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| issue date = 03/31/1994
| issue date = 03/31/1994
| title = Monthly Operating Repts for Mar 1994 for Surry Power Station Units 1 & 2.W/940412 Ltr
| title = Monthly Operating Repts for Mar 1994 for Surry Power Station Units 1 & 2.W/940412 Ltr
| author name = BOWLING M L, MASON D, OLSEN C
| author name = Bowling M, Mason D, Olsen C
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:e e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 April 12, 1994 U. S. Nuclear Regulatory Commission Attention:
{{#Wiki_filter:e                                     e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 April 12, 1994 U. S. Nuclear Regulatory Commission                                               Serial No.      94-215 Attention: Document Control Desk                                                 NO/RPC:vlh Washington, D. C. 20555                                                           Docket No$ .. , .50'."280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:
Document Control Desk Washington, D. C. 20555 Gentlemen:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of March 1994.
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Serial No. 94-215 NO/RPC:vlh Docket No$ .. , .50'."280 50-281 License Nos. DPR-32 DPR-37 Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of March 1994. Very truly yours, /~i~ M. L. Bowling, ;7anager Nuclear Licensing  
Very truly yours,
& Programs Enclosure cc:
      /~i~
* U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W. Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRG Senior Resident Inspector Surry Power Station -----940418036~  
M. L. Bowling, ;7anager Nuclear Licensing & Programs Enclosure cc:
~4b33i--~~\ PDR ADOCK 05000280 R . PDR I ------------~-----* ---*--___ .:._. _, _* -__ _;!
* U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.
Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRG Senior Resident Inspector Surry Power Station 940418036~ ~4b33i- -~~\
PDR ADOCK 05000280 R
    ---- ---- --~- --
                      .             PDR I
 
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT NO. 94m03 Approved:
VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT NO. 94m03 Approved:
TABLE OF CONTENTS Section eurry Monthly Operating Report No. 94-03 Page 2of 25 Page Operating Data Report -Unit No. 1 .........................................................................................................
 
3 Operating Data Report -Unit No. 2 .........................................................................................................
eurry Monthly Operating Report No. 94-03 Page 2of 25 TABLE OF CONTENTS Section                                                                                                                                  Page Operating Data Report - Unit No. 1 .........................................................................................................3 Operating Data Report - Unit No. 2 .........................................................................................................4 Unit Shutdowns and Power Reductions - Unit No. 1.................................................................................... 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................... 6 Average Daily Unit Power Level - Unit No. 1.............................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 .............................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................... 9 Summary of Operating Experience - Unit No. 2 ....................................................................................... 10 Facility Changes That Did Not Require NRC Approval ............................................................................... 11 Procedure or Method of Operation Changes That Did Not Require NRC Approval ........................................... 20 Tests and Experiments That Did Not Require NRC Approval ...................................................................... 22 Chemistry Report ............................................................................................................................. 23 Fuel Handling - Unit No. 1 ................................................................................................................... 24 Fuel Handling - Unit No. 2 ................................................................................................................... 24 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ................................................................................................... 25
4 Unit Shutdowns and Power Reductions  
 
-Unit No. 1 ....................................................................................
41,urry Monthly Operating Report
5 Unit Shutdowns and Power Reductions  
                                                                                          ..                     No. 94-03 Page 3of 25 OPERATING DATA REPORT Docket No.:     50-280 Date:     04-06-94 Completed By:    D. Mason Telephone:     (804) 365-2459
-Unit No. 2 ....................................................................................
: 1. Unit Name: .................................................. . Surry Unit 1
6 Average Daily Unit Power Level -Unit No. 1 ..............................................................................................
: 2. Reporting Period: ........................................ .. March, 1994
7 Average Daily Unit Power Level -Unit No. 2 ..............................................................................................
: 3. Licensed Thermal Power (MWt): ...................... .               2441
8 Summary of Operating Experience  
: 4. Nameplate Rating (Gross MWe): ...................... .               847.5
-Unit No. 1 .........................................................................................
: 5. Design Electrical Rating (Net MWe): ................ ..               788
9 Summary of Operating Experience  
: 6. Maximum Dependable Capacity (Gross MWe): .. ..                       820
-Unit No. 2 .......................................................................................
: 7. Maximum Dependable Capacity (Net MWe): ...... ..                     781
10 Facility Changes That Did Not Require NRC Approval ...............................................................................
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
11 Procedure or Method of Operation Changes That Did Not Require NRC Approval ...........................................
: 9. Power Level To Which Restricted, If Any (Net MWe):
20 Tests and Experiments That Did Not Require NRC Approval ......................................................................
: 10. Reasons For Restrictions, If Any:
22 Chemistry Report .............................................................................................................................
This Month             YTD                 Cumulative
23 Fuel Handling -Unit No. 1 ...................................................................................................................
: 11. Hours In Reporting Period ..........................                 744.0               2160.0             186480.0
24 Fuel Handling -Unit No. 2 ...................................................................................................................
: 12. Number of Hours Reactor Was Critical ..........                       171.6               680.8             124488.0
24 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications  
: 13. Reactor Reserve Shutdown Hours ...............                         0                   0                 3774.5
...................................................................................................
: 14. Hours Generator On-Line ...........................                   141.8               647.9             122326.9
25 41,urry Monthly Operating Report .. No. 94-03 Page 3of 25 OPERATING DATA REPORT Docket No.: Date: Completed By: 50-280 04-06-94 D. Mason Telephone:  
: 15. Unit Reserve Shutdown Hours.....................                       0                   0                 3736.2
(804) 365-2459 1. Unit Name: .................................................. . 2. Reporting Period: ........................................  
: 16. Gross Thermal Energy Generated (MWH) ......                       256304.9           1001728.0           284169473.1
.. 3. Licensed Thermal Power (MWt): ...................... . 4. Nameplate Rating (Gross MWe): ...................... . 5. Design Electrical Rating (Net MWe): ................  
: 17. Gross Electrical Energy Generated (MWH) ....                       84040.0           ~35055.0             92874603.0
.. 6. Maximum Dependable Capacity (Gross MWe): .. .. 7. Maximum Dependable Capacity (Net MWe): ...... .. Surry Unit 1 March, 1994 2441 847.5 788 820 781 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative  
: 18. Net Electrical Energy Generated (MWH) ........                     80306.0           317769.0             88144870.0
: 11. Hours In Reporting Period ..........................
: 19. Unit Service Factor ...................................               19.1%               30.0%               65.6%
744.0 2160.0 186480.0 12. Number of Hours Reactor Was Critical ..........
: 20. Unit Availability Factor...............................               19.1%               30.0%               67.6%
171.6 680.8 124488.0 13. Reactor Reserve Shutdown Hours ...............
: 21. Unit Capacity Factor (Using MDC Net) ...........                       13.8%               18.8%               60.9%
0 0 3774.5 14. Hours Generator On-Line ...........................
: 22. Unit Capacity Factor (Using DER Net) ...........                       13.7%               18.7%               60.0%
141.8 647.9 122326.9 15. Unit Reserve Shutdown Hours .....................
: 23. Unit Forced Outage Rate ............................                   0%                   0%                 17.4%
0 0 3736.2 16. Gross Thermal Energy Generated (MWH) ...... 256304.9 1001728.0 284169473.1  
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
: 17. Gross Electrical Energy Generated (MWH) .... 84040.0 ~35055.0 92874603.0  
None
: 18. Net Electrical Energy Generated (MWH) ........ 80306.0 317769.0 88144870.0  
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 19. Unit Service Factor ...................................
19.1% 30.0% 65.6% 20. Unit Availability Factor ...............................
19.1% 30.0% 67.6% 21. Unit Capacity Factor (Using MDC Net) ...........
13.8% 18.8% 60.9% 22. Unit Capacity Factor (Using DER Net) ...........
13.7% 18.7% 60.0% 23. Unit Forced Outage Rate ............................
0% 0% 17.4% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): None 25. If Shut Down at End of Report Period, Estimated Date of Start-up:  
: 26. Unit In Test Status (Prior to Commercial Operation):
: 26. Unit In Test Status (Prior to Commercial Operation):
FORECAST INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION ACHIEVED 
FORECAST               ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
-aurry Monthly Operating Report -No. 94-03 Page 4of 25 OPERATING DATA REPORT Docket No.: 50-281 04-06-94 D. Mason Date: Completed By: Telephone:  
 
(804) 365-2459 1 . Unit Name: .................................................. . 2. Reporting Period: ......................................... . 3. Licensed Thermal Power (MWt): ...................... . 4. Nameplate Rating (Gross MWe): ...................... . 5. Design Electrical Rating (Net MWe): ................. . 6. Maximum Dependable Capacity (Gross MWe): ... . 7. Maximum Dependable Capacity (Net MWe): ....... . Surry Unit 2 March, 1994 2441 847.5 788 820 781 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons: 9. Power Level To Which Restricted, If Any (Net MWe): 10. Reasons For Restrictions, If Any: This Month YTD Cumulative  
                                  -                                                       aurry Monthly Operating Report
: 11. Hours In Reporting Period ..........................
                                                                                            -                     No. 94-03 Page 4of 25 OPERATING DATA REPORT Docket No.:     50-281 Date:    04-06-94 Completed By:    D. Mason Telephone:     (804) 365-2459
744.0 2160.0 183360.0 12. Number of Hours Reactor Was Critical ..........
: 1. Unit Name: .................................................. . Surry Unit 2
744.0 2160.0 122236.3 13. Reactor Reserve Shutdown Hours ...............
: 2. Reporting Period: ......................................... . March, 1994
0 0 328.1 14. Hours Generator On-Line ...........................
: 3. Licensed Thermal Power (MWt): ...................... .             2441
744.0 2160.0 120375.6 15. Unit Reserve Shutdown Hours .....................
: 4. Nameplate Rating (Gross MWe): ...................... .               847.5
0 0 0 16. Gross Thermal Energy Generated (MWH) ...... 1754374.1 5183840.1 280859582.5  
: 5. Design Electrical Rating (Net MWe): ................. .               788
: 17. Gross Electrical Energy Generated (MWH) .... 585635.0 1736585.0 91682209.0  
: 6. Maximum Dependable Capacity (Gross MWe): ... .                       820
: 18. Net Electrical Energy Generated (MWH) ........ 565310.0 1675337.0 87007407.0  
: 7. Maximum Dependable Capacity (Net MWe): ....... .                     781
: 19. Unit Service Factor ...................................
: 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
100.0% 100.0% 65.6% 20. Unit Availability Factor ...............................
: 9. Power Level To Which Restricted, If Any (Net MWe):
100.0% 100.0% 65.6% 21. Unit Capacity Factor (Using MDC Net) ...........
: 10. Reasons For Restrictions, If Any:
97.3% 99.3% 60.9% 22. Unit Capacity Factor (Using DER Net) ...........
This Month             YTD               Cumulative
96.4% 98.4% 60.2% 23. Unit Forced Outage Rate ............................
: 11. Hours In Reporting Period ..........................                 744.0               2160.0             183360.0
0.0% 0.0% 13.9% 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each): Maintenance, June 4, 1994, 22 Days 25. If Shut Down at End of Report Period, Estimated Date of Start-up:  
: 12. Number of Hours Reactor Was Critical ..........                       744.0               2160.0             122236.3
: 13. Reactor Reserve Shutdown Hours ...............                         0                   0                 328.1
: 14. Hours Generator On-Line ...........................                   744.0               2160.0             120375.6
: 15. Unit Reserve Shutdown Hours .....................                       0                   0                     0
: 16. Gross Thermal Energy Generated (MWH) ......                     1754374.1           5183840.1           280859582.5
: 17. Gross Electrical Energy Generated (MWH) ....                     585635.0           1736585.0             91682209.0
: 18. Net Electrical Energy Generated (MWH) ........                   565310.0           1675337.0             87007407.0
: 19. Unit Service Factor ...................................               100.0%               100.0%               65.6%
: 20. Unit Availability Factor...............................               100.0%               100.0%               65.6%
: 21. Unit Capacity Factor (Using MDC Net) ...........                       97.3%               99.3%               60.9%
: 22. Unit Capacity Factor (Using DER Net) ...........                       96.4%               98.4%               60.2%
: 23. Unit Forced Outage Rate ............................                   0.0%                 0.0%               13.9%
: 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Maintenance, June 4, 1994, 22 Days
: 25. If Shut Down at End of Report Period, Estimated Date of Start-up:
: 26. Unit In Test Status (Prior to Commercial Operation):
: 26. Unit In Test Status (Prior to Commercial Operation):
FORECAST INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION ACHIEVED (1) -urry Monthly Operating Report No. 94-03 Page 5 of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%) REPORT MONTH: March, 1994 (2) (3) (4) (5) Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 04-06-94 Completed by: Craig Olsen
FORECAST             ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
* Telephone:  
 
(804) 365-2155 Duration Method of Reason Shutting Down Rx LER No. System Component Cause & Corrective Action to Date Type Hours Code Code Prevent Recurrence (1) F: Forced S: Scheduled (4) (2) REASON: None During the Reporting Period A -Equipment Failure (Explain)
                                                                                -urry Monthly Operating Report No. 94-03 Page 5 of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%)
B Maintenance or Test C Refueling D Regulatory Restriction E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
REPORT MONTH: March, 1994 Docket No.:   50-280 Unit Name:   Surry Unit 1 Date: 04-06-94 Completed by:   Craig Olsen
Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) (3) METHOD: 1 -Manual 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)  
* Telephone:   (804) 365-2155 (1)                  (2)        (3)                (4)        (5)
(5) Exhibit 1 -Same Source. 
Method Duration                 of       LER     System Component Cause & Corrective Action to Date     Type     Hours     Reason    Shutting    No.      Code       Code     Prevent Recurrence Down Rx None During the Reporting Period (1)                           (2)                                                  (3)
(1) Date Type 940315 s (1) F: Forced S: Scheduled (4) aurry Monthly Operating Report No. 94-03 Page 6of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%} REPORT MONTH: March, 1994 (2) (3) (4) Method (5) Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 04-06-94 Completed-by:*
F:   Forced                 REASON:                                            METHOD:
Craig Olsen Telephone:  
S:   Scheduled               A - Equipment Failure (Explain)                     1 - Manual B     Maintenance or Test                           2 - Manual Scram.
(804) 365-2155 Duration of LER System Component Cause & Corrective Action to Hours 12.8 Reason B (2) REASON: Shutting No. Down Rx NIA NIA A -Equipment Failure (Explain)
C     Refueling                                     3 - Automatic Scram.
B Maintenance or Test C Refueling D Regulatory Restriction Code Code TA TRB E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)
D     Regulatory Restriction                       4 - Other (Explain)
Prevent Recurrence Reduced power to 75% to perform governor valve freedom of movement test. (3) METHOD: 1 -Manual 2 -Manual Scram. 3 -Automatic Scram. 4 -Other (Explain)  
E     Operator Training & Licensing Examination F     Administrative G     Operational Error (Explain)
(5) Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report (LER) File (NUREG 0161) Exhibit 1 -Same Source.
(4)                                                                                (5)
MONTH: March, 1994 Day 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS
Exhibit G - Instructions for Preparation of Data Entry Sheets                   Exhibit 1 - Same Source.
&urry Monthly Operating Report No. 94-03 Page 7of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 04-06-94 Completed by: Pat Kessler Telephone:
for Licensee Event Report (LER) File (NUREG 0161)
365-2790 Average Daily Power Level Average Daily Power Level (MWe-Net)
 
Day (MWe-Net) 0 17 0 0 18 0 0 19 0 0 20 0 0 21 0 0 22 0 0 23 0 0 24 0 0 25 0 0 26 168 0 27 370 0 28 554 0 29 671 0 30 791 0 31 792 0 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.
aurry       Monthly Operating Report No. 94-03 Page 6of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%}
MONTH: March, 1994 Day 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 INSTRUCTIONS tltsurry Monthly Operating Report No. 94-03 Page 8 of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 04-06-94 Completed by: Pat Kessler Telephone*:
REPORT MONTH: March, 1994 Docket No.:   50-281 Unit Name:   Surry Unit 2 Date: 04-06-94 Completed-by:*   Craig Olsen Telephone:   (804) 365-2155 (1)                  (2)        (3)                (4)      (5)
365-2790.
Method Duration                 of       LER     System Component Cause & Corrective Action to Date    Type      Hours     Reason   Shutting     No.     Code    Code      Prevent Recurrence Down Rx 940315      s      12.8        B        NIA       NIA       TA       TRB     Reduced power to 75% to perform governor valve freedom of movement test.
Average Daily Power Level Average Daily Power level (MWe-Net) Day (MWe-Net) 771 17 758 774 18 758 773 19 758 773 20 749 772 21 749 772 22 752 772 23 752 771 24 751 771 25 752 770 26 751 764 27 758 763 28 757 764 29 755 760 30 753 718 31 756 762 On this format, list the average daily unit power level in MWe -Net for each day in the reporting month. Compute to the nearest whole megawatt.
(1)                          (2)                                                (3)
esurry Monthly Operating Report No. 94-03 Page 9 of 25  
F:  Forced                  REASON:                                            METHOD:
S:  Scheduled              A - Equipment Failure (Explain)                    1 - Manual B    Maintenance or Test                          2 - Manual Scram.
C    Refueling                                    3 - Automatic Scram.
D    Regulatory Restriction                      4 - Other (Explain)
E    Operator Training & Licensing Examination F    Administrative G    Operational Error (Explain)
(4)                                                                              (5)
Exhibit G - Instructions for Preparation of Data Entry Sheets                   Exhibit 1 - Same Source.
for Licensee Event Report (LER) File (NUREG 0161)
 
                                                                                      &urry Monthly Operating Report No. 94-03 Page 7of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.:   50-280 Unit Name:   Surry Unit 1 Date: 04-06-94 Completed by:   Pat Kessler Telephone:   365-2790 MONTH:      March, 1994 Average Daily Power Level                         Average Daily Power Level Day                    (MWe-Net)                   Day                   (MWe- Net) 1                          0                     17                         0 2                          0                     18                         0 3                          0                       19                         0 4                          0                     20                         0 5                          0                     21                         0 6                          0                     22                         0 7                          0                     23                         0 8                          0                     24                         0 9                          0                     25                         0 10                          0                     26                         168 11                          0                     27                         370 12                          0                     28                         554 13                          0                     29                         671 14                          0                     30                         791 15                          0                     31                         792 16                          0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
tltsurry Monthly Operating Report No. 94-03 Page 8 of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.:   50-281 Unit Name: Surry Unit 2 Date: 04-06-94 Completed by:   Pat Kessler Telephone*: 365-2790.
MONTH:      March, 1994 Average Daily Power Level                         Average Daily Power level Day                    (MWe- Net)                   Day                   (MWe-Net) 1                        771                       17                       758 2                        774                       18                       758 3                        773                       19                       758 4                        773                     20                         749 5                        772                     21                         749 6                        772                     22                         752 7                        772                     23                         752 8                        771                     24                         751 9                        771                     25                         752 10                        770                     26                         751 11                        764                     27                         758 12                        763                     28                         757 13                        764                       29                       755 14                        760                       30                       753 15                        718                       31                       756 16                        762 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.
 
esurry Monthly Operating Report No. 94-03 Page 9 of 25


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTH/YEAR:
OF OPERATING EXPERIENCE MONTH/YEAR: March, 1994 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
March, 1994 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.
UNIT ONE:
UNIT ONE: 03/01/94 03/24/94 03/26/94 03/27/94 03/28/94 03/29/94 03/30/94 03/31/94 0000 The reporting period began with the Unit in the refueling shutdown mode. 2023 Reactor critical.
03/01/94         0000     The reporting period began with the Unit in the refueling shutdown mode.
0215 Unit on-line, started power increase.
03/24/94          2023     Reactor critical.
0255 Stopped power increase at 26%, 215 MWe, to perform flux mapping. 0258 Started power increase.
03/26/94          0215     Unit on-line, started power increase.
0000 Stopped power increase at 70% power, 578 MWe, to perform flux mapping. 0600 Started power increase.
0255     Stopped power increase at 26%, 215 MWe, to perform flux mapping.
1700 Stopped power increase at 96%, 800 MWe. 0339 Started power increase.
03/27/94          0258     Started power increase.
0425 Stopped power increase at 98%, 816 MWe. 1350 Started power increase.
03/28/94          0000     Stopped power increase at 70% power, 578 MWe, to perform flux mapping.
1418 Stopped power increase at 100%, 830 MWe. 2054 Started power reduction for core output evaluation.
03/29/94          0600     Started power increase.
2130 Stopped power reduction at 98% power, 820 MWe. 2400 The reporting period ended with the Unit at 98% power, 820 MWe, pending Engineering evaluation of reactor core power level.
1700     Stopped power increase at 96%, 800 MWe.
UN!TTwo: 03/01/94 03/10/94 03/15/94 03/19/94 03/31/94 esurry Monthly Operating Report No. 94-03 Page 10 of 25  
03/30/94          0339     Started power increase.
0425     Stopped power increase at 98%, 816 MWe.
1350     Started power increase.
1418     Stopped power increase at 100%, 830 MWe.
2054     Started power reduction for core output evaluation.
2130     Stopped power reduction at 98% power, 820 MWe.
03/31/94          2400     The reporting period ended with the Unit at 98% power, 820 MWe, pending Engineering evaluation of reactor core power level.
 
esurry Monthly Operating Report No. 94-03 Page 10 of 25


==SUMMARY==
==SUMMARY==
OF OPERATING EXPERIENCE MONTH/YEAR:
OF OPERATING EXPERIENCE MONTH/YEAR: March, 1994 UN!TTwo:
March, 1994 0000 The reporting period began with the Unit at 98% power, 810 MWe due to Steam Generator "C" level oscillations.
03/01/94 0000 The reporting period began with the Unit at 98% power, 810 MWe due to Steam Generator "C" level oscillations.
2012 Started power reduction to stabilize Steam Generator "C" level oscillations 2030 Stopped power reduction at 97%, 800 MWe. 091 O Started power reduction to perform governor valve freedom of movement test, 2-0SP-TM-001. 1340 Stopped power reduction at 75%, 620 MWe. 1415 Started power increase after completion of governor valve freedom of movement test. 2200 Stopped power increase at 97%, 800 MWe. 2255 Started power reduction to stabilize Steam Generator "C" level oscillations.
03/10/94 2012 Started power reduction to stabilize Steam Generator "C" level oscillations 2030 Stopped power reduction at 97%, 800 MWe.
2300 Stopped power reduction at 96%, 785 MWe 2400 The reporting period ended with the Unit operating at 96% power, 785 MWe, due to Steam Generator "C" level oscillations.
03/15/94 091 O Started power reduction to perform governor valve freedom of movement test, 2-0SP-TM-001.
EWR 90-228 DCP 91-05-1 TM S1-94-12 EWR 89-132 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
1340 Stopped power reduction at 75%, 620 MWe.
March, 1994 Engineering Work Request (Safety Evaluation No. 91-009) -Surry Monthly Operating Report No. 94-03 Page 11 of 25 02-28-94 Engineering Work Request 90-228 replaced the Residual Heat Removal system mechanical pump seals with an updated balanced seal. This change extends the life of the seal and minimizes seal leakage. Installation of the new balanced seal did not affect the original system design or function.
1415 Started power increase after completion of governor valve freedom of movement test.
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 91-268) 03-02-94 Design Change Package 91-05-1 removed the resistance temperature device (RTD) bypass piping system and replaced it with thermowell mounted RTDs directly in the RCS hot and cold leg pipes. The modification did not degrade the performance or increase the challenges to equipment assumed to function during an accident condition.
2200 Stopped power increase at 97%, 800 MWe.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-053) 03-03-94 Temporary Modification (TM) S1-94-12 de-energized Gaseous Drains System solenoid operated valve, 1-DG-SOV-100, and installed a mechanical jumper that bypassed 1-DG-SOV-100, thereby maintaining primary drain transfer tank pressure control valve, 1-DG-PCV-100, in the open position.
03/19/94 2255 Started power reduction to stabilize Steam Generator "C" level oscillations.
This modification was implemented to prevent spurious alarms that result from electrical noise that is generated when 1-DG-SOV-100 is energized to open 1-DG-PCV-100.
2300 Stopped power reduction at 96%, 785 MWe 03/31/94 2400 The reporting period ended with the Unit operating at 96% power, 785 MWe, due to Steam Generator "C" level oscillations.
The Unit was at cold or refueling shutdown while the TM was in place. During these plant conditions, the operation of the Primary Drains System was not affected.
 
The mechanical jumper was tested following installation and the operation of 1-DG-PCV-100 was verified following its removal. Therefore, an unreviewed safety question did not exist. Engineering Work Request 03-03-94 Engineering Work Request 89-132 installed and secured cable tray covers which restores the Cable Tray System to Regulatory Guide 1.75 and IEEE STD 384-1974 commitments of the 10 CFR 50 Appendix R Report. This resolved Appendix R and seismic integrity nonconformances that existed for Station cable trays. Therefore, an unreviewed safety question did not exist.
                                                            -Surry Monthly Operating Report No. 94-03 Page 11 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 EWR 90-228  Engineering Work Request                                               02-28-94 (Safety Evaluation No. 91-009)
SE 94-054 SE 94-055 DC P 92-043-1 FS 94-08 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
Engineering Work Request 90-228 replaced the Residual Heat Removal system mechanical pump seals with an updated balanced seal.
March, 1994 Safety Evaluation -Surry Monthly Operating Report No. 94-03 Page 12 of 25 03-04-94 Safety Evaluation 94-054 was performed to assess the removal of the baskets on the traveling water screens at the high and low level intake structures during an extreme cold weather period to prevent ice from forming and reducing the flow through the screens. * * * *' '1 The evaluation concluded that, while the temporary removal of the related baskets would allow more debris to pass by the screens, sufficient cooling water flow and heat exchanger heat transfer area would remain available for the heat exchangers to function as designed.
This change extends the life of the seal and minimizes seal leakage. Installation of the new balanced seal did not affect the original system design or function.
Therefore, an unreviewed safety question did not exist. Safety Evaluation 03-04-94 Safety Evaluation 94-055 was performed to assess an increase in the intake canal level from 30 feet to 32 feet to provide for increased cooling water inventory during an extreme cold weather period in which ice formation at the low level intake structure could result in reduced circulating water pump availability.
The evaluation concluded that the temporary change in canal level would not impact the integrity of the intake canal structure or affect the margin of safety of Technical Specifications.
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 93-176) 03-04-94 Design Change Package 92-043-1 replaced the pressurizer safety valves (PSVs) with safety valves that are designed to seal tighter under pressurizer steam conditions and discharge pipe loads. A loop seal drain line was installed to allow the loop seal to continuously drain condensation from the loop seal which allowed the removal of the loop seal ovens. Implementation of these changes eliminated the concern of Reactor Coolant System (RCS) over pressurization due to the PSV loop seals. Virginia Power calculations SM-727 and SM-700 indicated that RCS pressure will remain below 2735 psig during limiting events. Therefore, an unreviewed safety question does not exist. UFSAR Change 03-07-94 (Safety Evaluation No. 94-058) Updated Final Safety Analysis Report Change 94-058 revised Sections 11.2.3.1.6, "RF Liquid Waste Evaporator System," and 11.2.4.1.4, "Evaporator Concentrate Operations," to reflect a change in the boron concentration in the Liquid Waste Evaporator System, which is located at the Surry Radwaste Facility.
The boron concentration was increased to reduce the volume of radioactive waste. This change did not impact safety-related systems or affect the margin of safety of Technical Specifications.
Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist.
TM S1-94-13 TM S1-94-14 DCP 92-41-1 EWR 93-002 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
DCP 91-05-1 Design Change Package                                                  03-02-94 (Safety Evaluation No. 91-268)
March, 1994 Temporary Modification (Safety Evaluation No. 94-059) &urry Monthly Operating Report No. 94-03 Page 13 of 25 03-07-94 Temporary Modification S1-94-13 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards
Design Change Package 91-05-1 removed the resistance temperature device (RTD) bypass piping system and replaced it with thermowell mounted RTDs directly in the RCS hot and cold leg pipes.
* ** (CLS) System circuits*
The modification did not degrade the performance or increase the challenges to equipment assumed to function during an accident condition. Therefore, an unreviewed safety question did not exist.
and* prevent a spurious' Hi-CLS signal during the replacement of relay 1-CLS-RLY-1 BM. The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required.
TM S1-94-12 Temporary Modification                                                03-03-94 (Safety Evaluation No. 94-053)
The operation of other systems was not affected.
Temporary Modification (TM) S1-94-12 de-energized Gaseous Drains System solenoid operated valve, 1-DG-SOV-100, and installed a mechanical jumper that bypassed 1-DG-SOV-100, thereby maintaining primary drain transfer tank pressure control valve, 1-DG-PCV-100, in the open position. This modification was implemented to prevent spurious alarms that result from electrical noise that is generated when 1-DG-SOV-100 is energized to open 1-DG-PCV-100.
Double verification of jumper installation/removal and post-maintenance testing was performed.
The Unit was at cold or refueling shutdown while the TM was in place. During these plant conditions, the operation of the Primary Drains System was not affected. The mechanical jumper was tested following installation and the operation of 1-DG-PCV-100 was verified following its removal. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-060) 03-07-94 Temporary Modification S1-94-14 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A1.
EWR 89-132  Engineering Work Request                                              03-03-94 Engineering Work Request 89-132 installed and secured cable tray covers which restores the Cable Tray System to Regulatory Guide 1.75 and IEEE STD 384-1974 commitments of the 10 CFR 50 Appendix R Report.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required.
This resolved Appendix R and seismic integrity nonconformances that existed for Station cable trays. Therefore, an unreviewed safety question did not exist.
The operation of other systems was not affected.
 
Double verification of jumper installation/removal and post-maintenance testing was performed.
                                                                  -Surry Monthly Operating Report No. 94-03 Page 12 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 SE 94-054    Safety Evaluation                                                          03-04-94 Safety Evaluation 94-054 was performed to assess the removal of the baskets on the traveling water screens at the high and low level intake structures during an extreme cold weather period to prevent ice from forming and reducing the flow through the screens.                                    *          * * *'       '1 The evaluation concluded that, while the temporary removal of the non-safety-related baskets would allow more debris to pass by the screens, sufficient cooling water flow and heat exchanger heat transfer area would remain available for the heat exchangers to function as designed. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 92-97) 03-08-94 Design Change Package 92-41-1 replaced a leaking level transmitter's manifold with three single valves since no direct replacement manifold was available.
SE 94-055    Safety Evaluation                                                           03-04-94 Safety Evaluation 94-055 was performed to assess an increase in the intake canal level from 30 feet to 32 feet to provide for increased cooling water inventory during an extreme cold weather period in which ice formation at the low level intake structure could result in reduced circulating water pump availability.
The change enhanced the system because a single failure of a valve will not require the replacement of a manifold.
The evaluation concluded that the temporary change in canal level would not impact the integrity of the intake canal structure or affect the margin of safety of Technical Specifications. Therefore, an unreviewed safety question did not exist.
The operation and function of the system was not altered. Therefore, an unreviewed safety question did not exist. Engineering Work Request (Safety Evaluation No. 93-035) 03-08-94 Engineering Work Request 93-002 completed steam generator wrapper modifications which involved permanent removal of all four wrapper plug assemblies, removal of a portion of the wrapper seal plates, and removal of the outer tube lane blocking devices. This modification reduces radiation exposure to personnel by reducing the effort and time required for wrapper entry. The modifications improve sludge lancing efficiency and improve access for foreign object search and recovery.
DC P 92-043-1 Design Change Package                                                      03-04-94 (Safety Evaluation No. 93-176)
The modifications do not affect the safety limits, surveillance requirements, limiting conditions of operations or system tests as described in the Technical Specifications.
Design Change Package 92-043-1 replaced the pressurizer safety valves (PSVs) with safety valves that are designed to seal tighter under pressurizer steam conditions and discharge pipe loads. A loop seal drain line was installed to allow the loop seal to continuously drain condensation from the loop seal which allowed the removal of the loop seal ovens.
Therefore, an unreviewed safety question did not exist.
Implementation of these changes eliminated the concern of Reactor Coolant System (RCS) over pressurization due to the PSV loop seals. Virginia Power calculations SM-727 and SM-700 indicated that RCS pressure will remain below 2735 psig during limiting events. Therefore, an unreviewed safety question does not exist.
TM S1-94-15 TM S1-94-16 TM S1-94-17 TM S1-94-18 TM S1-94-19 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
FS 94-08      UFSAR Change                                                                03-07-94 (Safety Evaluation No. 94-058)
March, 1994 Temporary Modifications (Safety Evaluation No. 94-062) &urry Monthly Operating Report No. 94-03 Page 14of 25 03-09-94 Temporary Modifications (TM) S1-94-15 and S1-94-16 removed containment sump trip valve, 1-DA-TV-1 OOA, for maintenance and installed a spool piece and electrical jumpers to *maintain" an* operable flow path frorri *containment sump pumps 1-DA-P-4A and 1-DA-P-48.
Updated Final Safety Analysis Report Change 94-058 revised Sections 11.2.3.1.6, "RF Liquid Waste Evaporator System," and 11.2.4.1.4, "Evaporator Concentrate Operations," to reflect a change in the boron concentration in the Liquid Waste Evaporator System, which is located at the Surry Radwaste Facility.
The Unit was at cold shutdown while the TM was in place. The containment sump trip valve closure interlocks, which would shut off pumps 1-DA-P-4A and 1-DA-P-4B, were defeated to allow pump operation to continue as needed. The pump interlocks of the redundant valve 1-DA-TV-1008 remained operable.
The boron concentration was increased to reduce the volume of radioactive waste. This change did not impact safety-related systems or affect the margin of safety of Technical Specifications. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-064) 03-10-94 Temporary Modification (TM) S1-94-17 installed electrical jumpers to bypass test switch 1-SI-CS-LC494-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.
 
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required.
                                                                  &urry Monthly Operating Report No. 94-03 Page 13 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-13      Temporary Modification                                                  03-07-94 (Safety Evaluation No. 94-059)
Double verification of jumper installation/removal and maintenance testing was performed.
Temporary Modification S1-94-13 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-066) 03-10-94 Temporary Modification (TM) S1-94-18 installed electrical jumpers to bypass test switch TS-LC-476-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.
            * ** (CLS) System circuits* and* prevent a spurious' Hi-CLS signal during the replacement of relay 1-CLS-RLY-1 BM.
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.
Double verification of jumper installation/removal and maintenance testing was performed.
Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-063) 03-10-94 Temporary Modification S1-94-19 installed electrical jumpers to maintain power to certain Unit 1 Safety Injection (SI) System circuits and prevent a spurious SI signal during the replacement of relay 1-SI-RL Y-FC-475-XA.
TM S1-94-14      Temporary Modification                                                   03-07-94 (Safety Evaluation No. 94-060)
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required.
Temporary Modification S1-94-14 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A1.
The operation of other systems was not affected.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.
Double verification of jumper installation/removal and post-maintenance testing was performed.
Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist.
DCP 92-41-1      Design Change Package                                                    03-08-94 (Safety Evaluation No. 92-97)
TM S1-94-20 TM S1-94-21 DCP 93-018-1 DCP 93-15-1 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
Design Change Package 92-41-1 replaced a leaking level transmitter's manifold with three single valves since no direct replacement manifold was available.
March, 1994 Temporary Modification (Safety Evaluation No. 94-065) -Surry Monthly Operating Report No. 94-03 Page 15 of 25 03-10-94 Temporary Modification (TM) S1 20 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection (RP) System Train "~" circuits during the replacement of rela:y TT-XB. * *
The change enhanced the system because a single failure of a valve will not require the replacement of a manifold. The operation and function of the system was not altered. Therefore, an unreviewed safety question did not exist.
* The activity was performed while Unit 1 was at cold shutdown and did not affect RP System Train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed.
EWR 93-002      Engineering Work Request                                                03-08-94 (Safety Evaluation No. 93-035)
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-068) 03-13-94 Temporary Modification (TM) S1-94-21 installed an electrical jumper to provide the proper input to the Unit 1 reactor coolant pump (RCP) "A" trip logic to enable the pump to be started. This TM was necessary since the loop "A" isolation valve "open" stem position switch was not in the correct position.
Engineering Work Request 93-002 completed steam generator wrapper modifications which involved permanent removal of all four wrapper plug assemblies, removal of a portion of the wrapper seal plates, and removal of the outer tube lane blocking devices.
The activity was performed while Unit 1 was at cold shutdown.
This modification reduces radiation exposure to personnel by reducing the effort and time required for wrapper entry. The modifications improve sludge lancing efficiency and improve access for foreign object search and recovery.         The modifications do not affect the safety limits, surveillance requirements, limiting conditions of operations or system tests as described in the Technical Specifications. Therefore, an unreviewed safety question did not exist.
The TM placed the RCP "A" trip logic in the normal state for power operation and did not affect the integrity or operation of the valve. Double verification of jumper installation/removal was performed.
 
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 93-175) 03-13-94 Design Change Package 93-018-1 re-routed the miniflow recirculation line due to a leak in the buried portion of the line. The line previously discharged directly into the Emergency Condensate Storage Tank and now discharges into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Flow Recirculation line. Although the mini-flow recirculation line has been re-routed to discharge into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Flow Recirculation line, the operation/performance of the Auxiliary Feedwater Pumps was not altered. Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 93-169) 03-14-93 Design Change Package 93-15-1 replaced 01-CS-MOV-102A and B valves and operators because of a less than satisfactory material condition due to high thrust seating loads. This was an in-kind replacement and had no affect on the consequences of any evaluated accidents.
                                                                &urry Monthly Operating Report No. 94-03 Page 14of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-15 Temporary Modifications                                                    03-09-94 TM S1-94-16 (Safety Evaluation No. 94-062)
Therefore, an unreviewed safety question did not exist..
Temporary Modifications (TM) S1-94-15 and S1-94-16 removed containment sump trip valve, 1-DA-TV-1 OOA, for maintenance and installed a spool piece and electrical jumpers to *maintain" an* operable flow path frorri *containment sump pumps 1-DA-P-4A and 1-DA-P-48.
DR S-94-0615 TM S1-94-22 TM S1-94-23 TM S1-94-24 e FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
The Unit was at cold shutdown while the TM was in place. The containment sump trip valve closure interlocks, which would shut off pumps 1-DA-P-4A and 1-DA-P-4B, were defeated to allow pump operation to continue as needed. The pump interlocks of the redundant valve 1-DA-TV-1008 remained operable. Therefore, an unreviewed safety question did not exist.
March, 1994 Deviation Report (Safety Evaluation No. 94-071) -Surry Monthly Operating Report No. 94-03 Page 16 of 25 03-14-94 Safety Evaluation 94-071 assessed the condition reported by Deviation Report S-94-0615 concerning the continued operation of Unit 1 with a small immobile foreign* object (wire approximately 1/8" to 5/32" diameter estimated to be less than 0.1 pounds) in the secondary side of Unit 1 steam generator (SG) "A". Attempts to remove the object have been unsuccessful.
TM S1-94-17 Temporary Modification                                                    03-10-94 (Safety Evaluation No. 94-064)
An evaluation of Unit 1 operation with the SG containing the foreign object was performed by Westinghouse Nuclear Safety. The evaluation concluded that the presence of the object will have no adverse effect on the pressure boundary integrity of the SG and does not create an unreviewed safety question provided future eddy current inspections support no tube degradation due to wear. Temporary Modification (Safety Evaluation No. 94-070) 03-14-94 Temporary Modification S1-94-22 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A02.
Temporary Modification (TM) S1-94-17 installed electrical jumpers to bypass test switch 1-SI-CS-LC494-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required.
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
The operation of other systems was not affected.
TM S1-94-18 Temporary Modification                                                    03-10-94 (Safety Evaluation No. 94-066)
Double verification of jumper installation/removal and post-maintenance testing was performed.
Temporary Modification (TM) S1-94-18 installed electrical jumpers to bypass test switch TS-LC-476-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-069) 03-14-94 Temporary Modification S1-94-23 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "A" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of Leakage Monitoring System relay 1-LM-RL Y-1 OOA 1. The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required.
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist.
TM S1-94-19 Temporary Modification                                                    03-10-94 (Safety Evaluation No. 94-063)
* Temporary Modification (Safety Evaluation No. 94-072) 03-15-94 Temporary Modification S1-94-24 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of CLS relay 1-CLS-RLY-1 B13. The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required.
Temporary Modification S1-94-19 installed electrical jumpers to maintain power to certain Unit 1 Safety Injection (SI) System circuits and prevent a spurious SI signal during the replacement of relay 1-SI-RLY-FC-475-XA.
The operation of other systems was not affected.
The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. The operation of other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
Double verification of jumper installation/removal and post-maintenance testing was performed.
 
Therefore, an unreviewed safety question did not exist.
                                                                  -Surry Monthly Operating Report No. 94-03 Page 15 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-20  Temporary Modification                                                     03-10-94 (Safety Evaluation No. 94-065)
TM S1-94-25 TM S1-94-26 DR S-94-0097 TM S1-94-27 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
Temporary Modification (TM) S1 20 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection (RP) System Train "~" circuits during the replacement of rela:y TT-XB.         *        *
March, 1994 Temporary Modification (Safety Evaluation No. 94-073) &urry Monthly Operating Report No. 94-03 Page 17of 25 03-16-94 Temporary Modification (TM) S1-94-25 installed an electrical jumper to bypass the failed Unit 1 Consequence Limiting Safeguards (CLS) alarm ~ircuit relay 1808 and
* The activity was performed while Unit 1 was at cold shutdown and did not affect RP System Train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
* clear Control Room annunciator 1-8-4, "CLS Coil Failure." * ** *
TM S1-94-21  Temporary Modification                                                     03-13-94 (Safety Evaluation No. 94-068)
Temporary Modification (TM) S1-94-21 installed an electrical jumper to provide the proper input to the Unit 1 reactor coolant pump (RCP) "A" trip logic to enable the pump to be started. This TM was necessary since the loop "A" isolation valve "open" stem position switch was not in the correct position.
The activity was performed while Unit 1 was at cold shutdown. The TM placed the RCP "A" trip logic in the normal state for power operation and did not affect the integrity or operation of the valve.             Double verification of jumper installation/removal was performed. Therefore, an unreviewed safety question did not exist.
DCP 93-018-1 Design Change Package                                                      03-13-94 (Safety Evaluation No. 93-175)
Design Change Package 93-018-1 re-routed the miniflow recirculation line due to a leak in the buried portion of the line. The line previously discharged directly into the Emergency Condensate Storage Tank and now discharges into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Full-Flow Recirculation line.
Although the mini-flow recirculation line has been re-routed to discharge into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Full-Flow Recirculation line, the operation/performance of the Auxiliary Feedwater Pumps was not altered. Therefore, an unreviewed safety question did not exist.
DCP 93-15-1  Design Change Package                                                      03-14-93 (Safety Evaluation No. 93-169)
Design Change Package 93-15-1 replaced 01-CS-MOV-102A and B valves and operators because of a less than satisfactory material condition due to high thrust seating loads.
This was an in-kind replacement and had no affect on the consequences of any evaluated accidents. Therefore, an unreviewed safety question did not exist..
 
e                                            -Surry Monthly Operating Report No. 94-03 Page 16 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 DR S-94-0615 Deviation Report                                                      03-14-94 (Safety Evaluation No. 94-071)
Safety Evaluation 94-071 assessed the condition reported by Deviation Report S-94-0615 concerning the continued operation of Unit 1 with a small immobile foreign* object (wire approximately 1/8" to 5/32" diameter estimated to be less than 0.1 pounds) in the secondary side of Unit 1 steam generator (SG) "A".
Attempts to remove the object have been unsuccessful.
An evaluation of Unit 1 operation with the SG containing the foreign object was performed by Westinghouse Nuclear Safety. The evaluation concluded that the presence of the object will have no adverse effect on the pressure boundary integrity of the SG and does not create an unreviewed safety question provided future eddy current inspections support no tube degradation due to wear.
TM S1-94-22  Temporary Modification                                                03-14-94 (Safety Evaluation No. 94-070)
Temporary Modification S1-94-22 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A02.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.
Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
TM S1-94-23  Temporary Modification                                                03-14-94 (Safety Evaluation No. 94-069)
Temporary Modification S1-94-23 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "A" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of Leakage Monitoring System relay 1-LM-RLY-1 OOA 1.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. Therefore, an unreviewed safety question did not exist.
* TM S1-94-24  Temporary Modification                                                03-15-94 (Safety Evaluation No. 94-072)
Temporary Modification S1-94-24 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of CLS relay 1-CLS-RLY-1 B13.
The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.
Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
 
                                                                  &urry Monthly Operating Report No. 94-03 Page 17of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-25    Temporary Modification                                                      03-16-94 (Safety Evaluation No. 94-073)
Temporary Modification (TM) S1-94-25 installed an electrical jumper to bypass the failed Unit 1 Consequence Limiting Safeguards (CLS) alarm ~ircuit relay 1808 and
* clear Control Room annunciator 1-8-4, "CLS Coil Failure."       *     ** *
* The subject Hi CLS System Train "B" relay is a spare that performs no function.
* The subject Hi CLS System Train "B" relay is a spare that performs no function.
The activity did not affect other systems or the Hi CLS System Train "A". The operability of the affected alarms were verified following the installation of the TM. Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-074) 03-16-94 Temporary Modification S1-94-26 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "B" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of relay 1-CLS-RL Y-2804. The activity was performed while Unit 1 was at cold shutdown when the CLS system was not required.
The activity did not affect other systems or the Hi CLS System Train "A". The operability of the affected alarms were verified following the installation of the TM.
Therefore, an unreviewed safety question did not exist. Deviation Report 03-17-94 (Safety Evaluation No. 94-076) Safety Evaluation 94-076 assessed the condition reported by Deviation Report S-94-0097 concerning continued station operation with a through-wall leak of charging pump service water discharge piping located in the Auxiliary Building.
The assessment concluded that the leak does not affect the design function of the Charging Service Water System, other safety-related systems, or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-075) 03-17-94 Temporary Modification S1-94-27 installed an electrical jumper to maintain power to. certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of relay 1-RP-RL Y-AFP1-XA.
The activity was performed while Unit 1 was shut down with the reactor trip and bypass breakers open. The operation of RPS train "B" and other systems was not affected.
Double verification of jumper installation/removal and maintenance testing was performed.
Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist.
EWR 88-476 TM S1-94-28 TM S1-94-29 DC P 93-036-1 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
TM S1-94-26    Temporary Modification                                                      03-16-94 (Safety Evaluation No. 94-074)
March, 1994 Engineering Work Request tltsurry Monthly Operating Report No. 94-03 Page 18 of 25 03-19-94 Engineering Work Request 88-476 assessed the spiking of instrumentation in the Nuclear Instrumentation system (NIS) cabinets and removed line conditioning transformers that had failed. It was determined that the power coming from the
Temporary Modification S1-94-26 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "B" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of relay 1-CLS-RLY-2804.
* Uninterruptible Power Supply system was sufficiently*clean as a source of power to the NIS System. Only one channel of NIS was altered at a time. Therefore, an unreviewed safety . question did not exist. Temporary Modification (Safety Evaluation No. 94-079) 03-21-94 Temporary Modification (TM) S1-94-28 installed an electrical jumper to maintain power to certain Unit 1 Reactor Protection (RP) System Train "B" circuits during the replacement of relay AST1-XB. The activity was performed while Unit 1 was below 350 °F/450 psig and did not affect RP System train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed.
The activity was performed while Unit 1 was at cold shutdown when the CLS system was not required. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Temporary Modification (Safety Evaluation No. 94-080) 03-22-94 Temporary Modification S1-94-29 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of RPS relay SV3XA. The activity was performed while Unit 1 was subcritical with all contrql rods inserted.
DR S-94-0097  Deviation Report                                                            03-17-94 (Safety Evaluation No. 94-076)
The operation of RPS Train "B" and other systems was not affected.
Safety Evaluation 94-076 assessed the condition reported by Deviation Report S-94-0097 concerning continued station operation with a through-wall leak of charging pump service water discharge piping located in the Auxiliary Building.
Double verification of jumper installation/removal and post-maintenance testing was performed.
The assessment concluded that the leak does not affect the design function of the Charging Service Water System, other safety-related systems, or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 93-165) 03-22-94 Design Change Package 93-036-1 replaced carbon steel piping with moly piping to mitigate flow accelerated corrosion.
TM S1-94-27    Temporary Modification                                                      03-17-94 (Safety Evaluation No. 94-075)
Temporary Modification S1-94-27 installed an electrical jumper to maintain power to. certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of relay 1-RP-RLY-AFP1-XA.
The activity was performed while Unit 1 was shut down with the reactor trip and bypass breakers open. The operation of RPS train "B" and other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
 
tltsurry Monthly OperatingNo.Report 94-03 Page 18 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 EWR 88-476      Engineering Work Request                                                 03-19-94 Engineering Work Request 88-476 assessed the spiking of instrumentation in the Nuclear Instrumentation system (NIS) cabinets and removed line conditioning transformers that had failed. It was determined that the power coming from the
* Uninterruptible Power Supply system was sufficiently*clean as a source of power to the NIS System.
Only one channel of NIS was altered at a time. Therefore, an unreviewed safety
              . question did not exist.
TM S1-94-28      Temporary Modification                                                   03-21-94 (Safety Evaluation No. 94-079)
Temporary Modification (TM) S1-94-28 installed an electrical jumper to maintain power to certain Unit 1 Reactor Protection (RP) System Train "B" circuits during the replacement of relay AST1-XB.
The activity was performed while Unit 1 was below 350 °F/450 psig and did not affect RP System train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
TM S1-94-29      Temporary Modification                                                   03-22-94 (Safety Evaluation No. 94-080)
Temporary Modification S1-94-29 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of RPS relay SV3XA.
The activity was performed while Unit 1 was subcritical with all contrql rods inserted. The operation of RPS Train "B" and other systems was not affected.
Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
DC P 93-036-1    Design Change Package                                                   03-22-94 (Safety Evaluation No. 93-165)
Design Change Package 93-036-1 replaced carbon steel piping with chrome-moly piping to mitigate flow accelerated corrosion.
Piping was replaced in the Main Steam Trap Discharge Header, the Secondary Plant Drain system and the Condensate system. This material replacement did not result in any changes to the system form, fit, function, or operation.
Piping was replaced in the Main Steam Trap Discharge Header, the Secondary Plant Drain system and the Condensate system. This material replacement did not result in any changes to the system form, fit, function, or operation.
Therefore, an unreviewed safety question did not exist.
Therefore, an unreviewed safety question did not exist.
TM S1-94-30 DCP 91-027-3 SE 94-082 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
 
March, 1994 Temporary Modification (Safety Evaluation No. 94-081) &urry Monthly Operating Report No. 94-03 Page 19 of 25 03-23-94 Temporary Modification S1-94-30 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "B" circuits during the *
                                                                    &urry Monthly Operating Report No. 94-03 Page 19 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-30      Temporary Modification                                                     03-23-94 (Safety Evaluation No. 94-081)
* replacement of RPS relay SRB-XB. The activity was performed while Unit 1 was at hot shutdown with the reactor trip breakers open. The operation of RPS Train "A" and other systems was not affected.
Temporary Modification S1-94-30 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "B" circuits during the
Double verification of jumper installation/removal and post-maintenance testing was performed.
            *
Therefore, an unreviewed safety question did not exist. Design Change Package (Safety Evaluation No. 93-060) 03-24-94 Design Change Package 91-027-3 modified the closed loop seal cooling circuit for the Low Head Safety Injection (LHSI) and Outside Recirculating Spray (ORS) Pumps. The modification included the replacement of the seal cooling coils with new seal coolers and the addition of isolation valves at the seal and cooler. This change eliminated the venting and filling difficulties with the LHSI and ORS pump seal cooling circuits which caused seal head tank low level alarms. The design of the new seal coolers and its cooling circuit meet the trequirements of ASM E Section VIII for design basis accident conditions to a rating of 170 psig/250° F which is consistent with the LHSI and ORS pump seal cooling circuits.
* replacement of RPS relay SRB-XB.
Therefore, an unreviewed safety question does not exist. Safety Evaluation 03-28-94 Safety Evaluation 94-082 was performed to assess a re-analysis of the Large Break Loss of Coolant Accident (LBLOCA) that used Westinghouse's ECCS Evaluation Model, denoted as the 1981 Model with BASH (computer code). The evaluation concluded that the analysis parameters were equivalent to, or conservative with respect to, those allowed by the Technical Specifications, and that the LBLOCA meets the requirements of 1 O CFR 50.46. Therefore, an unreviewed safety question does not exist.
The activity was performed while Unit 1 was at hot shutdown with the reactor trip breakers open. The operation of RPS Train "A" and other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.
1-0P-Sl-002 O-MOP-SW-010 O-MOP-SW-011 O-EPM-0105-01
DCP 91-027-3    Design Change Package                                                     03-24-94 (Safety Evaluation No. 93-060)
&urry Monthly Operating Report No. 94-03 Page 20 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
Design Change Package 91-027-3 modified the closed loop seal cooling circuit for the Low Head Safety Injection (LHSI) and Outside Recirculating Spray (ORS)
March, 1994 Operating Procedure (Safety Evaluation No. 94-057) 03-06-94 Operating Procedure 1-0P-Sl-002, "Safety Injection Accumulators", was temporarily changed to provide instructions for installing a temporary mechanical jumper to permit the Unit 1 refueling water storage tank recirculation pumps to be used to fill the Safety Injection (SI) System accumulators while the SI hydro pump is out of service. The mechanical jumper was installed when the Unit was at cold/refueling shutdown and the SI System was not required.
Pumps. The modification included the replacement of the seal cooling coils with new seal coolers and the addition of isolation valves at the seal and cooler.
The jumper was rated for the pressure of the associated piping flow path, inspected for leakage after it was placed in service, and removed before the Unit left cold shutdown.
This change eliminated the venting and filling difficulties with the LHSI and ORS pump seal cooling circuits which caused seal head tank low level alarms. The design of the new seal coolers and its cooling circuit meet the trequirements of ASM E Section VIII for design basis accident conditions to a rating of 170 psig/250° F which is consistent with the LHSI and ORS pump seal cooling circuits.
Therefore, an unreviewed safety question did not exist. Maintenance Operating Procedures (Safety Evaluation No. 94-061) 03-07-94 Maintenance Operating Procedures O-MOP-SW-010, "Removal From Service of the Unit 1 Service Water Supply Header'' and O-MOP-SW-011, "Return to Service of the Unit 1 Service Water Supply Header" were developed to provide instructions for removing the Service Water Supply Header from service (and returning it to service) to permit the replacement of degraded equipment.
Any blank flanges used during the performance of these procedures will meet the criteria for the piping class for which they are installed and a leak test will be performed to verify the adequacy of the installation.
These procedures will be performed within the Limiting Conditions for Operation as defined by the Technical Specifications.
Therefore, an unreviewed safety question does not exist. Electrical Preventive Maintenance Procedure (Safety Evaluation No. 94-067) 03-11-94 Electrical Preventive Maintenance Procedure O-EPM-0105-01 , "Appendix R EL T Eight Hour Duration Test" was developed to provide instructions for conducting performance discharge tests for emergency lighting, replacing lamp heads, and performing minor cleaning.
This procedure may be implemented while the units are at power and will be performed for only one fire area at a time. Battery powered lanterns are provided in the Appendix R cabinet for use by Operations personnel during the test and for the 24 hour post test period in which the emergency lighting batteries are being recharged.
This activity will not affect the probability of occurrence or the consequences of any previously analyzed accidents.
Therefore, an unreviewed safety question does not exist.
Therefore, an unreviewed safety question does not exist.
1-IPT-RP-TM-001 2-IPT-RP-TM-001 1-PT-8.2 -Surry Monthly Operating Report No. 94-03 Page 21 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC* APPROVAL MONTH/YEAR:
SE 94-082        Safety Evaluation                                                          03-28-94 Safety Evaluation 94-082 was performed to assess a re-analysis of the Large Break Loss of Coolant Accident (LBLOCA) that used Westinghouse's LOCA-ECCS Evaluation Model, denoted as the 1981 Model with BASH (computer code).
March, 1994 Instrument Periodic Test Procedures (Safety Evaluation No. 94-077) 03-17-94 Instrument Periodic Test Procedures 1/2-IPT-RP-TM-001, "Turbine Trip Signal to Reactor Protection System Functional Test" were developed to provide instructions for installing electrical jumpers to permit testing of the turbine trip signal to the Reactor Protection System.
The evaluation concluded that the analysis parameters were equivalent to, or conservative with respect to, those allowed by the Technical Specifications, and that the LBLOCA meets the requirements of 10 CFR 50.46. Therefore, an unreviewed safety question does not exist.
* The procedures will be performed on only one channel of the circuitry at a time and at less than 10% reactor power, thereby preventing a spurious reactor trip. The installation and removal of the electrical jumpers will be independently verified.
 
Therefore, an unreviewed safety question does not exist. Instrumentation Periodic Test Procedure (Safety Evaluation No. 93-075, Revision 1) 03-18-94 Periodic Test procedure 1-PT-8.2, "Reactor Protection Logic," was temporarily changed to provide instructions for testing the Station service bus undervoltage automatic start signal for the Turbine-Driven Auxiliary Feedwater Pump (TDAFWP) and the steam generator low-low level TDAFWP trip signal. The procedure included administrative control steps for the steam generator (SG) blowdown permissive key switches to ensure proper operation of the SG blowdown trip valves during the performance of the procedure.
                                                                  &urry Monthly Operating Report No. 94-03 Page 20 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 1-0P-Sl-002    Operating Procedure                                                        03-06-94 (Safety Evaluation No. 94-057)
During the performance of this test, the SG blowdown permissive key switches were placed under administrative control when in the permissive mode. The procedural steps directed an operator to place the key switches in the normal position in the event of an Auxiliary Feedwater System automatic start signal. This action ensured the operability of the SG blowdown trip valves. Therefore, an unreviewed safety question did not exist.
Operating Procedure 1-0P-Sl-002, "Safety Injection Accumulators", was temporarily changed to provide instructions for installing a temporary mechanical jumper to permit the Unit 1 refueling water storage tank recirculation pumps to be used to fill the Safety Injection (SI) System accumulators while the SI hydro pump is out of service.
&urry Monthly Operating Report No. 94-03 Page 22 of 25 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR:
The mechanical jumper was installed when the Unit was at cold/refueling shutdown and the SI System was not required. The jumper was rated for the pressure of the associated piping flow path, inspected for leakage after it was placed in service, and removed before the Unit left cold shutdown. Therefore, an unreviewed safety question did not exist.
March, 1994 None During the Reporting Period Primary Coolant Analysis Gross Radioactivity, µCi/ml Susoended Solids, oom Gross Tritium, µCi/ml 1131, µCi/ml 113111133 Hydroaen, cc/ka Lithium, oom Boron -1 o, oom* Oxvaen, (DO), oom Chloride, oom pH at 25 degree Celsius Boron -1 O = Total Boron x 0.196 Comments:
O-MOP-SW-010  Maintenance Operating Procedures                                            03-07-94 O-MOP-SW-011  (Safety Evaluation No. 94-061)
None CHEMISTRY REPORT MONTH/YEAR:
Maintenance Operating Procedures O-MOP-SW-010, "Removal From Service of the Unit 1 Service Water Supply Header'' and O-MOP-SW-011, "Return to Service of the Unit 1 Service Water Supply Header" were developed to provide instructions for removing the Service Water Supply Header from service (and returning it to service) to permit the replacement of degraded equipment.
March, 1994 Unit No. 1 Max. Min. Ava. 2.81 E-1 2.03E-4 3.01 E-2 0.150 < 0.01 0.050 9.73E-3 5.40E-3 7.57E-3 2.53E-4 3.61E-5 1.04E-4 ---36.8 4.9 22.0 3.48 < 0.1 2.34 481.0 . 229.3 400.3 6.0 0.005 2.48 0.050 0.001 0.005 6.29 4.42 4.91 -Surry Monthly Operating Report No. 94-03 Page 23 of 25 Unit No. 2 Max. Min. Ava. 2.19E-1 1.15E-1 1.56E-1 < 0.1 < o.*1 < 0.1 6.95E-1 6.49E-1 6.72E-1 2.71 E-4 4.62E-5 7.90E-5 0.09 0.05 0.07 43.0 35.0 38.4 2.31 2.06 2.19 174.6 159.3 167.5 0.005 0.005 0.005 0.050 0.002 0.008 6.57 6.19 6.44 New or Spent Fuel Shipment Date Stored or Number Received FUEL HANDLING UNITS 1 & 2 MONTH/YEAR:
Any blank flanges used during the performance of these procedures will meet the criteria for the piping class for which they are installed and a leak test will be performed to verify the adequacy of the installation. These procedures will be performed within the Limiting Conditions for Operation as defined by the Technical Specifications. Therefore, an unreviewed safety question does not exist.
March, 1994 Number of Assemblies per Shipment Assembly Number ANSI Number &urry Monthly Operating Report No. 94-03 Page 24of 25 Initial Enrichment New or Spent Fuel Shipping Cask Activity No Fuel Received or Stored During the Reporting Period.
O-EPM-0105-01  Electrical Preventive Maintenance Procedure                                03-11-94 (Safety Evaluation No. 94-067)
e &urry Monthly Operating Report No. 94-03 Page 25 of 25 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETIED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR:
Electrical Preventive Maintenance Procedure O-EPM-0105-01 , "Appendix R ELT Eight Hour Duration Test" was developed to provide instructions for conducting performance discharge tests for emergency lighting, replacing lamp heads, and performing minor cleaning.
March, 1994 None During the Reporting Period.}}
This procedure may be implemented while the units are at power and will be performed for only one fire area at a time. Battery powered lanterns are provided in the Appendix R cabinet for use by Operations personnel during the test and for the 24 hour post test period in which the emergency lighting batteries are being recharged. This activity will not affect the probability of occurrence or the consequences of any previously analyzed accidents. Therefore, an unreviewed safety question does not exist.
 
                                                                    -Surry Monthly Operating Report No. 94-03 Page 21 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC* APPROVAL MONTH/YEAR: March, 1994 1-IPT-RP-TM-001  Instrument Periodic Test Procedures                                       03-17-94 2-IPT-RP-TM-001  (Safety Evaluation No. 94-077)
Instrument Periodic Test Procedures 1/2-IPT-RP-TM-001, "Turbine Trip Signal to Reactor Protection System Functional Test" were developed to provide instructions for installing electrical jumpers to permit testing of the turbine trip signal to the Reactor Protection System.
* The procedures will be performed on only one channel of the circuitry at a time and at less than 10% reactor power, thereby preventing a spurious reactor trip.
The installation and removal of the electrical jumpers will be independently verified. Therefore, an unreviewed safety question does not exist.
1-PT-8.2        Instrumentation Periodic Test Procedure                                   03-18-94 (Safety Evaluation No. 93-075, Revision 1)
Periodic Test procedure 1-PT-8.2, "Reactor Protection Logic," was temporarily changed to provide instructions for testing the Station service bus undervoltage automatic start signal for the Turbine-Driven Auxiliary Feedwater Pump (TDAFWP) and the steam generator low-low level TDAFWP trip signal. The procedure included administrative control steps for the steam generator (SG) blowdown permissive key switches to ensure proper operation of the SG blowdown trip valves during the performance of the procedure.
During the performance of this test, the SG blowdown permissive key switches were placed under administrative control when in the permissive mode. The procedural steps directed an operator to place the key switches in the normal position in the event of an Auxiliary Feedwater System automatic start signal. This action ensured the operability of the SG blowdown trip valves. Therefore, an unreviewed safety question did not exist.
 
                                                  &urry Monthly Operating Report No. 94-03 Page 22 of 25 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 None During the Reporting Period
 
                                                                          -Surry Monthly Operating Report No. 94-03 Page 23 of 25 CHEMISTRY REPORT MONTH/YEAR: March, 1994 Unit No. 1                   Unit No. 2 Primary Coolant Analysis          Max.         Min.     Ava. Max.      Min.        Ava.
Gross Radioactivity, &#xb5;Ci/ml            2.81 E-1     2.03E-4   3.01 E-2 2.19E-1  1.15E-1      1.56E-1 Susoended Solids, oom                  0.150        < 0.01      0.050   < 0.1   < o.*1       < 0.1 Gross Tritium, &#xb5;Ci/ml                  9.73E-3      5.40E-3    7.57E-3  6.95E-1   6.49E-1     6.72E-1 1131, &#xb5;Ci/ml                          2.53E-4    ~ 3.61E-5  1.04E-4  2.71 E-4 4.62E-5     7.90E-5 113111133                                  -            -          -    0.09     0.05         0.07 Hydroaen, cc/ka                          36.8          4.9        22.0    43.0     35.0         38.4 Lithium, oom                            3.48        < 0.1      2.34    2.31     2.06         2.19 Boron - 1 o, oom*                      481.0      . 229.3      400.3  174.6     159.3       167.5 Oxvaen, (DO), oom                        6.0        0.005       2.48  0.005     0.005       0.005 Chloride, oom                          0.050         0.001      0.005  0.050    0.002       0.008 pH at 25 degree Celsius                  6.29          4.42      4.91    6.57     6.19         6.44 Boron - 1O = Total Boron x 0.196 Comments:
None
 
                                                                            &urry Monthly Operating Report No. 94-03 Page 24of 25 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: March, 1994 New or Spent                    Number of                                                 New or Spent Fuel Shipment Date Stored or  Assemblies       Assembly          ANSI            Initial Fuel Shipping Number      Received      per Shipment       Number           Number       Enrichment Cask Activity No Fuel Received or Stored During the Reporting Period.
 
e                                       &urry Monthly Operating Report No. 94-03 Page 25 of 25 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETIED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: March, 1994 None During the Reporting Period.}}

Latest revision as of 03:58, 23 February 2020

Monthly Operating Repts for Mar 1994 for Surry Power Station Units 1 & 2.W/940412 Ltr
ML18152A340
Person / Time
Site: Surry  Dominion icon.png
Issue date: 03/31/1994
From: Bowling M, Mason D, Olsen C
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
94-215, NUDOCS 9404180309
Download: ML18152A340 (26)


Text

e e VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 April 12, 1994 U. S. Nuclear Regulatory Commission Serial No.94-215 Attention: Document Control Desk NO/RPC:vlh Washington, D. C. 20555 Docket No$ .. , .50'."280 50-281 License Nos. DPR-32 DPR-37 Gentlemen:

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNITS 1 AND 2 MONTHLY OPERATING REPORT Enclosed is the Monthly Operating Report for Surry Power Station Units 1 and 2 for the month of March 1994.

Very truly yours,

/~i~

M. L. Bowling, ;7anager Nuclear Licensing & Programs Enclosure cc:

  • U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, N. W.

Suite 2900 Atlanta, Georgia 30323 Mr. M. W. Branch NRG Senior Resident Inspector Surry Power Station 940418036~ ~4b33i- -~~\

PDR ADOCK 05000280 R


---- --~- --

. PDR I

VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION MONTHLY OPERATING REPORT REPORT NO. 94m03 Approved:

eurry Monthly Operating Report No. 94-03 Page 2of 25 TABLE OF CONTENTS Section Page Operating Data Report - Unit No. 1 .........................................................................................................3 Operating Data Report - Unit No. 2 .........................................................................................................4 Unit Shutdowns and Power Reductions - Unit No. 1.................................................................................... 5 Unit Shutdowns and Power Reductions - Unit No. 2 .................................................................................... 6 Average Daily Unit Power Level - Unit No. 1.............................................................................................. 7 Average Daily Unit Power Level - Unit No. 2 .............................................................................................. 8 Summary of Operating Experience - Unit No. 1 ......................................................................................... 9 Summary of Operating Experience - Unit No. 2 ....................................................................................... 10 Facility Changes That Did Not Require NRC Approval ............................................................................... 11 Procedure or Method of Operation Changes That Did Not Require NRC Approval ........................................... 20 Tests and Experiments That Did Not Require NRC Approval ...................................................................... 22 Chemistry Report ............................................................................................................................. 23 Fuel Handling - Unit No. 1 ................................................................................................................... 24 Fuel Handling - Unit No. 2 ................................................................................................................... 24 Description of Periodic Test(s) Which Were Not Completed Within the Time Limits Specified in Technical Specifications ................................................................................................... 25

41,urry Monthly Operating Report

.. No. 94-03 Page 3of 25 OPERATING DATA REPORT Docket No.: 50-280 Date: 04-06-94 Completed By: D. Mason Telephone: (804) 365-2459

1. Unit Name: .................................................. . Surry Unit 1
2. Reporting Period: ........................................ .. March, 1994
3. Licensed Thermal Power (MWt): ...................... . 2441
4. Nameplate Rating (Gross MWe): ...................... . 847.5
5. Design Electrical Rating (Net MWe): ................ .. 788
6. Maximum Dependable Capacity (Gross MWe): .. .. 820
7. Maximum Dependable Capacity (Net MWe): ...... .. 781
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period .......................... 744.0 2160.0 186480.0
12. Number of Hours Reactor Was Critical .......... 171.6 680.8 124488.0
13. Reactor Reserve Shutdown Hours ............... 0 0 3774.5
14. Hours Generator On-Line ........................... 141.8 647.9 122326.9
15. Unit Reserve Shutdown Hours..................... 0 0 3736.2
16. Gross Thermal Energy Generated (MWH) ...... 256304.9 1001728.0 284169473.1
17. Gross Electrical Energy Generated (MWH) .... 84040.0 ~35055.0 92874603.0
18. Net Electrical Energy Generated (MWH) ........ 80306.0 317769.0 88144870.0
19. Unit Service Factor ................................... 19.1% 30.0% 65.6%
20. Unit Availability Factor............................... 19.1% 30.0% 67.6%
21. Unit Capacity Factor (Using MDC Net) ........... 13.8% 18.8% 60.9%
22. Unit Capacity Factor (Using DER Net) ........... 13.7% 18.7% 60.0%
23. Unit Forced Outage Rate ............................ 0% 0% 17.4%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

None

25. If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

- aurry Monthly Operating Report

- No. 94-03 Page 4of 25 OPERATING DATA REPORT Docket No.: 50-281 Date: 04-06-94 Completed By: D. Mason Telephone: (804) 365-2459

1. Unit Name: .................................................. . Surry Unit 2
2. Reporting Period: ......................................... . March, 1994
3. Licensed Thermal Power (MWt): ...................... . 2441
4. Nameplate Rating (Gross MWe): ...................... . 847.5
5. Design Electrical Rating (Net MWe): ................. . 788
6. Maximum Dependable Capacity (Gross MWe): ... . 820
7. Maximum Dependable Capacity (Net MWe): ....... . 781
8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
9. Power Level To Which Restricted, If Any (Net MWe):
10. Reasons For Restrictions, If Any:

This Month YTD Cumulative

11. Hours In Reporting Period .......................... 744.0 2160.0 183360.0
12. Number of Hours Reactor Was Critical .......... 744.0 2160.0 122236.3
13. Reactor Reserve Shutdown Hours ............... 0 0 328.1
14. Hours Generator On-Line ........................... 744.0 2160.0 120375.6
15. Unit Reserve Shutdown Hours ..................... 0 0 0
16. Gross Thermal Energy Generated (MWH) ...... 1754374.1 5183840.1 280859582.5
17. Gross Electrical Energy Generated (MWH) .... 585635.0 1736585.0 91682209.0
18. Net Electrical Energy Generated (MWH) ........ 565310.0 1675337.0 87007407.0
19. Unit Service Factor ................................... 100.0% 100.0% 65.6%
20. Unit Availability Factor............................... 100.0% 100.0% 65.6%
21. Unit Capacity Factor (Using MDC Net) ........... 97.3% 99.3% 60.9%
22. Unit Capacity Factor (Using DER Net) ........... 96.4% 98.4% 60.2%
23. Unit Forced Outage Rate ............................ 0.0% 0.0% 13.9%
24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):

Maintenance, June 4, 1994, 22 Days

25. If Shut Down at End of Report Period, Estimated Date of Start-up:
26. Unit In Test Status (Prior to Commercial Operation):

FORECAST ACHIEVED INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION

-urry Monthly Operating Report No. 94-03 Page 5 of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%)

REPORT MONTH: March, 1994 Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 04-06-94 Completed by: Craig Olsen

  • Telephone: (804) 365-2155 (1) (2) (3) (4) (5)

Method Duration of LER System Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence Down Rx None During the Reporting Period (1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram.

C Refueling 3 - Automatic Scram.

D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source.

for Licensee Event Report (LER) File (NUREG 0161)

aurry Monthly Operating Report No. 94-03 Page 6of 25 UNIT SHUTDOWN AND POWER REDUCTION (EQUAL To OR GREATER THAN 20%}

REPORT MONTH: March, 1994 Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 04-06-94 Completed-by:* Craig Olsen Telephone: (804) 365-2155 (1) (2) (3) (4) (5)

Method Duration of LER System Component Cause & Corrective Action to Date Type Hours Reason Shutting No. Code Code Prevent Recurrence Down Rx 940315 s 12.8 B NIA NIA TA TRB Reduced power to 75% to perform governor valve freedom of movement test.

(1) (2) (3)

F: Forced REASON: METHOD:

S: Scheduled A - Equipment Failure (Explain) 1 - Manual B Maintenance or Test 2 - Manual Scram.

C Refueling 3 - Automatic Scram.

D Regulatory Restriction 4 - Other (Explain)

E Operator Training & Licensing Examination F Administrative G Operational Error (Explain)

(4) (5)

Exhibit G - Instructions for Preparation of Data Entry Sheets Exhibit 1 - Same Source.

for Licensee Event Report (LER) File (NUREG 0161)

&urry Monthly Operating Report No. 94-03 Page 7of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-280 Unit Name: Surry Unit 1 Date: 04-06-94 Completed by: Pat Kessler Telephone: 365-2790 MONTH: March, 1994 Average Daily Power Level Average Daily Power Level Day (MWe-Net) Day (MWe- Net) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 168 11 0 27 370 12 0 28 554 13 0 29 671 14 0 30 791 15 0 31 792 16 0 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

tltsurry Monthly Operating Report No. 94-03 Page 8 of 25 AVERAGE DAILY UNIT POWER LEVEL Docket No.: 50-281 Unit Name: Surry Unit 2 Date: 04-06-94 Completed by: Pat Kessler Telephone*: 365-2790.

MONTH: March, 1994 Average Daily Power Level Average Daily Power level Day (MWe- Net) Day (MWe-Net) 1 771 17 758 2 774 18 758 3 773 19 758 4 773 20 749 5 772 21 749 6 772 22 752 7 772 23 752 8 771 24 751 9 771 25 752 10 770 26 751 11 764 27 758 12 763 28 757 13 764 29 755 14 760 30 753 15 718 31 756 16 762 INSTRUCTIONS On this format, list the average daily unit power level in MWe - Net for each day in the reporting month. Compute to the nearest whole megawatt.

esurry Monthly Operating Report No. 94-03 Page 9 of 25

SUMMARY

OF OPERATING EXPERIENCE MONTH/YEAR: March, 1994 The following chronological sequence by unit is a summary of operating experiences for this month which required load reductions or resulted in significant non-load related incidents.

UNIT ONE:

03/01/94 0000 The reporting period began with the Unit in the refueling shutdown mode.

03/24/94 2023 Reactor critical.

03/26/94 0215 Unit on-line, started power increase.

0255 Stopped power increase at 26%, 215 MWe, to perform flux mapping.

03/27/94 0258 Started power increase.

03/28/94 0000 Stopped power increase at 70% power, 578 MWe, to perform flux mapping.

03/29/94 0600 Started power increase.

1700 Stopped power increase at 96%, 800 MWe.

03/30/94 0339 Started power increase.

0425 Stopped power increase at 98%, 816 MWe.

1350 Started power increase.

1418 Stopped power increase at 100%, 830 MWe.

2054 Started power reduction for core output evaluation.

2130 Stopped power reduction at 98% power, 820 MWe.

03/31/94 2400 The reporting period ended with the Unit at 98% power, 820 MWe, pending Engineering evaluation of reactor core power level.

esurry Monthly Operating Report No. 94-03 Page 10 of 25

SUMMARY

OF OPERATING EXPERIENCE MONTH/YEAR: March, 1994 UN!TTwo:

03/01/94 0000 The reporting period began with the Unit at 98% power, 810 MWe due to Steam Generator "C" level oscillations.

03/10/94 2012 Started power reduction to stabilize Steam Generator "C" level oscillations 2030 Stopped power reduction at 97%, 800 MWe.

03/15/94 091 O Started power reduction to perform governor valve freedom of movement test, 2-0SP-TM-001.

1340 Stopped power reduction at 75%, 620 MWe.

1415 Started power increase after completion of governor valve freedom of movement test.

2200 Stopped power increase at 97%, 800 MWe.

03/19/94 2255 Started power reduction to stabilize Steam Generator "C" level oscillations.

2300 Stopped power reduction at 96%, 785 MWe 03/31/94 2400 The reporting period ended with the Unit operating at 96% power, 785 MWe, due to Steam Generator "C" level oscillations.

-Surry Monthly Operating Report No. 94-03 Page 11 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 EWR 90-228 Engineering Work Request 02-28-94 (Safety Evaluation No.91-009)

Engineering Work Request 90-228 replaced the Residual Heat Removal system mechanical pump seals with an updated balanced seal.

This change extends the life of the seal and minimizes seal leakage. Installation of the new balanced seal did not affect the original system design or function.

Therefore, an unreviewed safety question did not exist.

DCP 91-05-1 Design Change Package 03-02-94 (Safety Evaluation No.91-268)

Design Change Package 91-05-1 removed the resistance temperature device (RTD) bypass piping system and replaced it with thermowell mounted RTDs directly in the RCS hot and cold leg pipes.

The modification did not degrade the performance or increase the challenges to equipment assumed to function during an accident condition. Therefore, an unreviewed safety question did not exist.

TM S1-94-12 Temporary Modification 03-03-94 (Safety Evaluation No.94-053)

Temporary Modification (TM) S1-94-12 de-energized Gaseous Drains System solenoid operated valve, 1-DG-SOV-100, and installed a mechanical jumper that bypassed 1-DG-SOV-100, thereby maintaining primary drain transfer tank pressure control valve, 1-DG-PCV-100, in the open position. This modification was implemented to prevent spurious alarms that result from electrical noise that is generated when 1-DG-SOV-100 is energized to open 1-DG-PCV-100.

The Unit was at cold or refueling shutdown while the TM was in place. During these plant conditions, the operation of the Primary Drains System was not affected. The mechanical jumper was tested following installation and the operation of 1-DG-PCV-100 was verified following its removal. Therefore, an unreviewed safety question did not exist.

EWR 89-132 Engineering Work Request 03-03-94 Engineering Work Request 89-132 installed and secured cable tray covers which restores the Cable Tray System to Regulatory Guide 1.75 and IEEE STD 384-1974 commitments of the 10 CFR 50 Appendix R Report.

This resolved Appendix R and seismic integrity nonconformances that existed for Station cable trays. Therefore, an unreviewed safety question did not exist.

-Surry Monthly Operating Report No. 94-03 Page 12 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 SE 94-054 Safety Evaluation 03-04-94 Safety Evaluation 94-054 was performed to assess the removal of the baskets on the traveling water screens at the high and low level intake structures during an extreme cold weather period to prevent ice from forming and reducing the flow through the screens. * * * *' '1 The evaluation concluded that, while the temporary removal of the non-safety-related baskets would allow more debris to pass by the screens, sufficient cooling water flow and heat exchanger heat transfer area would remain available for the heat exchangers to function as designed. Therefore, an unreviewed safety question did not exist.

SE 94-055 Safety Evaluation 03-04-94 Safety Evaluation 94-055 was performed to assess an increase in the intake canal level from 30 feet to 32 feet to provide for increased cooling water inventory during an extreme cold weather period in which ice formation at the low level intake structure could result in reduced circulating water pump availability.

The evaluation concluded that the temporary change in canal level would not impact the integrity of the intake canal structure or affect the margin of safety of Technical Specifications. Therefore, an unreviewed safety question did not exist.

DC P 92-043-1 Design Change Package 03-04-94 (Safety Evaluation No.93-176)

Design Change Package 92-043-1 replaced the pressurizer safety valves (PSVs) with safety valves that are designed to seal tighter under pressurizer steam conditions and discharge pipe loads. A loop seal drain line was installed to allow the loop seal to continuously drain condensation from the loop seal which allowed the removal of the loop seal ovens.

Implementation of these changes eliminated the concern of Reactor Coolant System (RCS) over pressurization due to the PSV loop seals. Virginia Power calculations SM-727 and SM-700 indicated that RCS pressure will remain below 2735 psig during limiting events. Therefore, an unreviewed safety question does not exist.

FS 94-08 UFSAR Change 03-07-94 (Safety Evaluation No.94-058)

Updated Final Safety Analysis Report Change 94-058 revised Sections 11.2.3.1.6, "RF Liquid Waste Evaporator System," and 11.2.4.1.4, "Evaporator Concentrate Operations," to reflect a change in the boron concentration in the Liquid Waste Evaporator System, which is located at the Surry Radwaste Facility.

The boron concentration was increased to reduce the volume of radioactive waste. This change did not impact safety-related systems or affect the margin of safety of Technical Specifications. Therefore, an unreviewed safety question did not exist.

&urry Monthly Operating Report No. 94-03 Page 13 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-13 Temporary Modification 03-07-94 (Safety Evaluation No.94-059)

Temporary Modification S1-94-13 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards

  • ** (CLS) System circuits* and* prevent a spurious' Hi-CLS signal during the replacement of relay 1-CLS-RLY-1 BM.

The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.

Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-14 Temporary Modification 03-07-94 (Safety Evaluation No.94-060)

Temporary Modification S1-94-14 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A1.

The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.

Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

DCP 92-41-1 Design Change Package 03-08-94 (Safety Evaluation No. 92-97)

Design Change Package 92-41-1 replaced a leaking level transmitter's manifold with three single valves since no direct replacement manifold was available.

The change enhanced the system because a single failure of a valve will not require the replacement of a manifold. The operation and function of the system was not altered. Therefore, an unreviewed safety question did not exist.

EWR 93-002 Engineering Work Request 03-08-94 (Safety Evaluation No.93-035)

Engineering Work Request 93-002 completed steam generator wrapper modifications which involved permanent removal of all four wrapper plug assemblies, removal of a portion of the wrapper seal plates, and removal of the outer tube lane blocking devices.

This modification reduces radiation exposure to personnel by reducing the effort and time required for wrapper entry. The modifications improve sludge lancing efficiency and improve access for foreign object search and recovery. The modifications do not affect the safety limits, surveillance requirements, limiting conditions of operations or system tests as described in the Technical Specifications. Therefore, an unreviewed safety question did not exist.

&urry Monthly Operating Report No. 94-03 Page 14of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-15 Temporary Modifications 03-09-94 TM S1-94-16 (Safety Evaluation No.94-062)

Temporary Modifications (TM) S1-94-15 and S1-94-16 removed containment sump trip valve, 1-DA-TV-1 OOA, for maintenance and installed a spool piece and electrical jumpers to *maintain" an* operable flow path frorri *containment sump pumps 1-DA-P-4A and 1-DA-P-48.

The Unit was at cold shutdown while the TM was in place. The containment sump trip valve closure interlocks, which would shut off pumps 1-DA-P-4A and 1-DA-P-4B, were defeated to allow pump operation to continue as needed. The pump interlocks of the redundant valve 1-DA-TV-1008 remained operable. Therefore, an unreviewed safety question did not exist.

TM S1-94-17 Temporary Modification 03-10-94 (Safety Evaluation No.94-064)

Temporary Modification (TM) S1-94-17 installed electrical jumpers to bypass test switch 1-SI-CS-LC494-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.

The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-18 Temporary Modification 03-10-94 (Safety Evaluation No.94-066)

Temporary Modification (TM) S1-94-18 installed electrical jumpers to bypass test switch TS-LC-476-TB on the Unit 1 Safety Injection (SI) System Train "B" circuitry to allow the switch to be replaced without rendering the circuits inoperable.

The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-19 Temporary Modification 03-10-94 (Safety Evaluation No.94-063)

Temporary Modification S1-94-19 installed electrical jumpers to maintain power to certain Unit 1 Safety Injection (SI) System circuits and prevent a spurious SI signal during the replacement of relay 1-SI-RLY-FC-475-XA.

The activity was performed while Unit 1 was at cold shutdown when the SI System was not required. The operation of other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

-Surry Monthly Operating Report No. 94-03 Page 15 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-20 Temporary Modification 03-10-94 (Safety Evaluation No.94-065)

Temporary Modification (TM) S1 20 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection (RP) System Train "~" circuits during the replacement of rela:y TT-XB. * *

  • The activity was performed while Unit 1 was at cold shutdown and did not affect RP System Train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-21 Temporary Modification 03-13-94 (Safety Evaluation No.94-068)

Temporary Modification (TM) S1-94-21 installed an electrical jumper to provide the proper input to the Unit 1 reactor coolant pump (RCP) "A" trip logic to enable the pump to be started. This TM was necessary since the loop "A" isolation valve "open" stem position switch was not in the correct position.

The activity was performed while Unit 1 was at cold shutdown. The TM placed the RCP "A" trip logic in the normal state for power operation and did not affect the integrity or operation of the valve. Double verification of jumper installation/removal was performed. Therefore, an unreviewed safety question did not exist.

DCP 93-018-1 Design Change Package 03-13-94 (Safety Evaluation No.93-175)

Design Change Package 93-018-1 re-routed the miniflow recirculation line due to a leak in the buried portion of the line. The line previously discharged directly into the Emergency Condensate Storage Tank and now discharges into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Full-Flow Recirculation line.

Although the mini-flow recirculation line has been re-routed to discharge into the Emergency Condensate Storage Tank via the Auxiliary Feedwater Pumps Full-Flow Recirculation line, the operation/performance of the Auxiliary Feedwater Pumps was not altered. Therefore, an unreviewed safety question did not exist.

DCP 93-15-1 Design Change Package 03-14-93 (Safety Evaluation No.93-169)

Design Change Package 93-15-1 replaced 01-CS-MOV-102A and B valves and operators because of a less than satisfactory material condition due to high thrust seating loads.

This was an in-kind replacement and had no affect on the consequences of any evaluated accidents. Therefore, an unreviewed safety question did not exist..

e -Surry Monthly Operating Report No. 94-03 Page 16 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 DR S-94-0615 Deviation Report 03-14-94 (Safety Evaluation No.94-071)

Safety Evaluation 94-071 assessed the condition reported by Deviation Report S-94-0615 concerning the continued operation of Unit 1 with a small immobile foreign* object (wire approximately 1/8" to 5/32" diameter estimated to be less than 0.1 pounds) in the secondary side of Unit 1 steam generator (SG) "A".

Attempts to remove the object have been unsuccessful.

An evaluation of Unit 1 operation with the SG containing the foreign object was performed by Westinghouse Nuclear Safety. The evaluation concluded that the presence of the object will have no adverse effect on the pressure boundary integrity of the SG and does not create an unreviewed safety question provided future eddy current inspections support no tube degradation due to wear.

TM S1-94-22 Temporary Modification 03-14-94 (Safety Evaluation No.94-070)

Temporary Modification S1-94-22 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of relay 1-CLS-RLY-1A02.

The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.

Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-23 Temporary Modification 03-14-94 (Safety Evaluation No.94-069)

Temporary Modification S1-94-23 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "A" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of Leakage Monitoring System relay 1-LM-RLY-1 OOA 1.

The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. Therefore, an unreviewed safety question did not exist.

Temporary Modification S1-94-24 installed electrical jumpers and lifted electrical leads to maintain power to certain Unit 1 Consequence Limiting Safeguards (CLS) System circuits and prevent a spurious Hi-CLS signal during the replacement of CLS relay 1-CLS-RLY-1 B13.

The activity was performed while Unit 1 was at cold shutdown when the CLS System was not required. The operation of other systems was not affected.

Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

&urry Monthly Operating Report No. 94-03 Page 17of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-25 Temporary Modification 03-16-94 (Safety Evaluation No.94-073)

Temporary Modification (TM) S1-94-25 installed an electrical jumper to bypass the failed Unit 1 Consequence Limiting Safeguards (CLS) alarm ~ircuit relay 1808 and

  • The subject Hi CLS System Train "B" relay is a spare that performs no function.

The activity did not affect other systems or the Hi CLS System Train "A". The operability of the affected alarms were verified following the installation of the TM.

Therefore, an unreviewed safety question did not exist.

TM S1-94-26 Temporary Modification 03-16-94 (Safety Evaluation No.94-074)

Temporary Modification S1-94-26 removed the control fuses for Unit 1 Consequence Limiting Safeguards (CLS) System Train "B" circuits to prevent a spurious Hi-Hi CLS signal during the replacement of relay 1-CLS-RLY-2804.

The activity was performed while Unit 1 was at cold shutdown when the CLS system was not required. Therefore, an unreviewed safety question did not exist.

DR S-94-0097 Deviation Report 03-17-94 (Safety Evaluation No.94-076)

Safety Evaluation 94-076 assessed the condition reported by Deviation Report S-94-0097 concerning continued station operation with a through-wall leak of charging pump service water discharge piping located in the Auxiliary Building.

The assessment concluded that the leak does not affect the design function of the Charging Service Water System, other safety-related systems, or reduce the Technical Specifications margin of safety. Therefore, an unreviewed safety question did not exist.

TM S1-94-27 Temporary Modification 03-17-94 (Safety Evaluation No.94-075)

Temporary Modification S1-94-27 installed an electrical jumper to maintain power to. certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of relay 1-RP-RLY-AFP1-XA.

The activity was performed while Unit 1 was shut down with the reactor trip and bypass breakers open. The operation of RPS train "B" and other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

tltsurry Monthly OperatingNo.Report 94-03 Page 18 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 EWR 88-476 Engineering Work Request 03-19-94 Engineering Work Request 88-476 assessed the spiking of instrumentation in the Nuclear Instrumentation system (NIS) cabinets and removed line conditioning transformers that had failed. It was determined that the power coming from the

  • Uninterruptible Power Supply system was sufficiently*clean as a source of power to the NIS System.

Only one channel of NIS was altered at a time. Therefore, an unreviewed safety

. question did not exist.

TM S1-94-28 Temporary Modification 03-21-94 (Safety Evaluation No.94-079)

Temporary Modification (TM) S1-94-28 installed an electrical jumper to maintain power to certain Unit 1 Reactor Protection (RP) System Train "B" circuits during the replacement of relay AST1-XB.

The activity was performed while Unit 1 was below 350 °F/450 psig and did not affect RP System train "A". The TM did not impact the operation of the Residual Heat Removal or other systems. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

TM S1-94-29 Temporary Modification 03-22-94 (Safety Evaluation No.94-080)

Temporary Modification S1-94-29 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "A" circuits during the replacement of RPS relay SV3XA.

The activity was performed while Unit 1 was subcritical with all contrql rods inserted. The operation of RPS Train "B" and other systems was not affected.

Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

DC P 93-036-1 Design Change Package 03-22-94 (Safety Evaluation No.93-165)

Design Change Package 93-036-1 replaced carbon steel piping with chrome-moly piping to mitigate flow accelerated corrosion.

Piping was replaced in the Main Steam Trap Discharge Header, the Secondary Plant Drain system and the Condensate system. This material replacement did not result in any changes to the system form, fit, function, or operation.

Therefore, an unreviewed safety question did not exist.

&urry Monthly Operating Report No. 94-03 Page 19 of 25 FACILITY CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 TM S1-94-30 Temporary Modification 03-23-94 (Safety Evaluation No.94-081)

Temporary Modification S1-94-30 installed electrical jumpers to maintain power to certain Unit 1 Reactor Protection System (RPS) Train "B" circuits during the

  • replacement of RPS relay SRB-XB.

The activity was performed while Unit 1 was at hot shutdown with the reactor trip breakers open. The operation of RPS Train "A" and other systems was not affected. Double verification of jumper installation/removal and post-maintenance testing was performed. Therefore, an unreviewed safety question did not exist.

DCP 91-027-3 Design Change Package 03-24-94 (Safety Evaluation No.93-060)

Design Change Package 91-027-3 modified the closed loop seal cooling circuit for the Low Head Safety Injection (LHSI) and Outside Recirculating Spray (ORS)

Pumps. The modification included the replacement of the seal cooling coils with new seal coolers and the addition of isolation valves at the seal and cooler.

This change eliminated the venting and filling difficulties with the LHSI and ORS pump seal cooling circuits which caused seal head tank low level alarms. The design of the new seal coolers and its cooling circuit meet the trequirements of ASM E Section VIII for design basis accident conditions to a rating of 170 psig/250° F which is consistent with the LHSI and ORS pump seal cooling circuits.

Therefore, an unreviewed safety question does not exist.

SE 94-082 Safety Evaluation 03-28-94 Safety Evaluation 94-082 was performed to assess a re-analysis of the Large Break Loss of Coolant Accident (LBLOCA) that used Westinghouse's LOCA-ECCS Evaluation Model, denoted as the 1981 Model with BASH (computer code).

The evaluation concluded that the analysis parameters were equivalent to, or conservative with respect to, those allowed by the Technical Specifications, and that the LBLOCA meets the requirements of 10 CFR 50.46. Therefore, an unreviewed safety question does not exist.

&urry Monthly Operating Report No. 94-03 Page 20 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 1-0P-Sl-002 Operating Procedure 03-06-94 (Safety Evaluation No.94-057)

Operating Procedure 1-0P-Sl-002, "Safety Injection Accumulators", was temporarily changed to provide instructions for installing a temporary mechanical jumper to permit the Unit 1 refueling water storage tank recirculation pumps to be used to fill the Safety Injection (SI) System accumulators while the SI hydro pump is out of service.

The mechanical jumper was installed when the Unit was at cold/refueling shutdown and the SI System was not required. The jumper was rated for the pressure of the associated piping flow path, inspected for leakage after it was placed in service, and removed before the Unit left cold shutdown. Therefore, an unreviewed safety question did not exist.

O-MOP-SW-010 Maintenance Operating Procedures 03-07-94 O-MOP-SW-011 (Safety Evaluation No.94-061)

Maintenance Operating Procedures O-MOP-SW-010, "Removal From Service of the Unit 1 Service Water Supply Header and O-MOP-SW-011, "Return to Service of the Unit 1 Service Water Supply Header" were developed to provide instructions for removing the Service Water Supply Header from service (and returning it to service) to permit the replacement of degraded equipment.

Any blank flanges used during the performance of these procedures will meet the criteria for the piping class for which they are installed and a leak test will be performed to verify the adequacy of the installation. These procedures will be performed within the Limiting Conditions for Operation as defined by the Technical Specifications. Therefore, an unreviewed safety question does not exist.

O-EPM-0105-01 Electrical Preventive Maintenance Procedure 03-11-94 (Safety Evaluation No.94-067)

Electrical Preventive Maintenance Procedure O-EPM-0105-01 , "Appendix R ELT Eight Hour Duration Test" was developed to provide instructions for conducting performance discharge tests for emergency lighting, replacing lamp heads, and performing minor cleaning.

This procedure may be implemented while the units are at power and will be performed for only one fire area at a time. Battery powered lanterns are provided in the Appendix R cabinet for use by Operations personnel during the test and for the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> post test period in which the emergency lighting batteries are being recharged. This activity will not affect the probability of occurrence or the consequences of any previously analyzed accidents. Therefore, an unreviewed safety question does not exist.

-Surry Monthly Operating Report No. 94-03 Page 21 of 25 PROCEDURE OR METHOD OF OPERATION CHANGES THAT DID NOT REQUIRE NRC* APPROVAL MONTH/YEAR: March, 1994 1-IPT-RP-TM-001 Instrument Periodic Test Procedures 03-17-94 2-IPT-RP-TM-001 (Safety Evaluation No.94-077)

Instrument Periodic Test Procedures 1/2-IPT-RP-TM-001, "Turbine Trip Signal to Reactor Protection System Functional Test" were developed to provide instructions for installing electrical jumpers to permit testing of the turbine trip signal to the Reactor Protection System.

  • The procedures will be performed on only one channel of the circuitry at a time and at less than 10% reactor power, thereby preventing a spurious reactor trip.

The installation and removal of the electrical jumpers will be independently verified. Therefore, an unreviewed safety question does not exist.

1-PT-8.2 Instrumentation Periodic Test Procedure 03-18-94 (Safety Evaluation No.93-075, Revision 1)

Periodic Test procedure 1-PT-8.2, "Reactor Protection Logic," was temporarily changed to provide instructions for testing the Station service bus undervoltage automatic start signal for the Turbine-Driven Auxiliary Feedwater Pump (TDAFWP) and the steam generator low-low level TDAFWP trip signal. The procedure included administrative control steps for the steam generator (SG) blowdown permissive key switches to ensure proper operation of the SG blowdown trip valves during the performance of the procedure.

During the performance of this test, the SG blowdown permissive key switches were placed under administrative control when in the permissive mode. The procedural steps directed an operator to place the key switches in the normal position in the event of an Auxiliary Feedwater System automatic start signal. This action ensured the operability of the SG blowdown trip valves. Therefore, an unreviewed safety question did not exist.

&urry Monthly Operating Report No. 94-03 Page 22 of 25 TESTS AND EXPERIMENTS THAT DID NOT REQUIRE NRC APPROVAL MONTH/YEAR: March, 1994 None During the Reporting Period

-Surry Monthly Operating Report No. 94-03 Page 23 of 25 CHEMISTRY REPORT MONTH/YEAR: March, 1994 Unit No. 1 Unit No. 2 Primary Coolant Analysis Max. Min. Ava. Max. Min. Ava.

Gross Radioactivity, µCi/ml 2.81 E-1 2.03E-4 3.01 E-2 2.19E-1 1.15E-1 1.56E-1 Susoended Solids, oom 0.150 < 0.01 0.050 < 0.1 < o.*1 < 0.1 Gross Tritium, µCi/ml 9.73E-3 5.40E-3 7.57E-3 6.95E-1 6.49E-1 6.72E-1 1131, µCi/ml 2.53E-4 ~ 3.61E-5 1.04E-4 2.71 E-4 4.62E-5 7.90E-5 113111133 - - - 0.09 0.05 0.07 Hydroaen, cc/ka 36.8 4.9 22.0 43.0 35.0 38.4 Lithium, oom 3.48 < 0.1 2.34 2.31 2.06 2.19 Boron - 1 o, oom* 481.0 . 229.3 400.3 174.6 159.3 167.5 Oxvaen, (DO), oom 6.0 0.005 2.48 0.005 0.005 0.005 Chloride, oom 0.050 0.001 0.005 0.050 0.002 0.008 pH at 25 degree Celsius 6.29 4.42 4.91 6.57 6.19 6.44 Boron - 1O = Total Boron x 0.196 Comments:

None

&urry Monthly Operating Report No. 94-03 Page 24of 25 FUEL HANDLING UNITS 1 & 2 MONTH/YEAR: March, 1994 New or Spent Number of New or Spent Fuel Shipment Date Stored or Assemblies Assembly ANSI Initial Fuel Shipping Number Received per Shipment Number Number Enrichment Cask Activity No Fuel Received or Stored During the Reporting Period.

e &urry Monthly Operating Report No. 94-03 Page 25 of 25 DESCRIPTION OF PERIODIC TEST(S) WHICH WERE NOT COMPLETIED WITHIN THE TIME LIMITS SPECIFIED IN TECHNICAL SPECIFICATIONS MONTH/YEAR: March, 1994 None During the Reporting Period.