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| REPORTABLE lie 5 REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX i ~' CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX Westinghouse ~ 'I B JB IMOD Electric Coro. y SUPPLEMENTAL REPORT EXPECTED (14) 11 MONTH DAY YEAR EXPECTED jYES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). Ix NO DATE (15) | | REPORTABLE lie 5 REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX i ~' CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX Westinghouse ~ 'I B JB IMOD Electric Coro. y SUPPLEMENTAL REPORT EXPECTED (14) 11 MONTH DAY YEAR EXPECTED jYES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). Ix NO DATE (15) |
| ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) | | ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) |
| On November 22, 1998, at 04:30, with Unit 1 at 28% power, control room annunciators alarmed indicating an incorrect level in steam generator (SG) "B" and a feedwater/steam flow mismatch. In response to an apparent increase in steam flow, the main feedwater regulating valve, 1-FW-FCV-1488, began to open further. Although a control room operator began to manually control 1-FW-FCV-1488 to try to prevent a high level condition, the "B" SG reached its high level turbine trip setpoint. The Unit 1 turbine automatically tripped, which was immediately followed by an automatic reactor trip. When the reactor coolant system cooled to the low average temperature (low Tavg) setpoint of 543°F, a safety injection (SI) actuation occurred. The SI initiation resulted from the low T avg condition coincident with an apparent high steam flow condition. The SI actuation was spurious since it resulted from an invalid signal. The event was caused by a short circuit in the summator for the main steam line "C" loop channel 111 flow transmitter. Root Cause Evaluation recommendations, designed to prevent the recurrence of a similar event, were implemented. The NRC was notified pursuant to 1O CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report I | | On November 22, 1998, at 04:30, with Unit 1 at 28% power, control room annunciators alarmed indicating an incorrect level in steam generator (SG) "B" and a feedwater/steam flow mismatch. In response to an apparent increase in steam flow, the main feedwater regulating valve, 1-FW-FCV-1488, began to open further. Although a control room operator began to manually control 1-FW-FCV-1488 to try to prevent a high level condition, the "B" SG reached its high level turbine trip setpoint. The Unit 1 turbine automatically tripped, which was immediately followed by an automatic reactor trip. When the reactor coolant system cooled to the low average temperature (low Tavg) setpoint of 543°F, a safety injection (SI) actuation occurred. The SI initiation resulted from the low T avg condition coincident with an apparent high steam flow condition. The SI actuation was spurious since it resulted from an invalid signal. The event was caused by a short circuit in the summator for the main steam line "C" loop channel 111 flow transmitter. Root Cause Evaluation recommendations, designed to prevent the recurrence of a similar event, were implemented. The NRC was notified pursuant to 10 CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report I |
| is being submitted pursuant to 10 CFR 50.73 (a)(2)(iv). | | is being submitted pursuant to 10 CFR 50.73 (a)(2)(iv). |
| NRC FORM 366 (6-1998) | | NRC FORM 366 (6-1998) |
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| * "C" SG steam line pressure indication was lower than the actual value. | | * "C" SG steam line pressure indication was lower than the actual value. |
| * "B" SG steam line flow was indicated when no flow was present. | | * "B" SG steam line flow was indicated when no flow was present. |
| The NRC was notified pursuant to 1O CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report is being submitted pursuant to 1O CFR 50.73 (a)(2)(iv) as an event that resulted in the automatic actuation of engineered safety features and the reactor protection system. | | The NRC was notified pursuant to 10 CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report is being submitted pursuant to 10 CFR 50.73 (a)(2)(iv) as an event that resulted in the automatic actuation of engineered safety features and the reactor protection system. |
| NRG FORM 366A (6-1998) | | NRG FORM 366A (6-1998) |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
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[Table view] Category:RO)
MONTHYEARML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. 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Procedures Revised ML18153A1971997-11-26026 November 1997 LER 97-012-00:on 971028,loss of Power to Latching Mechanism on Several Doors Occurred.Caused by Tripping of Breaker in Security Distribution Panel in Central Alarm Station (CAS) Panel.Breakers in Affected CAS Panel Reset ML18153A1921997-11-25025 November 1997 LER 97-010-00:on 971028,discovered Missed Fire Protection Surveillance Pt.Caused by Personnel Error.Satisfactorily Completed PT Procedure 0-OPT-FP-009 & Diesel Driven Fire Pump 1-FP-P-2 Declared operable.W/971125 Ltr ML18153A1831997-11-12012 November 1997 LER 97-009-00:on 971014,declared Intake Canal Level Probes Inoperable Due to Marine Growth.Cause Indeterminate.Divers Inspected,Cleaned & Returned Probes to Operable Status & Initiated Interdepartmental Team to Investigate Cause ML18153A1791997-11-0707 November 1997 LER 97-008-00:on 971011,invalid Actuation of ESF Occurred. Caused by Personnel Errors.Main CR Bottled Air Sys Isolated & Containment Hydrogen Analyzer Heat Tracing Actuation Signal Reset ML18153A1721997-10-30030 October 1997 LER 97-007-00:on 970930,determined That Plant Was Outside App R Design Basis Due to Vital Bus Isolation Issue.Caused by Personnel Error.Installed Circuit Protective Device During Oct 1997 Refueling Outage ML18153A1421997-06-10010 June 1997 LER 97-001-01:on 970123,shutdown Occurred Due to Drain Line Weld Leak.Inspected & Tested Turbine Trip Actuation circuitry.W/970610 Ltr ML18153A1391997-05-28028 May 1997 LER 97-005-00:on 970502,Unit 1 Power Range Nuclear Instrumentation Was Inoperable Due to Personnel Error.Sro & STA That Were Involved in Event Were Counseled ML18153A1291997-04-18018 April 1997 LER 97-006-00:on 970320,loss of Refueling Integrity Due to Inadequate Containment Closure Process & Verification.Fuel Movement Stopped IAW Action Statement Requirements of TS 3.10.B.W/970418 Ltr ML18153A1281997-04-15015 April 1997 LER 97-004-00:on 970317,main Steam Safety Valve Was Outside as Found Setpoint Tolerance.Specific Cause Unknown,However, Minor Setpoint Drift Can Be Expected.No Immediate Corrective Actions performed.W/970415 Ltr ML18153A1241997-04-0808 April 1997 LER 97-002-01:on 970116,one Train of Auxiliary Ventilation Sys Was Inoperable Outside of Ts.Caused by Personnel Error. Submitted Deviation Rept Re Reverse Rotation of Fan & Work Request to Adjust linkage.W/970408 Ltr ML18153A1191997-03-19019 March 1997 LER 97-001-00:on 970218,manual Reactor Trip & ESF Actuation Occurred Due to Loss of EHC Control Power.Caused by Momentary Short.Relay Card Was replaced.W/970319 Ltr ML18153A1201997-03-19019 March 1997 LER 97-003-00:on 970219,loss of Pressurizer Heaters Resulted in Manual U1 Trip & U2 ESF Actuation.Caused by Loss of Group C Pressurizer Proportional Heaters.Reactor Trip Breakers Were Verified open.W/970319 Ltr ML18153A1131997-02-20020 February 1997 LER 97-001-00:on 970123,shutdown Occurred Due to Steam Drain Line Weld Leak.Management Was Notified & Shift Supervisor Invoked Requirements of TS 4.15.C.1.W/undtd Ltr ML18153A1101997-02-13013 February 1997 LER 97-002-00:on 970116,one Train of Auxiliary Ventilation Sys Declared Inoperable.Caused by Personnel Error.Properly Adjusted Damper 1-VS-MOD-58B & Exited Seven Day LCO on 970116.W/970214 Ltr ML18153A0951997-01-0202 January 1997 LER 97-002-00:on 961213,automatic Reactor Trip Occurred During Planned Shutdown.Caused by Steam Flow/Feedwater Flow Mismatch.Rps Functioned as Designed & Plant Placed in Hot Shutdown ML18153A0931996-12-12012 December 1996 LER 96-008-00:on 961112,water Gas Decay Tank Oxygen Analyzer Pressure Sensors Inoperable Due to Vendor Supplied Equipment Not Meeting Procurement specifications.Post-implementation Procedures Revised & Transducers replaced.W/961212 Ltr ML18153A0691996-09-19019 September 1996 LER 96-007-00:on 960821,failed to Complete Fire Detection Zone Inspections within Required Time Period.Caused by Personnel Error.Counseled Personnel Re Fire Detection Zone Inspections & Revised Fire Watch training.W/960920 Ltr ML18153A0481996-08-26026 August 1996 LER 96-005-00:on 960803,manual Reactor Trip.Caused by Loss of Electro Hydraulic Control Pressure.Repaired Two Compression Fitting Union Connections on Leaking Fitting & Performed Evaluations on Other tubing.W/960826 Ltr ML18153A0521996-08-20020 August 1996 LER 96-004-01:on 960510,discovered Hydrogen Analyzers Inoperable.Caused by Procedural Deficiencies.Implemented Permanent Changes to Hydrogen Analyzer Instrument Calibr Procedures.W/960820 Ltr ML18153A0321996-07-30030 July 1996 LER 96-006-01:on 960618,anti-corrosion Coating Had Not Been Reapplied to Station Battery 2B.Caused by Procedural Error in That Verbatim TS Compliance Not Reflected in Procedures. Coating Was Applied to batteries.W/960730 Ltr ML18153A0281996-07-17017 July 1996 LER 96-006-00:on 960618,failed to Apply anti-corrosion Coating to Station Battery 2B.Caused by Procedural Error. Applied anti-corrosion Coating to Batteries & Revised TS 4.6.C.1.f Re Battery Coating requirements.W/960717 Ltr ML18153A0141996-07-0202 July 1996 LER 96-004-00:on 960606,turbine/reactor Trip Occurred.Caused by High Level in Steam Generator B.Placed Plant in Hot Shutdown Condition,Calculated Shutdown Margin & Monitored Critical Safety Function Status trees.W/960702 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18152A2811999-10-12012 October 1999 Technical Basis for Elimination of Nozzle Inner Radius Insps (for Nozzles Other than Reactor Vessel),Technical Basis for ASME Section XI Code Case N-619. ML18152B3531999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Surry Power Station,Units 1 & 2.With 991012 Ltr ML18152B6651999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Surry Power Station Units 1 & 2.With 990915 Ltr ML18152B4421999-08-27027 August 1999 LER 99-006-00:on 990802,determined That Plant Was Outside of App R Design Basis Due to Fire Barrier Deficiencies. Caused by Original Plant Design Deficiencies.Fire Watches Were Established & Mods Have Been Completed.With 990827 Ltr ML18152B4411999-08-27027 August 1999 LER 99-005-00:on 990731,effluent Radiation Monitors Were Declared Inoperable.Caused by Degraded Heat Trace Circuits for Monitors Sample Suction Line.Degraded Heat Trace Circuit Was Replaced & Addl Heat Trace Is Being Installed ML18151A3981999-08-13013 August 1999 SPS Unit 2 ISI Summary Rept for 1999 Refueling Outage. ML18152B3771999-08-13013 August 1999 LER 99-004-00:on 990714,TS Violation Due to non-safety Related Fans Effect on CR Boundary Was Noted.Cause of Event Has Not Yet Been Determined.Cable Spreading Room Doors Were Operned to Reduce Pressure in Rooms ML18152B3791999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Surry Power Station,Units 1 & 2.With 990811 Ltr ML18152B3911999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Surry Power Station,Units 1 & 2.With 990713 Ltr ML18152B4341999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Surry Power Station,Units 1 & 2.With 990614 Ltr ML20195E2401999-05-31031 May 1999 Rev 2 to COLR for SPS Unit 2 Cycle 16 Pattern Ag ML18152B4181999-05-18018 May 1999 LER 99-002-00:on 990425,MSSVs Tested Out of Tolerance for as Found Setpoint.Caused by Minor Setpoint Drift.No Immediate Action Required.Deviation Rept Submitted for Each Valve.With 990518 Ltr ML18152B4161999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Surry Power Station Units 1 & 2.With 990512 Ltr ML18152B4111999-04-28028 April 1999 LER 99-003-00:on 990331,potential Loss of Charging Pumps Was Noted.Caused by Main CR Fire.Station Deviation Was Issued on 990331.With 990428 Ltr ML18152B6511999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Surry Power Station Units 1 & 2 ML18153A2741999-03-29029 March 1999 LER 99-002-00:on 990301,prematurely Released Fire Watches Resulted in Violation of TS 3.21.B.7.Caused by Inadequate Procedure.Procedure for Opening & Sealing Fire Stops Was Revised on 990212 ML18153A2681999-03-19019 March 1999 LER 98-013-01:on 981122,turbine/reactor Tripped on High Due to Short Circuit in Summator for MSL C Loop Channel III Flow Transmitter.Replaced 1-MS-FT1494 Summator & Module Repair Procedure Revised.With 9903190 Ltr ML18152B7331999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Surry Power Station,Units 1 & 2.With 990310 Ltr ML18152B5421999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Surry Power Station,Units 1 & 2.With 990210 Ltr ML18151A3031999-01-29029 January 1999 ISI Summary Rept for 1998 Refueling Outage,Including Form NIS-1, Owners Rept for ISIs & Form NIS-2, Owners Rept for Repairs & Replacements. ML18152B7261999-01-21021 January 1999 LER 99-001-00:on 981222,auxiliary Feedwater Pipe Support Missed Surveillance.Caused by Personnel Error.Station Deviation Rept Was Submitted.Two Supports in Question Received Required Code Insp & Were Found Acceptable ML18152B6011998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Surry Power Station,Units 1 & 2.With 990115 Ltr ML18152B5781998-12-16016 December 1998 LER 98-014-00:on 981126,manual Reactor Trip in Response to Main Feedwater Regulating Valve Failure Occurred.Caused by Dislocation of Retaining Clip in Positioner.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B5811998-12-16016 December 1998 LER 98-013-00:on 981122,turbine/reactor Trip on High SG Level Occurred.Caused by Instrument Failure.Control Room Operators Placed Unit in Safe,Shutdown Condition ML18152B7121998-12-0404 December 1998 LER 98-S01-00:on 981105,noted Failure to Deactivate Station Access Badge.Caused by Human Error.Licensee Will Now Deactivate Station Badges Before Clearance Is Revoked & Process for Badge Deactivations Have Been Strengthened ML18152B7041998-12-0101 December 1998 LER 98-012-00:on 981102,noted That EDGs Were Concurrently Inoperable.Caused by Required Testing Per TS 3.16.B.1.a.2. Redundant EDG Was Returned to Svc within Two Hour Period, Following Satisfactory Testing.With 981201 Ltr ML18152B7081998-11-30030 November 1998 Rev 0 to COLR for Surry 1 Cycle 16,Pattern Un. ML18152B5721998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Surry Power Station,Units 1 & 2.With 981214 Ltr ML18152B6161998-11-0606 November 1998 LER 98-011-00:on 981008,diesel Driven Fire Pump Failed to Start During Performance of Monthly Operability Test.Caused by Faulty Overspeed Trip Device Failure.Diesel Driven Fire Pump Declared Inoperable ML18152B6241998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Surry Power Station Units 1 & 2.With 981111 Ltr ML18152B6081998-10-23023 October 1998 LER 98-010-01:on 980715,intake Canal Level Probes Were Inoperable Due to Marine Growth.Caused by Design of Canal Level Instrumentation.Canal Level Probes Will Continue to Be Monitored More Closely ML18152B6881998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Surry Power Station Units 1 & 2.With 981012 Ltr ML18153A3271998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Surry Power Station,Units 1 & 2 ML18152B7811998-07-31031 July 1998 LER 98-010-00:on 980715,low Intake Canal Level Instrument Channel I Was Declared Inoperable to Allow Testing of Intake Canal Level Probe 1-CW-LE-102.Subject Probe Was Cleaned by Diver,Tested & Channel I Was Returned to Operable Status ML18153A3161998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Surry Power Station Units 1 & 2.W/980807 Ltr ML18152B7621998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Surry Power Station,Units 1 & 2.W/980707 Ltr ML18153A2581998-06-0303 June 1998 LER 98-009-00:on 980509,nonisolable Leak of Reactor Coolant Pump Seal Injection Line Weld,Was Discovered.Caused by Lack of Fusion or Thermal Fatigue Coupled W/Vibration Stress Due to Loose Rod Hanger.Rcp Seal Injection Line Removed ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML18153A3141998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Surry Power Station,Units 1 & 2.W/980610 ML18152B8241998-05-22022 May 1998 LER 98-008-00:on 980228,auxiliary Ventilation Fans Were Noted in Condition Outside of Design Basis.Caused by Failure to Recognize Potential Impact of Certain Design Basis Accident Scenarios.No Corrective Actions Needed ML18152B8161998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Surry Power Station Units 1 & 2.W/980508 Ltr ML18152B7951998-04-29029 April 1998 LER 98-007-00:on 980330,radiation Monitors Were Declared Inoperable.Caused by Change in Operating Temperature Range. Preplanned Alternate Method of Monitoring Was Initiated IAW TS Table 3.7-6 ML18153A2511998-04-22022 April 1998 LER 98-006-00:on 980324,unisolable Through Wall Leak of RCP Thermowell Was Noted.Cause of Leak Is Unknown.Rtd Will Be Replaced ML18153A2521998-04-22022 April 1998 LER 98-005-01:on 980212,fire Watch Insp Exceeded One Hour. Caused by Lack of Attention to Detail by Individual Involved.Individual Involved Was Coached on Requirement to Perform Fire Watch Patrols within Required Time Frame ML20217P9941998-04-0707 April 1998 Safety Evaluation Granting Licensee Third 10-yr Inservice Insp Program Relief Requests SR-018 - Sr-024 ML18153A2951998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Sps,Units 1 & 2.W/ 980408 Ltr ML18153A2391998-03-13013 March 1998 LER 98-005-00:on 980212,fire Watch Insp Frequency Exceeded One H Occurred.Category 2 Root Cause Evaluation Being Conducted to Determine Cause of Event.Station Deviation Issued ML18153A2341998-03-0909 March 1998 LER 98-003-00:on 980226,no Procedural Guidance for Maintaining EDG Minimum Fuel Supply During Loop,Was Identified.Caused by Absence of Procedural Instructions. Deviation Rept Submitted to Document Deviating Condition ML18153A2301998-03-0606 March 1998 LER 98-004-00:on 980206,fire Watch Was Released Prematurely Resulting in Violation of Ts.Caused by Inadequate Planning of Repair Activity.Work Orders Will Include Ref to Applicable Procedures Developed to Assist in Repairs ML18153A2251998-03-0404 March 1998 LER 98-002-00:on 980202,automatic Turbine Trip Resulted in Automatic Reactor Trip.Caused Degraded Generator Voltage Regulator sub-component Failure.Placed Plant in Safe Hot SD & Replaced Intermittent Relay & Relay Socket 1999-09-30
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10CFR50.73 Virginia Electric And Power Company Surry Power Station 5570 Hog Island Road Surry, Virginia 23883 March 19, 1999 U. S. Nuclear Regulatory Commission Serial No.: 98-726A Attention: Document Control Desk SPS: BCB Washington, D. C. 20555 Docket No.: 50-280 License No.: DPR-32
Dear Sirs:
Pursuant to 10 CFR 50.73, Virginia Electric and Power Company hereby submits the following Licensee Event Report applicable to Surry Power Station Unit 1.
Report No. 50-280/1998-013-01 This report has been reviewed by the Station Nuclear Safety and Operating Committee and will be forwarded to the Management Safety Review Committee for its review.
Very truly yours, E. S. Grecheck Site Vice President Enclosure Commitments contained in this letter: None 9903300383 990319 PDR ADOCK 05000280 S PDR
e cc: U. S. Nuclear Regulatory Commission Region II Atlanta Federal Center 61 Forsyth Street, SW, Suite 23T85 Atlanta, Georgia 30303 Mr. R. A. Musser NRG Senior Resident Inspector Surry Power Station
e e NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB NO. 3150-0104 EXPIRES 06/30/2001 (6-1998) Estimated burden per response to comply with this mandatory information collection request: 50 hrs. Reported lessons learned are incorporated into LICENSEE EVENT REPORT (LER) the licensing process and fed back to industry. Forward comments regarding burden estimate to the Records Management Branch (T-6 F33),
U.S. Nuclear Regulatory Commission. Washington, DC 20555-0001, and to (See reverse for required number of the Paperwork Reduction Project (3150-0104), Office of Management and digits/characters for each block) Budget, Washington, DC 20503. If an information collection does not display acurrently valid 0MB control number. the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE(3)
SURRY POWER STATION, Unit 1 05000-280 1 OF 4 TITLE(4)
Turbine/Reactor Trip on High Steam Generator Level Due to Instrument Failure EVENT DATE (5) LER NUMBER 6) REPORT DATE (7) OTHER FACILITIES INVOLVED 8)
MONTH DAY YEAR YEAR ISEQUENTIAL NUMBER REVISION NUMBER MONTH DAY YEAR FACILITY NAME DOCKET NUMBER 05000 --
FACILITY NAME DOCKET NUMBER 11 22 1998 1998 - 013 -- 01 03 19 1999 n~nnn --
I OPERATING I THIS REPORT IS SUBMITIED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) (11)
MODE {9) N I 20.2201(b) 20.2203(a)(2)(v) 50.73(a)(2l(il 50.73(aH2Hviii) 20.2203(a)(1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50. 73(a)(2)(x) 0 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203/a\(4) X 50.73(a)(2Hivl OTHER
-NAME 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 50.36(c)(1 l 50.36(c)(2)
LICENSEE CONTACT FOR THIS LER (12)
E. S. Grecheck, Site Vice President
- 50. 73(aH2Hv) 50.73(a)(2)(vii)
TELEPHONE NUMBER (Include Area Code)
(757) 365-2000 Specify in Abstract below or in NRC Form 366A COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABLE lie 5 REPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX i ~' CAUSE SYSTEM COMPONENT MANUFACTURER TO EPIX Westinghouse ~ 'I B JB IMOD Electric Coro. y SUPPLEMENTAL REPORT EXPECTED (14) 11 MONTH DAY YEAR EXPECTED jYES SUBMISSION (If yes, complete EXPECTED SUBMISSION DATE). Ix NO DATE (15)
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On November 22, 1998, at 04:30, with Unit 1 at 28% power, control room annunciators alarmed indicating an incorrect level in steam generator (SG) "B" and a feedwater/steam flow mismatch. In response to an apparent increase in steam flow, the main feedwater regulating valve, 1-FW-FCV-1488, began to open further. Although a control room operator began to manually control 1-FW-FCV-1488 to try to prevent a high level condition, the "B" SG reached its high level turbine trip setpoint. The Unit 1 turbine automatically tripped, which was immediately followed by an automatic reactor trip. When the reactor coolant system cooled to the low average temperature (low Tavg) setpoint of 543°F, a safety injection (SI) actuation occurred. The SI initiation resulted from the low T avg condition coincident with an apparent high steam flow condition. The SI actuation was spurious since it resulted from an invalid signal. The event was caused by a short circuit in the summator for the main steam line "C" loop channel 111 flow transmitter. Root Cause Evaluation recommendations, designed to prevent the recurrence of a similar event, were implemented. The NRC was notified pursuant to 10 CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report I
is being submitted pursuant to 10 CFR 50.73 (a)(2)(iv).
NRC FORM 366 (6-1998)
e e NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) DOCKET (2) LEA NUMBER 16) PAGE (3)
YEAR I SEQUENTIAL NUMBER REVISION NUMBER SURRY POWER STATION, Unit 1 05000 -- 280 1998 - 013 -- 01 2 OF 4 TEXT (If more space is required, use additional copies of NRG Form 366A) (17)
1.0 DESCRIPTION
OF THE EVENT On November 22, 1998, at 04:30, with Unit 1 at 28% power, control room annunciators
[EIIS-IB] alarmed indicating an incorrect level in steam generator (SG) "B" [EIIS-AB,SG]
and a difference between the feedwater and steam flow parameters. In response to an apparent increase in steam flow, the main feedwater regulating valve [EIIS-SJ,FCV],
- 1-FW-FCV-1488, began to open further. Although a control room operator began to manually control 1-FW-FCV-1488 to fry to prevent a high level condition, the "B" SG reached its high level turbine trip setpoint. As designed, the Unit 1 turbine [EIIS-TA,TRB]
automatically tripped, which was immediately followed by an automatic reactor trip
[EIIS-JC].
The auxiliary feedwater pumps [EIIS-BA-P] started as designed and provided flow to the SGs. When the reactor coolant system (RCS) cooled to the low average temperature I
(low Tavg) setpoint of 543°F, a safety injection (SI) [EIIS-BQ] actuation occurred. The SI initiation resulted from the low Tavg condition coincident with an apparent high steam flow condition (one steam flow instrumentation channel,[EIIS-JB,CHA] for each of SGs "A" and "C" had been placed in the tripped condition, prior to the event, to facilitate system maintenance). Emergency diesel generators (EDG) [EIIS-EK,EDG] Nos. 1 and 3 automatically started upon SI initiation. Following verification that the SI actuation had been spurious, the SI was terminated and the EDGs were shutdown.
The RCS reached a minimum temperature of approximately 535°F and subsequently stabilized at 547°F. The reactivity shutdown margin was calculated following the RCS cooldown to ensure that Technical Specification and administrative shutdown margin limits were satisfied.
The following discrepancies were noted during the post-trip response:
- Intermediate position was indicated in the control room when 1-FW-FCV-1488 was fully closed.
- "C" SG steam line pressure indication was lower than the actual value.
- "B" SG steam line flow was indicated when no flow was present.
The NRC was notified pursuant to 10 CFR 50.72 (b)(2)(ii) on November 22, 1998 at 07:20. This report is being submitted pursuant to 10 CFR 50.73 (a)(2)(iv) as an event that resulted in the automatic actuation of engineered safety features and the reactor protection system.
NRG FORM 366A (6-1998)
e e NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) D0CKET(2) LEA NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER I REVISION NUMBER SURRY POWER STATION, Unit 1 05000 -- 280 1998 - 013 -- 01 3 OF 4 TEXT (If more space is required, use additional copies of NRG Form 366A). (17) 2.0 SIGNIFICANT SAFETY CONSEQUENCES AND IMPLICATIONS This event resulted in no safety consequences or implications. The SI actuation was spurious since it resulted from an invalid signal (i.e., an actual high steam flow condition did not exist). Appropriate operator actions were taken in accordance with emergency operating procedures to ensure the performance of system automatic actions and to respond to abnormal conditions. The. unit was quickly brought to a stable, no-load condition. Therefore, the health and safety of the public were not affected at any time during this event.
3.0 CAUSE
- A Category 1 Root Cause Evaluation (RCE) was initiated on November 22, 1998, to determine the cause of this event and to recommend corrective actions. The. RCE concluded that the event was caused by a short circuit in the summator for the main steam line "C" loop channel Ill flow transmitter [EIIS-JB,FIT], 1-MS-FT-1494. The short circuit resulted in circulating ground currents which caused the "B" loop channel Ill steam flow parameter to be greater than the actual value. The "B" loop channel Ill was affected through its power supply, which is common to the "C" loop channel Ill. As a result of the false steam flow indication, 1-FW-FCV-1488 opened rapidly to increase feedwater flow to the "B" SG. The level in the "B" SG increased to the high level turbine trip setpoint before control room operators could intervene.
The 1-MS-FT-1494 summator had been replaced and was in the process of being returned to service when the event occurred. The RCE investigation revealed that the module repair testing procedure did not include the defective portion of the summator's circuit board. As a result, the fault was not identified before installation.
4.0 IMMEDIATE CORRECTIVE ACTION($)
Following the reactor trip, control room operators acted promptly to place the unit in a safe, shutdown condition in accordance with emergency and other operating procedures.
The Shift Technical Advisor monitored the critical safety function status trees to ensure that plant parameters remained acceptable.
NRC FORM 366A (6-1998)
" e e NRC FORM 366A U-5. NUCLEAR REGULATORY COMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1) D0CKET(2) LEA NUMBER (6) PAGE (3)
YEAR I SEQUENTIAL NUMBER I REVISION NUMBER SURRY POWER STATION, Unit 1 05000 -- 280 1998 - 013 -- 01 4 OF 4 TEXT (If more space is required, use additional copies of NRG Form 366A) (17) 5.0 ADDITIONAL CORRECTIVE ACTIONS The1-MS-FT-1494 summatorwas replaced. The installation of a new summator corrected the "C" SG steam line pressure and "B" SG steam line flow indication discrepancies.
The limit switches[EIIS-ZIS] for 1-FW-FCV-1488 were adjusted and the valve was tested satisfactorily.
The RCE team evaluated unit conditions and systems response contributing to the RCS cooldown following the reactor trip. The team concluded that the cooldown was normal considering: 1) the decay heat load was approximately 15% of the full-power equilibrium value (the event occurred at the beginning of reactor core life and the unit had been at power, below 30%, for less than one day), 2) SG "B" had been overfed as the unit responded to the apparent increase in steam flow, and 3) the cooling effect of auxiliary feedwater flow.
6.0 ACTIONS TO PREVENT RECURRENCE The module repair testing procedure was revised to include the defective portion of the summator's circuit board. Spare modules were tested in accordance with the revised procedure.
7.0 SIMILAR EVENTS None 8.0 MANUFACTURER/MODEL NUMBER Westinghouse Electric Corporation Signal Summator Assembly No. 4111084-001 9.0 ADDITIONAL INFORMATION Unit 1 was returned to service on November 23, 1998.
Unit 2 was operating at 100% power and was not affected by this event.
NRC FORM 366A (6-1998)