ML19308D183

From kanterella
Revision as of 22:57, 21 February 2020 by StriderTol (talk | contribs) (StriderTol Bot change)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 78-005/03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity
ML19308D183
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 02/02/1978
From: Cooper J
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19308D179 List:
References
LER-78-005-03L, LER-78-5-3L, NUDOCS 8002270651
Download: ML19308D183 (2)


Text

. _- . . . _ _ _ - - - _ . ______ _ - - - _

1 .

U.S.NUCLEAA REGULAfoeY COase.assacas i N,RC i.n ,7oAas 388

~* LICENSEE EVENT REPORT EXHISIT A l j

ietsui e=Nr oA TYM ALL REQUIRED INFopMafloNa l CoNtRob StoCo i I I i 1 I IQ '

[TTTl lF 1 ,,,,.mu LI Q. R) P 3 Iglu0 l 0 l- i O Oi 0 j Og0 ; ;0 i 0lgg 4: l i1gl ; 1u lgg q _lg . , , * .

'l

, . , .,u. .. n u - ... n .. ven a r...

con v j .

i lalil

, e

[**,"c' M u

)l 0! 51ooc..,

0 -101301 w ...

21gi.o : i to ol9

,. . I 718 l@l n ,o.re a O!2 ! al2a.noI 7 I al@

> ...c. .a 4

avsNr ossCmPTICN AND PACS ASLE CoNSEQbENCES notified Unit 3 that during the performange g i n mode 1 operation, Units 1 &

I

, of the :able Tunnel Sump Pump Operability, SP-322, one of the two sump , f

, , , , , , pumpe fail ed to start contrary to Tech Spec 3.8.1.1.a. No safety hazard , ,

i

,, ,,, , as both emergency diesel generators were available and verified operable. ,

g ,, , , Breaker vr.rification SP-321 was performed satisfactorily. Maintenance 1

,,,,,, restored the sump pump operable within seven hours. Second occurrence. ~ g

,,,,,, Refer to LER 78-002/03L-0. i OE C 6 $69 Q 4 C3980%4%TECD4 3 Si. [

u,,w. it i s I@ t,,sj@ L,,Aj@ IP I Ul Mf H X[,jg@

b4C008[,,,CJ@

u (,,2,J m @

.gviticae CCC:Jte .spo.et S.E.Q.t.;

.4 s t,fi.6 =.t %C3 - ..

o.e,.3

@ ,,a.=;*j"

_u i 'I I L-.-J u

10 I O f Si

.. u y,,

iO!31 i LI a

8u W

u

=w a:n 'ww , x.u : .;:. u *i: = .zie:..

t_ zJ O I o lo 1 0 9= 1 L.L.I@ NJO Iz !@ lM 0 710 f@

g.u@g.u@ u,u@

. . . 2 . .,

CAUSE DESCMif f1 cps AND CORRICflVE ACTIONS

, , , c , g The cause of this event was to failure of the starr control bulb switch g , of the sump pump installed on 4 January 1978. The current capacity of the, t

, start switch supplied with packaged pump was inadequate. The switch was ,

l 7 , renewed with one of a higher current capacity and operability of the pump ,

, , , , , was restored. ,

's,*.'j 7 *.:ws= we= ,t.v.s @ 5'E:NSI*  : se: t.* :ss:=*t . a @

I,,+1 W @ lot 615 lgl NA l Q gl Operator obsarration l e g,,,,,, ga.,,,, u .: - n-

  • m..2%...u.:,@

n,s.- @i u ... ...m m,. .z,j (

@. .. ..u .Ly,,,1@l i

4% s o.on u i NA i tvw.ge tvet  !!S:.T*04 i n t 1 16 10 i Ol@W@l" A l

..,m.

..u ,'s'aiu=u: -.:%@

t i i- 5l 10  ! 0 i Ol@l NA I F P 11 12 33 T' ' *

  • 5 3'j',".',~48 * ' @

NA R b., @lu I

- '#c ' 5 C' u

, R g,Q*L..j .e%@

, NA f ri :::::::  : ,

e . . 2 g << o sa

] . Cocoer ,,cy, (904) 7o5 4486'

%Avs cs >=cea,

, l.

. '8002 270 ( W l

,g

. . . , , SUPPLEMENTARI INFORMATION N

1. Repor No.: 50-302/78-005/03L-0
2. Facility: CrystalRiverdnit #3
3. Raport Date: 2 February 1978
4. Occurrence Date: 9 January 1978
5. Identification of occurrence:

Failure of one cable tunnel pump sump to start creating a condition contrary to Technical Specification 3.8.1.1.a.

6. Conditions Prior to Occurrence:

Mode 1 operation.

7. Description of Occurrence:

i At 0001, the Units 1 & 2 Shift Supervisor notified Unit 3 that when performing the .

Cable Tunnel Sump Pros Operability Surveillance Procedurs SP-322, one of the two sump pumps failed c: start. The one hour Action Statement of Technical Specification 3.8.1.1. was entered md both emergency diesel generators were verified operable and the Breaker Verificacica, SP-321, was performed. Units 1 & 2 maintenance restored operability of the sump pump at 0640 and SP-322 was complaced satisfactorily.

Designation of Apparent Cause:

The current capacity of the start control bulb switch for the pump installed en 4 January 1978 was inadequate, the switch failed rendering the pump inoperable.

9. Analysis of Occurrence:

There was no safety hazard to the plant or general public as both "3A" and "33" emergency diesel generators were available and verified operable.

10. Corrective Action: -

No corrective serion necessary as installation of a start control bulb switch of adequate current capacity restored operability of the pump.

l.. Failure Data:

This is the second occurrence of this event as reported by LER 78-002/03L-0.

. p l i

l l

l . . - - . _ .