ML19283B782

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LER 79-019/03L-0 on 790223:motor Driven Emergency Feedwater Pump Discharge Pressure Gauge EF-2-PI Was Out of Calibr. Caused by Inoperable Dampening Snubber Located in Sensing Line.Snubber Was Replaced
ML19283B782
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 03/16/1979
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19283B783 List:
References
LER-79-019-03L, LER-79-19-3L, NUDOCS 7903230135
Download: ML19283B782 (2)


Text

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NRC FORM 366 U.S NUCLEAR REGULATORY CoMMis34CN

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gi out of calibration. This created an event contrary to'Technien1 9nocificaHlon

, 3.3.3.5. Entered action statement "a". Redundancy N/A. No hazard to the i

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, The indicator was calibrated and a functional test performed with'satisfactorry results. The indicator was returned to service at 2245 3/12/79. No l

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, SUPPLEMT.NTARY INFORMATION Report No.: 50-302/79-019/03L-0 Facility: Crystal River Unit #3 Report Date: 15 March 1979 Occurrence Date: 23 February 1979 Identification of Occurrence:

One remote shutdown instrumentation channel inoperable contrary to Technical Specification 3.3.3.5.

Conditions Prior to Occurrence:

Mode 3 operation (hot standby)

Description of Occurrence:

While conducting routine plant surveillance, it was discovered that the motor driven emergency feedwater pump discharge pressure gauge EF-2-PI, was out of calibration. Further investigation revealed that the dampening snubber located in the sensing line to the gauge had failed. The snubber was eplaced. The indicator was calibrated, tested, and returned to service 3/12/79.

Designation of Apparent Cause:

The cause of this event is attributed to an inoperable dampening ,

snubber located in the sensing line to the indicator.

Analysis of Occurrence:

No hazard to the plant or general public as the plant was in a safe shutdown condition.

Corrective Action:

The dampening snubber was replaced. The indicator was calibrated in accordanca with SP-169 and tested per SP-349, " Emergency Feedwater System Operability Demonstration." The indicator was returned to service 3/12/79. No further corrective action required.

First occurrence reported for EF-2-PI.

Failure Data:

First occurrence reported for EF-2-PI.

/rc