ML17286A345

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Monthly Operating Rept for Sept 1990 for WNP-2
ML17286A345
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 09/30/1990
From: Hutchison L
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
Shared Package
ML17286A344 List:
References
NUDOCS 9010160286
Download: ML17286A345 (4)


Text

OPERATING DATA REPORT WNP-2 Ol-Oct-90

1. DOCKET: 50-397
2. REPORTING PERIOD: Sep-90 OUTAGE + ON-LINE HOURS 720
3. UTILITY CONTACT: LEONARD HUTCHXSON (509) 377-2486
4. LICENSED THERMAL POWER (MWt): 3323
5. NAMEPLATE RATING (GROSS MWe): 1200.9
6. DESIGN ELECTRICAL RATING (NET MWe): 1100
7. MAXIMUM DEPENDABLE CAPACITY (GROSS MWe): 1140
8. MAXIMUM DEPENDABLE CAPACITY (NET MWe): 1095
9. XF CHANGES OCCUR ABOVE SINCE LAST REPORT, GIVE REASONS:

None.

10. POWER TO WHICH RESTRICTED, IF ANY (NET MWe):
11. REASONS FOR RESTRICTIONS, XF ANY:

MONTH YEAR CUMULATIVE

12. REPORT PERIOD HOURS 720 6551 50815.2
13. HOURS REACTOR CRITICAL 631.6 3954.2 37029.4
14. RX RESERVE SHTDWN HRS 0.0 0.0 340.4
15. HRS GENERATOR ON LXNE 602.7 3834.0 35681.7
16. UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 381.7
17. GROSS THERMAL ENERGY (MWH) 1934743 11919244 100263684
18. GROSS ELECTRICAL ENERGY (MWH) 643190 3955030 33358980
19. NET ELECTRICAL ENERGY (MWH) 616853 3779242 32065385
20. UNXT SERVICE FACTOR 83.74 58.5% 70.2%
21. UNXT AVAILABILITYFACTOR 83.74 58 5+o 71 '~o
22. UNIT CAPACITY FACTOR (MDC NET) 78.24 52 7+o 57 '~o
23. UNIT CAPACITY FACTOR (DER NET) 77.94 50.64 57.6<
24. UNIT FORCED OUTAGE RATE 16.34 3. O~o 8 ~ O~o
25. FORCED OUTAGE HOURS 117.3 117.3 3113.4 26 ~ SHUTDOWNS SCHEDULED OVER THE NEXT 6 MONTHS (TYPE g DATE ~ DURATION)

None.

27. XF CURRENTLY SHUTDOWN ESTIMATED STARTUP DATE:

9010160286 901008 PDR ADOCK 05000397 R PDC

DOCKET NO. 50-397 UNIT NAME WNP-2 DATE 9/1/90 REPCAT PERIOD Kl.

SHS 9/25/90 F Sept. I990 mcnth, year VE M<<

117.3

'mm A

Tl ~ LNIT SiIUTOONNS E%

/ REDUCTIONS MBIN COMPLETED BY TELEPi ONE (509) 377-2486 PREVE T R C fRENC Plant was forced down by low OEH control system pressure.

A broken nipple on autostop hydraulic oil system resulted I

i in decreasing OEH pressure which forced a rapid downpower with a manua] scram being initiated at 40K peer. Repairs were oade and the hydraulic system tested prior to returning unit to service.

I RH36 9/22/90 S Reduced power to perfem a control rod sequence exchange.

l. WNP-2 incurred one forced outage and one power reduction in Septetber as described above.

I SuhtWRY SYSTEM h COMPONENT F-Forced A-Equip Failure F-Admin I-Manual Exhibit F h H S-Sched Q-.Maint or Test G-Oper Error 2-Manual Scram Instructions for C-Ref ue ling H-Other 3-Auto Scram Preparation of D-Regulatory Res triction 4-Continued Data Entry Sheet E-Operator Training 5-Reduced Load Licensee Event Report

& License Examination 9-Other (LER) File (NUREG-0161)

~ ~

A

~ I ~ A GE DAILY UNIT POWER LEVEL DOCKET NO.

50-397 WNP-2 UNIT DATE 9/1/90 COMPLETED BY LB Hutchison PHONE (509) 377-2486 September 1990 MONTH DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (t~wE-Net) (MwE-Net) 1065 17. 1068

2. 1064 18. 1069 1064 19. 1066 3.

1061 20. 1068 1058 1069

5. 21.

1062 850

6. 22.

1041 895

7. 23.

1058 1045

8. 24.

1060 249

9. 25.

1063

10. 26.

1038 27 1062 '8.

12.

1067 0

13. 29.

1058 432

14. 30.

1060

15. 31.

1064 INSTRUCTIONS On this form, list 'the average daily unit power level in a(We-Net for each day in the reporting month. Compute to the nearest whole megawatt.

These figures will be used to plot a graph for each reporting month. Note that when maximum dependable capacity is used for the net electrical rating of the unit, there may be occasions when the daily average power level exceeds the 100" line (or the restricted power level line). In such cases, the average daily unit power output sheet should be footnoted to explain the apparent anomaly.