05000280/LER-1980-016-03, /03L-0:on 800916,w/unit Operating Steady State at 100% power,TV-SS-201B Would Not Remain Closed When Control Switch Was Released.Cause Undetermined.Inside Trip Valve Closed & Air Secured to TV-SS-201B

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/03L-0:on 800916,w/unit Operating Steady State at 100% power,TV-SS-201B Would Not Remain Closed When Control Switch Was Released.Cause Undetermined.Inside Trip Valve Closed & Air Secured to TV-SS-201B
ML18139A603
Person / Time
Site: Surry  
Issue date: 10/16/1980
From: Joshua Wilson
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML18139A602 List:
References
LER-80-016-03L-02, LER-80-16-3L-2, NUDOCS 8010200499
Download: ML18139A603 (2)


LER-1980-016, /03L-0:on 800916,w/unit Operating Steady State at 100% power,TV-SS-201B Would Not Remain Closed When Control Switch Was Released.Cause Undetermined.Inside Trip Valve Closed & Air Secured to TV-SS-201B
Event date:
Report date:
2801980016R03 - NRC Website

text

Re' FORM 366 7:771,

e LICENSEE EVENT REPORT

_U.S. N~CLEAR R_EGULATORY COMMISSlON (Pl.EASE PRINT OR TYPE ALL REQUIRED INFORMATION)

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I With the Unit operating steady state at 100% power, it was found that TV-SS-201B would

=uIJ 1not stay closed.when closed from control room. This 1.s contrary to T.S.3.8.A.l and is

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1reportable as per T.S.6.6.2.b.(2).

The inside trip valve, TV-SS-201A, was operable and

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!would have closed if needed for containment isolation, therefore the health and safety

]:JI] 1of the general public were not affected.

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ATTACHMENT 1 e

e SURRY POWER STATION, UNIT 2 DOCKET NO:

50-281 REPORT NO:

80-016/031-0 EVENT DATE:

09-16-80 TITLE OF REPORT:

TRIP VALVE TV-SS-201B MALFUNCTION

1.

Description of Event

With the unit operating steady state at 100% power,.it was found that TV-SS-201B would not remain closed when the control switch was released.

This is contrary to T.S.-3.8:A.l and is reportable per T.S.-6.6.2.B(2).

2.

Probable Consequences:

If isolation of this line had been required, the inside trip valve (TV-SS-201A) would have closed.

Containment int~grit'y would therefore have been maintained and the health and safety of the general public were not affected.

3.

Cause

4.
5.

The inspection of the Trip Valves limit switches and associated components did not reveal any problems.

The valve was successfully cycled and the malfunction could not be repeated.

Therefore the exact cause cannot be determined.

Immediate Corrective Action

The immediate corrective action was to close the inside trip valve and secure air to TV-SS-201B.

Subsequent Corrective Action:

  • The elcetricians inspected TB-SS-201B, cycled it satisfactory, and returned the valve to service.
6.

Action Taken to Prevent Recurrence:

None

7.

Generic Implications:

None