|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:RO)
MONTHYEARML20046B4841993-07-30030 July 1993 LER 93-006-00:on 930703,auxiliary Feedwater Signal Inadvertently Actuated Due to Personnel Error.Equipment Reset to Normal Lineup & Fuses Removed for Reinstallation Prior to Reactor startup.W/930730 Ltr ML20045H7611993-07-16016 July 1993 LER 93-007-00:on 930626,CR Alarm Received,Indicating Excessive Temp on Reactor Coolant Pump Motor Stator 1-04 & Manual Trip Initiated.Caused by RTD Failure.Rtd Terminations Disconnected & AOP revised.W/930716 Ltr ML20045A9911993-06-11011 June 1993 LER 93-004-00:on 930514,failure to Satisfy TS Surveillance for Verification of Valve Position Due to Valve Discrepancies Discovered During DBD Review.Valve Cap & Clearance installed.W/930611 Ltr ML20045A4681993-06-0303 June 1993 LER 93-003-00:on 930504,manual Reactor Trip Occurred Following Inadvertent Closure of Fwiv.Caused by Instrumentation Channel Error.Maint Performed on Affected Instrumentation channels.W/930603 Ltr ML20044G4071993-05-26026 May 1993 LER 93-006-00:on 930426,failure to Satisfy TS Surveillance Requirement for Primary Plant ESF Exhaust Filtration Unit Noted.Caused by Poor Labeling,Specification of Wrong Procedure & Discrepancy in Parts list.W/930526 Ltr ML20024H1581991-05-21021 May 1991 LER 91-016-00:on 910418,failure of Check Valve to Prevent Backflow Discovered.Caused by Mfg Error in Machining Process of Valve Body Casting.Valves Reassembled & Scheduled to Receive testing.W/910521 Ltr ML20024G7211991-04-25025 April 1991 LER 91-012-00:on 910326,potential Gas Binding of Centrifugal Charging Pumps Due to Voids in Boric Acid Gravity Feed Line Identified.Caused by Hydrogen Coming Out of Solution in Lower Pressure Ccp Suction header.W/910425 Ltr ML20024G6801991-04-22022 April 1991 LER 91-010-00:on 910322,unit 1 Operated Outside Tech Spec Due to Auxiliary Feedwater Sys Test Line Isolation Valve Not Closed.Root Cause Not Determined.Providing Addl Guidance to Operators & Operators Monitoring valves.W/910422 Ltr ML20029B6421991-03-12012 March 1991 LER 91-004-00:on 910210,potential Transformer Drawer Opened at Bottom of Switchgear Bus 1A3 Auxiliary Cubicle,Causing Load Shed Signal & Reactor Trip.Caused by Personnel Error. Labels Attached to Switchgear bus.W/910312 Ltr ML20028G9551990-09-27027 September 1990 LER 90-026-00:on 900828,surveillance Missed Due to Inadequate Procedural Requirements.Caused by Inadequate Manual Surveillance Scheduling Methods.Station Procedures revised.W/900927 Ltr ML20044A1351990-06-26026 June 1990 LER 90-017-00:on 900527,main Feedwater Flow Control Valve Failed Closed,Resulting in Reduced Feedwater Flow & Decreasing Steam Generator Water Level.Caused by Failure of Solenoid Valve Coil.Solenoid Coil replaced.W/900626 Ltr ML20044A3281990-06-22022 June 1990 LER 90-016-00:on 900521,engineering Determined That Three Atmospheric Relief Valves Declared Inoperable Resulting in Entry Into Tech Spec Limiting Condition for Operation 3.0.3. Pneumatic Controls Drifted Out of calibr.W/900622 Ltr ML20043H1971990-06-19019 June 1990 LER 90-015-00:on 900520,chemistry Sample Special Condition Surveillance Missed.Caused by Procedural Error.Procedures Revised to Provide Appropriate Cautions Re Required Sample. W/900619 Ltr ML20043G1121990-06-13013 June 1990 LER 90-014-00:on 900514,containment Penetration Improperly Isolated While Containment Isolation Valve Made Inoperable for Repairs.Caused by Inadequate Review of Work Order. Supervisor Counseled & Shift Order issued.W/900613 Ltr ML20043F1571990-06-0808 June 1990 LER 90-013-00:on 900509,while Installing Jumpers Across Feedwater Pump Speed Controllers,Pump Coastdown Occurred, Resulting in Loss of Feedwater Flow & Reactor Trip.Caused by Inadequate Procedure Review.Review performed.W/900608 Ltr ML20043E4511990-06-0707 June 1990 LER 90-012-00:on 900508,control Room Personnel Failed to Satisfy Time Limit for Completion of Action Required by Tech Specs Re Plant Radiation Monitoring.Caused by Personnel Error.Individual Counseled & Procedure revised.W/900607 Ltr ML20043F4941990-06-0404 June 1990 LER 90-011-00:on 900504,Pressure Instrument Root Isolation Valve 1SI-8961 Open When Procedure Indicated Valve Should Be Locked Closed.Caused by Lack of Clear Instructions Re Definition of Physical Work. Valve locked.W/900604 Ltr ML20043C0201990-05-29029 May 1990 LER 90-010-00:on 900428 & 29,2-h Surveillance Interval, Including 25% Extension Allowed by Tech Spec 4.0.2,exceeded. Caused by Personnel Error.Procedure Enhancements Initiated & Personnel Involved counseled.W/900529 Ltr ML20043A6691990-05-18018 May 1990 LER 90-009-00:on 900421,reactor Trip Occurred Due to Accidental Bumping of Source Range Reactor Trip Reset/Block Previously Bypassed for Power Operation.Order Issued Suspending Cleaning of Control boards.W/900518 Ltr ML20043A6131990-05-16016 May 1990 LER 90-008-00:on 900416,Train a Diesel Generator Rendered Inoperable Due to Failure to Complete post-work Operability Testing on Starting Air Receiver Check Valve 01. Caused by Inadequate Review.Procedure revised.W/900516 Ltr ML20043A6111990-05-16016 May 1990 LER 90-007-00:on 900416,ESF Actuation Signal Occurred, Resulting in Train a of Control Room Air Conditioning Sys Shifting to Emergency Recirculation Mode.Caused by Personnel Error.Handswitch Added to Radiation monitor.W/900516 Ltr ML20043A4201990-05-14014 May 1990 LER 90-006-00:on 900412,P-6 Permissive Signal Received & Source Range Flux Doubling (Srfd) Actuation Occurred.Caused by Inadvertent Reset of Srfd Block.Integrated Plant Operations Procedures changed.W/900514 Ltr ML20012B6491990-03-0909 March 1990 LER 90-001-00:on 900209,reactor Protection Sys Actuation Occurred Due to Spike on Range Channel.Appropriate Source Range Procedures Revised to Require Insertion of Flux Doubling Signal Block Prior to withdrawal.W/900309 Ltr 1993-07-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217E8021999-10-0707 October 1999 CPSES Unit 1 Cycle 8 Colr ML20217G4151999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Cpses,Units 1 & 2 ML20212F7671999-09-24024 September 1999 SER Granting Relief Request C-4 Pursuant to 10CFR50.55a(g)(6)(i) for Unit 2,during First 10-year ISI Interval & Relief Requests B-15,B-16 & B-17 Pursuant to 10CFR50.55a(g)(6)(i) ML20216J5701999-09-16016 September 1999 Rev 2 to CPSES Unit 2 Cycle 5 Colr TXX-9920, Monthly Operating Repts for Aug 1999 for Cpses.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Cpses.With ML20211M2981999-08-0606 August 1999 Rev 1 to CPSES Fuel Storage Licensing Rept, CPSES Credit for Soluble Boron & Expansion of Spent Fuel Storage Capacity, Consisting of Revised Title Page and 4-1 ML20210U4081999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Cpses,Units 1 & 2 ML20210D8321999-07-23023 July 1999 Safety Evaluation Accepting Relief Requests Re Use of 1998 Edition of Subsections IWE & Iwl of ASME Code for Containment Insp ML20209H7661999-07-15015 July 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Comanche Peak Steam Electric Station,Units 1 & 2 ML20209H2721999-07-0909 July 1999 2RF04 Containment ISI Summary Rept First Interval,First Period,First Outage ML20209H2631999-07-0909 July 1999 2RF04 ISI Summary Rept First Interval,Second Period,Second Outage ML20209G7501999-07-0808 July 1999 SER Finding That Licensee Individual Plant Exam of External Events Complete with Regard to Info Requested by Suppl 4 to GL 88-20 & That IPEEE Results Reasonable Given Design, Operation & History of Comanche Peak Steam Electric Station ML20196L0191999-07-0808 July 1999 Safety Evaluation Granting Request Relief B-6 (Rev 2),B-7 (Rev2),B-12,B-13,B-14 & C-9,pursuant to 10CFR50.55a(g)(6)(i).Technical Ltr Rept Also Encl ML20210J9391999-06-30030 June 1999 CPSES Commitment Matl Change Evaluation Rept 0003,for 970802-990630 ML20209G0801999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Cpses,Units 1 & 2 ML20196J0621999-06-29029 June 1999 Safety Evaluation Supporting Proposed Changes to Emergency Plan Re Licenses NPF-87 & NPF-89 Respectively ML20195G5141999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Comanche Peak Steam Electric Station,Units 1 & 2.With ML20216E0711999-05-21021 May 1999 1999 Graded Exercise - Comanche Peak Steam Electric Station ML20206Q0091999-05-14014 May 1999 Safety Evaluation Accepting GL 92-08, Thermo-Lag 330-1 Fire Barriers, Dtd 921217,for Comanche Peak Electric Station,Unit 1 ML20206H2061999-05-0606 May 1999 SER Accepting Exemption to App K Re Leading Edge Flowmeter for Plant,Units 1 & 2 ML20196L2241999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Cpses,Units 1 & 2 ML20205R5701999-04-14014 April 1999 Rev 6 to ER-ME-067, TU Electric Engineering Rept,Evaluation of Thermo-Lag Fire Barrier Sys ML18016A9011999-04-12012 April 1999 Part 21 Rept Re Defect in Component of DSRV-16-4,Enterprise DG Sys.Caused by Potential Problem with Connecting Rod Assemblies Built Since 1986,that Have Been Converted to Use Prestressed Fasteners.Affected Rods Should Be Inspected ML20205J7831999-04-0101 April 1999 Rev 0 to ERX-99-001, CPSES Unit 2 Cycle 5 Colr ML20205N3101999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Cpses,Units 1 & 2 ML20204H6371999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Comanche Peak Units 1 & 2 ML20205N1481999-02-28028 February 1999 Corrected Monthly Operating Rept for Feb 1999 for CPSES, Units 1 & 2 ML20203A4881999-02-0303 February 1999 Safety Evaluation Granting Requests for Relief B-3 - B-6,C-2 & C-3 for Plant,Unit 2 ML20210J9201999-02-0101 February 1999 CPSES 10CFR50.59 Evaluation Summary Rept 0008,for 970802- 990201 ML20202D0101999-01-27027 January 1999 Safety Evaluation Supporting First 10-yr Interval ISI Program Plan Requests for Relief B-9,B-10 & B-11 for CPSES, Unit 1 ML20199E9961998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Cpses,Units 1 & 2 ML20207D6091998-12-31031 December 1998 1998 Annual Operating Rept for Cpses,Units 1 & 2. with ML20197K2371998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Cpses,Units 1 & 2 ML20195F3161998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Cpses,Units 1 & 2 ML20154M8841998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Cpses,Units 1 & 2 ML20154B5741998-09-30030 September 1998 Safety Evaluation Re Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety- Related Motor-Operated Valves. Licensee Has Established Acceptable Program ML20151W0361998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Cpses,Units 1 & 2. with ML20151Q1211998-08-14014 August 1998 Rev 0 to Control of Hazard Barriers ML20237C4061998-08-14014 August 1998 Safety Evaluation Supporting Request to Implement Risk Informed IST Program ML20237C6721998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Cpses,Units 1 & 2 ML20236V3121998-07-29029 July 1998 Final Part 21 Rept Re Enterprise DSR-4 & DSRV-4 Edgs.Short Term Instability Was Found During post-installation Testing & Setup as Part of Design mod/post-work Testing Process. Different Methods Were Developed to Correct Problem ML20236R0711998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Cpses,Units 1 & 2 ML20249B2581998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Cpses,Units 1 & 2 ML20248A1671998-05-22022 May 1998 Interim Part 21 Re Enterprise DSR-4 & DSRV-4 Emergency diesel.Post-installation Testing Revealed,High Em/Rfi Levels Affected New Controllers,Whereas Original Controllers Were unaffected.Follow-up Will Be Provided No Later than 980731 ML20247G3241998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Cpses,Units 1 & 2 ML20216B8661998-04-0101 April 1998 Rev 0 to ERX-98-001, CPSES Unit 1 Cycle 7 Colr ML20216J3061998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Cpses,Units 1 & 2 ML20216J1861998-02-28028 February 1998 Monthly Operating Repts for Feb 1998 for Comanche Peak Steam Electric Station ML20197A6951998-02-24024 February 1998 Inservice Insp Summary Rept,First Interval,Second Period, First Outage ML20199J5391998-02-0202 February 1998 CPSES Commitment Matl Change Evaluation Rept 0002 for 960202-970801 1999-09-30
[Table view] |
Text
..
t '
sa N
- =" =::: ~
L -
Log # TXX-93238 C
._. 3 File # .10020 1UELECTRIC ef. # 0. ( )( )(B) 0 June 11,i1993 wmiam J. Cahm, Jr.
l- o,,, vu rmwa
~
.U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555
SUBJECT:
COMANCHE PEAK STEAM ELECTRIC STATION (CPSES)
DOCKET NO. 50-446 A CONDITION PR0HIBITED BY TECHNICAL SPECIFICATIONS LICENSEE EVENT REPORT 93-004-00 Gentlemen:
Enclosed is Licensee Event Report 93-004-00 for Comanche Peak Steam Electric Station Unit 1 " Failure to Satisfy Technical Specification Surveillance Requirement for Verification of Valve Positions".
Sincerely, WAinJ celdL Jo William J. Cahill, Jr.
By: b J.'J. Kelley, Jr.
Vice President of Nuclear Operations OB:tg Enclosure j cc: Mr. J. L. Milhoan, Region IV j Mr. L. A. Yandell, Region IV '
Resident Inspectors, CPSES (2) 150028 9306160040 930611 M ADOCK 05000446 h /
/ /p/
PDR C .. PM r$1 P.O. Box 1002 Glen Rose, Texas 76043-2002 . l' 0 l l
. Enclosure to TXX-93238 kHC f OHM 3e6 U.S NUCLEAR RE GULA1 DRY COMM:SSON APPRDVED OMB NO. 31504104 EXPRES:4" O 92 ESTIM ATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORM ATOP COLLECTON REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDINC auRDEN ESTIMATE TO THs RECORDS ANo REPORTS MANAGEMEN-LICENSEE EVENT REPORT (LER) BRANCH (P.530), U.S. NUCLE AR REGULAlDR, COMMISSON, WASHINGTON.
DC. 23555, AND TO THE PAPERWORK REDUCTON PRO.!ECT (3150-0104).
OFFICE OF M ANAGEMENT AND BUDGET. WASHINGTON, DC. 20503.
f acdry Naas p) *mel Nontier (2) y Page L31 COMANCHE PEAK-UNIT 2 05000446 6 1IOr 10 6
"~'"
FAILURE TO SATISFY TECHNICAL SPECIFICATION SURVEILLANCE FOR VERIFICATION OF VALVE POSITION
- .~ -_. , ,_em - - _ .
M. O., v. v. we = M. O., v, y,~ E$"Vl0l0l l l Ols 1 14 9l3 9l3 -
0l0l4 -
0l0 016 1l1 93 N/A 0 5 Ol0 0
,_,, a., _ . ._ _ e r__. . . - m,_. . ,._ e. . o ,
N _ 2C 402$)) _ 20.40a(C) ,
m73ta;@(w) _ 7311(D)
+ w*n 2040S(a41)(fl mmc)(1) 50 73(aK2Xv) 7311(c) hT 0l2l9 aoeS*me **m maaea 20maxme 8 m73:a)m(i) _
m73(a>2rvi.xA) o*- Sadr m as^u's=^) ' ~"a T=t Nac rarm
_ 20 -s- m.) _ muaw _
mnaw)e 20 43'm a)(11M 50 73 a12fiq 50 73 a):2)f r)
Lt.ansee Contacs For The LER (12) __.
Nare Area Gcm.ie Tempiore hier D. J. REIMER, MANAGER, SYSTEM ENGINEERING 8 1 7 8 9 7 -
5 5 8 4 Corgnole One L#e Fa Eacti Cor'vonent Fasare Descreed in Ths Runori (13)
C&me Systeni CagpierW Mariutacturer Ciksim SyEtern Can'ptrilFW Mandactuf'er <[> >
y gg >
N J 'l l Ill Ill ,
l lll lll ,
l lll lll I lll lll uanm (a
'Mvoar S$rmernerita Report E xpected (14) E sected Sarra.eun
"" "5)
Se, g , . co e E.:ecteo S-on O.iei @,. l l Atstract (t tillt to 1400 spaces. Le., a;peonernatory tFiuen smgie space typourrnian tries) (16)
On May 14,1993, an operations procedure reviewer discovered that position verification, as required by Technical Specifications (T/S) for some Process Sampling valves, was not incorporated into CPSES Uns 2 procedures. The overall cause of this event was a lack of requirements for reviews by Operations personnel of design changes issued during Unit 2 construction and a lack of attention to detal' concerning the specific design change involved in the event. Corrective actions included veitying valve positions, incorporating the position verification for the valves in appropriate procedures and performing reviews for generic implications.
Enc 1cisure to TXX-93238 sc ,mo uA us u m - m w ww.s m s j igynoyco oy, , 3,,,,
ESTIMATED BURDEN PER RES SE T LICENSEE EVENT REPORT (LER) "'" "*E S " " ""S ' "*^"
BURDEN ESTIMATE TO TH
MPLY WCTH THIS INCORMATOA TEXT CONTINUATION *"* "'""""E" RECORDS AND REPORTS MANAGE MEN'
"'"*^'"""""'**'"***""
- DC. 20555, AND TO THE PAPERWORK REDUCTON 104L PROJECT (31 f sory Na~e p) OFTCE OF MANAGEMENT ANDBUDGET, WASHINGTON DC 73503.
Wer Neta El)
LLH terw (6) vow Pap (3)
COMANCHE PEAK-UNI lq l p !7 +gy m n , n . . - .~,e> ~T 2 ,, p n015l0l0l0l4l416 9 3, -l0 'O 4 -
0 '0; Ol2l cc Ol 6 1.
DESCRIPTION OF THE REPORTABLE EVENT \
A.
REPORTABLE EVENT CLASSIFICATION _
Technical Specification surveillance was .
requirednot performe B.
PLANT OPERATING CONDITIONS PRIOR TO THE EVEN On May 14,1993, Comanche Peak Steam Electric Station (CPSES percent rated thermal power. Integrated Startup Testing was atwas 29 in progress C. .
INOPERABLE AT THE START OF TO THE EVENT TRIBUTED THE EVEN ERE There event. were no inoperable structures, systems or components that contributed to the D.
APPROXIMATE TIMESNARRATIVE
SUMMARY
OF THE EVENT, least once per 31 days, CONTAINMENT .
ar at at rated by verifying that INTEGR l
l all manual valves outside containment, needed toe.isolate a penet ,
I On February 26,1992, and on June 25,1992, Design Change Author ons (DCAs)
Containment isolation manual valves ng (Ells: (ISV)(K rawings. The i DCAs failed to document on these drawings that the valves were to be l
and capped. Because these drawings were used ockedto closed prepare the proc verify closure of containment isolation valves per T/S 4.6.1.1a, Proces 2PS-0030,2PS-0510,2PS-0511, and 2PS-0512 no (drain valves adjace containment penetrations) were not incorporated into these procedures .
. Enclo'sure to TXX-93238 NHC FOHW 3%A U.S NAEAR hiGJLATOM COMM'5580f5 APPROVED OMB NO. 31504104 EXPIRES: v2Ht2 ESTMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATch
' MECM RWEM: E HRS. @ WAR MMENTS REGARDE LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTC MANAGEMEN" !
S"'""'**"*"5""*""'**'"***""*
TEXT CONTINUATION DC. 20555. AND TO THE PAPERWORK REDUCTON PROJECT (31504104).
OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON.DC.20503.
F a:alry Narre p) Dams 4 Nunter (2) LER Nuntu, (6) Page Q) ,
voar , ya mie :
CM1ANCHE PEAK-UNIT 2 015l010l0l4l4l6 9 3 -
0 0 4 -
0l0 0 2 cr 0 6
- 1. . - . ..c. .- - N e muANon
[
- 1. DESCRIPTION OF THE REPORTABLE EVENT A. REPORTABLE EVENT CLASSIFICATION Any operation or condition prohibited by the Technical Specifications. A required ;
Technical Specification surveillance was not performed.
B. PLANT OPERATING CONDITIONS PRIOR TO THE EVENT On May 14,1993, Comanche Peak Steam Electric Station (CPSES) Unit 2 was at 29 percent rated thermal power. Integrated Startup Testing was in progress.
C. STATUS OF STRUCTURES, SYSTEMS, OR COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT There were no inoperable structures, systems or components that contributed to the event. :
D. NARRATIVE
SUMMARY
OF THE EVENT, INCLUDING DATES AND '
APPROXIMATE TIMES ,
t Technical Specification Surveillance Requirement 4.6.1.1a requires in part that at least once per 31 days, CONTAINMENT INTEGRITY be demonstrated by verifying that '
all manual valves outside containment, needed to isolate a penetration, are closed.
On February 26,1992, and on June 25,1992, Design Change Authorizations (DCAs) were initiated by CPSES Unit 2 Engineering to incorporate Process Sampling Containment isolation manual valves (Ells: (ISV)(KN)) into vital station drawings. The DCAs failed to document on these drawings that the valves were to be locked closed ,
and capped. Because these drawings were used to prepare the procedures to verify closure of containment isolation valves per T/S 4.6.1.1a, Process Sampling valves 2PS-0030,2PS-0510,2PS-0511, and 2PS-0512 (drain valves adjacent to ;
containment penetrations) were not incorporated into these procedures.
Enclosure to TXX-93238 NHC FOHM St0A u.5. N4d.As hHah. ATOAt C,OMM255.ON APPROVED OWB NO. 31MW EXPIRES:4/3n2 .
ESTIM ATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORM ATch
" ' " " " ; " ""S~' "**" ""'"'8 "'"'" "
LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMEN' (
TEXT CONTINUATION " " ' ' * * ' " " ' ~ " " ^ " " " ^ ' " * """ ***"" *-
DC. 205!.5. AND TO THE PAPERWORK REDUCTON PROJECT Q1tA0104).
OFFICE OF WANAGEMENT AND BUDGET WASHINGTON, DC. P0503. !
F aater Nrs p) Orxmet Nu' rte (2) LLH Nortts (6) Page Qi
~ w:: en COMANCHE PEAK-UNI: 0l5l0l010l4 4 6 9 3 -
0 0 4 -
0 0 0 3 w 0 6 i.%. u-,,- -- +c w .m o a E. THE METHOD OF DISCOVERY OF EACH COMPONENT OR SYSTEM FAILURE, OR PROCEDURAL OR PERSONNEL ERROR On May 14,1993, an Operations procedure reviewer (utility, licensed) performed a review of a draft revision to Design Basis Document (DBD)-ME-013 " Containment isolation System." During this review, the procedure reviewer discovered that the Primary Sampling Valves were not properly identified as Containment Penetration Non-Automatic Isolation Valves on the flow diagram, in the DBD or in Operations and j Chemistry procedures. ;
l
- 11. COMPONENT OR SYSTEM FAILURES A. FAILURE MODE, MECHANISM, AND EFFECT OF EACH FAILED COMPONENT j
l Not applicable - there were no component failures associated with this event.
B. DURATION OF SAFETY SYSTEM TRAIN INOPERABILITY Not applicable - there was no safety related equipment rendered inoperable during or i as a result of the event.
C. SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT The field conditions and programs for Containment Isolation consist of: 1) use of double isolation barriers,2) periodic testing,3) administrative control of manual isolation valves, and 4) surveillance of automatic isolation valves. These activities meet requirements and ensure the Containment isolation System performs its intended function. Incorrect positioning of a manualisolation valve on these penetrations would have been detected via normal plant activities. Under postulated accident conditions the Containment isolation System would have satisfactorily performed its intended safety function.
l d
1
.. _ . n.
Enclosure to TXX-93238 tNC FORM at4A L5. NM Aa FsGAATOHv GOMM50N APPROVED DMB NO. 31504104 )
EXPIRES:4'XMt2 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATOA
" '** "' " ** " " " * ' ' ""*" *""'"*"E""""
LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMEN' TEXT CONTINUATION ****"'"**""*""'"^""""***""*""""-
DC. 20555. AND TO THE PAPERWORK REDUCTON PROJECT (3150-0104L OFFOE OF MANAGEMENT AND BUDGET. WASHINGTON. DC.20503.
F acay Name p) Dochel Nureer (2) LEH Nurmer (6) Page p)
- e = e= ;
COMANCHE PEAK-UNIT 2 0 5 0 0 0 4 4 6 9 3 -
0 0 4 -
0 0 0 4 or 0 6 .
i.m.m. - .r - - ~acso,m m ypn III. CAUSE OF THE EVENT The following causes contributed to this event. A review of the design change process i used during the construction phase indicated that procedures did not require that changes affecting a DBD be included in the design change document being prepared. Rather, the DBD was to be reviewed to roll up all affected changes as the Unit 2 work scope neared completion. The valve discrepancies were discovered during the DBD review to roll up all design changes.
The procedures also did not require an Interdisciplinary Review (IDR) by Systems ,
Engineering or a review by Operations personnel for impact on Operations programs and i procedures unless the system had been turned over to Operations.
More attention to detail by the design change engineers during origination, review and approval may have precluded the event. Neither the originator nor reviewers identified the need for locked closed valves (similar to Unit 1), the need for a DBD change, or the need to change Operations procedures.
IV. CORRECTIVE ACTION l i
A. IMMEDIATE Upon discovery, Operations personnel were dispatched to verify the valve positions.
The as-found condition of the valves (May 14,1993) were:
2PS-0030 - CLOSED, uncapped.
2PS-0510 - CLOSED, capped.
2PS-0511 - CLOSED, capped.
2PS-0512 - CLOSED, capped.
Immediate corrective actions included installing the valve cap and hanging a clearance to administratively maintain the valves closed.
A review of Unit 1 drawings and procedures indicated that the valves were listed and designated correctly on Unit 1 documents.
. En, closure to TXX-93238 tec FOHM MA LLb. NJCLEAR niCmAATORY COMut5hiON APPROVED OMB NO. 31504104 [
EXPIRES:4'3Mt2 ;
ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATIOk i ME Tl N R@EST: SM HRS. FORWARD COMMNS REGARDING LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMEN' i-
"*""***S""^*"'**'"*""'*S'"'*^*"'""'"-
TEXT CONTINUATION '. 20555. AND TO THE PAPERWORK REDUCTIOh, PROJECT (3150-0104
(
t F acuny Nane (y Domst Norter (2) LEH Nurmer 16) Page (3)
~ u w w ,
COMANCHE PEAK-UNIT 2 0 5 0 0 0l4 4 6 9 3 -
0 0 4 -
0 0 0 5 ce 0 6 i.e. - . a--c so,-.m n ;
B. ACTIONS TO PREVENT RECURRENCE j Applicable design documents and operations procedures will be updated to reflect the position and status of the valves discussed in this report. The appropriate surveillances will be performed. 7 Operations performed a review of other Unit 2 Containment penetrations as depicted j on vital station mechanical drawings. This review compared the valves associated i with each penetration to the valves listed ;n surveillance procedures. Additionally, the results of the comparison were reviewed against the DBD-ME-013 listing of these ,
valves. This review determined that the drawings, surveillance procedures and the t DBD contained the required valves and were consistent with each other.
Engineering reviewed the Design Change Notice in question and a sampling of other Design Change Notices prepared by Unit 2 Engineering (construction phase) personnel that affected DBDs. A design drawing and FSAR figure were identified to !
be incorrect. These discrepancies did not affect operability and applicable documents will be corrected. [
The Unit 2 construction program is no longer in effect. Design activities are being f performed under Unit 1/ Unit 2 procedures. Under these procedures, Engineering personnel perform IDR on plant changes. In addition, Design Modifications or Minor Modifications receive Operations impact Assessments. This process assesses the impact of a design change on Nuclear Operations programs and procedures. The two unit program has not produced errors similar to the one described in this event. ;
V. PREVIOUS SIMILAR EVENTS ;
CPSES Units 1 and 2 have submitted a number of Licensee Event Reports (LER) concerning missed surveillances. This report identifies the causes of this event to be a lack of requirements for operational reviews of design changes during Unit 2 construction and inattention to detail during the design change process. None of the previous LERs associated with missed surveillances identified the cause(s) as inadequate design control.
Although some of the LERs discussed personnel error or inattention to detail, none were related to the design change process. LER 50-445/92-015-00 " Personnel Error Leading to Potential Inoperability of Blackout Sequencer" (which did not discuss a missed l
r
Ehclosure to TXX-93238 l wc FoHM 3w,A u.5. NJC.E AR HEGudicav' GOvuis50N APPROVED OMB NO 31201*W EXPIRES:t irv02 $
ESTtMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATOh
"'"""E"; * ""' ' "**" * ""'"'" "'**"
- LICENSEE EVENT REPORT (LER) BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMEN^
TEXT CONTINUATION ""'""'"""""'""'**'""*""'***""*
DC. 20555. AND TO THE PAPERWORK REDUCTON PROJCCT (31WD104).
OFFCE OF MANAGEMENT AND BUDGET.WASHNGTON,DC.20503.
Facey Naae (1) DtxM Nurts (2) LER Nu"tser (6) Page Q)
- m- 4 m
COMANCHE PEAK-UNIT 2 0 5 0 0 0 4 4 6 9 3 -
0 0 4 -
0 0 0 6 ce 0 6 !
Test (11 f cre spum a tmaurea. <me a20numm N c Form 3t4A sp (17) l surveillance) identified the root cause and contributing factors to be related to inadequate ,
design controls; however, the causes and contributing factors were different from those described in this event. The corrective actions taken for LER-92-015-00 would not have l precluded this event.
I