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{{#Wiki_filter:.r AC CELZRATZD DISTRIBUTION DEMONSTRATION SYSTEM  
{{#Wiki_filter:. r AC CELZRATZD         DISTRIBUTION       DEMONSTRATION           SYSTEM REGULATORY INFORMATION DIST      TION SYSTEM (RIDS)
ACCESSION NBR:8809220139      DOC.DATE: 88/        NOTARIZED: NO          DOCKET g FACIL:STN-50-528 Palo Verde Nuclear Statio ,      Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station,    Unit 2, Arizona Publi Palo Verde Nuclear Station,    Unit 3, Arizona Publi 05000530 05000529"'TN-50-530
                                                                                                  ~
AUTH. NAME        AUTHOR AFFILIATION                                                        )'l BLOOM,T.J.        Arizona Nuclear Power  Project (formerly Arizona Public Serv "~
HAYNES,J.G.        Arizona Nuclear Power  Project (formerly Arizona Public Serv,(
RECIP.NAME        RECIPIENT AFFILIATION R


==SUBJECT:==
==SUBJECT:==
Monthly operating repts for Aug.1988 fo alo Verde Nuclear Generating Station Unit 1,2&3.880 3 tr.DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL (SIZE:/~TITLE: Monthly Operating Report (per Tech Spec/s D 8 05000528"'5000529
Monthly operating repts for Aug. 1988 fo       alo Verde Nuclear                       I Generating Station Unit 1,2 & 3. 880 3         tr.
/05000530 A 4 D NOTES:Standardized plant.Standardized plant.Standardized plant.RECIPIENT ID CODE/NAME PD5 PD DAVIS,M RECIPIENT ID CODE/NAME PD5 LA CHAN,T LICITRA,E COPIES LTTR ENCL 5 5 1 0 COPIES LTTR ENCL 1 0 1 0 1 0 D'r j S REGULATORY INFORMATION DIST TION SYSTEM (RIDS)ACCESSION NBR:8809220139 DOC.DATE: 88/NOTARIZED:
DISTRIBUTION CODE: IE24D     COPIES RECEIVED:LTR     ENCL   ( SIZE: /~                       D TITLE: Monthly Operating   Report (per Tech Spec/s 8
NO DOCKET g FACIL:STN-50-528 Palo Verde Nuclear Statio , Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529"'TN-50-530 Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530~AUTH.NAME AUTHOR AFFILIATION
NOTES:Standardized   plant.
)'l BLOOM,T.J.
Standardized plant.
Arizona Nuclear Power Project (formerly Arizona Public Serv"~HAYNES,J.G.
Standardized plant.
Arizona Nuclear Power Project (formerly Arizona Public Serv,(RECIP.NAME RECIPIENT AFFILIATION R I INTERNAL: ACRS AEOD/DS P/TPAB NRR/DLPQ/PEB 11 NRR/~DRBP/
05000528"'5000529 05000530
PB 10 REG EZLE 01 10 10 1 1 1 1 1 1 1 1 AEOD/DOA ARM TECH ADV NRR/DOEA/EAB ll NUDOCS-ABSTRACT RGN5 1 1 2 2 1 1 1 1 1 1 EXTERNAL: EGGG WILLIAMS, S NRC PDR NOTES 1 1 1 1 LPDR NSIC 1 1 1 1 R I, D 8;ji A D;$TOTAL NUMBER OF COPIES REQUIRED: LTTR 34 ENCL 30 f1P NRC MONTHLY OPERATING REPORT DOCKET NO.50-528 UNIT NAME PVNGS-1 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 OPERATING STATUS 1.2.3.4.5.6.7.8.9.10.Unit Name: Palo Verde Nuclear Generatin Station Unit 1 Reporting Period: Au ust 1988 Licensed Thermal Power (MWt): 3800 Nameplate Rating (Gross MWe): 1403 Design Electrical Rating (Net MWe): 1270 Maximum Dependable Capacity (Gross MWe): 1303 Maximum Dependable Capacity (Net MWe):~122 If Changes Occur In Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons: N A Power Level to Which Restricted, If Any (Net MWe): None Reasons For Restrictions, If Any: N A This Month Cumulative 22 728 0 12 812 1 Yr.-to-Date 744 0 5 856 0 2 834 9 Hours in Reporting Period Number of Hours Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy Generated (MWH)Gross Electrical Energy Generated (MWH)Net Electrical Energy Generated (MWH)Unit Service Factor Unit Availability Factor Unit Capacity Factor (Using MDC Net)Unit Capacity Factor (Using DER Net)Unit Forced Outage Rate Shutdowns Scheduled Over'Next one 11, 12.124 0 13.0 0 0 0 0 0 2 659.8 12 376 9 30 5 14.15.0 0 0 0 0 0 16.44 643 529 0 15 485 200 0 9 610 692 0 69 686.0 17.11 200.0 3 341 900.0 18.14 447 94 0 3 119 869 0 0 0 45 4 54 5 4 1 19'0.21 54.5%45 4a 4 1 52 1 43 6 0 0 22.50 1 N~IAGI'u SO YiOG.OO (OIO SO 25.8u MQ OQ%6X Q OK 00Cl 690.E'409 32.0 6 Months (Type, Date, and Duration of Each): of Startup: 0 INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION Achieved 05 25 85 Forecast~05 85~06 85~11 85~06 10 85 01/128 86~~Zf.((A/2264A If Shutdown At End of Report Period, Estimated Date N A
                                                                                                  /
~~4 IL AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.50-528 UNIT NAME PVNGS-1 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 MONTH: AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 17 18 19 20 21 191 22 23 24 0 25 10 26 27 12 28 0 13 29 30 15 31 145 16 fl REFUEL'ING INFORMATION DOCKET NO.50-528 UNIT NAME PVNGS-1 DATE , i09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 1.Scheduled date for next refueling shutdown.03/21/89 2.Scheduled date for restart following refueling.
A 4
05/29/89 3.Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
RECIPIENT         COPIES          RECIPIENT        COPIES                        D ID CODE/NAME       LTTR ENCL      ID CODE/NAME       LTTR ENCL PD5 LA               1    0    PD5 PD                5    5 CHAN,T               1     0   DAVIS,M                1   0                         D'r LICITRA,E            1    0                                                              j S
To be determined 4.Scheduled date for submitting proposed licensing action and supporting information.
INTERNAL: ACRS                 10  10    AEOD/DOA              1    1 AEOD/DS P/TPAB NRR/DLPQ/PEB 11 NRR/~DRBP/ PB 10 1
1 1
1 1
1 ARM TECH ADV NRR/DOEA/EAB NUDOCS-ABSTRACT ll    2 1
1 2
1 1
REG EZLE      01    1     1   RGN5                  1   1 EXTERNAL: EGGG WILLIAMS,S       1     1   LPDR                  1   1 NRC PDR              1     1   NSIC                  1   1 NOTES R
I, D
8; ji A
D;
                                                                                                $
TOTAL NUMBER OF COPIES REQUIRED: LTTR       34   ENCL   30
 
f1 P
 
NRC MONTHLY OPERATING REPORT DOCKET NO. 50-528 UNIT NAME   PVNGS-1 DATE         09 09 88 COMPLETED BY T J     Bloom TELEPHONE     602   371-4187 OPERATING STATUS
: 1. Unit Name:   Palo Verde Nuclear Generatin Station Unit 1
: 2. Reporting Period: Au ust 1988
: 3. Licensed Thermal Power (MWt): 3800
: 4. Nameplate Rating (Gross MWe): 1403
: 5. Design Electrical Rating (Net MWe):         1270
: 6. Maximum Dependable Capacity (Gross MWe): 1303
: 7. Maximum Dependable Capacity (Net MWe):       ~122
: 8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)
Since Last Report, Give Reasons:   N A
: 9. Power Level   to Which Restricted, If Any (Net   MWe): None
: 10. Reasons For Restrictions, If Any: N A This Month           Yr.-to-Date         Cumulative 11,    Hours  in Reporting Period            744 0                 5 856 0           22 728 0
: 12. Number of Hours Reactor Was Critical                         124 0                2 834 9            12 812 1
: 13. Reactor Reserve Shutdown Hours                                   0 0                     0 0                 0 0
: 14. Hours Generator On-Line                30 5                2 659.8           12 376 9
: 15. Unit Reserve Shutdown Hours                                    0 0                     0 0                 0 0
: 16. Gross Thermal Energy Generated (MWH)                        69 686.0         9 610 692 0         44 643 529 0
: 17. Gross Electrical Energy Generated (MWH)                        11 200.0         3 341 900.0         15 485 200 0
: 18. Net Electrical Energy Generated (MWH)                          0 0             3 119 869 0         14 447 94 0 19    Unit Service Factor                      4 1                45 4                 54 5
          '0.
Unit Availability Factor                4 1                45 4a                54.5%
21    Unit Capacity Factor (Using MDC Net)                          0 0                43 6                52 1
: 22. Unit Capacity Factor
'uN
~IAGI (Using DER Net)
Unit Forced Outage Rate 50 1 32.0 YiOG.         Shutdowns Scheduled Over 'Next  6 Months (Type, Date, and Duration of Each):
SO OO            one (OIO SO
: 25. If Shutdown  At  End of Report Period, Estimated  Date of Startup:
8u MQ N A OQ                                  0
%6X                                                                      Forecast    Achieved Q                    INITIAL CRITICALITY                                 ~05 85      05 25 85 OK                    INITIAL ELECTRICITY                                ~06 85       ~06 10 85 00Cl 690.E                COMMERCIAL OPERATION                                ~11 85       01/128 86
                                                                                                    ~~ Zf
      '409 A/2264A                                                                                      .((
 
    ~ ~
4 IL
 
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-528 UNIT NAME   PVNGS-1 DATE         09 09 88 COMPLETED BY T J   Bloom TELEPHONE     602   3 1-418 MONTH: AUGUST 1988 DAY     AVERAGE DAILY POWER LEVEL             DAY       AVERAGE DAILY POWER LEVEL 17 18 19 20 21                 191 22 23 24                     0 25 10                                             26 27 12                                             28                     0 13                                             29 30 15                                             31                 145 16
 
fl REFUEL'ING INFORMATION DOCKET NO. 50-528 UNIT NAME   PVNGS-1 DATE       , i09 09 88 COMPLETED BY T J     Bloom TELEPHONE     602   3 1-418
: 1. Scheduled date   for next refueling shutdown.
03/21/89
: 2. Scheduled date   for restart following refueling.
05/29/89
: 3. Will refueling or resumption of operation thereafter require     a Technical Specification   change or other license   amendment?
To be determined
: 4. Scheduled date   for submitting proposed licensing action and supporting information.
ll/88 (If necessary).
ll/88 (If necessary).
5.Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
: 5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
To be determined 6.The number of fuel assemblies a)In the core.241 b)In the spent fuel storage pool.7.Licensed spent fuel storage capacity.80 1329 Intended change in spent fuel storage capacity.None 8.Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.2004 (18 Month reloads and full core discharge capability).
To be determined
F  
: 6. The number   of fuel assemblies a)     In the core.       241 b)     In the spent fuel storage pool.           80
: 7. Licensed spent fuel storage capacity.           1329 Intended change in spent fuel storage capacity.         None
: 8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.
2004 (18 Month reloads and   full core discharge capability).
 
F


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE FOR THE MONTH ll I DOCKET NO.50-528 UNIT NAME PVNGS-1 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE'02 3 1-4187 AUGUST 1988 08/01 08/13 08/14 08/18 08/19 08/20 08/21 08/21 08/21 0000 1834 0409 1906 0123 2048 0250 0700 (approx.)1124 Unit 1 is in Mode 5.Unit 1 entered Mode 4.Unit 1 entered Mode 3.Unit 1 entered Mode 2~Unit 1 entered Mode 1.Main generator synchronized to the grid.Reactor power is at 19%.Reactor power is at 54%.Main turbine trip resulted from the failure of a flow switch in the stator coolant flow trip circuit.Following the turbine trip, the reactor tripped on high pressurizer pressure as a result of the premature closing of two steam bypass control valves.The unit was stabilized in Mode 3.08/27 08/27 08/27 08/27 0208 0459 0816 0826 Unit 1 entered Mode 2.Unit 1 entered Mode l.Main generator synchronized to the grid.Reactor trip was initiated due to low steam generator level.The trip occurred following the synchronization of the unit to the grid when a main feedwater pump tripped.The unit was stabilized in Mode 3.08/29 08/30 08/31 08/31 1840 0539 0815 2400 Unit 1 entered Mode 2.Unit 1 entered Mode l.Main generator synchronized to the grid.Reactor power at 38%.
OF OPERATING EXPERIENCE FOR THE MONTH ll I DOCKET NO. 50-528 UNIT NAME   PVNGS-1 DATE         09 09 88
0 I''I," Pl SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.50-528 UNIT NAME PVNGS-1 COMPLETED BY T.J Bloom-Method of Duration Shutting System Component No.Date Typei Hours Reason2 Down Reactor LER No.Code4 Code~Cause and Corrective Action to Prevent Recurrence 8 8/21 140.9 1-88-021 TJ JI 7 7/6 F 476.8 A 4 1-88-010 EA EA NSBU XFMR FS PCV A fault on the 13.8kV bus resulted in a fire of the unit auxiliary transformer.
                                                                        '02 COMPLETED BY T TELEPHONE J   Bloom 3 1-4187 AUGUST 1988 08/01       0000      Unit 1 is in  Mode 5.
The resultant loss of power led to a reactor trip.Main turbine trip due to a failed flow switch in the stator cooling water system.Reactor trip resulted when two steam bypass control valves prematurely closed.The flow switch has been replaced and the valves are under evaluation.
08/13       1834      Unit 1 entered  Mode  4.
9 8/27 95.8 H 1-88-024 Reactor trip on low steam generator level resulted from a main feedwater pump trip.The root cause is under evaluation.
08/14       0409      Unit 1 entered  Mode 3.
F-Forced S-Scheduled Reason: A-Equipment Failure (Explain)B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training 4 License Examination F-Administrative G-Operational Error H-Other (Explain)-5-Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continuation from Previous Month 5-Reduction of 20)l or Greater in the Past 24 Hours 9-Other-(Explain)
08/18       1906      Unit 1 entered  Mode 2  ~
Exhibit F-Instructions for Preparation of the Data Entry Sheets for Licensee Event Report (LER)File (HUREG D161)Exhibit H-Same Source I]<
08/19       0123      Unit 1 entered  Mode  1.
NRC MONTHLY OPERATING REPORT OPE TING STATUS DOCKET NO.50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 l.2.3.4.5.6.7.8.9.10 Unit Name: Palo Uerde Nuclear Generati Station Unit 2 Reporting Period: Au ust 1988 Licensed Thermal Power (MWt): 3800 Nameplate Rating (Gross MWe): 1403 Design Electrical Rating (Net MWe): 1270 Maximum Dependable Capacity (Gross MWe): 1303 Maximum Dependable Capacity (Net MWe): 1221 If Changes Occur In Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons: N A Power Level to Which Restricted, If Any (Net MWe): None Reasons For Restrictions, If Any: N A 11.12.13.14.15.16.17.18.19.20.21.22.23.24, Hours in Reporting Period Number of Hours Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy Generated (MWH)Gross Electrical Energy Generated (MWH)Net Electrical Energy Generated (MWH)Unit Service Factor Unit Availability Factor Unit Capacity Factor (Using MDC Net)Unit Capacity Factor (Using DER Net)Unit Forced Outage Rate Shutdowns Scheduled Over Next None This Month 744 0 744 0 0 0 0 0 0 2 13 036 0 934 600 0 8 8 076 0 100 0 100 0 Yr.-to-Date 5 856 0 3 000 6 0 0 2 886 0 0.0 10 526 988 0 3 664 400 0 3 420 109 0 49 3a 49 3 Cumulative 17 112 0 12 275 7 0 0 12 012 2 0 0 43 734 155.0 15 325 670 0 14 356 991.0 0.2 0 2 96 7 68 66 1 5.1 0 Oa 6 Months (Type, Date, and Duration of Each): 25.If Shutdown At End of Report Peri'od, Estimated Date of Startup: N A INITIAL CRITICALITY, INITIAL ELECTRICITY COMMERCIAL OPERATION-6-Forecast~03 86 Achieved 04/618 86 11 86 09/919 86~06 86 05/520 86 0 0 AVERAGE DAILY UNIT POWER LEVEL MONTH: AUGUST 1988 DOCKET NO.50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 1 240 17 1 234 1 245 18 1 233 1 24 19 1 231 1 246 1 188 20 21 1 234 1 235 1 21 22 1 233 1 239 23 1 229 1 34 1 229 1 238 25 1'28 10 1 239 26 1 228 1 238 27 1 230 12 13 14 15 1 241 1 244 1 245 1 239 28 29 30 31 1 231 1 230 483 461 16 1 238 REFUELING INFORMATION DOCKET NO.50-529 UNIT NAME PVNGS-2 DATE COMPLETED BY T J Bloom 1, Scheduled date for next refueling shutdown.09/15/89 2.Scheduled date for restart following refueling.
08/20       2048      Main generator synchronized to the  grid.
11/24/89 3.Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
08/21       0250      Reactor power  is at  19%.
To be determined 4.Scheduled date for submitting proposed licensing action and supporting information.
08/21       0700       Reactor power  is at  54%.
To be determined 5.Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
(approx.)
To be determined 6.The number of fuel assemblies a)In the core.241 b)In the spent fuel storage pool.7.Licensed spent fuel storage capacity.108 1329 Intended change in spent fuel storage capacity.None 8.Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.2004 (18 Month reloads and full core discharge capability).
08/21      1124       Main turbine  trip resulted from the failure of a flow switch  in the stator coolant flow trip circuit. Following the turbine trip, the reactor tripped on high pressurizer pressure as a result of the premature closing of two steam bypass control valves. The unit was stabilized in Mode 3.
[s  
08/27      0208      Unit 1 entered   Mode 2.
08/27      0459      Unit 1 entered   Mode l.
08/27      0816      Main generator synchronized to the   grid.
08/27      0826      Reactor trip was initiated due to low steam generator level. The trip occurred following the synchronization of the unit to the grid when a main feedwater pump tripped. The unit was stabilized in Mode 3.
08/29      1840      Unit 1 entered   Mode 2.
08/30      0539      Unit 1 entered Mode l.
08/31      0815      Main generator synchronized to the   grid.
08/31      2400      Reactor power at  38%.
 
0 I
    ''I,"
Pl
 
SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.       50-528 UNIT  NAME      PVNGS-1 COMPLETED BY    T. J    Bloom-Method  of                                        Cause and    Corrective Duration              Shutting                  System  Component            Action to No. Date    Typei        Hours    Reason2    Down Reactor    LER No. Code4    Code~          Prevent Recurrence 7    7/6      F          476.8      A            4        1-88-010      EA      NSBU        A  fault  on the 13.8kV bus EA      XFMR        resulted in    a fire of the unit auxiliary transformer.
The resultant loss of power led to  a  reactor  trip.
8    8/21                  140. 9                            1-88-021      TJ      FS          Main turbine    trip  due  to a JI      PCV          failed flow switch in the stator cooling water system. Reactor trip resulted when two steam bypass control valves prematurely closed. The flow switch has been replaced and the valves are under evaluation.
9     8/27                  95.8     H                      1-88-024                          Reactor trip on low steam generator level resulted from a main feedwater pump trip. The root cause      is under evaluation.
F-Forced        Reason:                                        Method:                    Exhibit F-Instructions S-Scheduled    A-Equipment Failure (Explain)                  1-Manual                    for Preparation of the Data B-Maintenance or Test                          2-Manual Scram              Entry Sheets for Licensee C-Refueling                                    3-Automatic Scram          Event Report (LER) File D-Regulatory Restriction                        4-Continuation from        (HUREG D161)
E-Operator Training 4 License Examination         Previous Month F-Administrative                               5-Reduction of 20)l G-Operational Error                               or Greater in the        Exhibit  H-Same  Source H-Other (Explain)                                 Past 24 Hours 9-Other-(Explain)
 
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NRC MONTHLY OPERATING REPORT DOCKET NO. 50-529 UNIT NAME    PVNGS-2 DATE          09 09 88 COMPLETED BY T J    Bloom TELEPHONE      602 371-4187 OPE TING STATUS
: l. Unit  Name:  Palo Uerde Nuclear Generati      Station Unit 2
: 2. Reporting Period: Au ust 1988
: 3. Licensed Thermal Power (MWt): 3800
: 4. Nameplate Rating (Gross MWe): 1403
: 5. Design Electrical Rating (Net MWe):            1270
: 6. Maximum Dependable Capacity (Gross MWe): 1303
: 7. Maximum Dependable Capacity (Net MWe):        1221
: 8. If  Changes Occur In Capacity Ratings (Items Number 3 Through 7)
Since Last Report, Give Reasons:      N A
: 9. Power Level to Which Restricted,    If Any  (Net MWe): None 10  Reasons For Restrictions,  If Any:   N A This Month          Yr.-to-Date          Cumulative
: 11. Hours  in Reporting Period            744 0                  5 856 0          17 112 0
: 12. Number of Hours Reactor Was  Critical                          744 0                  3 000 6          12 275 7
: 13. Reactor Reserve Shutdown Hours                                    0 0                        0 0                0 0
: 14. Hours Generator On-Line                    0                  2 886 0          12 012 2
: 15. Unit Reserve Shutdown Hours                                    0 0                        0.0                0 0
: 16. Gross Thermal Energy Generated (MWH)                    2  13 036 0          10 526 988 0          43 734 155.0
: 17. Gross Electrical Energy Generated (MWH)                      934 600 0          3  664 400 0        15 325 670 0
: 18. Net Electrical Energy Generated (MWH)                      8 8 076 0          3  420 109 0        14 356 991.0
: 19. Unit Service Factor                    100 0                  49 3a                  0.2
: 20. Unit Availability Factor              100 0                  49 3                  0 2
: 21. Unit Capacity Factor (Using MDC Net)                         96 7                                        68
: 22. Unit Capacity Factor (Using DER Net)                                                                     66 1
: 23. Unit Forced Outage Rate                                        0 Oa                  5.1 24, Shutdowns Scheduled Over Next   6 Months (Type, Date, and Duration      of Each):
None
: 25. If Shutdown  At  End of Report Peri'od, Estimated  Date of Startup:
N A Forecast      Achieved INITIAL CRITICALITY,                                ~03 86        04/618 86 INITIAL ELECTRICITY                                  ~06 86        05/520 86 COMMERCIAL OPERATION                                  11 86        09/919 86
 
0 0 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-529 UNIT NAME    PVNGS-2 DATE        09 09 88 COMPLETED BY T J    Bloom TELEPHONE    602  3 1-418 MONTH: AUGUST 1988 DAY      AVERAGE DAILY POWER LEVEL            DAY        AVERAGE DAILY POWER LEVEL 1 240                          17                1 234 1 245                          18                1 233 1 24                          19                1 231 1 246                          20                1 234 1 188                          21                1 235 1 21                          22                1 233 1 239                          23                1 229 1  34                                            1 229 1 238                          25               1'28 10              1 239                          26                1 228 1 238                          27                1 230 12              1 241                          28                1 231 13              1 244                          29                1 230 14              1 245                          30                  483 15              1 239                          31                  461 16              1 238
 
REFUELING INFORMATION DOCKET NO. 50-529 UNIT NAME   PVNGS-2 DATE COMPLETED BY T J   Bloom 1,  Scheduled date  for next refueling  shutdown.
09/15/89
: 2. Scheduled date  for restart following refueling.
11/24/89
: 3. Will refueling or resumption of operation thereafter require      a Technical Specification  change or  other license    amendment?
To be determined
: 4. Scheduled date  for submitting  proposed licensing action and supporting information.
To be determined
: 5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
To be determined
: 6. The number  of fuel assemblies a)    In the core.       241 b)    In the spent fuel storage pool.           108
: 7. Licensed spent fuel storage capacity.            1329 Intended change in spent fuel storage capacity.          None
: 8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.
2004 (18 Month   reloads and   full core discharge capability).
 
[s


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO.50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPJ.ETED BY T J Bloom TELEPHONE 602 3 1-418 08/01 08/05 0000 1130 Reactor power at 100$.Reactor power reduced to 90$due to leak in low pressure feedwater heater 2C.08/06 08/30 1339 0225 Reactor power at 100%.Reactor power reduced to 408 for repair of suspected condenser tube leak.08/31 2400 Reactor power at 68%.  
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO. 50-529 UNIT NAME   PVNGS-2 DATE         09 09 88 COMPJ.ETED BY T J     Bloom TELEPHONE     602 3 1-418 08/01 0000 Reactor power at 100$ .
08/05 1130  Reactor power reduced to 90$ due to leak in low pressure feedwater heater 2C.
08/06 1339 Reactor power at 100%.
08/30 0225  Reactor power reduced to 408 for repair of suspected   condenser tube leak.
08/31 2400 Reactor power at 68%.


SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.50-529 UNIT NAME PVNGS-2.DATE COMPLETED BY T.J.Bloom No.Date Type1 Duration Hours Method of Shutting System Component Reason Down Reactor LER No.Code Code Cause and Corrective Action to Prevent Recurrence 3 8/30 F N/A N/A N/A N/A Reactor power reduced to 40%in order to repair suspected condenser tube leak.1 F-Forced S-Scheduled Reason: A-Equipment Failure (Explain)8-Maintenance or Test C-Ref uel ing D-Regulatory Restriction E-Operator Training S License Examination F-Administrative G-Operational Error H-Other (Explain)Method: 1-Manual 2-Manual Scram 3-Automatic Scram 4-Continuation from Previous Month 5-Reduction of 20X or Greater in the Past 24 Hours 9-Other-(Explain)
SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-529 UNIT NAME     PVNGS-2 .
Exhibit F-instructions for Preparation of the Data Entry Sheets for Licensee Event Report (LER)File (HUREG 0161)Exhibit H-Same Source
DATE COMPLETED BY   T. J. Bloom Method  of                                        Cause and  Corrective Duration              Shutting                  System  Component          Action to No. Date   Type1         Hours   Reason     Down Reactor   LER No.       Code     Code         Prevent Recurrence 3     8/30     F           N/A                               N/A             N/A     N/A         Reactor power reduced to 40% in order to repair suspected condenser tube leak.
1 F-Forced         Reason:                                        Method:                    Exhibit F-instructions S-Scheduled     A-Equipment Failure (Explain)                   1-Manual                    for Preparation of the Data 8-Maintenance or Test                           2-Manual Scram              Entry Sheets for Licensee C-Ref uel ing                                   3-Automatic Scram          Event Report (LER) File D-Regulatory Restriction                       4-Continuation from        (HUREG  0161)
E-Operator Training S License Examination         Previous Month F-Administrative                               5-Reduction of 20X G-Operational Error                               or Greater in the        Exhibit  H-Same  Source H-Other (Explain)                                 Past 24 Hours 9-Other-(Explain)


NRC MONTHLY OPERATING REPORT DOCKET NO.50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 OPERATING STATUS 1.2.3.4.5.6~7.8.9.10 Unit Name: Palo Verde Nuclear Generatin Station Unit 3 Reporting Period: Au ust 1988 Licensed Thermal Power (MWt): 3800 Nameplate Rating (Gross MWe): 1403 Design Electrical Rating (Net MWe):~12 0 Maximum Dependable Capacity (Gross MWe): 1303 Maximum Dependable Capacity (Net MWe):~122 If Changes Occur In Capacity Ratings (Items Number 3 Through 7)Since Last Report, Give Reasons: N A Power Level to Which Restricted, If Any (Net MWe): one Reasons For Restrictions, If Any: N A This Month Yr.-to-Date Cumulative 11.12.13.14.15.16.17.18.19.20.21.22.23.24.Hours in Reporting Period Number of Hours Reactor Was Critical Reactor Reserve Shutdown Hours Hours Generator On-Line Unit Reserve Shutdown Hours Gross Thermal Energy Generated (MWH)Gross Electrical Energy Generated (MWH)Net Electrical Energy Generated (MWH)Unit Service Factor Unit Availability Factor Unit Capacity Factor (Using MDC Net)Unit Capacity Factor (Using DER Net)Unit Forced Outage Rate Shutdowns Scheduled Over Next None 44 0 5 688 0 5 688 0 329 5 273 5 273 7 0 0 313 4 0 0 5 250 0 0 0 5 250.0 0 0 0 0 0.0 1 084 459 0 375 000 0 330 551 0 42 1 42 1 19 470 031.0 6 846 500 0 6 443 090 0 92 3 92 3 19 470 031.0 6 846 500.0 6 443 090.0 92 3 92 3a 36 4 92 8 92 8 89.2 7%6 Months (Type, Date, and Duration of Each): 25'f Shutdown At End of Report Period, Estimated Date of Startup: N A INITIAL CRITICALITY INITIAL ELECTRICITY'OMMERCIAL OPERATION h-11-Forecast Achieved 07787 10/025 87~08 11/128 87~09 8~01 08 88  
NRC MONTHLY OPERATING REPORT DOCKET NO.       50-530 UNIT NAME       PVNGS-3 DATE             09 09 88 COMPLETED BY T J         Bloom TELEPHONE         602   3 1-418 OPERATING STATUS
: 1. Unit Name:   Palo Verde Nuclear Generatin Station Unit 3
: 2. Reporting Period: Au ust 1988
: 3. Licensed Thermal Power (MWt): 3800
: 4. Nameplate Rating (Gross MWe): 1403
: 5. Design Electrical Rating (Net MWe):                               ~12 0 6 ~  Maximum Dependable Capacity (Gross MWe): 1303
: 7. Maximum Dependable Capacity (Net MWe):                           ~122
: 8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)
Since Last Report, Give Reasons:                       N A
: 9. Power Level   to Which Restricted, If Any (Net                         MWe): one 10  Reasons For   Restrictions, If Any: N A This Month           Yr.-to-Date           Cumulative
: 11. Hours   in Reporting Period                                 44 0                 5 688 0               5 688 0
: 12. Number  of Hours Reactor Was  Critical                                              329                   5 273                   5 273 7
: 13. Reactor Reserve Shutdown Hours                                                        0 0                      0 0                      0 0
: 14. Hours Generator On-Line                                    313 4                 5 250 0               5 250.0
: 15. Unit Reserve Shutdown Hours                                                        0 0                       0 0                     0.0
: 16. Gross Thermal Energy Generated (MWH)                                        1 084 459 0           19 470  031.0         19 470   031.0
: 17. Gross Electrical Energy Generated (MWH)                                          375 000 0            6 846   500 0         6 846  500.0
: 18. Net Electrical Energy Generated (MWH)                                          330 551 0           6 443 090 0           6 443 090.0
: 19. Unit Service Factor                                        42 1                    92 3                   92 3
: 20. Unit Availability Factor                                    42 1                    92 3                    92 3a
: 21. Unit Capacity Factor (Using MDC Net)                                            36 4                   92 8                   92 8
: 22. Unit Capacity Factor (Using DER Net)                                                                                            89.2
: 23. Unit Forced Outage Rate                                                                                        7%
: 24. Shutdowns Scheduled Over Next                        Months (Type, Date, and Duration       of Each):
    'f 6
None 25      Shutdown At End                     of Report Period, Estimated     Date of Startup:
N A Forecast        Achieved INITIAL CRITICALITY                                                       07787         10/025 87 INITIAL                                                  h
                                                                                    ~08             11/128 87
                                                                                                    ~01 08 88 ELECTRICITY'OMMERCIAL OPERATION                                ~09 8


AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-418 MONTH: AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 17 18 19 294 20 1 168 21 1 231 22 23 1 244 1 244 24 1 245 25 850 10 26 1 138 27 1 243 12 28 1 246 13 29 1 24 14 30 1 249 15 31 1 250 16  
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-530 UNIT NAME     PVNGS-3 DATE         09 09 88 COMPLETED BY T J     Bloom TELEPHONE     602 371-418 MONTH: AUGUST 1988 DAY     AVERAGE DAILY POWER LEVEL             DAY       AVERAGE DAILY POWER LEVEL 17 18 19                 294 20               1 168 21               1 231 22               1 244 23              1 244 24               1 245 25                 850 10                                             26               1 138 27               1 243 12                                           28               1 246 13                                           29               1 24 14                                             30               1 249 15                                             31               1 250 16


REFUELING INFORMATION DOCKET NO.50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-4187 1.Scheduled date for next refueling shutdown.03/03/89 2.Scheduled date for restart following refueling.
REFUELING INFORMATION DOCKET NO.     50-530 UNIT NAME       PVNGS-3 DATE         09 09 88 COMPLETED BY T J       Bloom TELEPHONE       602   3 1-4187
05/27/89 3.4.Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?'es, these are expected to include the following:
: 1. Scheduled date for next refueling   shutdown.
2.1.1.1, 3/4 1.1.2, 3/4 1.1.3, 3/4 1.3.1, 3/4 1.3.6, 3/4 2.1, 3/4 2.3, 3/4 2.4, 3/4 2.5, 3/4 2.8, 3/4 3.1, 3/4 3.2.Scheduled date for submitting proposed licensing action and supporting information.
03/03/89
11/88 5.Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
: 2. Scheduled date for restart following refueling.
'The fuel vendor for the next five reloads will be Combustion Engineering.
05/27/89
6.The number of fuel assemblies a)In the core.241 b)In the spent fuel storage pool.0 7.Licensed spent fuel storage capacity.1329 Intended change in spent fuel storage capacity.None 8.Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.2005 (18 Month reloads and full core discharge capability).
: 3. Will refueling or resumption of operation thereafter require             a Technical Specification change or other license   amendment?'es, these are expected to include the following: 2.1.1.1, 3/4 1.1.2, 3/4 1.1.3, 3/4 1.3.1, 3/4 1.3.6, 3/4 2.1, 3/4 2.3, 3/4 2.4, 3/4 2.5, 3/4 2.8, 3/4 3.1, 3/4 3.2.
II  
: 4. Scheduled date for submitting proposed licensing action and supporting information.
11/88
: 5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
                                                                                  '
The fuel vendor for the next five reloads will be           Combustion Engineering.
: 6. The number of fuel assemblies a)     In the core.     241 b)     In the spent fuel storage pool.                     0
: 7. Licensed spent fuel storage capacity.                   1329 Intended change in spent fuel storage capacity.                 None
: 8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.
2005 (18 Month reloads and full core discharge capability).
 
II


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO.50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 AUGUST 1988 08/01 0000 Unit 3 in Mode 1 at approximately 8%reactor power following a lightening strike of the B-phase main transfer (main turbine trip resulted).
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO. 50-530 UNIT NAME   PVNGS-3 DATE         09 09 88 COMPLETED BY T J   Bloom TELEPHONE     602 371-4187 AUGUST 1988 08/01       0000       Unit 3 in Mode 1 at approximately 8% reactor power following   a lightening strike of the B-phase main transfer (main turbine   trip resulted).
08/01 08/01 08/18 08/18 08/18 08/19 08/20 08/21 08/21 08/22 08/25 1625 1759 0620 1525 2238 1900 (approx.)0639 1329 1830 0007 0304 Unit 3 entered Mode 2.Unit 3 entered Mode 3.Unit 3 entered Mode 2.Unit 3 entered Mode 1.Main generator synchronized to the grid.Reactor power at 44%Reactor power at 100%.Reactor power reduced to 95%following a turbine load reduction which was made in response to high backpressure in condenser'C'nd a high alarm on condensate demineralizer inlet temperature.
08/01       1625       Unit 3 entered Mode 2.
Reactor power at 97.5%.Reactor power at 100%.Reactor power stabilized at 50%following a reactor power cutback which resulted from the'B'eedwater pump tripping during the weekly surveillance testing.08/25 0645 08/31 2400 08/26'0831 Reactor power at 65%.Reactor power,'at 100%.Reactor power at 100%.
08/01      1759      Unit 3 entered Mode 3.
H f SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.50-530 UNIT NAME PVNGS-3 DATE COMPLETED BY T.J.Bloom'No.Date Typei Duration Hours Reason2 Method of Shutting Down Reactor LER No.System Component Code4 Code5 Cause and Corrective Action to Prevent Recurrence 6 07/31 F 430.6 H N/AP N/AP N/AP Turbine trip occurred when~a lighting strike tripped the B-phase main transformer on 7/31.Unit 3 subsequently manually shutdown to inspect/repair any damaged equipment.
08/18      0620      Unit 3 entered Mode 2.
7 08/25 F N/A N/AP N/AP N/AP Reactor power reduced to 50$following a reactor power cutback which resulted from the'B'eedwater pump tripping during surveillance testing.F-Forced S-Scheduled Reason: A-Equipment Failure (Explain)8-Haintenance or Test C-Refueling D-Regulatory
08/18      1525      Unit 3 entered Mode 1.
'Restriction E-Operator Training 5 License Examination F-Administrative G-Operational Error H-Other (Explain)Hethod: 1-Hanual 2-Hanua l Scram 3-Automatic Scram 4-Continuation from Previous Month 5-Reduction of 20K or Greater in the Past 24 Hours 9-Other-(Explain)
08/18      2238      Main generator synchronized to the grid.
Exhibit F-instructions for Preparation of the Data Entry Sheets for Licensee Event Report (LER)File (HUREG 0161)Exhibit H-Same Source
08/19      1900      Reactor power at 44%
(approx.)
08/20      0639      Reactor power at 100%.
08/21      1329      Reactor power reduced to 95% following a turbine load reduction which was made in response to high backpressure in condenser a high alarm on condensate demineralizer inlet temperature.
                                                                                      'C'nd 08/21      1830      Reactor power at 97.5%.
08/22      0007      Reactor power at 100%.
08/25      0304      Reactor power stabilized at 50% following a reactor power cutback which resulted from the 'B'eedwater pump tripping during the weekly surveillance testing.
08/25       0645       Reactor power at 65%.
08/26 '
0831      Reactor power,'at 100%.
08/31      2400      Reactor power at 100%.
 
H f
 
SHUTDOWNS AND POWER REDUCTIONS
                                                                                                                                    '
DOCKET NO. 50-530 UNIT NAME     PVNGS-3 DATE COMPLETED BY T. J. Bloom Method  of                                        Cause and  Corrective Duration                Shutting                  System  Component          Action to No. Date   Typei       Hours     Reason2   Down Reactor   LER No.     Code4     Code5         Prevent Recurrence 6     07/31     F         430.6       H                     N/AP           N/AP     N/AP       Turbine   trip occurred when~
a lighting strike tripped the B-phase main transformer on 7/31. Unit 3 subsequently manually shutdown to inspect/repair any damaged equipment.
7     08/25     F         N/A                               N/AP           N/AP     N/AP       Reactor power reduced to 50$ following a reactor power cutback which resulted from the pump  tripping
                                                                                                                        'B'eedwater during surveillance testing.
F-Forced       Reason:                                        Hethod:                    Exhibit F-instructions S-Scheduled     A-Equipment Failure (Explain)                   1-Hanual                    for Preparation of the Data 8-Haintenance or Test                           2-Hanua l Scram            Entry Sheets for Licensee C-Refueling                                     3-Automatic Scram          Event Report (LER) File D-Regulatory 'Restriction                       4-Continuation from        (HUREG  0161)
E-Operator Training 5 License Examination         Previous Month F-Administrative                               5-Reduction of 20K G-Operational Error                               or Greater in the        Exhibit  H-Same  Source H-Other (Explain)                                 Past 24 Hours 9-Other-(Explain)
 
Arizona Nuclear Power Project P.O. BOX 52034  ~ PHOENIX, ARIZONA85072-2034 212-00363-JGH/TJB September 13, 1988 Docket Nos. STN  50-528/529/530 Document Control Desk U. S. Nuclear Regulatory Commission Mail Station Pl-137 Washington, D.C. 20555
 
==Dear  Sirs:==


Arizona Nuclear Power Project P.O.BOX 52034~PHOENIX, ARIZONA 85072-2034 212-00363-JGH/TJB September 13, 1988 Docket Nos.STN 50-528/529/530 Document Control Desk U.S.Nuclear Regulatory Commission Mail Station Pl-137 Washington, D.C.20555
Subj ect:    Palo Verde Nuclear Generating Station (PVNGS)
Units 1, 2 and 3 Monthly Operating Reports        for    August 1988 File'8-024-404          88-056-026 Attached are the Monthly Operating Reports for August 1988 prepared and submitted pursuant to Specification 6.9.1.6 of Appendix A (Technical Specifications) to the Palo Verde Nuclear Generating Station, Units 1, 2 and 3 Operating Licenses. By copy of this letter, we are also forwarding a copy of the Monthly Operating Reports to the Regional Administrator of the Region V Office.
If you have  any questions,      please contact Mr. T. J. Bloom, at (602) 371-4187.
Very  truly yours, J. G. Haynes Vice President Nuclear Production JGH/TJB/dim Attachments cc:  ED E. Van Brunt,    Jr.          (all w/attachments)
D. B. Karner J. A. Amenta A. C. Gehr M. J. Davis J. B. Martin INPO Records  Center


==Dear Sirs:==
f
Subj ect: Palo Verde Nuclear Generating Station (PVNGS)Units 1, 2 and 3 Monthly Operating Reports for August 1988 File'8-024-404 88-056-026 Attached are the Monthly Operating Reports for August 1988 prepared and submitted pursuant to Specification 6.9.1.6 of Appendix A (Technical Specifications) to the Palo Verde Nuclear Generating Station, Units 1, 2 and 3 Operating Licenses.By copy of this letter, we are also forwarding a copy of the Monthly Operating Reports to the Regional Administrator of the Region V Office.If you have any questions, please contact Mr.T.J.Bloom, at (602)371-4187.Very truly yours, J.G.Haynes Vice President Nuclear Production JGH/TJB/dim Attachments cc: ED E.Van Brunt, Jr.D.B.Karner J.A.Amenta A.C.Gehr M.J.Davis J.B.Martin INPO Records Center (all w/attachments)
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Revision as of 10:50, 29 October 2019

Monthly Operating Repts for Aug 1988 for Palo Verde Nuclear Generating Station Units 1,2 & 3.W/880913 Ltr
ML17304A531
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 08/31/1988
From: Bloom T, Haynes J
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
NUDOCS 8809220139
Download: ML17304A531 (33)


Text

. r AC CELZRATZD DISTRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DIST TION SYSTEM (RIDS)

ACCESSION NBR:8809220139 DOC.DATE: 88/ NOTARIZED: NO DOCKET g FACIL:STN-50-528 Palo Verde Nuclear Statio , Unit 1, Arizona Publi 05000528 STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi Palo Verde Nuclear Station, Unit 3, Arizona Publi 05000530 05000529"'TN-50-530

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AUTH. NAME AUTHOR AFFILIATION )'l BLOOM,T.J. Arizona Nuclear Power Project (formerly Arizona Public Serv "~

HAYNES,J.G. Arizona Nuclear Power Project (formerly Arizona Public Serv,(

RECIP.NAME RECIPIENT AFFILIATION R

SUBJECT:

Monthly operating repts for Aug. 1988 fo alo Verde Nuclear I Generating Station Unit 1,2 & 3. 880 3 tr.

DISTRIBUTION CODE: IE24D COPIES RECEIVED:LTR ENCL ( SIZE: /~ D TITLE: Monthly Operating Report (per Tech Spec/s 8

NOTES:Standardized plant.

Standardized plant.

Standardized plant.

05000528"'5000529 05000530

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A 4

RECIPIENT COPIES RECIPIENT COPIES D ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 0 PD5 PD 5 5 CHAN,T 1 0 DAVIS,M 1 0 D'r LICITRA,E 1 0 j S

INTERNAL: ACRS 10 10 AEOD/DOA 1 1 AEOD/DS P/TPAB NRR/DLPQ/PEB 11 NRR/~DRBP/ PB 10 1

1 1

1 1

1 ARM TECH ADV NRR/DOEA/EAB NUDOCS-ABSTRACT ll 2 1

1 2

1 1

REG EZLE 01 1 1 RGN5 1 1 EXTERNAL: EGGG WILLIAMS,S 1 1 LPDR 1 1 NRC PDR 1 1 NSIC 1 1 NOTES R

I, D

8; ji A

D;

$

TOTAL NUMBER OF COPIES REQUIRED: LTTR 34 ENCL 30

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NRC MONTHLY OPERATING REPORT DOCKET NO. 50-528 UNIT NAME PVNGS-1 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 OPERATING STATUS

1. Unit Name: Palo Verde Nuclear Generatin Station Unit 1
2. Reporting Period: Au ust 1988
3. Licensed Thermal Power (MWt): 3800
4. Nameplate Rating (Gross MWe): 1403
5. Design Electrical Rating (Net MWe): 1270
6. Maximum Dependable Capacity (Gross MWe): 1303
7. Maximum Dependable Capacity (Net MWe): ~122
8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)

Since Last Report, Give Reasons: N A

9. Power Level to Which Restricted, If Any (Net MWe): None
10. Reasons For Restrictions, If Any: N A This Month Yr.-to-Date Cumulative 11, Hours in Reporting Period 744 0 5 856 0 22 728 0
12. Number of Hours Reactor Was Critical 124 0 2 834 9 12 812 1
13. Reactor Reserve Shutdown Hours 0 0 0 0 0 0
14. Hours Generator On-Line 30 5 2 659.8 12 376 9
15. Unit Reserve Shutdown Hours 0 0 0 0 0 0
16. Gross Thermal Energy Generated (MWH) 69 686.0 9 610 692 0 44 643 529 0
17. Gross Electrical Energy Generated (MWH) 11 200.0 3 341 900.0 15 485 200 0
18. Net Electrical Energy Generated (MWH) 0 0 3 119 869 0 14 447 94 0 19 Unit Service Factor 4 1 45 4 54 5

'0.

Unit Availability Factor 4 1 45 4a 54.5%

21 Unit Capacity Factor (Using MDC Net) 0 0 43 6 52 1

22. Unit Capacity Factor

'uN

~IAGI (Using DER Net)

Unit Forced Outage Rate 50 1 32.0 YiOG. Shutdowns Scheduled Over 'Next 6 Months (Type, Date, and Duration of Each):

SO OO one (OIO SO

25. If Shutdown At End of Report Period, Estimated Date of Startup:

8u MQ N A OQ 0

%6X Forecast Achieved Q INITIAL CRITICALITY ~05 85 05 25 85 OK INITIAL ELECTRICITY ~06 85 ~06 10 85 00Cl 690.E COMMERCIAL OPERATION ~11 85 01/128 86

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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-528 UNIT NAME PVNGS-1 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 MONTH: AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 17 18 19 20 21 191 22 23 24 0 25 10 26 27 12 28 0 13 29 30 15 31 145 16

fl REFUEL'ING INFORMATION DOCKET NO. 50-528 UNIT NAME PVNGS-1 DATE , i09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418

1. Scheduled date for next refueling shutdown.

03/21/89

2. Scheduled date for restart following refueling.

05/29/89

3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

To be determined

4. Scheduled date for submitting proposed licensing action and supporting information.

ll/88 (If necessary).

5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.

To be determined

6. The number of fuel assemblies a) In the core. 241 b) In the spent fuel storage pool. 80
7. Licensed spent fuel storage capacity. 1329 Intended change in spent fuel storage capacity. None
8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.

2004 (18 Month reloads and full core discharge capability).

F

SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH ll I DOCKET NO. 50-528 UNIT NAME PVNGS-1 DATE 09 09 88

'02 COMPLETED BY T TELEPHONE J Bloom 3 1-4187 AUGUST 1988 08/01 0000 Unit 1 is in Mode 5.

08/13 1834 Unit 1 entered Mode 4.

08/14 0409 Unit 1 entered Mode 3.

08/18 1906 Unit 1 entered Mode 2 ~

08/19 0123 Unit 1 entered Mode 1.

08/20 2048 Main generator synchronized to the grid.

08/21 0250 Reactor power is at 19%.

08/21 0700 Reactor power is at 54%.

(approx.)

08/21 1124 Main turbine trip resulted from the failure of a flow switch in the stator coolant flow trip circuit. Following the turbine trip, the reactor tripped on high pressurizer pressure as a result of the premature closing of two steam bypass control valves. The unit was stabilized in Mode 3.

08/27 0208 Unit 1 entered Mode 2.

08/27 0459 Unit 1 entered Mode l.

08/27 0816 Main generator synchronized to the grid.

08/27 0826 Reactor trip was initiated due to low steam generator level. The trip occurred following the synchronization of the unit to the grid when a main feedwater pump tripped. The unit was stabilized in Mode 3.

08/29 1840 Unit 1 entered Mode 2.

08/30 0539 Unit 1 entered Mode l.

08/31 0815 Main generator synchronized to the grid.

08/31 2400 Reactor power at 38%.

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SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-528 UNIT NAME PVNGS-1 COMPLETED BY T. J Bloom-Method of Cause and Corrective Duration Shutting System Component Action to No. Date Typei Hours Reason2 Down Reactor LER No. Code4 Code~ Prevent Recurrence 7 7/6 F 476.8 A 4 1-88-010 EA NSBU A fault on the 13.8kV bus EA XFMR resulted in a fire of the unit auxiliary transformer.

The resultant loss of power led to a reactor trip.

8 8/21 140. 9 1-88-021 TJ FS Main turbine trip due to a JI PCV failed flow switch in the stator cooling water system. Reactor trip resulted when two steam bypass control valves prematurely closed. The flow switch has been replaced and the valves are under evaluation.

9 8/27 95.8 H 1-88-024 Reactor trip on low steam generator level resulted from a main feedwater pump trip. The root cause is under evaluation.

F-Forced Reason: Method: Exhibit F-Instructions S-Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of the Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (HUREG D161)

E-Operator Training 4 License Examination Previous Month F-Administrative 5-Reduction of 20)l G-Operational Error or Greater in the Exhibit H-Same Source H-Other (Explain) Past 24 Hours 9-Other-(Explain)

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NRC MONTHLY OPERATING REPORT DOCKET NO. 50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 OPE TING STATUS

l. Unit Name: Palo Uerde Nuclear Generati Station Unit 2
2. Reporting Period: Au ust 1988
3. Licensed Thermal Power (MWt): 3800
4. Nameplate Rating (Gross MWe): 1403
5. Design Electrical Rating (Net MWe): 1270
6. Maximum Dependable Capacity (Gross MWe): 1303
7. Maximum Dependable Capacity (Net MWe): 1221
8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)

Since Last Report, Give Reasons: N A

9. Power Level to Which Restricted, If Any (Net MWe): None 10 Reasons For Restrictions, If Any: N A This Month Yr.-to-Date Cumulative
11. Hours in Reporting Period 744 0 5 856 0 17 112 0
12. Number of Hours Reactor Was Critical 744 0 3 000 6 12 275 7
13. Reactor Reserve Shutdown Hours 0 0 0 0 0 0
14. Hours Generator On-Line 0 2 886 0 12 012 2
15. Unit Reserve Shutdown Hours 0 0 0.0 0 0
16. Gross Thermal Energy Generated (MWH) 2 13 036 0 10 526 988 0 43 734 155.0
17. Gross Electrical Energy Generated (MWH) 934 600 0 3 664 400 0 15 325 670 0
18. Net Electrical Energy Generated (MWH) 8 8 076 0 3 420 109 0 14 356 991.0
19. Unit Service Factor 100 0 49 3a 0.2
20. Unit Availability Factor 100 0 49 3 0 2
21. Unit Capacity Factor (Using MDC Net) 96 7 68
22. Unit Capacity Factor (Using DER Net) 66 1
23. Unit Forced Outage Rate 0 Oa 5.1 24, Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

None

25. If Shutdown At End of Report Peri'od, Estimated Date of Startup:

N A Forecast Achieved INITIAL CRITICALITY, ~03 86 04/618 86 INITIAL ELECTRICITY ~06 86 05/520 86 COMMERCIAL OPERATION 11 86 09/919 86

0 0 AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 MONTH: AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 1 240 17 1 234 1 245 18 1 233 1 24 19 1 231 1 246 20 1 234 1 188 21 1 235 1 21 22 1 233 1 239 23 1 229 1 34 1 229 1 238 25 1'28 10 1 239 26 1 228 1 238 27 1 230 12 1 241 28 1 231 13 1 244 29 1 230 14 1 245 30 483 15 1 239 31 461 16 1 238

REFUELING INFORMATION DOCKET NO. 50-529 UNIT NAME PVNGS-2 DATE COMPLETED BY T J Bloom 1, Scheduled date for next refueling shutdown.

09/15/89

2. Scheduled date for restart following refueling.

11/24/89

3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

To be determined

4. Scheduled date for submitting proposed licensing action and supporting information.

To be determined

5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.

To be determined

6. The number of fuel assemblies a) In the core. 241 b) In the spent fuel storage pool. 108
7. Licensed spent fuel storage capacity. 1329 Intended change in spent fuel storage capacity. None
8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.

2004 (18 Month reloads and full core discharge capability).

[s

SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO. 50-529 UNIT NAME PVNGS-2 DATE 09 09 88 COMPJ.ETED BY T J Bloom TELEPHONE 602 3 1-418 08/01 0000 Reactor power at 100$ .

08/05 1130 Reactor power reduced to 90$ due to leak in low pressure feedwater heater 2C.

08/06 1339 Reactor power at 100%.

08/30 0225 Reactor power reduced to 408 for repair of suspected condenser tube leak.

08/31 2400 Reactor power at 68%.

SHUTDOWNS AND POWER REDUCTIONS DOCKET NO. 50-529 UNIT NAME PVNGS-2 .

DATE COMPLETED BY T. J. Bloom Method of Cause and Corrective Duration Shutting System Component Action to No. Date Type1 Hours Reason Down Reactor LER No. Code Code Prevent Recurrence 3 8/30 F N/A N/A N/A N/A Reactor power reduced to 40% in order to repair suspected condenser tube leak.

1 F-Forced Reason: Method: Exhibit F-instructions S-Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of the Data 8-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Ref uel ing 3-Automatic Scram Event Report (LER) File D-Regulatory Restriction 4-Continuation from (HUREG 0161)

E-Operator Training S License Examination Previous Month F-Administrative 5-Reduction of 20X G-Operational Error or Greater in the Exhibit H-Same Source H-Other (Explain) Past 24 Hours 9-Other-(Explain)

NRC MONTHLY OPERATING REPORT DOCKET NO. 50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-418 OPERATING STATUS

1. Unit Name: Palo Verde Nuclear Generatin Station Unit 3
2. Reporting Period: Au ust 1988
3. Licensed Thermal Power (MWt): 3800
4. Nameplate Rating (Gross MWe): 1403
5. Design Electrical Rating (Net MWe): ~12 0 6 ~ Maximum Dependable Capacity (Gross MWe): 1303
7. Maximum Dependable Capacity (Net MWe): ~122
8. If Changes Occur In Capacity Ratings (Items Number 3 Through 7)

Since Last Report, Give Reasons: N A

9. Power Level to Which Restricted, If Any (Net MWe): one 10 Reasons For Restrictions, If Any: N A This Month Yr.-to-Date Cumulative
11. Hours in Reporting Period 44 0 5 688 0 5 688 0
12. Number of Hours Reactor Was Critical 329 5 273 5 273 7
13. Reactor Reserve Shutdown Hours 0 0 0 0 0 0
14. Hours Generator On-Line 313 4 5 250 0 5 250.0
15. Unit Reserve Shutdown Hours 0 0 0 0 0.0
16. Gross Thermal Energy Generated (MWH) 1 084 459 0 19 470 031.0 19 470 031.0
17. Gross Electrical Energy Generated (MWH) 375 000 0 6 846 500 0 6 846 500.0
18. Net Electrical Energy Generated (MWH) 330 551 0 6 443 090 0 6 443 090.0
19. Unit Service Factor 42 1 92 3 92 3
20. Unit Availability Factor 42 1 92 3 92 3a
21. Unit Capacity Factor (Using MDC Net) 36 4 92 8 92 8
22. Unit Capacity Factor (Using DER Net) 89.2
23. Unit Forced Outage Rate 7%
24. Shutdowns Scheduled Over Next Months (Type, Date, and Duration of Each):

'f 6

None 25 Shutdown At End of Report Period, Estimated Date of Startup:

N A Forecast Achieved INITIAL CRITICALITY 07787 10/025 87 INITIAL h

~08 11/128 87

~01 08 88 ELECTRICITY'OMMERCIAL OPERATION ~09 8

AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-418 MONTH: AUGUST 1988 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL 17 18 19 294 20 1 168 21 1 231 22 1 244 23 1 244 24 1 245 25 850 10 26 1 138 27 1 243 12 28 1 246 13 29 1 24 14 30 1 249 15 31 1 250 16

REFUELING INFORMATION DOCKET NO. 50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 3 1-4187

1. Scheduled date for next refueling shutdown.

03/03/89

2. Scheduled date for restart following refueling.

05/27/89

3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?'es, these are expected to include the following: 2.1.1.1, 3/4 1.1.2, 3/4 1.1.3, 3/4 1.3.1, 3/4 1.3.6, 3/4 2.1, 3/4 2.3, 3/4 2.4, 3/4 2.5, 3/4 2.8, 3/4 3.1, 3/4 3.2.
4. Scheduled date for submitting proposed licensing action and supporting information.

11/88

5. Important Licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.

'

The fuel vendor for the next five reloads will be Combustion Engineering.

6. The number of fuel assemblies a) In the core. 241 b) In the spent fuel storage pool. 0
7. Licensed spent fuel storage capacity. 1329 Intended change in spent fuel storage capacity. None
8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.

2005 (18 Month reloads and full core discharge capability).

II

SUMMARY

OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO. 50-530 UNIT NAME PVNGS-3 DATE 09 09 88 COMPLETED BY T J Bloom TELEPHONE 602 371-4187 AUGUST 1988 08/01 0000 Unit 3 in Mode 1 at approximately 8% reactor power following a lightening strike of the B-phase main transfer (main turbine trip resulted).

08/01 1625 Unit 3 entered Mode 2.

08/01 1759 Unit 3 entered Mode 3.

08/18 0620 Unit 3 entered Mode 2.

08/18 1525 Unit 3 entered Mode 1.

08/18 2238 Main generator synchronized to the grid.

08/19 1900 Reactor power at 44%

(approx.)

08/20 0639 Reactor power at 100%.

08/21 1329 Reactor power reduced to 95% following a turbine load reduction which was made in response to high backpressure in condenser a high alarm on condensate demineralizer inlet temperature.

'C'nd 08/21 1830 Reactor power at 97.5%.

08/22 0007 Reactor power at 100%.

08/25 0304 Reactor power stabilized at 50% following a reactor power cutback which resulted from the 'B'eedwater pump tripping during the weekly surveillance testing.

08/25 0645 Reactor power at 65%.

08/26 '

0831 Reactor power,'at 100%.

08/31 2400 Reactor power at 100%.

H f

SHUTDOWNS AND POWER REDUCTIONS

'

DOCKET NO. 50-530 UNIT NAME PVNGS-3 DATE COMPLETED BY T. J. Bloom Method of Cause and Corrective Duration Shutting System Component Action to No. Date Typei Hours Reason2 Down Reactor LER No. Code4 Code5 Prevent Recurrence 6 07/31 F 430.6 H N/AP N/AP N/AP Turbine trip occurred when~

a lighting strike tripped the B-phase main transformer on 7/31. Unit 3 subsequently manually shutdown to inspect/repair any damaged equipment.

7 08/25 F N/A N/AP N/AP N/AP Reactor power reduced to 50$ following a reactor power cutback which resulted from the pump tripping

'B'eedwater during surveillance testing.

F-Forced Reason: Hethod: Exhibit F-instructions S-Scheduled A-Equipment Failure (Explain) 1-Hanual for Preparation of the Data 8-Haintenance or Test 2-Hanua l Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Regulatory 'Restriction 4-Continuation from (HUREG 0161)

E-Operator Training 5 License Examination Previous Month F-Administrative 5-Reduction of 20K G-Operational Error or Greater in the Exhibit H-Same Source H-Other (Explain) Past 24 Hours 9-Other-(Explain)

Arizona Nuclear Power Project P.O. BOX 52034 ~ PHOENIX, ARIZONA85072-2034 212-00363-JGH/TJB September 13, 1988 Docket Nos. STN 50-528/529/530 Document Control Desk U. S. Nuclear Regulatory Commission Mail Station Pl-137 Washington, D.C. 20555

Dear Sirs:

Subj ect: Palo Verde Nuclear Generating Station (PVNGS)

Units 1, 2 and 3 Monthly Operating Reports for August 1988 File'8-024-404 88-056-026 Attached are the Monthly Operating Reports for August 1988 prepared and submitted pursuant to Specification 6.9.1.6 of Appendix A (Technical Specifications) to the Palo Verde Nuclear Generating Station, Units 1, 2 and 3 Operating Licenses. By copy of this letter, we are also forwarding a copy of the Monthly Operating Reports to the Regional Administrator of the Region V Office.

If you have any questions, please contact Mr. T. J. Bloom, at (602) 371-4187.

Very truly yours, J. G. Haynes Vice President Nuclear Production JGH/TJB/dim Attachments cc: ED E. Van Brunt, Jr. (all w/attachments)

D. B. Karner J. A. Amenta A. C. Gehr M. J. Davis J. B. Martin INPO Records Center

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