Units 1 & 2 ML20100Q7161996-02-29029 February 1996 Monthly Operating Repts for Feb 1996 for Braidwood Units 1 & 2 ML20100Q7051996-01-31031 January 1996 Revised Monthly Operating Rept for Jan 1996 for Braidwood Unit 1 ML20097D4171996-01-31031 January 1996 Monthly Operating Repts for Jan 1996 for Braidwood Nuclear Power Station ML20100Q7021995-12-31031 December 1995 Revised Monthly Operating Rept for Dec 1995 for Braidwood Unit 1 ML20096E6191995-12-31031 December 1995 Monthly Operating Repts for Dec 1995 for Braidwood Nuclear Power Station Units 1 & 2 ML20095F0481995-11-30030 November 1995 Monthly Operating Repts for Nov 1995 for Braidwood Nuclear Generating Station ML20094H1031995-10-31031 October 1995 Monthly Operating Repts for Oct 1995 for Braidwood Nuclear Generating Station 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & ML20217N3711999-10-13013 October 1999 Safety Evaluation Supporting Amends 111,111,104 & 104 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety ML20212A8261999-09-0808 September 1999 Safety Evaluation Supporting Amends 103 & 103 to Licenses NPF-72 & NPF-77,respectively BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML17191B4101999-07-27027 July 1999 Safety Evaluation Accepting Alternative to Licenses NPF-72, NPF-77,NPF-37,NPF-66,NPF-19,NPF-25,NPF-11,NPF-18,DPR-29 & DPR-30,respectively ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With 05000456/LER-1998-004-02, :on 980903,MSSVs Were Tested in Excess of Required Setpoint.Caused by Suspected Metallic Bonding. Evaluated Disc Removed from One of Valves & Reviewed Historical Data to Assess Cause of Test Failures1999-06-16016 June 1999
- on 980903,MSSVs Were Tested in Excess of Required Setpoint.Caused by Suspected Metallic Bonding. Evaluated Disc Removed from One of Valves & Reviewed Historical Data to Assess Cause of Test Failures
05000457/LER-1999-003-03, :on 990519,spurious Spiking of Indication on Intermediate Range Neutron Flux Channel N36 Resulted in Unit 2 Reactor Trip.Cause Unknown.Personnel Stabilized Reactor in Shutdown Condition Using Appropriate Emergency Procedures1999-06-15015 June 1999
- on 990519,spurious Spiking of Indication on Intermediate Range Neutron Flux Channel N36 Resulted in Unit 2 Reactor Trip.Cause Unknown.Personnel Stabilized Reactor in Shutdown Condition Using Appropriate Emergency Procedures
05000456/LER-1999-001-06, :on 990516,both Trains of LPSI Were Declared Inoperable.Caused by Leakage of SI Accumulator Water.Design Changes Were Implemented to Install Local High Point Vents in Common Portion of Rh Sys Piping to 1B & 1C RCS1999-06-15015 June 1999
- on 990516,both Trains of LPSI Were Declared Inoperable.Caused by Leakage of SI Accumulator Water.Design Changes Were Implemented to Install Local High Point Vents in Common Portion of Rh Sys Piping to 1B & 1C RCS
ML20207E8891999-06-0202 June 1999 Safety Evaluation Supporting Amends 109,109,102 & 102 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station 05000457/LER-1999-002-02, :on 990424,ESFA Was Noted.Caused by High Water Level in 2C Sg.Sg Blowdown Sys Was Placed in Operation & SG Water Level Was Returned to Normal Operating Range1999-05-21021 May 1999
- on 990424,ESFA Was Noted.Caused by High Water Level in 2C Sg.Sg Blowdown Sys Was Placed in Operation & SG Water Level Was Returned to Normal Operating Range
ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations 05000457/LER-1999-001-03, :on 990414,reactor Tripped Due to Main Generator & Turbine Trip.Caused by Spurious Generator Stator Ground relay,GIX-104 Relay,Actuation.Voltage Regulator Parts Replacement Program Was Developed.With1999-05-14014 May 1999
- on 990414,reactor Tripped Due to Main Generator & Turbine Trip.Caused by Spurious Generator Stator Ground relay,GIX-104 Relay,Actuation.Voltage Regulator Parts Replacement Program Was Developed.With
ML20206G6031999-05-0303 May 1999 Safety Evaluation Supporting Amends 108,108,101 & 101 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With ML20206B5531999-04-23023 April 1999 Safety Evaluation Supporting Amends 107,107,100 & 100 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively BW990016, Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205D6641999-03-26026 March 1999 Safety Evaluation Supporting Amends 99 & 99 to Licenses NPF-72 & NPF-77,respectively ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20196A0721999-03-16016 March 1999 Cycle 8 COLR in ITS Format & W(Z) Function ML20207J4371999-03-0808 March 1999 ISI Outage Rept for A1R07 ML20204H9941999-03-0303 March 1999 Non-proprietary Rev 4 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations BW990010, Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Braidwood Generating Station,Units 1 & 2.With ML20206U9011999-02-15015 February 1999 COLR for Braidwood Unit 2 Cycle 7. Page 1 0f 13 of Incoming Submittal Was Not Included BW990004, Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Braidwood Generating Station,Units 1 & 2.With ML20205M7061998-12-31031 December 1998 Unicom Corp 1998 Summary Annual Rept. with BW990001, Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Braidwood Generating Station,Units 1 & 2.With ML20206B4001998-12-31031 December 1998 Annual & 30-Day Rept of ECCS Evaluation Model Changes & Errors for Byron & Braidwood Stations ML20206U9081998-12-17017 December 1998 Cycle 8 COLR in ITS Format & W(Z) Function 05000456/LER-1998-006-05, :on 981117,failure to Test Contacts as Required by TS Identified.Caused by Inadequate Surveillance Procedure Development Prior to Initial Plant start-up.Appropriate Limiting Condition Entered1998-12-16016 December 1998
- on 981117,failure to Test Contacts as Required by TS Identified.Caused by Inadequate Surveillance Procedure Development Prior to Initial Plant start-up.Appropriate Limiting Condition Entered
05000456/LER-1998-007-06, :on 981118,non-conservative Error Detected in Vendor Analysis Code Resulted in Bdps Being Determined Inoperable.Caused by Personnel Error.C/As Will Be Performed as Necessary Under Westinghouse Corrective Action Program1998-12-16016 December 1998
- on 981118,non-conservative Error Detected in Vendor Analysis Code Resulted in Bdps Being Determined Inoperable.Caused by Personnel Error.C/As Will Be Performed as Necessary Under Westinghouse Corrective Action Program
BW980076, Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Braidwood Generating Station,Units 1 & 2.With ML20196A4191998-11-19019 November 1998 Safety Evaluation Accepting QA TR CE-1-A,Rev 66 Re Changes in Independent & Onsite Review Organization by Creating NSRB 05000456/LER-1998-005-08, :on 981004,noted That make-up Fan 0VC03CA Failed to Start.Caused by Apparent MCC Motor Starter Malfunction.Motor Starter Was Replaced on 9810151998-11-0303 November 1998
- on 981004,noted That make-up Fan 0VC03CA Failed to Start.Caused by Apparent MCC Motor Starter Malfunction.Motor Starter Was Replaced on 981015
ML20195D3561998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Braidwood Generating Station,Units 1 & 2.With ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20154N1641998-10-15015 October 1998 Safety Evaluation Supporting Amends 105,105,97 & 97 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively 1999-09-08
[Table view] |
Text
_ _ _ _ . . _ , .. , . . _ ._ _ --- - -
.,e
. Commonwcalth Edinoa Company
~
.)
, .' 1 .* 'liraklwmni Generating Station Jl
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.I :
Route C1,llox Mi
) 15taceville, IL 60107-9619 l
-TelH15-15&2801 1
- l. June 7,1995 1
T BW/95-0067 l i :
c I l 1 1
} Document Control Desk _. .
i U.S. Nuclear Regulatory Commission j Washington, D.C. 20555 l i'.
- j. Gentlemen:
?
3 Enclosed for your information is the Monthly Performance Report covering Braidwood 1
{.
Nuclear Generating Station for the period May 1 through May 31,1995.
j
- Yours truly,
.i I
j 4.2 .'hawy T. J. Tulon
\
Station Manager L Braidwood Nuclear Station -
1
- TJT/PS/dia
[ o:\correspuesteno\bwdletrs. doc l
Attachments i
o j_ cc- J. B. Martin, U.S.N.R.C., Region ill R. R. Assa, U.S.N.R.C. 3 l.D.N.S. !
l U.S.N.R.C. Resident inspector, Braidwood U INPO Records Center 4
D. L. Farrar, Nuclear Regional Service Mgr. .
- j. D. M.' Saccomando, Nuclear Ucensing Admin.' j j D. R. Eggett, Nuclear Engineering Dept. j K. Kaup, Site Vice President, Braidwood j
. NFS, PWR Plant Support .
- P. L. Habel, Unit 1 Operating Engineer.
j J. P. Kuchenbecker, Unit 2 Operating Engineer- ]
- .. l.D.N.S. Resident inspector, Braidwood j
'J. M. Bunecicky, Westinghouse -
- j. D. R. Seavers, A.N.I. 1
!- 9506200036 950531 ?
j- PDR ADOCK 05000456 R PDR A l'nicom Company -
l l
l BRAIDWOOD NUCLEAR POWER STATION I l
l UNIT 1 AND UNIT 2 1
l l MONTHLY PERFORMANCE REPORT Comed i l
1 l
NRC DOCKET NO. 050456, LICENSE NO. NPF - 72 NRC DOCKET NO. 050-457, LICENSE NO. NPT - 77
)
l l l l
l I
I
s
{;.- ,,
i
' A. OPERATING DATA REPORT . !
Docket No: 50-456 i Unit: Braidwood 1 1 i Date: 06/06/1995 ,
[ Completed by: Paul Stanczak j Telephone: 815-458-2801, .
OPERATING STATUS 1
- s. 1) Reporting Period: May 1995 Gross Hours: 144 1 1.
a ~, _
- 2) Currently Authorized Power Level (MWt): 2111 !
3 Design Electrical Rating (MWe-gross): 111% ]
Design Electrical Rating (MWe-net): 112Q . {
}._ Max Dependable Capacity (MWe-gross): 11Z1 l l Max Dependable Capacity (MWe-net): 11RQ .I I
I
- 3) Powerlevel to which restricted (if Any): M9ng
' 4) Reasons for restrictions (if Any): N9 fit j This Mo. Yr to Date Cumulative
- 5) Report Period Hours: 744.0 .3,623.0 59,936.0 l-
- 6) Hours Reactor Critical: 744.0 - 2,925.0 ' 47,523.8-
- 7) RX Reserve Shutdown Hours: .0. .0 .0
- 8) Hours Generator on Line: 744.0 2,882.5 46,848.3
- 9) . Unit Reserve Shutdown Hours: .0 .0 .0
- 10) Gross Thermal Energy (MWHt): 2,509,594.1 9,426,404.3 149,375,296.1
- 11) Gross Elect. Energy (MWH): 872,049.0 3,272,655.0 49,776,477.0
- 12) Net Elect. Energy (MWH): 838,888.0 3,142,692.0 47,675,512.0
- 13) Reactor Service Factor: 100.0 80.7 79.3 1
- 14) Reactor Availability Factor: 100.0 80.7 79.3. !I
- 15) Unit Service Factor: 100.0 79.6 78.2
- 16) Unit Availability Factor- 100.0 79.6 78.2
- 17) Unit Capacity Factor (MDC NET): 100.7 77.4 71.0 )
- 18) Unit Capacity Factor (DER NET): 100.7 77.4 71.0 I
- 19) Unit Forced Outage Rate: 0.0 6.0 8.3
- 20) Unit Forced Outage Hours: 0.0 184.0 4214.5
- 21) Shutdown Schedule Over Next 6 Months: N/A
- 22) If Shutdown at End of Reporting Period, Estimated Date of Startup:
l . .
1
! B. AVERAGE DAILY UNIT NET POWER LEVEL LOG Docket No: 50-456 Unit: Braidwood 1 Date: 06/06/1995 Completed by: Paul Stanczak Telephone: 815-458-2801 MONTH: May 1995 Qay MWe-net Qay MWe-net .
l
- 1) 1118 16) 1128 *
, 2) 1118 17) 1137 *
- 3) 1121
- 4) 1120 19) 1139 *-
- 5) 1121
- l 6) 1120. 21)- 1107 l 7) 1131
- 8) 113-5
- 9) 1121
- 10) 1127
- 11) 1125
- 13) 1114 28) 1139 *
- 14) 1037 29) 1140*
- 15) 1132
- 31) 1135 *
- Due to condenser efficiency i
l l
t C. - UNIT SHUTDOWNS / REDUCTIONS Docket No.: 50-456 l Unit: Braidwood 1 Date: 06106/95 Completed by: Paul Stanc;:ak Telephone: 815-458-2801 REPORT PERIOD: May 1995 LER Cause & Corrective Action h Date ' hee _ Hours Reason Method Number System Component to Prevent Recurrence N/A
SUMMARY
. Unit i entered the month of May 1995 with 100% capability.
The Unit operated routinely for the remainder of the month.
TYPE REASON METHOD SYSTEM & COMPONENT F Forced A -Equipment Failure Maint or Test 1 - Manual D - Scheduled B - Maint or Test 2 - Manual Scram Exhibit F & Instructions for C - Refueling 3 - Auto Scram Preparation of Data Entry Sheet D -Regulatory Restriction 4 - Continued Licensee Event Repost (LER) File E - Operator Training & Licensee Examination 5 -Reduced Load (NUREG-0161).
F - Administration G - Operator Error H - Other e
Y
- ~ . m ,
~ y
l D. SAFETY / RELIEF VALVE OPERATIONS l
Docket No.: 50 - 456 _
Unit: Braidwood 1 Date: 06/06/95 Completed by: Tom Cole Telephone: 815-458-2803 Valves No. & Type Plant Date Actuated Actuation Condition Description of Event None i
t 5
1 ee 9
k e
,. . - - ~ - - . ._. . - _ _ _ _ _ - _ _ _ _ _,
A. OPERATING DATA REPORT Docket No: 50 457 !
Unit: Braidwood 2 l
- Date .06/06/1995; )
Completed by: Paul Stanczak Telephone: 815-458 2801 j
OPERATING STATUS -
- 1) Reporting Period: May 1995 Gross Hours': Z_44 i
- 2) . Currently Authorized Power Level (MWt): M11 Design Electrical Rating (MWe-gross): .1.1Z1 I Design Electrical Rating (MWe-net): '1129.
Max Dependable Capacity (MWe-gross): 11ZE .
7 Max Dependable Capacity (MWe-net): . j.12Q ,
1
- 3) Power level to which restricted (if Any): N9nt 7,-
I
- 4) Reasons for restriction.a (if Any): N9.D1 I This Mo. Yr to Date Cumulative
- 5) ' Report Period Hours: 744.0 - 3,623.0 .58,018.0
- 6) Hours Reactor Critical: 598.5 3,452.0 48,284.4
- 7) RX Reserve Shutdown Hours: .0 .0
.0
)
- 8) Hours Generator on Line: 593.5 3,446.8 . 47,889.1 i
- 9) Unit Reserve Shutdown Hours: '0
. .0 .0
- 10) Gross Thermal Energy (MWHt): 1,941,114.8 11,523,776.9, .150,491,054.4
.11) Gross Elect. Energy (MWH): 662,048.0 3,993,766.0 50,013,555.0-
.12) Net Elect. Energy (MWH): 635,751.0 ~ 3,851,261.0 47,953,981.0 j
- 13) Reactor Service Factor: 80.4 95.3 ~ 83.2
- 14) Reactor Availability Factor: 80.4 95.3 ~ 83.2 l' 15) Unit Service Factor: -79.8 95.1. 82.5
- 16) Unit Availability Factor: 79.8 95.1 82.5
- 17) Unit Capacity Factor (MDC NET): 76.3- 94.9 73.8
- 18) Unit Capacity Factor (DER NET): ' 76.3 94.9 73.8
- 19) Unit Forced Outage Rate: 20.2 4.9 5.8
- 20) Unit Forced Outage Hours: 150.5. 176.3 - 2947.6 l 21) Shutdown Schedule Over Next 6 Months: N/A k
l 22) If Shutdown at end of Reporting Period, i
Estimated Date of Startup:
B. AVERAGE DAILY UNIT NET POWER LEVEL LOG ;
Docket No: 50 - 457 Unit: Braklwood 2 Date: 06/06/1995 Completed by: Paul Stanczak Telephone: 815-458-2801 MONTH: May 1995 l
1 Ray MWe-net Ray Mwe-net
- 1) -15 16) 1125 * ,
- 2) -15 17) 1124 *
- 3) -15 18) 1126 *
- 4) -15 19) 1126 * )
- 5) -15 20) 1126 *
- 6) -15 21) 1127 *
- 7) 137 22) 1079
- 8) 700 23) 1124 *
- 9) 1124
- 10) 1116 25) '1124 *
- 11) 1122
- 12) 1124
- 13) 1126
- 14) 1127
- 15) 1124
- 31) 1101 l
- Due to condenser efficiency l
1 C. UNIT SHUTDOWNS / REDUCTIONS ,
Docket No.: 50 -457
. Unit: Braidwood 2 Date: 06/06/95 Completed by: Paul Stanczak Telephone: 815-458-2801 >
REPORT PERIOD: May 1995 ;
LER Cause & Corrective Action ,
. No2 Date Type Hours Reason . Method Number System Component to Prevent Recurrence i
28 950429 F 150.5 A 4 457-200-94-00900. RC ~ Valve Unit was forced to shutdown due to ;
a leak in valve packing on valve l 2RC8003C, Repairwas completed ,
and the unit was placed back on line.
i 1
F
SUMMARY
Unit 2 entered the month of May 1995 in a maintenance outage, following a unit shut down on 4-29-95. The Unit was placed on line 5-7-95 and operated routinely for the remainder of the month.
TYPE REASON . METHOD SYSTEM & COMPONENT F.- Forced ' A - Equipment Failure Maint or Test - 1 - Manual t S - Scheduled B - Maint or Test 2 - Manual Scram Exhibit F & Instructions for C - RefuelinD 3 - Auto Scram ' Preparation of Data Entry Sheet .
D - Regulatory Restriction 4 - Continued Licensee Event Report (LER) File E - Operator Training & Licensee Examination 5 - Reduced Load (NUREG-0161).
- F - Administration G - Operator Error
. H. - Other '
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D. SAFETY / RELIEF VALVE CPERATIONS Docket No.: 50 - 457 Unit: Braidwood 2 Date: 06/06/96 Completed by: Tom Cole '-
Telephone: 815-458-2801 Vanves No. & Type Plant Date Actuated - Actuation Condition Description of Event None i
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