ML021130086

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IR 05000361/2001-014, IR 05000362/2001-014: 12/30/2001-03/23/2002; Southern California Edison; San Onofre Nuclear Generating Station, Units 2 & 3; Integrated Resident and Regional Report; Operability Evaluations; Event Followup
ML021130086
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 04/22/2002
From: Clay Johnson
NRC/RGN-IV/DRP/RPB-C
To: Ray H
Southern California Edison Co
References
IR-01-014
Download: ML021130086 (25)


See also: IR 05000361/2001014

Text

April 22, 2002

Harold B. Ray, Executive Vice President

Southern California Edison Co.

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, California 92674-0128

SUBJECT: NRC INTEGRATED INSPECTION REPORT 50-361/01-14; 50-362/01-14

Dear Mr. Ray:

On March 23, 2002, the NRC completed an inspection at your San Onofre Nuclear Generating

Station, Units 2 and 3, facility. The enclosed report documents the inspection findings which

were discussed on January 4, 11, and 18 and March 25, 2002, with Mr. R. Krieger,

Mr. D. Nunn, and other members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Within these areas, the inspection consisted of selected examination of procedures and

representative records, observations of activities, and interviews with personnel.

Based on the results of this inspection, the NRC has identified two issues that were evaluated

under the Significance Determination Process as having very low safety significance (Green).

The NRC has also determined that violations are associated with these issues. These

violations are being treated as noncited violations (NCVs), consistent with Section VI.A of the

Enforcement Policy. These NCVs are described in the subject inspection report. If you contest

the violation or significance of these NCVs, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the

Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza

Drive, Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

San Onofre Nuclear Generating Station, Units 2 and 3, facility.

Immediately following the terrorist attacks on the World Trade Center and the Pentagon, the

NRC issued an advisory recommending that nuclear power plant licensees go to the highest

level of security, and all promptly did so. With continued uncertainty about the possibility of

additional terrorist activities, the Nations nuclear power plants remain at the highest level of

security and the NRC continues to monitor the situation. This advisory was followed by

additional advisories and, although the specific actions are not releasable to the public, they

generally include increased patrols, augmented security forces and capabilities, additional

security posts, heightened coordination with law enforcement and military authorities, and more

limited access of personnel and vehicles to the sites. The NRC has conducted various audits of

Southern California Edison Co. -2-

your responses to these advisories and your ability to respond to terrorist attacks with the

capabilities of the current design basis threat. From these audits, the NRC has concluded that

your security program is adequate at this time.

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response, if any, will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/

Claude E. Johnson, Chief

Project Branch C

Division of Reactor Projects

Dockets: 50-361

50-362

Licenses: NPF-10

NPF-15

Enclosure:

NRC Inspection Report

50-361/01-14; 50-362/01-14

cc w/enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, California 92101

Gary L. Nolff

Power Projects/Contracts Manager

Riverside Public Utilities

2911 Adams Street

Riverside, California 92504

Southern California Edison Co. -3-

Eileen M. Teichert, Esq.

Supervising Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, California 92522

R. W. Krieger, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, California 92674-0128

David Spath, Chief

Division of Drinking Water and

Environmental Management

P.O. Box 942732

Sacramento, California 94234-7320

Michael R. Olson

San Onofre Liaison

San Diego Gas & Electric Company

P.O. Box 1831

San Diego, California 92112-4150

Ed Bailey, Radiation Control Program Director

Radiologic Health Branch

State Department of Health Services

P.O. Box 942732 (MS 178)

Sacramento, California 94234-7320

Steve Hsu

Radiologic Health Branch

State Department of Health Services

P.O. Box 942732

Sacramento, California 94327-7320

Mayor

City of San Clemente

100 Avenida Presidio

San Clemente, California 92672

Robert A. Laurie, Commissioner

California Energy Commission

1516 Ninth Street (MS 31)

Sacramento, California 95814

Southern California Edison Co. -4-

Douglas K. Porter

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, California 91770

Dwight E. Nunn, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, California 92674-0128

Southern California Edison Co. -5-

Electronic distribution by RIV:

Regional Administrator (EWM)

DRP Director (KEB)

DRS Director (ATH)

Senior Resident Inspector (CCO1)

Branch Chief, DRP/C (CEJ1)

Senior Project Engineer, DRP/C (WCW)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Scott Morris (SAM1)

SONGS Site Secretary (SFN1)

Dale Thatcher (DFT)

R:\_SO23\2001\SO2001-14RP-CCO.wpd

RIV:C:DRP/C SRI RI PE:DRP/C C:DRS/EMB

CEJohnson CCOsterholtz JGKramer RVAzua CSMarschall

RVAzua for E - RVAzua E - RVAzua /RA/ LEEllershaw for

concurrence 4/16/02 4/16/02 4/16/02 4/17/02

C:DRS/PSB signature

GMGood CEJohnson

/RA/ /RA/

4/16/02 4/22/02

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets: 50-361

50-362

Licenses: NPF-10

NPF-15

Report: 50-361/01-14

50-362/01-14

Licensee: Southern California Edison Co.

Facility: San Onofre Nuclear Generating Station, Units 2 and 3

Location: 5000 S. Pacific Coast Hwy.

San Clemente, California

Dates: December 30, 2001, through March 23, 2002

Inspectors: C. C. Osterholtz, Senior Resident Inspector

J. G. Kramer, Resident Inspector

R. V. Azua, Project Engineer

C. A. Clark, Reactor Inspector

P. J. Elkmann, Emergency Preparedness Inspector

L. E. Ellershaw, Senior Reactor Inspector

M. F. Runyan, Senior Reactor Inspector

Approved By: Claude Johnson, Chief, Project Branch C

SUMMARY OF FINDINGS

San Onofre Nuclear Generating Station, Units 2 and 3

NRC Inspection Report 50-361/01-14; 50-362/01-14

IR05000361-01-14, IR05000362-01-14: 12/30/2001-03/23/2002; Southern California Edison;

San Onofre Nuclear Generating Station, Units 2 & 3; Integrated Resident and Regional Report;

Operability Evaluations; Event Followup

The inspection was conducted by resident, regional reactor, and emergency preparedness

inspectors. This inspection identified two Green findings, both of which were noncited

violations. The significance of the issues is indicated by their color (Green White, Yellow, Red)

using IMC 0609 Significance Determination Process.

Cornerstone: Mitigating Systems

A. Inspector Identified Findings

  • Green. The inspectors identified a noncited violation for the licensees lack of corrective

action to mitigate a water hammer condition in screenwash system piping until prompted

by the inspectors. This issue was more than minor because this condition had the

potential to affect the operability of the safety-related saltwater cooling pumps. This was

a violation of 10 CFR Part 50, Appendix B, Criteria XVI.

The finding was considered to have very low safety significance because the

screenwash piping remained within ANSI codes for allowable stress, no actual rupture of

screenwash piping occurred, and the operability of the saltwater cooling pumps was not

actually affected by the condition. This violation is in the licensees corrective action

program as Assignment 26 to Action Request 010300938 (Section 1R15.2).

B. Licensee Identified Findings

A violation of very low safety significance was identified by the licensee and reviewed by

the inspectors. Corrective actions taken or planned by the licensee appear reasonable.

This violation is listed in Section 4OA3.1.

Report Details

Summary of Plant Status:

Both units began the inspection period at approximately 100 percent power. On

February 27, 2002, Unit 3 automatically tripped from 100 percent power due to a temporary loss

of offsite power during maintenance activities in the San Diego Gas and Electric portion of the

switchyard. Unit 3 vital power and power for the Unit 3 reactor coolant pumps automatically

transferred to Unit 2. Unit 3 emergency diesel generators (EDGs) automatically started and ran

unloaded. Switchyard maintenance activities were terminated and a root cause evaluation was

initiated. The San Diego Gas and Electric portion of the switchyard was returned to a normal

lineup and Unit 3 startup was initiated on March 2, 2002. Unit 3 entered Mode 1 on March 3

and achieved approximately 100 percent power on March 5. Both units remained at

100 percent power throughout the rest of this inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness

1R02 Evaluations of Changes, Tests, or Experiments (71111.02)

a. Inspection Scope

The inspectors reviewed a selected sample of 15 licensee-performed 10 CFR 50.59

evaluations to verify that the licensee had appropriately considered the conditions under

which the licensee may make changes to the facility or procedures or conduct tests or

experiments without prior NRC approval.

The inspectors reviewed an additional 28 licensee-performed 10 CFR 50.59 screenings,

in which the licensee had determined that evaluations were not required, to ensure that

the licensees exclusion of a full evaluation was consistent with the requirements of

10 CFR 50.59.

The inspectors evaluated the effectiveness of the licensees corrective action process to

identify and correct problems regarding licensee performance associated with

10 CFR 50.59 requirements. In this effort, the inspectors reviewed 10 action

requests (ARs) and the subsequent corrective actions pertaining to licensee-identified

problems and errors in the performance of licensing basis impact evaluations. The

review was performed to ensure that problems and deficiencies were being identified

and that appropriate corrective actions were being taken. In addition, the inspectors

reviewed the most recent licensee 10 CFR 50.59 program audit to determine whether

the licensee conducted sufficient in-depth analyses to allow for the identification and

subsequent resolution of problems or deficiencies. The inspectors also reviewed the

10 CFR 50.59 training curriculum provided by the licensee and the qualification records

of a sample of those independent technical reviewers identified in the screening and

evaluation forms.

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b. Findings

No findings of significance were identified.

1R04 Equipment Alignments (71111.04)

a. Inspection Scope

The inspectors performed partial walkdown of the following trains of equipment during

maintenance outages of their redundant trains. The inspectors physically verified critical

portions of the trains to identify any discrepancies between the existing and proper

alignment as determined by system piping and instrumentation drawings and plant

procedures:

  • Low pressure safety injection (LPSI) system during maintenance on

Valve 2HV9328, LPSI header valve to reactor coolant system Loop 2A, on

February 20, 2002 (Unit 2)

San Diego Gas and Electric portion of the switchyard on February 27, 2002

reactor coolant system Loop 2B, on March 12, 2002 (Unit 3)

  • EDG 3G002 during maintenance on EDG 3G003 on March 12, 2002 (Unit 3)

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

a. Inspection Scope

The inspectors performed routine fire inspection tours, and reviewed relevant records,

for the following plant areas important to reactor safety:

  • Unit 3 Train A safety-related pump room
  • Unit 3 Train B safety-related pump room
  • Unit 3 AFW pump room
  • Unit 2 2P190 charging pump room
  • Unit 2 2P192 charging pump room

The inspectors observed the material condition of plant fire protection equipment, the

control of transient combustibles, and the operational status of barriers. The inspectors

compared in-plant observations with the commitments in the portions of the Updated

Fire Hazards Analysis Report.

-3-

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification (71111.11)

a. Inspection Scope

The inspectors observed licensed operator requalification training activities, including

the licensed operators performance and the evaluators critique. The inspectors

compared performance in the simulator on March 7, 2002, with performance observed

in the control room during this inspection period. In addition, the inspectors reviewed

ARs 020201525 and 020300055.

The inspectors placed an emphasis on high-risk licensed operator actions, operator

activities associated with the emergency plan, and previous lessons learned items.

These items were evaluated to ensure that operator performance was consistent with

protection of the reactor core during postulated accidents.

b. Findings

No findings of significance were identified.

1R12 Maintenance Rule Implementation (71111.12)

1. Quarterly Review

a. Inspection Scope

The inspectors reviewed the implementation of the requirements of the Maintenance

Rule (10 CFR 50.65) to verify that the licensee had conducted appropriate evaluations

of equipment functional failures, maintenance preventable functional failures, unplanned

capacity loss factor, and system unavailability. The inspectors reviewed root causes

and corrective action determinations for equipment failures and reviewed performance

goals for ensuring corrective action effectiveness. The inspectors discussed the

evaluations with the reliability engineering supervisor and the system engineers. The

following systems were reviewed:

  • Unit 2 Train B AFW
  • Unit 3 Train A AFW

b. Findings

No findings of significance were identified.

-4-

.2 Periodic Evaluation Reviews

a. Inspection Scope

The inspectors reviewed the licensees reports documenting the performance of the last

two Maintenance Rule periodic effectiveness assessments. These two periodic

evaluations covered the second quarter of 1997 through the second quarter of 2001.

The inspectors verified that the licensees program had monitored risk-significant

functions associated with structures, systems, and components using reliability and

unavailability criteria. Additionally, the performance of nonrisk-significant functions were

monitored using plant level criteria.

The inspectors reviewed the conclusions reached by the licensee with regard to the

balance of reliability and unavailability for specific maintenance rule functions. This

review was conducted by examining the licensees evaluation of all risk-significant

functions that had exceeded performance criteria during the evaluation periods.

The inspectors also examined the licensees evaluation of program activities associated

with the placement of Maintenance Rule Program risk-significant functions in

Categories (a)(1) and/or (a)(2). Additionally, the inspectors reviewed the periodic

evaluation conclusions reached by the licensee for the following systems: AFW,

component cooling water, high pressure safety injection, LPSI, and main steam.

b. Findings

No findings of significance were identified.

.3 Identification and Resolution of Problems

a. Inspection Scope

The inspectors evaluated the use of the corrective action system within the Maintenance

Rule Program for issues identified in the AFW, component cooling water, high pressure

safety injection, LPSI, and main steam systems. This review was accomplished by the

examination of a sample of the ARs, maintenance rule evaluations, maintenance work

orders, Maintenance Rule Expert Panel meeting minutes, control room logs, and other

documents listed in the attachment. The purpose of this review was to establish that the

corrective action program was entered at the appropriate threshold for the purposes of:

  • Implementation of the corrective action process when a performance criterion

was exceeded;

  • Correction of performance-related issues or conditions identified during the

periodic evaluation; and

  • Correction of generic issues or conditions identified during programmatic

surveillances, audits, or assessments.

-5-

The inspectors verified that the identification of problems and implementation of

corrective action were acceptable.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a. Inspection Scope

The inspectors verified the accuracy and completeness of assessment documents and

that the licensees program was being appropriately implemented. The inspectors also

ensured that plant personnel were aware of the appropriate licensee-established risk

category, according to the risk assessment results and licensee program procedures.

The inspectors also reviewed selected emergent work items to ensure that overall plant

risk was being properly managed and that appropriate corrective actions were being

properly implemented.

The inspectors reviewed the effectiveness of risk assessment and risk management for

the following:

  • The San Onofre Core Damage Risk Summary dated April 20, 2000
  • Emergent work associated with age-related affects requiring replacement of

Potter and Brumfield relays in the Units 2 and 3 emergency feedwater actuation

systems reported on January 29, 2002 (AR 010900371 and Licensee Event

Report (LER) 361; 362/2002-001-00)

  • Emergent work associated with a failure of the Unit 3 Train A component cooling

water surge tank backup nitrogen pressure regulator on January 31, 2002

(AR 020101559)

  • Emergent work associated with Train A Emergency Chiller ME336 after it failed a

surveillance test on February 3, 2002 (AR 020200107)

  • Emergent work associated with a body-to-bonnet steam leak on Valve 2MR608,

Unit 2 main steam root valve, identified on February 19, 2002 (AR 020200945)

  • Risk assessment associated with maintenance activities on the LPSI system

during maintenance on Valve 2HV9328, LPSI header valve to reactor coolant

system Loop 2A, on February 20, 2002 (Unit 2)

  • Emergent work associated with seating Valve 2MU074, Unit 2 LPSI to reactor

coolant Loop 2A check valve, to prevent unnecessary leakage from Safety

Injection Tank T009 on February 20, 2002 (AR 020200987)

-6-

  • Emergent work associated with a steam leak identified on Valve 3HV4716, the

Unit 3 turbine-driven AFW pump steam supply throttle valve (AR 020300566)

b. Findings

No findings of significance were identified.

1R14 Personnel Performance During Nonroutine Plant Evolutions (71111.14)

.1 Operations Response to Automatic Reactor Trip

a. Inspection Scope

The inspectors observed Operations personnel respond to an automatic reactor trip of

Unit 3 when a temporary loss of offsite power occurred during switchyard maintenance

activities on February 27, 2002. The inspectors observed control room operators

successfully manipulate emergency operating instructions to put the plant in a stable

shutdown configuration.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

.1 Quarterly Review

a. Inspection Scope

The inspectors reviewed selected operability evaluations to evaluate technical adequacy

and to verify that operability was justified. The inspectors considered the impact on

compensatory measures for the condition being evaluated, and referenced the Updated

Final Safety Analysis Report and Technical Specifications. The inspectors also

discussed the evaluations with cognizant licensee personnel.

The inspectors reviewed the operability evaluations and cause assessments

documented in the following ARs to ensure operability was properly justified:

  • AR 020100733: Saltwater heat exchanger differential pressure rose from

6.5 psid to 12.8 psid while approaching a low tide (Unit 2)

  • AR 011001222: Main feed pump turbine speed could not be raised above

3600 rpm during startup (Unit 2)

  • AR 020101370: EDG lubricating oil analysis (Units 2 and 3)

-7-

b. Findings

No findings of significance were identified.

.2 Water Hammer Operability Assessment

a. Inspection Scope

The inspectors reviewed an operability assessment (OA) associated with

AR 010300938, generated on March 19, 2001, to evaluate degradation of piping

supports on secondary screen wash piping in the Unit 2 saltwater cooling pump room

above the saltwater cooling pumps.

b. Findings

The inspectors reviewed the OA for AR 010300938 (Assignment 3), which indicated that

piping support degradation in the Unit 2 screenwash piping was probably due to

improper rigging activities. The OA indicated that there is no evidence of water

hammer and excess loading from thermal growth of this seawater line seems unlikely.

The support may have been damaged by some past rigging practice. However, as no

credit for the support function at the three-way support location appears to be needed,

no further degradation is expected. The OA concluded that the piping support was not

necessary and, with no additional degradation expected, the screenwash system was

declared operable and the OA was closed on March 21, 2001.

The inspectors reviewed the apparent cause assessment (ACE) for AR 010300938

(Assignment 12) generated in April 2001, which indicated that An investigation made by

Station Technical . . . personnel indicated that there is no possibility that the support was

used to rig heavy equipment load that could cause the failure of this support. The ACE

concluded that the damage to the piping support was caused by water hammer incurred

in the system when two screenwash pumps were started simultaneously. The ACE

further recommended that the water hammer could be prevented by changing

procedures to stagger screenwash pump starts or by relocating the screenwash orifice

plate to ensure that it would be in a section of piping filled with water prior to a

screewash pump start. This would prevent flow retardation due to an air/water interface

at the orifice plate when screenwash pumps are started.

The inspectors had questions regarding cumulative water hammer effects in the

screenwash piping, because the piping is located directly above the safety-related

saltwater cooling pumps. On December 17, 2001, the inspectors contacted licensee

Engineering personnel to ask what corrective action was planned and how the water

hammer affected screenwash system operability. An Engineering representative

indicated that a water hammer condition did not exist and referenced the OA for

AR 010300938 that indicated that the degradation was probably due to improper rigging

activities. The inspectors informed the representative that AR 010300938 included an

ACE that discussed the water hammer and proposed possible corrective actions to

mitigate it. The representative was unaware the evaluation existed.

-8-

The licensee immediately generated a new OA for AR 010300938 (Assignment 25) and

initiated a new ACE (Assignment 26) to determine why the original OA was not revised

to consider the identified water hammer condition. The new OA was completed on

December 18, 2001, and determined that screenwash piping had continued to meet the

requirements of ANSI B31.1 for allowable piping stresses. The inspectors reviewed the

new OA and concluded that it was satisfactory. The new ACE identified multiple

examples of previous ARs dating back to 1996 that had been generated as a result of

screenwash system piping degradation that could be attributed to water hammer in the

screenwash system. The licensee could not determine when the practice of starting

screenwash pumps simultaneously started, but determined it was some time prior to

1988. Corrective actions to prevent water hammer by changing plant configuration and

procedures to require a staggered screenwash pump start were initiated.

The new ACE also concluded that lack of overall ownership of the issue directly

contributed to the water hammer analysis being missed for overall operability evaluation

and corrective action determination. The licensee initiated a program to establish

ownership for critical activities, such as ARs which require cause assessments. The

program assigns a single point of contact to ensure that appropriate corrective actions

are implemented, requires followup on corrective actions for effectiveness once taken,

and provides for periodic reporting of such issues to licensee management. The

licensee was performing a pilot of the program during this inspection period and planned

to fully implement the program on March 25, 2002.

The inspectors evaluated the significance of the issue using the Significance

Determination Process. The inspectors determined that the issue had a credible impact

on safety due to the potential for water hammer to cause a rupture in screenwash

system piping which could result in causing inoperability of safety-related saltwater

cooling pumps located directly below the piping (Group 1 question answered yes). The

issue could therefore affect the operability of a mitigating system (Group 2 question

answered yes). However, the finding was considered to have very low safety

significance because the screenwash piping remained within ANSI codes for allowable

stress, no actual rupture of screenwash piping occurred, and the operability of the

saltwater cooling pumps was not actually affected by the condition.

10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that measures shall be

established to assure that conditions adverse to quality are promptly identified and

corrected. Contrary to the above, the licensee did not implement corrective actions to

correct a water hammer condition in screenwash piping that had existed since 1996 until

prompted by the inspectors. This violation of 10 CFR Part 50 is being treated as a

noncited violation (NCV 361; 362/2001014-01) consistent with section VI.A of the

Enforcement Policy. This violation is in the licensees corrective action program as

Assignment 26 to AR 010300938.

-9-

1R16 Operator Workarounds (71111.16)

a. Inspection Scope

The inspectors reviewed operator workarounds to evaluate their cumulative effect on the

operators ability to implement abnormal or emergency procedures. The inspection

included a review of criteria and processes used for identifying and tracking deficiencies

as operator workarounds. The review also focused on the length of time the identified

workarounds had been in existence and efforts initiated to resolve them.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

a. Inspection Scope

On January 2, 2002, the inspectors observed a modification to component cooling water

Pump 3P024 that deleted the low pressure automatic start function and added a safety

injection actuation signal indicating light. The inspectors reviewed Work

Order 01091099000 and Field Change Notices F26055E, F26056E, and F26710E. In

addition, the inspectors reviewed AR 000900187 and its associated 10 CFR 50.59

evaluation.

b. Findings

No findings of significance were identified.

1R19 Postmaintenance Testing (71111.19)

a. Inspection Scope

The inspectors observed and/or reviewed postmaintenance testing for the following

activities to verify that the test procedures and activities adequately demonstrated

system operability:

  • Unit 3 EDG 3G002 postmaintenance test per Procedure SO23-3-3.23, Diesel

Generator Monthly and Semi-annual Testing, Revision 20, performed on

February 2, 2002, following routine scheduled maintenance

  • Train A Emergency Chiller ME336 postmaintenance test per

Procedure SO23-3-3.20, Monthly Creacus Test, Control Room Cooler Exercise

Run and ECWS Minimum Operability Verification, Revision 15, performed on

February 7, 2002, following replacement of a failed control circuit card

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Valve HV4714 postmaintenance test per Procedure SO23-3-3.60.6, Auxiliary

Feedwater Pump and Valve Testing, Revision 7, performed on March 5, 2002,

following routine scheduled maintenance

  • Unit 2 AFW Pump 2MP504 postmaintenance test per Procedure SO23-2-4,

Auxiliary Feedwater System Operation, Revision 18, performed on

March 5, 2002, following routine scheduled maintenance

  • Unit 3 EDG 3G003 postmaintenance tests per Maintenance

Orders 01090770000, Centrifugal Governor and Shutdown Solenoid Test, and

01090858000, Perform Overspeed Test . . . Inspect/Lubricate Linkages.

Perform Operability Test of the Overspeed Solenoid, performed on

March 15, 2002, following routine scheduled maintenance

The inspectors determined that the effect of testing on the plant had been adequately

addressed, the tests were adequate for the scope of the maintenance work performed,

and the acceptance criteria were clear and consistent with design and licensing basis

documents.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed and/or reviewed performance and documentation for the

following surveillance tests to verify that the structures, systems, and components were

capable of performing their intended safety functions and to assess their operational

readiness:

  • Train A Emergency Chiller ME336 monthly surveillance test per

Procedure SO23-3- 3.20, Monthly CREACUS [control room emergency air

cleanup system] Test, Control Room Cooler Exercise Run, and ECWS Minimum

Operability Verification, Revision 15, performed on January 1, 2002

  • Unit 3 EDG 3G002 monthly surveillance test per Procedure SO23-3-3.23, Diesel

Generator Monthly and Semi-Annual Testing, Revision 20, performed on

January 26, 2002

  • Unit 2 EDG 2G003 monthly surveillance test per Procedure SO23-3-3.23, Diesel

Generator Monthly and Semi-Annual Testing, Revision 20, performed on

February 3, 2002

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test per SO23-3-3.30.1, ECCS Online Valve Test, Revision 5, performed on

February 20, 2002

The inspectors also reviewed the licensees evaluation of the periodicity requirements

for surveillance testing of control element drive mechanism backup circuit breakers.

The inspectors referenced Licensee Controlled Specification 3.8.100, Containment

Penetration Conductor Overcurrent Protective Devices, and AR 010100470 as part of

the review.

The inspectors discussed the adequacy of the current methodology used to implement

the requirements of Technical Specification 5.5.2.12, Ventilation Filter Testing

Program, with licensee personnel. The inspectors reviewed Regulatory Guide 1.52,

ASME N510-1989, ANSI N510-1975, and surveillance test data.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the following temporary plant modifications to verify that the

safety functions of safety systems were not affected:

  • Temporary Facility Modification 3-02-GNJ-001, Revision 0, "Disable CEDM

Cooling Unit (3ME404) Fan Motor 3ME404B so that the cooling unit can operate

with a single fan (3ME404A)."

  • Temporary Facility Modification C-02-KAA-001, Revision 0, "Temporary

configuration of the Respiratory and Service Air System while Respiratory and

Service Air System Air Compressor SA2423MC445 is out of Service."

b. Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a. Inspection Scope

The inspectors performed an in-office review of Revision 16 to Emergency Plan

Implementing Procedure SO123-VIII-1, Recognition and Classification of

Emergencies, submitted December 5, 2001, against 10 CFR 50.54(q) to determine if

the revision decreased the effectiveness of the emergency plan.

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b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a. Inspection Scope

The inspectors verified the accuracy of data reported by the licensee for the following

performance indicator to ensure that the performance indicator color was correct for

both Units 2 and 3:

  • IE2 Scram with Loss of Normal Heat Removal

The inspectors reviewed the performance indicator data for all four quarters of 2001.

The inspectors reviewed NEI 99-02, Regulatory Assessment Performance Indicator

Guideline, and licensee operating logs. The inspectors discussed the status of the

performance indicator and compilation of data with Engineering personnel.

b. Findings

No findings of significance were identified.

4OA3 Event Followup (71153)

.1 (Closed) LER 361; 362/2001-003-00: one train of control room emergency air cleanup

system (CREACUS) inoperable due to unlatched circuit board.

On October 4, 2001, operators did not properly change the recorder paper and therefore

unknowingly left a circuit board unlatched, which caused the flow-indicating controller

and one train of the CREACUS to be inoperable. This was a violation of Technical

Specifications 3.0.4 and 3.0.3 for Units 2 and 3, respectively. This issue was

characterized as a noncited violation and as Green using the Significance Determination

Process.

On October 22, 2001, a control room operator discovered that the CREACUS Train B

flow control system was inoperable. During investigation of the issue, the licensee

determined that the flow-indicating controller had been inoperable from the last time the

Train B recorder paper was changed (October 4, 2001). Since that time Unit 2 had

changed modes of operation and, for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> on October 11, 2001, the

Train A CREACUS unit was also inoperable.

The inspectors evaluated the significance of the issue. The inspectors determined that

the issue had a credible impact on safety because the issue affected the operability of a

safety-related train of CREACUS (Group 1 question answered yes). The inspectors

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also determined that the issue could affect the integrity of the control room envelope

(Group 2 question answered yes). However, since the issue only represented a

degradation of the radiological barrier function of the control room, the issue screened

as Green using the Significance Determination Process.

Technical Specification 3.0.4 requires, in part, that, when a limiting condition for

operation is not met, entry into a mode or other specified condition of the applicability

shall not be made. Technical Specification 3.0.3 requires, in part, that, when a limiting

condition for operation and the associated actions are not met, the unit shall be placed

in a mode in which the limiting condition for operation is not applicable. Contrary to the

above, on October 22, 2001, the licensee changed modes on Unit 2 and entered

Mode 1 with an inoperable CREACUS unit and, on October 11, 2001, the licensee did

not follow the actions of Technical Specification 3.0.3 on Unit 3 when both CREACUS

trains were inoperable. This violation of Technical Specifications is being treated as a

noncited violation consistent with Section VI.A of the NRC Enforcement Policy

(NCV 361; 362/2001014-02). This violation is in the licensees corrective action

program as AR 011001218.

.2 (Closed) LER 361; 362/2002-001-00: aging phenomenon affects certain Potter and

Brumfield relays

The inspectors reviewed this LER and determined that the licensees root cause

determination and proposed corrective actions were appropriate. This LER is closed.

4OA5 Other

(Closed) Inspection Followup Item 361-362/1998014-002: re-evaluate quality standards

for non-Class 1e components for seismic qualifications

Regional inspectors reviewed this issue and determined that the licensee had taken

appropriate actions in its evaluations. This item is closed.

4OA6 Meetings

Exit Meeting Summary

The inspectors presented the inspection results to Mr. R. Krieger, Mr. D. Nunn, and

other members of licensee management at exit meetings on January 4, 11, and 18 and

March 25, 2002. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

ATTACHMENT

SUPPLEMENTAL INFORMATION

PARTIAL LIST OF PERSONS CONTACTED

Licensee

R. Krieger, Vice President, Nuclear Generation

R. Allen, Supervisor, Reliability Engineering

C. Anderson, Manager, Site Emergency Preparedness

D. Axline, Licensing Engineer

D. Brieg, Manager, Maintenance Engineering

R. Clark, Manager, Quality Engineering and Programs

G. Cook, Supervisor, Compliance

J. Fee, Manager, Maintenance

M. Hug, Supervisor, Emergency Planning

C. McAndrews, Project Manager, Corrective Action Program

J. McGaw, Senior Engineer, Strategic Issues

M. McKinley, Manager, Nuclear Training Department

M. Goettel, Manager, Business Planning and Financial Services

J. Hirsch, Manager, Chemistry

J. Madigan, Manager, Health Physics

D. Nunn, Vice President, Engineering and Technical Services

R. Osborne, Supervisor, Design Engineering

J. Ramsdell, Maintenance Rule Coordinator, Engineering Program, Systems Engineering

R. Richter, Supervisor, Fire Protection Engineering

A. Scherer, Manager, Nuclear Oversight and Regulatory Affairs

P. Shaffer, Superintendent, Plant Maintenance

M. Short, Manager, Systems Engineering

T. Vogt, Plant Superintendent, Units 2 and 3 Operations

R. Waldo, Manager, Operations

ITEMS OPENED, CLOSED, OR DISCUSSED

Opened and Closed

361; 362/2001014-01 NCV Lack of corrective actions for screenwash system

water hammer (Section 1R15.2)

361; 362/2001014-02 NCV Inoperable train of the CREACUS system

(Section 4OA3.1)

Closed

361; 362/2001-003-00 LER One train of CREACUS inoperable due to

unlatched circuit board (Section 4OA3.1)

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361; 362/2002-001-00 LER Aging phenomenon affects certain Potter and

Brumfield relays (Section 4OA3.2)

361; 362/1998014-02 IFI Re-evaluate quality standards for non-Class 1E

components for seismic qualifications

(Section 4OA5)

LIST OF ACRONYMS USED

ACE apparent cause assessment

AFW auxiliary feedwater

AR action request

CFR Code of Federal Regulations

CREACUS control room emergency air cleanup system

EDG emergency diesel generator

IFI inspection followup item

LER licensee event report

LPSI low pressure safety injection

NCV noncited violation

NRC Nuclear Regulatory Commission

OA operability assessment

DOCUMENTS REVIEWED

The following documents were selected and reviewed by the inspectors to accomplish the

objectives and scope of the inspection and to support any findings:

PROCEDURES

NUMBER DESCRIPTION REVISION

SO123-XV-5.3 Maintenance Rule Program 3

SO123-XV-50 Corrective Action Process 3

SO123-XV-44 10 CFR 50.59 Program 4

SO123-XV-44.1 10 CFR 50.59 Program Resource Manual 0

SO123-XV-50 Corrective Action Process 3, EC 3

SO123-XX-1 Action Request/Maintenance Order Initiation and 13, TCN 2

Processing

S0123-XV-5.10 Temporary Facility Modification 0

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10 CFR 50.59 SCREENINGS

010701278-2 010800553-2 010901320-1 011001416-2

010800105-1 010800694-6 011000054-1 011100612-1

010800164-2 010501745-2 011000263-1 011100472-2

010800185-1 010101990-46 010900460-2 011101242-1

010800390-1 010801123-1 011001564-1 010900537-6

010800472-1 010900152-1 011001242-3 011200624-1

010800321-3 010501150-6 011100186-1 011200729-1

ARs

991200682 990700036 010801307 010500189

010301442 000400390 011000765 001101113

010400670 000501153 010700635 010801632

990501611 000701407 011101300 010901320

990501011 010401054

10 CFR 50.59 EVALUATIONS

010800825-2 010301442-4 010600258-2 010800321-4

010100068-2 010501009-3 010600270-1 010900537-2

010200212-2 010501433-4 010601031-4 011000765-4

010200708-1 010501350-3

010400217-1

MISCELLANEOUS DOCUMENTS

TITLE/NUMBER REVISION

DATE

SCES-018-01:10CFR50.59 Program Audit 12/12/2001

SONGS Maintenance Rule Program Periodic (a)(3) Assessment 11/16/01

SONGS Maintenance Rule Program Periodic (a)(3) Assessment 11/23/99

Maintenance Rule Evaluation Guideline 11/17/97

Independent Assessment of Maintenance Rule Implementation 09/05/01

Surveillance Report SOS-045-01, Maintenance Rule Program 05/09/01

Site Technical Service Audit SCES-924-99 11/05/99

Maintenance Rule Quarterly Performance Summary Report - 3Q01 10/31/01

Maintenance Rule Quarterly Performance Summary Report - 4Q00 01/31/01

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SONGS State of The System Report for Auxiliary Feed Water System 01/17/02

SONGS State of The System Report for Component Cooling Water System 01/17/02

SONGS State of The System Report for High Pressure Safety Injection 01/17/02

System

SONGS State of The System Report for High Pressure Safety Injection & 01/17/02

Shutdown Cooling System

SONGS State of The System Report for Main Steam System 01/17/02

Control Room Logs 10/10-17/01

ACE 010801543-2

Work Authorization Record 3-0101538

Work Authorization Record 2-0100168

RSAS Operating Instruction SO23-1-2, Sections 6.2 and 6.3

Updated Final Safety Analysis Report, Section 9.3.1, "RSAS/IAS"

Maintenance Rule Evaluations (listed per applicable AR numbers)

980100940 000801364 001102003 010201709

980701447 000801366 001102004 010301123

000101639 001001494 010102354 011001024

000201542

Maintenance Work Orders

00317200 00505820 96080638 99060581

00502840 00505860 96121091 99070119

00502880 00506940 97061197 99121969

00505284 00507000 99051426 99970110

MEETING MINUTES - Maintenance Rule Expert Panel (listed per date of meeting)

02/24/00 08/17/00 01/25/01 06/21/01

03/23/00 08/24/00 02/28/01 07/19/01

04/20/00 09/21/00 03/22/01 08/23/01

05/18/00 10/18/00 04/19/00 09/20/01

06/29/00 11/30/00 05/24/01 10/18/01

07/20/00 12/21/00