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| issue date = 10/16/1980
| issue date = 10/16/1980
| title = LER 80-065/03L-0:on 800917,w/unit at Refueling Shutdown, MOV-SW-103B Did Not Operate Electrically During Flush of Recirculation Spray Heat Exchangers.Cause Undetermined,But Marine Growth Suspected.Valve Manually Cycled
| title = LER 80-065/03L-0:on 800917,w/unit at Refueling Shutdown, MOV-SW-103B Did Not Operate Electrically During Flush of Recirculation Spray Heat Exchangers.Cause Undetermined,But Marine Growth Suspected.Valve Manually Cycled
| author name = WILSON J L
| author name = Wilson J
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| author affiliation = VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
| addressee name =  
| addressee name =  
Line 17: Line 17:


=Text=
=Text=
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--*--------**----~-----------------* . 'R~ FORM,36c 7-77) e LICENSEE EVENT REPORT _U.S. NUCLEAR,REGUL~TORY COMMISSION CONIROL BLOCK: I I G) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 l V I ~1~E~Jtc~o~
  'R~ FORM,36c 7-77) e             LICENSEE EVENT REPORT
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LhJG) I o I s Io Io I o I 2 I s I o IG)! o I 9 I 1 I 7 I s l o JG) I 1 I o I 1 I 6 I s I o 10 8 60 61 DOCKE, \/UMBER 68 69 EVENT CAiE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
  ~ lVI ~1~E~Jtc~o~                           I i 1JG\ 5OI OI - I O~~cJ~E ,L~s~RO I - IO I O                         2!0l: I\1dE~sE\ ~JEi ~l©ls1 c~T s! 0
IJ]J I With the unit at refueling.
:ON'T                                                                                         .
shutdown, MOV-SW-103B did not operate electrically during a TID \ flush of the Recirc Spray heat exchangers.
IE]               ~~;~~        LhJG) I oI s Io Io I o I 2 I s I o IG)! o I 9 I 1 I 7 I s l o JG) I 1 I o I 1 I 6 I s I o 10 8                     60           61           DOCKE, \/UMBER               68       69     EVENT CAiE             74       75         REPORT DATE             80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
This valve is one of 4 valves which can Im I admit cooling water to the heat exchangers.
IJ]J I With the unit at refueling. shutdown, MOV-SW-103B did not operate electrically during a TID \ flush                 of the Recirc Spray heat exchangers.                                     This valve is one of 4 valves which can Im I admit                   cooling water to the heat exchangers.                                     The* other 3 valves were operable, therefore!
The* other 3 valves were operable, therefore! I the health and safety of the general public were not affected.
  ~            I the   health and safety of the general public were not affected.                                                           This is contrary to
This is contrary to ]]]] \T.S.-3.14.A.6 and is reportable per T.S.-6.6.2.b(2). ' 8 SYSTEM .CODE I wjA 18 9 10 CAUSE CAUSE CODE Si.!6C0DE COMPONENT CDDE iu@ Lu@ lv!A!1Jv!ElxJ8  
)))) \T.S.-3.14.A.6 and is reportable per T.S.-6.6.2.b(2).
,, 12 1:l 18 SEQUENTIAL OCCURRENCE COMP. SU8C0DE lJLl@) 19 REF'ORT TYPE VALVE SUSCODE Lill@ 20 Q LE ?.IRO c-VENT YEAR REPORT NO. CODE v..v REPORT' I 8 I O I I I I O j 6 1 s I l / I I O I 3 I L!:_J NUMBER 21 22 23 :24 26 27 2E 29 30 :;1 PRIME C:OMP. SUPPLIER REVISION NO. LQ.J 3:2 COMPONENT MANUFACTURER 80
80 SYSTEM             CAUSE          CAUSE                                                        COMP.            VALVE
* ACT10N FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 TAKEN ACTION ON PLANT METJ-;00 HOURS SUBMITIED FORM SUS. ~@W@ w@ Lu lo lo I ol ol W@ WC§) 33 34 35 36 37 41 * ,42 W@ I Pl 31 41 ol CAUSE DESCRIPTION AND CORRECTIVE ACTlONS @) 43 CII9J !Because of operational restrictions MOV-SW-103B 1.s not exe.rcised except during refueling  
                                      .CODE             CODE       Si.!6C0DE                 COMPONENT CDDE                     SU8C0DE            SUSCODE
[TIIJ \shutdown.
~
The exact cause* for failure of MQV"""SW'*"l03B cannot be determined, however marine growth is su~pected.
'        8 I
Lill] 8 9 FACILITY STATUS % POWER OTHE:'< ST,O.TUS METHOD CF A ~7 so _2ill Ul.J@ i o I o I, o l@)!..._ __ N_A ___ ...... DISCOVERY DISCOVERY DESCRIPTION
9 wjA 10 18 ,,iu@ Lu@ lv!A!1Jv!ElxJ8 lJLl@) Lill@
'3,, ~~l~_I_n_s~p_e_c_t_i_o_n
12             1:l                             18             19                20 SEQUENTIAL                         OCCURRENCE             REF'ORT                         REVISION Q     LE ?.IRO c-VENT YEAR                                 REPORT NO.                             CODE                   TYPE                              NO.
______________
v..v REPORT' NUMBER I 8 I OI 21        22 I I 23 I Oj 6 1s I
....., 8 9 10 12 11 44 ACTIVITY CONTENT Q\ RELEASED OF RELEASE AMOUNT OF ,>.CTIVITY  
:24          26 l/ I 27 I OI 3 I 2E        29 L!:_J 30 LQ.J
\::V ~@) ~@._) ___ N_A..;...,*
:;1             3:2 ACT10N     FUTURE               EFFECT         SHUTDOWN                             ~    ATTACHMENT         NPRD-4           PRIME C:OMP.                COMPONENT TAKEN     ACTION             ON PLANT         METJ-;00                 HOURS ~            SUBMITIED       FORM SUS.           SUPPLIER              MANUFACTURER
____ __, S 9 ,o ,, 45 46 80 4S NA .LOCATION OF i'\ELEASE
              ~@W@
@ ao ?ERSONNEL EXPOSURES Q IO NtM~r O 1@i'Y~El@  
33          34 w@
... D_Es_c_R_IP-Tl_O_N_o_:::s
35 Lu 36 lo lo I ol ol 37                    ~
____ N_;A;.;;,_
W@
_________________________
41
_..; 8 9 11 ,2 :3 ?ERSONNELINJURIES 50 NUMSER DESCRIPTION~
* WC&sect;)
j O ! 0 \ 0 l@.___ ________ N_A __________________
                                                                                                                            ,42 W@ I 43 Pl 31 41 ol
_ 9 11 12 80 LOSS OF OR DAMAGE TO FACILITY "3\ TYPE DESCRIPTION V LU@.__ __________
                                                                                                                                                                                        ~7 CAUSE DESCRIPTION AND CORRECTIVE ACTlONS @)
N_A ________________
CII9J         !Because of operational restrictions MOV-SW-103B 1.s not exe.rcised except during refueling
___,.____.
[TIIJ \shutdown. The exact cause* for failure                                           of MQV"""SW'*"l03B         cannot be determined, however marine growth is su~pected.
9 10 60 PUBLICITY G\ ISSUEDQ 0 DESCRIPTION }TI] ~CJ,__ ____________
Lill]
N_A _____________ NRC USE ONLY I I I I I 1
8     9                                                                                                                                                                       so FACILITY                                                                     METHOD CF                                                                A STATUS             % POWER                     OTHE:'< ST,O.TUS           DISCOVERY                                DISCOVERY DESCRIPTION            '3,,
* I I I I I I '8 08 s 10 .-;,<<.., 10 2 0 QA-ef,/~ ?OE? .:.PE~ _J_._L_._W_i_ls_o_n
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_______ _ 68 69 30 ( 804) 357-3184 P~'.OM=: ,0 N ::, ; C 1-. * *
8   9               10               12     11                             44       45        46                                                                            80 ACTIVITY       CONTENT                                             Q\
* e ATTACHMENT 1 SURRY POWER STATION, UNIT 1 DOCKET NO: 50-280 REPORT NO: 80-065/031-0 EVENT DATE: 09-17-80 Title of Report: MOV-'SW-103B Valve Non-function
RELEASED OF RELEASE                       AMOUNT OF ,>.CTIVITY     \::V                                             .LOCATION OF i'\ELEASE          @
: 1. Event
~            ~@) ~@._)___N_A..;...,*_ _ _ ___,                                                               NA S   9               ,o           ,,                                                       4S                                                                                 ao
                  ?ERSONNEL EXPOSURES                           Q
~            IO   NtM~r     O 1@i'Y~El@ ...D_Es_c_R_IP-Tl_O_N_o_:::s
_ _ _ _N_;A;.;;,__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __..;
8   9               11       ,2         :3                                                                                                                                 50
                  ?ERSONNELINJURIES                   ~
NUMSER                 DESCRIPTION~
jO    !0     \ 0   l@.___________N_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __
9               11       12                                                                                                                                             80 LOSS OF OR DAMAGE TO FACILITY           "3\
TYPE         DESCRIPTION                 V LU@.___ _ _ _ _ _ _ _ _ _N_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____,.____.
9           10                                                                                                                                                           60 PUBLICITY               G\                                                                                                                 NRC USE ONLY ISSUEDQ DESCRIPTION            ~                                                                                                                                              ,0
}TI] ~CJ,______________N_A_ _ _ _ _ _ _ _ _ _ _ _ _~
0 II    I I I   1* I   I I I I I N
                                                                                                                                                                                            ~
'8 08 s                   10 .-;,<<..,                                                                                                         68    69                              30  ;
10 2 0 QA-ef,/~ ?OE? .:.PE~ _J_._L_._W_i_ls_o_n_ _ _ _ _ _ __                                                        P~'.OM=:
( 804)          357-3184                      C
 
1-.
ATTACHMENT 1 e
SURRY POWER STATION, UNIT 1 DOCKET NO:     50-280
* 1.
REPORT NO:
Title of Report:
80-065/031-0 EVENT DATE: 09-17-80 Event


== Description:==
== Description:==


With the during a 3.14.A.6 unit at refueling shutdown-, MOV-SW-103B did flush of the Recirc Spray heat exchangers.
MOV-'SW-103B Valve Non-function With the unit at refueling shutdown-, MOV-SW-103B did not operate electrically during a flush of the Recirc Spray heat exchangers. This is contrary to T.S.
and is reportable per T.S.-6.6.  
3.14.A.6 and is reportable per T.S.-6.6. 2. b(2).
: 2. b(2). not operate electrically This is contrary to T.S. 2. Probable Consequences:
: 2. Probable Consequences:
MOV-SW-103B admits service water to the header which supplies cooling~ water to the Recirc Spray heat exchangers.
MOV-SW-103B admits service water to the header which supplies cooling~ water to the Recirc Spray heat exchangers. This valve is one of four redundant valves that will supply
This valve is one of four redundant valves that will supply the Recirc Spray heat exchangers with service water. ( . The redundant MOV-:'s were shown to be functional, therefore the health and safety of the general public were not affected.  
(
: 3. Cause: 4. There were no electrical or mechanical deficiencies found with MOV-SW-103B when it was inspec-ted subsequent to the aforementioned event. This valve is only cycled during refueling shutdown due to operational restrictions associated with Recirc Spray heat exchangers a?d* therefore could have been stuck -be-cause--o-f-marine growth_. * , / ' Immediate Actions: The immediate actions were to cycle the valve manually (following this cycling the valve operated electrically) and submitt an MR to have the valve inspected.  
the Recirc Spray heat exchangers with service water.
: 5. Subsequent Corrective Action: The subsequent corrective action was to.dissemble and clean the valve. 6. Action to Prevent Recurrence:
The redundant MOV-:'s were shown to be functional, therefore the health and safety of the general public were not affected.
According to past records, there have not been a similar occurance involving MOV-SW-103A,B,C, or D, this appears to be an isolated case, therefore no future action is required . .7. Generic Implications:
: 3. Cause:
None}}
There were no electrical or mechanical deficiencies found with MOV-SW-103B when it was inspec-ted subsequent to the aforementioned event. This valve is only cycled during refueling shutdown due to operational restrictions associated with Recirc Spray heat exchangers a?d* therefore could have been
* 4.
stuck -be-cause--o-f- marine growth_.
* Immediate Actions:
                                                ~ , / '
The immediate actions were to cycle the valve manually (following this cycling the valve operated electrically) and submitt an MR to have the valve inspected.
: 5. Subsequent Corrective Action:
The subsequent corrective action was to.dissemble and clean the valve.
: 6. Action to Prevent Recurrence:
According to past records, there have not been a similar occurance involving MOV-SW-103A,B,C, or D, this appears to be an isolated case, therefore no future action is required .
    .7. Generic Implications:
None
*}}

Latest revision as of 12:45, 17 March 2020

LER 80-065/03L-0:on 800917,w/unit at Refueling Shutdown, MOV-SW-103B Did Not Operate Electrically During Flush of Recirculation Spray Heat Exchangers.Cause Undetermined,But Marine Growth Suspected.Valve Manually Cycled
ML18139A754
Person / Time
Site: Surry Dominion icon.png
Issue date: 10/16/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A602 List:
References
LER-80-065-03L-01, LER-80-65-3L-1, NUDOCS 8010200513
Download: ML18139A754 (2)


Text

. .


~. ------------- -------------------------*--------*-*---------- . **- **------*-*- --*--------**----~-----------------*

'R~ FORM,36c 7-77) e LICENSEE EVENT REPORT

_U.S. NUCLEAR,REGUL~TORY COMMISSION CONIROL BLOCK: I IG) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

~ lVI ~1~E~Jtc~o~ I i 1JG\ 5OI OI - I O~~cJ~E ,L~s~RO I - IO I O 2!0l: I\1dE~sE\ ~JEi ~l©ls1 c~T s! 0

ON'T .

IE] ~~;~~ LhJG) I oI s Io Io I o I 2 I s I o IG)! o I 9 I 1 I 7 I s l o JG) I 1 I o I 1 I 6 I s I o 10 8 60 61 DOCKE, \/UMBER 68 69 EVENT CAiE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@

IJ]J I With the unit at refueling. shutdown, MOV-SW-103B did not operate electrically during a TID \ flush of the Recirc Spray heat exchangers. This valve is one of 4 valves which can Im I admit cooling water to the heat exchangers. The* other 3 valves were operable, therefore!

~ I the health and safety of the general public were not affected. This is contrary to

)))) \T.S.-3.14.A.6 and is reportable per T.S.-6.6.2.b(2).

80 SYSTEM CAUSE CAUSE COMP. VALVE

.CODE CODE Si.!6C0DE COMPONENT CDDE SU8C0DE SUSCODE

~

' 8 I

9 wjA 10 18 ,,iu@ Lu@ lv!A!1Jv!ElxJ8 lJLl@) Lill@

12 1:l 18 19 20 SEQUENTIAL OCCURRENCE REF'ORT REVISION Q LE ?.IRO c-VENT YEAR REPORT NO. CODE TYPE NO.

v..v REPORT' NUMBER I 8 I OI 21 22 I I 23 I Oj 6 1s I

24 26 l/ I 27 I OI 3 I 2E 29 L!:_J 30 LQ.J
1 3
2 ACT10N FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPRD-4 PRIME C:OMP. COMPONENT TAKEN ACTION ON PLANT METJ-;00 HOURS ~ SUBMITIED FORM SUS. SUPPLIER MANUFACTURER

~@W@

33 34 w@

35 Lu 36 lo lo I ol ol 37 ~

W@

41

  • WC§)

,42 W@ I 43 Pl 31 41 ol

~7 CAUSE DESCRIPTION AND CORRECTIVE ACTlONS @)

CII9J !Because of operational restrictions MOV-SW-103B 1.s not exe.rcised except during refueling

[TIIJ \shutdown. The exact cause* for failure of MQV"""SW'*"l03B cannot be determined, however marine growth is su~pected.

Lill]

8 9 so FACILITY METHOD CF A STATUS  % POWER OTHE:'< ST,O.TUS DISCOVERY DISCOVERY DESCRIPTION '3,,

_2ill Ul.J@ i o I o I, o l@)!...___N_A_ _ _...... ~~l~_I_n_s~p_e_c_t_i_o_n_ _ _ _ _ _ _ _ _ _ _ _ _ _.....,

8 9 10 12 11 44 45 46 80 ACTIVITY CONTENT Q\

RELEASED OF RELEASE AMOUNT OF ,>.CTIVITY \::V .LOCATION OF i'\ELEASE @

~ ~@) ~@._)___N_A..;...,*_ _ _ ___, NA S 9 ,o ,, 4S ao

?ERSONNEL EXPOSURES Q

~ IO NtM~r O 1@i'Y~El@ ...D_Es_c_R_IP-Tl_O_N_o_:::s

_ _ _ _N_;A;.;;,__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __..;

8 9 11 ,2 :3 50

?ERSONNELINJURIES ~

NUMSER DESCRIPTION~

jO !0 \ 0 l@.___________N_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __

9 11 12 80 LOSS OF OR DAMAGE TO FACILITY "3\

TYPE DESCRIPTION V LU@.___ _ _ _ _ _ _ _ _ _N_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____,.____.

9 10 60 PUBLICITY G\ NRC USE ONLY ISSUEDQ DESCRIPTION ~ ,0

}TI] ~CJ,______________N_A_ _ _ _ _ _ _ _ _ _ _ _ _~

0 II I I I 1* I I I I I I N

~

'8 08 s 10 .-;,<<.., 68 69 30  ;

10 2 0 QA-ef,/~ ?OE? .:.PE~ _J_._L_._W_i_ls_o_n_ _ _ _ _ _ __ P~'.OM=:

( 804) 357-3184 C

1-.

ATTACHMENT 1 e

SURRY POWER STATION, UNIT 1 DOCKET NO: 50-280

  • 1.

REPORT NO:

Title of Report:

80-065/031-0 EVENT DATE: 09-17-80 Event

Description:

MOV-'SW-103B Valve Non-function With the unit at refueling shutdown-, MOV-SW-103B did not operate electrically during a flush of the Recirc Spray heat exchangers. This is contrary to T.S.

3.14.A.6 and is reportable per T.S.-6.6. 2. b(2).

2. Probable Consequences:

MOV-SW-103B admits service water to the header which supplies cooling~ water to the Recirc Spray heat exchangers. This valve is one of four redundant valves that will supply

(

the Recirc Spray heat exchangers with service water.

The redundant MOV-:'s were shown to be functional, therefore the health and safety of the general public were not affected.

3. Cause:

There were no electrical or mechanical deficiencies found with MOV-SW-103B when it was inspec-ted subsequent to the aforementioned event. This valve is only cycled during refueling shutdown due to operational restrictions associated with Recirc Spray heat exchangers a?d* therefore could have been

  • 4.

stuck -be-cause--o-f- marine growth_.

  • Immediate Actions:

~ , / '

The immediate actions were to cycle the valve manually (following this cycling the valve operated electrically) and submitt an MR to have the valve inspected.

5. Subsequent Corrective Action:

The subsequent corrective action was to.dissemble and clean the valve.

6. Action to Prevent Recurrence:

According to past records, there have not been a similar occurance involving MOV-SW-103A,B,C, or D, this appears to be an isolated case, therefore no future action is required .

.7. Generic Implications:

None