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| number = ML16141A117
| number = ML16141A117
| issue date = 05/10/2016
| issue date = 05/10/2016
| title = Surry Power Station, Unit 2, Inspection Report for the Fall 2015 Refueling Outage
| title = Inspection Report for the Fall 2015 Refueling Outage
| author name = Lawrence D C
| author name = Lawrence D
| author affiliation = Virginia Electric & Power Co (VEPCO)
| author affiliation = Virginia Electric & Power Co (VEPCO)
| addressee name =  
| addressee name =  
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission Attention:
{{#Wiki_filter:VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission                   Serial No. 16-196 Attention: Document Control Desk                             SPS-LIC/CGL    RO Washington, DC 20555-0001                                     Docket No. 50-281
Document Control Desk Washington, DC 20555-0001 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE Serial No. SPS-LIC/CGL Docket No.
* License No. DPR-37 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE Technical Specification 6.6.A.3 for Surry Power Station Units 1 and 2 requires the submittal of a Steam Generator Tube Inspection Report to the NRC within 180 days after Tavg exceeds 200°F following completion of an inspection performed in accordance with Technical Specification 6.4.Q, Steam Generator Program. Attached is the Surry Unit 2 report for the Fall 2015 refueling outage.
* License No. 16-196 RO 50-281 DPR-37 Technical Specification 6.6.A.3 for Surry Power Station Units 1 and 2 requires the submittal of a Steam Generator Tube Inspection Report to the NRC within 180 days after T avg exceeds 200°F following completion of an inspection performed in accordance with Technical Specification 6.4.Q, Steam Generator Program. Attached is the Surry Unit 2 report for the Fall 2015 refueling outage. If you have any questions concerning this information, please contact Mrs. Candee G. Lovett at (757) 365-2178.
If you have any questions concerning                   this information, please   contact Mrs. Candee G. Lovett at (757) 365-2178.
Douglas Lawrence Director S ation Safety & Licensing Surry Power Station  
Douglas     Lawrence Director S ation Safety & Licensing Surry Power Station


==Attachment:==
==Attachment:==
Surry Unit 2 Steam Generator Tube                  Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None


Surry Unit 2 Steam Generator Tube Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager-Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager -North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 ATTACHMENT 1 SURRY UNIT 2 Serial No.: 16-196 Docket No.: 50-281 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)
Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager- Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager - North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station
SURRY UNIT 2 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting
 
* requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C. This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM). Surry Unit 2 exceeded 200°F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.
Serial No.: 16-196 Docket No.: 50-281 ATTACHMENT 1 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)
In the discussion below bold italicized wording represents TS verbiage and the required . information is provided directly below each reporting requirement.
 
A list of acronyms is attac;;hed at the end of this report. " A report shall be submitted Within 180 days after Tavg exceeds following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program.
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting
11 The report shall include: a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is in Table 1.
* requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C.
* The only scope expansions required in SG A and SG C were those ne.ce§sary.
This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM).
to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications.
Surry Unit 2 exceeded 200°F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.
The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.
In the discussion below bold italicized wording represents TS verbiage and the required
. information is provided directly below each reporting requirement. A list of acronyms is attac;;hed at the end of this report.                                                                     "
A report shall be submitted Within 180 days after Tavg exceeds -~JJ0 9F: following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program. 11 The report shall include:
: a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is RfOY,id~d in         ~
                                                                                                      ,}
Table 1.
* The only scope expansions required in SG A and SG C were those ne.ce§sary. to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications. The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.
No bobbin inspections or cold leg tubesheet inspections were performed.
No bobbin inspections or cold leg tubesheet inspections were performed.
The primary side work scope also included as-found and as-left visual examinations in the hot
The primary side work scope also included as-found and as-left visual examinations in the hot
* and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations. ,}
* and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations.
Secondary Side Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 During the Surry Unit 2 Fall 2015 RFO , a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed.
 
This included all accessible steam drum components and structures , including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insert i ons through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs. Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A , B , and C at the top of t he tubesheet , in the annulus, and in the no-tube lane as necessary. Table 1 -Eddy Current Testing Examination Scope Scope Description Extent SGA SG SGC B Bobbin Coil Exams Full Length TEHTEC 2849 2831 H/L CandyCane (Row 3-5) 07CTEH 278 282 H/L Straight (R 1-2) 07HTEH 185 182 H/L Straiqht Restricted 07HTEH 1 C/L CandyCane Restricted 02HTEC 1 C/L Straight Restricted 07CTEC 1 2 C/L Straight (R1-5) 07CTEC 462 463 Array Exams H/L TSH Array (Non-Baffle Plate) TSH01H 834 444 843 H/L TSH A r ray (Baff l e Plate) T SHBPH 2478 1260 2453 C/L TSC Array (Non-Baffle Plate) TSC01C 834 842 C/L TSC Arra y (Baffle Pla t e) TSCBPC 2478 2453 MRPC Exams Ubend +Poin tŽ (Row 1-2) 07H07C 185 182 MRPC S pe c i a l Interes t H/L Previo u s I ndications Various 120 172 H/L Previous Restricted 02H03 1 C/L Previous Restricted Various 8 H/L Current Indications Various 97 7 92 Ubend Current Indications Various 2 1 C/L Previous Indications Various 8 7 C/L Current Indications Various 36 20 Indications For Mag8ias Probe Various 1 2 Additional RPC TEHTSH 2 Total 10848 1713 10838
Serial No. : 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 Secondary Side During the Surry Unit 2 Fall 2015 RFO, a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed. This included all accessible steam drum components and structures, including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insertions through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs . Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A, B, and C at the top of the tubesheet, in the annulus, and in the no-tube lane as necessary.
: b. Degradation mechanisms found Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14 Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage. c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.
Table 1 - Eddy Current Testing Examination Scope SG Scope Description             Extent     SGA             SGC B
Table 2 -Inspection Method for Applicable Degradation Modes .. *Degradation  
Bobbin Coil Exams Full Length                             TEHTEC       2849           2831 H/L CandyCane (Row 3-5)                 07CTEH       278             282 H/L Straight (R 1-2)                   07HTEH       185             182 H/L Straiqht Restricted                 07HTEH                         1 C/L CandyCane Restricted               02HTEC                         1 C/L Straight Restricted                 07CTEC         1             2 C/L Straight (R1-5)                     07CTEC       462             463 Array Exams H/L TSH Array (Non-Baffle Plate)       TSH01H       834   444     843 H/L TSH Array (Baffle Plate)           TSHBPH      2478   1260   2453 C/L TSC Array (Non-Baffle Plate)       TSC01C       834             842 C/L TSC Array (Baffle Plate)           TSCBPC       2478           2453 MRPC Exams Ubend +Point' (Row 1-2)                 07H07C       185             182 MRPC Special Interest H/L Previous Indications                Various     120             172 H/L Previous Restricted                 02H03                         1 C/L Previous Restricted                 Various                       8 H/L Current Indications                 Various     97       7     92 Ubend Current Indications               Various       2               1 C/L Previous Indications                 Various       8               7 C/L Current Indications                 Various     36             20 Indications For Mag8ias Probe           Various       1               2 Additional RPC                         TEHTSH                 2 Total     10848   1713   10838
' Classification.'  
 
: Mechanism,
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14
* Loi;ation Probe Type. .. ""' . . . . .. : '"
: b. Degradation mechanisms found Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage.
''',,:.' "*-' ... Existing Tube Wear Anti-Vibration Bars Bobbin -Detection and Sizing Existing OD Pitting Top-of-Tubesheet Bobbin and +PointŽ-Detection
: c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.
+PointŽ -Sizing Existing Tube Wear Tube Support Plate Bobbin -Detection
Table 2 - Inspection Method for Applicable Degradation Modes
+PointŽ -Sizing Existing Tube Wear Freespan and TIS Bobbin and +PointŽ -Detection (foreign objects) +PointŽ -Sizing Potential ODSCC Hot Leg Top-of-Tubesheet  
      '                    *Degradation Classification.'       : Mechanism,   ..
+PointŽ -Detection and Sizing PWSCC Potential PWSCC Tube Ends NIA* Potential Tube Wear Flow Distribution Baffle Bobbin -Detection
* Loi;ation                     .Probe
+PointŽ -Sizing Bulges, Dents, Manufacturing Potential ODSCC Anomalies, and Above-+PointŽ -Detection and Sizing PWSCC Tubesheet Overexpansions (OVR) Potential ODSCC Tubesheet Crevice in +PointŽ -Detection and Sizing Tubes With NTEs Potential Tube Slippage Within Tubesheet Bobbin Detection Potential PWSCC Tubesheet
                                                                                        .      Type..
+PointŽ -Detection and Sizing Overexpansions (OXP) Potential ODSCC Row 1 and 2 Li-bends +PointŽ -Detection and Sizing PWSCC Potential ODS CC Freespan and Tube Supports Bobbin -Detection
                                                        '" ~',,      ''',,:.'                     "*-'
+PointŽ -Sizing *Inspection not required per technical specification alternate repair criteria.
Existing             Tube Wear           Anti-Vibration Bars         Bobbin - Detection and Sizing Bobbin and +Point'- Detection Existing             OD Pitting         Top-of-Tubesheet
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14 d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified.
                                                                                      +Point' - Sizing Bobbin - Detection Existing             Tube Wear           Tube Support Plate
Tables 3 through 6 provide information regarding these indications.
                                                                                      +Point' - Sizing Tube Wear                                       Bobbin and +Point' - Detection Existing                                Freespan and TIS (foreign objects)                                         +Point' - Sizing ODSCC Potential                             Hot Leg Top-of-Tubesheet       +Point' - Detection and Sizing PWSCC Potential               PWSCC                 Tube Ends                           NIA*
Table 3 -AVB Indications for SG A SGA 25 57 AV2 16 21 SGA 26 ' 9 AV4 12 10 I SGA 26 ' 86 AV3 17 21 SGA 29 28 AV3 NR 13 SGA 29 70 AV2 11 11 SGA 30 12 AV1 10 10 , ,,;:-... $GA 30 64 AV2 7 8 ----* SGA 33 26 AV4 NR 12 SGA 36 62 AV2 24* 21 I SGA 36 62 AV3 14 16 SGA 36 62 AV4 27 31 SGA 36 66 AV2 12 16 I SGA 36 66 ' AV3 " 10 13 i *' *:.::* . . -..... -SGA 37 20 AV1 13 12 .. --* -SGA 37 20 AV4 12 10 SGA 38 57. AV1 13 13 SGA 38 70 AV3 NR 11 SGA 38 72 AV4 23 26 SGA 38 74 AV4 17 22 SGA 40 25 AV4 12 8. SGA 40 49 AV1 11 15 SGA 40 49 AV2 10 10 SGA 40 49 AV3 11 11 SGA 40 65 AV2 18 21 SGA 40 65 AV3 10 15 SGA 40 65 AV4 10 9 SGA 40 66 AV3. 9 14 " -**--.....
Bobbin - Detection Potential             Tube Wear         Flow Distribution Baffle
-
                                                                                      +Point' - Sizing Bulges, Dents, Manufacturing ODSCC           Anomalies, and Above-Potential                                                            +Point' - Detection and Sizing PWSCC         Tubesheet Overexpansions (OVR)
-*-b
Tubesheet Crevice in Potential              ODSCC                                        +Point' - Detection and Sizing Tubes With NTEs Potential           Tube Slippage         Within Tubesheet                 Bobbin Detection Tubesheet Potential               PWSCC                                         +Point' - Detection and Sizing Overexpansions (OXP)
* tlli (°AT\IW ** '/i: *.eP.':* o* .... *:**** '* ETSS '96041':1  
ODSCC Potential                               Row 1 and 2 Li-bends         +Point' - Detection and Sizing PWSCC Bobbin - Detection Potential               ODS CC       Freespan and Tube Supports
',*
                                                                                      +Point' - Sizing
; : *;)2012: ..
        *Inspection not required per technical specification alternate repair criteria.
* 201,:s .. SGA 42 62 AV3 NR 10 SGA 44 35 AV1 NR 10 SGA 44 38 AV2 11 9 SGA 45 44 AV2 11 11 SGA 46 45 AV1 13 10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C :::):*:: .....
 
j-r**"' .,, : J, ' "
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14
*  
: d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified. Tables 3 through 6 provide information regarding these indications.
(% TW).*. * **  
Table 3 -AVB Indications for SG A SGA       25       57   AV2   16       21 26 '                                   I                                      "
; L -,.SG.-. " -_;. ' .: ETSs,' 96041'..:l Row Col '\  
SGA                  9   AV4   12       10 SGA       26       86 ' AV3   17       21 SGA       29       28   AV3   NR       13 SGA       29       70   AV2   11       11 SGA       30       12   AV1   10       10                       ~--
' ' ' _,._-No. ' ': : ; ' ' . 20tf5'; . **;<<.*' ._: ..... *;**. SGC 24' 8 AV4 9 10 SGC 25 9 AV1 8 8 SGC 25 9 AV3 11 10 SGC 25 27 AV1 18 17 SGC . 25 27 AV2 32 32 SGC 25 27 AV3 13 12 SGC 25 29 AV2 12 8 -SGC 25 29 AV3 26 20 SGC 26 26 AV3 17 19 SGC 26 26 AV4 17 17 -SGC 26 39 AV3 20 15 SGC 27 84 AV4 11 7 SGC 31 65 AV2 17 13 SGC 31 69 AV2 26 19 SGC 31 69 AV3 20 17 SGC 31 75 AV3 11 13 SGC 31 75 AV4 16 13 SGC 33 59 AV3 21 19 SGC 33 59 AV4 11 12 SGC 33 67 AV3 NR 10 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14 T
                                                                                              ,,;:- ... ~
---.... . ..;..... 
                      $GA       30       64   AV2     7       8                                               -~v SGA       33       26   AV4   NR       12 SGA       36       62   AV2   24*     21     I SGA       36       62   AV3   14       16 SGA       36       62   AV4   27       31 SGA       36       66   AV2   12       16     I                                       -~--
,, " " ' ,"*" -**
SGA       36       66 ' AV3 " 10         13     i                   *'
\: . .Row **-Col . *,*. __ ,. -.*>< ' ,,_*No.*** . ' . ' *, :: . ': ' ' ' ,,, ,; '! ;:.'*:> .;.. SGC 33 68 AV1 SGC 33 68 AV2 SGC 33 69 AV1 SGC. 33 69 AV2 SGC 33 70 AV1 SGC 33 70 AV3 SGC 34 29 AV3 SGC 34 29 AV4 SGC 34 79 AV1 SGC 35 77 AV2 SGC 35 77 AV3 SGC 37 63 AV2 SGC 37 73 AV3 SGC 37 75 AV3
SGA       37       20   AV1   13       12                       .. ~.                -~,:
* SGC. 38 28 AV1 SGC 38 28 AV3 SGC 38 30 AV2 SGC 38 43 AV3 SGC *38 73 AV1 SGC 38 73 AV2 SGC 38 74 AV2 SGC 39 50 AV3 SGC 39 ' 53 AV3 SGC 39 55 AV3 SGC 39 55 AV3 SGC ' 39 55 AV4 SGC 39 71 AV3 SGC 39 72 AV4 SGC 40 33 AV2 SGC 40 33 AV3 SGC 40 63 AV2 SGC 40 63 AV3 SGC 40 63 AV4 ' . c:>ep111:4,(%
SGA       37       20   AV4   12       10 SGA       38       57. AV1   13       13 SGA       38       70   AV3   NR       11 SGA       38       72   AV4   23       26 SGA       38       74   AV4   17       22 SGA       40       25   AV4   12       8.
ffl):. *.
SGA       40       49   AV1   11       15 SGA       40       49   AV2   10       10 SGA       40       49   AV3   11       11 SGA       40       65   AV2   18       21 SGA       40       65   AV3   10       15 SGA       40       65   AV4   10       9 SGA       40       66   AV3. 9       14
* ETSS. 9604 t .. * -: ; ,::2012 ,:, '20f5. 18 20 20 19 10 9 13 11 10 8 16 16 11 12 17 16 8 11 10 11 10 10 13 11 15 17 12 11 10 7 17 14 12 13 15 11 11 9 9 8* 8 8 14 13 30 28 27 25 18 12 26 25 12 8 5 10 23 24 23 25 9 9 19 15 19 16 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 -ii
 
--Y.;,.:-, ....... *:-11. , .. .[., .... :;. .. :;;,; ('. -r;-
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14
., .,.:.   
                                                                                        -*-b*.eP.':*
.* AVB Depth (% TW) . **s8 Row Col No. ' E:TSS 96041.1 * ' ' ' . 201'2 2015 SGC 41 35 AV3 NR 11 SGC 41 64 AV1 11 9 SGC 41 . 66 AV3 12 14 SGC 41 68 AV4 10 10 SGC 43 39 AV2 16 13 SGC 43 61 AV1 25 22 SGC 43 63 AV1 14 15 SGC 44 61 AV1 11 10 SGC 45 58 AV3 NR 13 SGC 46 45 AV2 8 11 SGC 46 45 AV3 NR 10 SGC 46 46 AV1 NR 10 SGC 46 46 AV2 NR 12 SGC 46 46 AV3 NR 13 SGC 46 46 AV4 NR 10 NR = Not Reported du!"ing the previous outage Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14
                                                                                        '/i:
'
* tlli (&deg;AT\IW o* .... *:******
':.bi l.'.\ ',c-113; ,, c;: 
                                                                                      '* ETSS '96041':1
' .* . . .. SG Row Col Location . . TSC+0.82 A 4 37 TSC+1.81 A 6 60 5H-0.59 A 11 45 TSH+0.96 A 15 16 TSH+0.23 A 17 16 TSH+0.04 A 18 16 TSH+0.02 A 32 27 TSC+0.02 A 33 27 TSC+0.12 A 39 24 TSH+0.45 A 42 52 TSC+0.26 A 43 61 BPH+0.56 A 43 64 BPH+0.62 Table 5 -Summary of Non-AVB Volumetric Degradation Identified
                      ,.-~
.* '" k . Signal Present prior to . . *
                                                                                    ;: *;)2012: ~: .
* Foreign ... ETSS Initially Cause Object {f,oTW) Repor;ted
* 201,:s .
*,, Current Outage? Remaining?
SGA                           42               62                 AV3               NR             10 SGA                           44               35                 AV1               NR             10 SGA                           44               38                 AV2               11               9 SGA                           45               44                 AV2                 11             11 SGA                           46               45                 AV1               13             10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C
I*, . ' .. *. ' ... 27901.1 20%TW 2015 Yes. No signal change Foreign No since 1995. Object 27901.1 27%TW 2015 Yes. No signal change Foreign No since 1995. Object 96910.1 13%TW 2009 Yes. No signal TSP Wear N/A change since 2002. 27901.1 27%TW 2012 Yes. No signal Foreign No change since 2006. Object 27901.1 25%TW 2012 No signal present Foreign No in 2006 exam. Object 27901.1 31 %TW 2002 Yes. No signal Foreign No change. Object 27901.1 30%TW 2002 Yes. No signal Foreign No change. Object 27901.1 20%TW 2006 Yes. No signal Foreign No change. Object 27901.1 25%TW 2006 Yes. No signal Foreign No change. Object 27901.1 20%TW 2009 Yes. No signal Foreign No change since 2006. Object 27901.1 20%TW 2009 Yes. No signal change Foreign No since 2009. Object 27901.1 23%TW 2009 Yes. No signal Foreign No change since 2002. Object .. Yes. Possible minor Foreign 27901.1 '24%TW 2009 sigriai'\;iiange 2002 to No 2009. No change since. Object Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Plugged? ' No No No No No No No No No No No No 1.1 ' '*Max Depth SG Row Col Location ETSS Initially***
:::):*::..... {~ii j-r**"' .,,
(%TW) ,
- ,.SG.- .
3C+0.47 96910.1 4%TW 2011 c 3 72 3C+0.48 96910.1 2%TW 2011 c 28 22 TSH+0.17 27901.1 29%TW 2014 TSH+0.52 27901.1 29%TW 2014 c 28 23 TSH+0.21 27901.1 29%TW 2014 c 28 71 TSH+0.27 27901.1 24%TW 2009 c 28 84 03H+0.50 96910.1 5%TW 2014 c 30 48 BPH+0.58 27901.1 20%TW 2015 c 30 74 TSH+6.47 27901.1 20%TW 2014 c 32 36 BPH+0.58 27901.1 19%TW 2009 c 33 17 TSH+2.69 27901.1 20%TW 2005 c 34 18 TSH+0.97 27901.1 22%TW 2005 c 34 20 TSH+0.91 27901.1 25%TW 2005 c 34 74 TSH+0.06 27901.1 27%TW 2005 ' .. c 35 19 TSH+0.32 27901.1 29%TW 2005 '. 'Signal*
: ~'"~~"'"' ~ J,
Prior to ,, , '; ci:rrent Outage?. Yes, in 1996 bobbin data. No RPC. Yes. No change since initial detection.
                                                '-'!;'~:,"':: ;
Yes. No change since initial detection.
L
Yes. No change since initial detection.
                                                                        ~xva~
Yes. No signal change since 1996. Yes, based on lookup. Unchanged since 1996. Yes. Present in 2014 X-Probe data with no change. Yes, based on lookup. Unchanged since 1996. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. No signal change. * ..
* r'*.~~bepM; (% TW).*. ***
No signal change. Cause TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Object ,,. .  
                                                                                      .: ETSs,' 96041'..:l
.. N/A No No No No N/A No No No No No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 " Plugged? No No No No No No No No No No No No No No   
'\**;<<.*' "-,~:.*,
.SG Row Col " 'ErSS l.,ocation, ' .. c 35 22 TSH+1.03 27901.1 c 35 30 TSH+0.11 27901.1 c 36 32 BPH+0.55 27901.1 c 36 68 TSH+0.17 27902.1 c 37 31 TSH+0.09 27901.1 c 37 32 TSH+0.02 27901.1 c 37 33 TSH+0.04 27901.1 c 37 34 TSH-0.06 27901.1 c 37 35 BPH+0.60 27901.1 c 37 54 TSH+0.12 27901.1 7C-0.48 96910.1 c 37 73 7C-0.52 96910.1 c 38 32 BPH+0.60 27901.1 c 38 53 TSH+0.08 27901.1 BPH+0.61 27901.1 ,* .. c 39 32 BPH+0.60 27901.1 '. *,Max Depth I* Initially' Signal Present P.rior.,to
              ~ "'~ '~1 '~ '
(%TW) k Reportecl
Row
* 'Current Outage? '*,*"' << " 29%1W 2005 Yes. No signal change. 35%TW 2005 Yes. No signal change. 21 %1W 2015 Yes. No change since 2008. 26%1W 2005 Yes. No signal change. 26%1W 2011 Yes, in 1996 3-coil data. No change. 23%1W 2011 Yes, in 2005 +Point&#x17d; data. No change. 26%1W 2011 Yes, in 1996 3-coil data. No change. 26%1W 2009 Yes. No signal change since 1996. 33%1W 2005 Yes. No signal change. 24%1W 2005 Yes. No signal change. 13%1W 2005 Yes. No change since initial detection.
: .;~
6%1W 2011 26%1W 2011 Yes, present in 2005 bobbin data. No RPC. 22%1W 2005 Yes. No signal change. 22%1W 2011 ":-* Yes,:*1:i'resent in 2005 bobbin data. No RPC. 24%1W 2011 . \'*, ;_; . '. (;:,. '* ...... ,-*, *' Cause Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Object Re1J1aining?
Col
No No No No No No No No No No N/A No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14 . Plugged? No No No No No No No No No No No No No No No 
                                            '>~:~\:;._
' *.i .. ' Maxbepth*  
_,._-No.
*Initially SG Row
                                                                ' ' ' ~~~~A'   ~-t  ~":*201.2.,~:- . 20tf5'; .
* Co( Locatio*n ETSS (%TW) .Reported
T J~~
*,* ' .. '**'* . ' i* c 39 34 BPH+0.57 27901.1 24%TW 2011 c 40 34 BPH+0.60 27901.1 22%TW 2011 c 44 42 TSH+0.12 27901.1 24%TW 2005 c 44 43 TSH+0.19 27901.1 26%TW 2005 c 44 47 TSH+0.06 27901.1 26%TW 2005 c 44 60 BPH+0.17 96910.1 7%1W 2015 c 45 42 TSH+0.26 27901.1 19%TW 2015 TSH+0.23 27901.1 23%TW c 45 43 TSH+0.24 27901.1 24%TW 2005 TSH+0.72 27901.1 20%TW c 45 47 TSH+0.17 27901.1 23%TW 2005 *.*. .
                                                                                                                                      ~1;,:
Present Prior to' ' ,-Current Outage? . . ' . Yes, present in 2005 bobbin data. No RPC. Yes, present in 2005 bobbin data. No RPC. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. Present in 2014 bobbin data with no change. Present in 2005 +Point&#x17d; data with no change. Yes. No signal change. Yes. No signal change. '*
SGC                         24'                 8                 AV4                 9             10 SGC                         25                 9                 AV1                 8               8
* l'i' .. "' Cause. .. Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object Remaining?
                                                                                                                                              .... -~
No No No No No N/A No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 Plugged? . No No No No No No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14 e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation.
SGC                         25                 9                 AV3               11             10                                       ~ ~
The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times. Table 6 -Circumferential PWSCC Indications
SGC                         25               27                   AV1               18             17 SGC                     . 25                   27                   AV2               32             32
><' : .+PointtM
                                                                                                                                                      *~
'
SGC                         25               27                   AV3               13             12                                     :.,---
* Max '* Arc: ; SG*,'.* Row *C.ol 'Ind* ' 1 l.ocatfon
                                                                                                                                                    ~~:*
* ' >'' >*' ,, '* .:J' , 1;:*t0r.9 tt\ * : 1 PD'1\, "' '' " ,*
SGC                        25                29                  AV2               12             8
* Volts. ( '' . SGC 6 41 SCI TEH +18.25" 0.88 65%TW 85&deg; 15 SGC 7 46 SCI TEH +15.56" 0.78 50%TW 78&deg; 11 SGC 27 65 SCI TEH +16.04" 1.30 60%TW 99&deg; 17 f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator.
  - SGC                         25                 29                   AV3               26             20 SGC                         26                 26                   AV3               17             19 SGC                         26                 26                   AV4               17 -            17 SGC                         26                 39                   AV3               20             15 SGC                         27                 84                   AV4               11             7 SGC                         31               65                   AV2               17             13 SGC                         31               69                   AV2               26             19 SGC                         31               69                   AV3               20             17 SGC                         31               75                   AV3               11             13 SGC                         31               75                   AV4               16             13 SGC                         33               59                   AV3               21             19 SGC                         33               59                   AV4               11             12 SGC                         33               67                   AV3               NR             10
., * }, Table 7 provides the plugging totals and percentages to date. SGA SG B SGC Total Table 7 -Tube Plugging Summary 3,342 3,342 3,342 10,026 .Tube's Plugged, :., * *. To Date* .* , .. 30 (0.9%) 19 (0.6%) 50 (1.5%) 99 (1.0%) g. The results of condition monitoring, including the results of tube pulls and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity.
 
Further, the results from the current outage inspection validate prior outage operational assessment assumptions.
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 I~:      ,"*" ,,
Tube pulls and in-situ pressure testing were not required during the current outage.
                                        ~'! .~"~~J* \: . -:~VB:
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14 h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.
c:>ep111:4,(%ffl):. *. *
During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG. i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident.
*,*..;_*s~:~:*:
* j. The results of the monitoring for tube axial displacement (slippage).
__ ,. .Row                **-Col . ,,_*No.***
If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
ETSS.; 9604 t ..:~ *
No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data 'j
                                                                              -    :           ~*
* from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 5 r-* 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were . identified) and will again be screened during the Spring 2017 RFO.
  .   ' . ~<~- '   '   ,,, ,; ' !   *,  :: . ':    '  ;:.'*:> .;.. ,::2012 ,:, '20f5.
AVB BPC BPH C/l ECT EFPM ETSS FOSAR GPD H/L MRPC NSAL NTE OD ODSCC OVR OXP PARC PLP PWSCC SC! SG SSC TEC TEH TSC TSH TSP TTS TW Acronyms Anti-Vibration Bar Baffle Plate Cold Baffle Plate Hot Cold Lea Eddy Current Testina Effective Full Power Month Eddy Current Technical Specification Sheets Foreiqn Obiect Search and Retrieval Gallons Per Dav Hot Lea Motorized Rotatina Pancake Coil Nuclear Safetv Advisory Letter No tube Exoansion Outer Diameter Outside Diameter Stress Corrosion Crackinq Over Roll Over Expansion Permanent Alternate Reoair Criteria Possible Loose Part Primary Water Stress Corrosion Crackina Single Circumferential Indication Steam Generator Stress Corrosion Crackina Tube End Cold-lea Tube End Hot-lea Top of Tube Sheet Cold-lea Top of Tube Sheet Hot-leq Tube Support Plate Top of Tube&heet Throuqh Wall Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14
  ~      '  ~'
' '
SGC              33                      68                AV1            18          20 SGC              33                    68                AV2           20          19 SGC             33                     69               AV1           10          9 SGC.             33                     69               AV2           13          11 SGC             33                     70               AV1           10          8 SGC               33                     70               AV3           16          16 SGC             34                     29               AV3           11          12 SGC             34                     29               AV4           17          16 SGC             34                     79               AV1             8          11 SGC               35                     77               AV2           10          11 SGC             35                     77               AV3           10          10 SGC             37                     63               AV2           13          11 SGC             37                     73                 AV3           15          17
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission Attention:
                                                                                                                      -ii              , ..
Document Control Desk Washington, DC 20555-0001 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE Serial No. SPS-LIC/CGL Docket No.
                                                                                                                        ;~
* License No. 16-196 RO 50-281 DPR-37 Technical Specification 6.6.A.3 for Surry Power Station Units 1 and 2 requires the submittal of a Steam Generator Tube Inspection Report to the NRC within 180 days after T avg exceeds 200&deg;F following completion of an inspection performed in accordance with Technical Specification 6.4.Q, Steam Generator Program. Attached is the Surry Unit 2 report for the Fall 2015 refueling outage. If you have any questions concerning this information, please contact Mrs. Candee G. Lovett at (757) 365-2178.
                                                                                                                                        .,~
Douglas Lawrence Director S ation Safety & Licensing Surry Power Station  
                                                                                                                                        .[.,
SGC              37                      75                AV3            12          11                                      ....  :;.
                                                                                                        ':~i                      .. :;;,;
* SGC. 38                                 28               AV1             10          7                                        ('.
                                                                                                                              -r;- ~-=J~~
SGC              38                    28                AV3           17          14                                            ~~
SGC               38                     30                 AV2           12          13
                                                                                                                                  ~'
SGC               38                     43               AV3           15          11
:,~Hr'.~
SGC             *38                     73               AV1           11          9        --Y.;,.:-,                    ::~:~
SGC               38                     73                 AV2           9          8*                      .......        -~--r:_
                                                                                                                      *:-11.
SGC               38                     74                 AV2           8          8                                          .,
SGC               39                     50               AV3           14          13 SGC               39 '                   53                 AV3           30          28 SGC               39                     55               AV3           27          25 SGC               39                     55               AV3           18          12 SGC ' 39                                 55               AV4           26          25 SGC               39                     71                 AV3           12          8 SGC               39                     72                 AV4           5          10 SGC             40                     33               AV2           23          24 SGC             40                     33               AV3           23          25 SGC             40                     63               AV2             9          9 SGC             40                     63               AV3           19          15 SGC             40                     63               AV4           19          16
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14 Depth (% TW) .
**s8      Row    Col    .* AVB '  E:TSS 96041.1
* No.
    ' '                         . 201'2    2015 SGC      41      35        AV3    NR        11 SGC      41      64        AV1    11         9 SGC      41    . 66        AV3    12       14 SGC      41      68        AV4    10       10 SGC      43      39        AV2    16        13 SGC      43      61        AV1    25        22 SGC      43      63        AV1    14        15 SGC      44      61        AV1    11       10 SGC      45      58        AV3    NR        13 SGC      46      45        AV2      8        11 SGC      46      45        AV3    NR        10 SGC      46      46        AV1    NR        10
                                                                  .)~1 SGC      46      46        AV2    NR        12
                                                                ' ~,;:;'.. l.'.\
SGC      46      46        AV3    NR        13
                                                    ':.bi                  ',c-113; SGC      46      46        AV4    NR        10                            ,,
c;:
NR = Not Reported du!"ing the previous outage
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Table 5 - Summary of Non-AVB Volumetric Degradation Identified
        . .   .* ..            .*        '" k    .
M~Depth      Initially    Signal Present prior to
                                                                                                            . . *
* Foreign ...
SG  Row     Col Location          ETSS                                                                Cause        Object      Plugged?
  ~
                        .. I*,              .'
{f,oTW) Repor;ted
                                                                        *,,    Current Outage?
                                                                                                            .. Remaining?
Yes. No signal change    Foreign TSC+0.82        27901.1          20%TW      2015                                                    No            No since 1995.        Object A    4      37 Yes. No signal change    Foreign TSC+1.81        27901.1          27%TW      2015                                                    No            No since 1995.        Object Yes. No signal A    6    60    5H-0.59        96910.1          13%TW      2009                                  TSP Wear        N/A          No change since 2002.
Yes. No signal        Foreign A    11    45  TSH+0.96        27901.1         27%TW      2012                                                    No            No change since 2006.       Object No signal present      Foreign A    15    16  TSH+0.23        27901.1          25%TW        2012                                                  No            No in 2006 exam.         Object Yes. No signal        Foreign A    17    16  TSH+0.04        27901.1         31 %TW      2002                                                  No            No change.         Object Yes. No signal        Foreign A   18      16  TSH+0.02        27901.1          30%TW        2002                                                  No          ~No change.          Object Yes. No signal        Foreign A   32    27  TSC+0.02        27901.1          20%TW        2006                                                  No            No change.         Object Yes. No signal        Foreign A   33     27   TSC+0.12         27901.1          25%TW        2006                                                  No            No change.           Object Yes. No signal        Foreign A   39    24  TSH+0.45        27901.1          20%TW        2009                                                  No            No change since 2006.       Object Yes. No signal change    Foreign A    42    52  TSC+0.26        27901.1          20%TW        2009                                                  No            No since 2009.         Object Yes. No signal        Foreign A    43    61  BPH+0.56        27901.1         23%TW       2009                                                  No            No change since 2002.       Object
                                                ..                           Yes. Possible minor Foreign A    43      64  BPH+0.62        27901.1       '24%TW         2009        sigriai'\;iiange 2002 to                  No            No Object 2009. No change since.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 1.1 '                                                                                              For~ign
                                  '*Max Depth      Initially***    'Signal* Pres~nf Prior to ,, ,                    ,,.
SG Row Col      Location  ETSS                                                                    Cause      Object     Plugged?
(%TW) , Reporte~              ci:rrent Outage?.
                                                                ';  ~
                                                                                                          . R~maining? ..
3C+0.47  96910.1       4%TW       2011                        Yes, in TSP c  3 72                                                                1996 bobbin data.                      N/A          No Wear 3C+0.48  96910.1       2%TW         2011                      No RPC.
Yes. No change since        Foreign c  28 22      TSH+0.17  27901.1       29%TW         2014                                                      No          No initial detection. Object Yes. No change since       Foreign TSH+0.52  27901.1       29%TW         2014                                                      No          No initial detection. Object c  28 23 Yes. No change since        Foreign TSH+0.21  27901.1       29%TW       2014                                                        No           No initial detection. Object Yes. No signal        Foreign c  28 71      TSH+0.27  27901.1       24%TW         2009                                                       No           No change since 1996.       Object Yes, based on lookup.         TSP c  28 84      03H+0.50 96910.1         5%TW        2014 Unchanged since 1996.        Wear N/A          No Yes. Present in 2014 Foreign c  30 48      BPH+0.58  27901.1       20%TW         2015              X-Probe data with no Object No          No change.
Yes, based on lookup.       Foreign c 30 74      TSH+6.47  27901.1       20%TW         2014                                                       No          No Unchanged since 1996.       Object Yes. No signal        Foreign c 32 36      BPH+0.58  27901.1       19%TW         2009 change.          Object No          No Yes. No signal        Foreign c 33 17      TSH+2.69  27901.1       20%TW         2005 change.            Object No          No Yes. No signal        Foreign c  34 18      TSH+0.97  27901.1       22%TW         2005 change.            Object No          No Yes. No signal        Foreign c 34 20      TSH+0.91  27901.1       25%TW         2005 change.            Object No          No Yes. No signal        Foreign c 34 74       TSH+0.06  27901.1       27%TW         2005 change.            Object No          No
                                    ' ~ ..                             *. '<yej'~<< No signal      Foreign c 35 19      TSH+0.32  27901.1       29%TW         2005 change.           Object No          No
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14
                      "                *,Max Depth I* Initially' Signal Present P.rior.,to
                                                                                                                        *t=or~ign
.SG Row  Col l.,ocation, 'ErSS                                                                              Cause        Object    Plugged?
(%TW)      k Reportecl *              'Current Outage?
Re1J1aining?
Yes. No signal      Foreign c  35  22  TSH+1.03    27901.1          29%1W            2005 change. Object No          No Foreign c  35  30  TSH+0.11    27901.1          35%TW          2005              Yes. No signal change.
Object No          No Yes. No change since         Foreign c  36  32  BPH+0.55    27901.1          21 %1W          2015 2008. Object No         No Yes. No signal     Foreign c  36  68  TSH+0.17    27902.1          26%1W            2005 change. Object No         No Yes, in 1996 3-coil data.     Foreign c  37  31  TSH+0.09    27901.1          26%1W            2011 No change.       Object No         No Yes, in 2005 +Point'        Foreign c  37  32  TSH+0.02    27901.1          23%1W            2011 data. No change.      Object No         No Yes, in 1996 3-coil data.      Foreign c  37  33  TSH+0.04    27901.1         26%1W            2011 No change.        Object No         No Yes. No signal      Foreign c  37  34 TSH-0.06    27901.1         26%1W            2009 change since 1996.       Object No          No Yes. No signal      Foreign c 37  35  BPH+0.60    27901.1         33%1W            2005 change. Object No          No Yes. No signal      Foreign c 37  54  TSH+0.12    27901.1         24%1W            2005 change. Object No          No 7C-0.48    96910.1           13%1W          2005 Yes. No change since          TSP c 37 73 initial detection. Wear N/A        No 7C-0.52      96910.1           6%1W          2011 Yes, present in 2005      Foreign c 38  32  BPH+0.60     27901.1         26%1W            2011 bobbin data. No RPC.          Object No          No Yes. No signal      Foreign c  38  53  TSH+0.08    27901.1         22%1W            2005 change.      Object No          No BPH+0.61    27901.1         22%1W            2011                                                          No          No
                                  ..,*    ":-*                                  Yes,:*1:i'resent in 2005  Foreign c 39  32 bobbin data. No RPC.        Object BPH+0.60     27901.1           24%1W          2011                                                          No          No
                                                  . \'*,          ?~ ;_; . '. (;:,. '* ,~ . . . ,-
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 SG
  ' Row*.i* Co(
Locatio*n    ETSS Maxbepth*  *Initially      . ~ignat. Present Prior to' ' ,-    "'
Cause.
Foreign Object  Plugged?
(%TW)    .Reported              Current Outage? .
              *,* ' ''~      ..          '**'* .  '  i*                                      . . '
                                                                                                        ..     Remaining?
Yes, present in 2005          Foreign c    39    34      BPH+0.57    27901.1  24%TW          2011 bobbin data. No RPC.           Object No        No Yes, present in 2005        Foreign c    40    34      BPH+0.60    27901.1  22%TW          2011 bobbin data. No RPC.           Object No        No Yes. No signal       Foreign c    44    42      TSH+0.12    27901.24%TW          2005 change.            Object No        No Yes. No signal       Foreign c    44    43      TSH+0.19    27901.1  26%TW          2005 change.             Object No        No Yes. No signal        Foreign c    44    47      TSH+0.06    27901.1  26%TW          2005 change.            Object No        No Yes. Present in 2014 c    44    60      BPH+0.17    96910.1  7%1W         2015              bobbin data with no        TSP Wear    N/A      No change.
Present in 2005 +Point'        Foreign c    45    42      TSH+0.26    27901.1  19%TW          2015 data with no change.         Object No        No TSH+0.23    27901.1  23%TW Yes. No signal        Foreign c    45    43      TSH+0.24    27901.1  24%TW          2005 change.             Object No       No TSH+0.72    27901.1 20%TW Yes. No signal        Foreign c    45    47      TSH+0.17    27901.1  23%TW          2005 change.            Object No       No
                                            *.*.               ~ '*
* l'i' ..
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14
: e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation. The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times.
Table 6 - Circumferential PWSCC Indications
: .+PointtM '
* Max        '* Arc:
SG*,'.* Row  *C.ol 'Ind* '    1l.ocatfon * ,*' >''* Volts.
                                                                  >*' ,, '* .:J'
                                                                              ~    ,:*.DE{~th'1** 1;:*t0r. 9 tt\ *:
1
                                                                                                                    ~
PD'1\,
(
SGC        6    41    SCI    TEH +18.25"              0.88              65%TW             85&deg;            15 SGC        7    46    SCI    TEH +15.56"              0.78              50%TW             78&deg;            11 SGC      27    65    SCI    TEH +16.04"              1.30              60%TW             99&deg;            17
: f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator.                                                                             .,          * },
Table 7 provides the plugging totals and percentages to date.
Table 7 - Tube Plugging Summary
                                                                              .Tube's Plugged, :., *
                                                                                *. To  Date* .* ,. ~
SGA                    3,342                                  30 (0.9%)
SG B                    3,342                                  19 (0.6%)
SGC                    3,342                                  50 (1.5%)
Total                  10,026                                  99 (1.0%)
: g. The results of condition            monitoring,      including          the        results      of    tube        pulls  and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity. Further, the results from the current outage inspection validate prior outage operational assessment assumptions. Tube pulls and in-situ pressure testing were not required during the current outage.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14
: h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.
During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG.
: i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from other~.sources is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from belo~(the H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields      a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident. *
: j. The results of the monitoring for tube axial displacement (slippage). If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
                                                                                    **~!.
No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data            'j
* from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 20~ 5      r- * 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were
. identified) and will again be screened during the Spring 2017 RFO.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14 Acronyms AVB  Anti-Vibration Bar BPC  Baffle Plate Cold BPH  Baffle Plate Hot C/l Cold Lea ECT  Eddy Current Testina EFPM  Effective Full Power Month ETSS  Eddy Current Technical Specification Sheets FOSAR  Foreiqn Obiect Search and Retrieval GPD  Gallons Per Dav H/L Hot Lea MRPC  Motorized Rotatina Pancake Coil NSAL  Nuclear Safetv Advisory Letter NTE  No tube Exoansion OD  Outer Diameter ODSCC  Outside Diameter Stress Corrosion Crackinq OVR  Over Roll OXP  Over Expansion PARC  Permanent Alternate Reoair Criteria PLP  Possible Loose Part PWSCC  Primary Water Stress Corrosion Crackina                        ?:.~
SC!  Single Circumferential Indication                                  ''
SG  Steam Generator SSC  Stress Corrosion Crackina TEC  Tube End Cold-lea TEH  Tube End Hot-lea TSC  Top of Tube Sheet Cold-lea TSH  Top of Tube Sheet Hot-leq TSP  Tube Support Plate TTS  Top of Tube&heet TW  Throuqh Wall
 
VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission                  Serial No. 16-196 Attention: Document Control Desk                              SPS-LIC/CGL    RO Washington, DC 20555-0001                                    Docket No. 50-281
* License No. DPR-37 VIRGINIA ELECTRIC AND POWER COMPANY SURRY POWER STATION UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE Technical Specification 6.6.A.3 for Surry Power Station Units 1 and 2 requires the submittal of a Steam Generator Tube Inspection Report to the NRC within 180 days after Tavg exceeds 200&deg;F following completion of an inspection performed in accordance with Technical Specification 6.4.Q, Steam Generator Program. Attached is the Surry Unit 2 report for the Fall 2015 refueling outage.
If you have any questions concerning                   this information, please   contact Mrs. Candee G. Lovett at (757) 365-2178.
Douglas     Lawrence Director S ation Safety & Licensing Surry Power Station


==Attachment:==
==Attachment:==
Surry Unit 2 Steam Generator Tube                  Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None


Surry Unit 2 Steam Generator Tube Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager-Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager -North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 ATTACHMENT 1 SURRY UNIT 2 Serial No.: 16-196 Docket No.: 50-281 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)
Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager- Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager - North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station
SURRY UNIT 2 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting
 
* requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C. This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM). Surry Unit 2 exceeded 200&deg;F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.
Serial No.: 16-196 Docket No.: 50-281 ATTACHMENT 1 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)
In the discussion below bold italicized wording represents TS verbiage and the required . information is provided directly below each reporting requirement.
 
A list of acronyms is attac;;hed at the end of this report. " A report shall be submitted Within 180 days after Tavg exceeds following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program.
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting
11 The report shall include: a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is in Table 1.
* requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C.
* The only scope expansions required in SG A and SG C were those ne.ce&sect;sary.
This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM).
to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications.
Surry Unit 2 exceeded 200&deg;F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.
The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.
In the discussion below bold italicized wording represents TS verbiage and the required
. information is provided directly below each reporting requirement. A list of acronyms is attac;;hed at the end of this report.                                                                     "
A report shall be submitted Within 180 days after Tavg exceeds -~JJ0 9F: following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program. 11 The report shall include:
: a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is RfOY,id~d in         ~
                                                                                                      ,}
Table 1.
* The only scope expansions required in SG A and SG C were those ne.ce&sect;sary. to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications. The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.
No bobbin inspections or cold leg tubesheet inspections were performed.
No bobbin inspections or cold leg tubesheet inspections were performed.
The primary side work scope also included as-found and as-left visual examinations in the hot
The primary side work scope also included as-found and as-left visual examinations in the hot
* and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations. ,}
* and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations.
Secondary Side Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 During the Surry Unit 2 Fall 2015 RFO , a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed.
 
This included all accessible steam drum components and structures , including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insert i ons through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs. Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A , B , and C at the top of t he tubesheet , in the annulus, and in the no-tube lane as necessary. Table 1 -Eddy Current Testing Examination Scope Scope Description Extent SGA SG SGC B Bobbin Coil Exams Full Length TEHTEC 2849 2831 H/L CandyCane (Row 3-5) 07CTEH 278 282 H/L Straight (R 1-2) 07HTEH 185 182 H/L Straiqht Restricted 07HTEH 1 C/L CandyCane Restricted 02HTEC 1 C/L Straight Restricted 07CTEC 1 2 C/L Straight (R1-5) 07CTEC 462 463 Array Exams H/L TSH Array (Non-Baffle Plate) TSH01H 834 444 843 H/L TSH A r ray (Baff l e Plate) T SHBPH 2478 1260 2453 C/L TSC Array (Non-Baffle Plate) TSC01C 834 842 C/L TSC Arra y (Baffle Pla t e) TSCBPC 2478 2453 MRPC Exams Ubend +Poin t&#x17d; (Row 1-2) 07H07C 185 182 MRPC S pe c i a l Interes t H/L Previo u s I ndications Various 120 172 H/L Previous Restricted 02H03 1 C/L Previous Restricted Various 8 H/L Current Indications Various 97 7 92 Ubend Current Indications Various 2 1 C/L Previous Indications Various 8 7 C/L Current Indications Various 36 20 Indications For Mag8ias Probe Various 1 2 Additional RPC TEHTSH 2 Total 10848 1713 10838
Serial No. : 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 Secondary Side During the Surry Unit 2 Fall 2015 RFO, a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed. This included all accessible steam drum components and structures, including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insertions through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs . Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A, B, and C at the top of the tubesheet, in the annulus, and in the no-tube lane as necessary.
: b. Degradation mechanisms found Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14 Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage. c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.
Table 1 - Eddy Current Testing Examination Scope SG Scope Description             Extent     SGA             SGC B
Table 2 -Inspection Method for Applicable Degradation Modes .. *Degradation  
Bobbin Coil Exams Full Length                             TEHTEC       2849           2831 H/L CandyCane (Row 3-5)                 07CTEH       278             282 H/L Straight (R 1-2)                   07HTEH       185             182 H/L Straiqht Restricted                 07HTEH                         1 C/L CandyCane Restricted               02HTEC                         1 C/L Straight Restricted                 07CTEC         1             2 C/L Straight (R1-5)                     07CTEC       462             463 Array Exams H/L TSH Array (Non-Baffle Plate)       TSH01H       834   444     843 H/L TSH Array (Baffle Plate)           TSHBPH      2478   1260   2453 C/L TSC Array (Non-Baffle Plate)       TSC01C       834             842 C/L TSC Array (Baffle Plate)           TSCBPC       2478           2453 MRPC Exams Ubend +Point' (Row 1-2)                 07H07C       185             182 MRPC Special Interest H/L Previous Indications                Various     120             172 H/L Previous Restricted                 02H03                         1 C/L Previous Restricted                 Various                       8 H/L Current Indications                 Various     97       7     92 Ubend Current Indications               Various       2               1 C/L Previous Indications                 Various       8               7 C/L Current Indications                 Various     36             20 Indications For Mag8ias Probe           Various       1               2 Additional RPC                         TEHTSH                 2 Total     10848   1713   10838
' Classification.'  
 
: Mechanism,
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14
* Loi;ation Probe Type. .. ""' . . . . .. : '"
: b. Degradation mechanisms found Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage.
''',,:.' "*-' ... Existing Tube Wear Anti-Vibration Bars Bobbin -Detection and Sizing Existing OD Pitting Top-of-Tubesheet Bobbin and +Point&#x17d;-Detection
: c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.
+Point&#x17d; -Sizing Existing Tube Wear Tube Support Plate Bobbin -Detection
Table 2 - Inspection Method for Applicable Degradation Modes
+Point&#x17d; -Sizing Existing Tube Wear Freespan and TIS Bobbin and +Point&#x17d; -Detection (foreign objects) +Point&#x17d; -Sizing Potential ODSCC Hot Leg Top-of-Tubesheet  
      '                    *Degradation Classification.'       : Mechanism,   ..
+Point&#x17d; -Detection and Sizing PWSCC Potential PWSCC Tube Ends NIA* Potential Tube Wear Flow Distribution Baffle Bobbin -Detection
* Loi;ation                     .Probe
+Point&#x17d; -Sizing Bulges, Dents, Manufacturing Potential ODSCC Anomalies, and Above-+Point&#x17d; -Detection and Sizing PWSCC Tubesheet Overexpansions (OVR) Potential ODSCC Tubesheet Crevice in +Point&#x17d; -Detection and Sizing Tubes With NTEs Potential Tube Slippage Within Tubesheet Bobbin Detection Potential PWSCC Tubesheet
                                                                                        .      Type..
+Point&#x17d; -Detection and Sizing Overexpansions (OXP) Potential ODSCC Row 1 and 2 Li-bends +Point&#x17d; -Detection and Sizing PWSCC Potential ODS CC Freespan and Tube Supports Bobbin -Detection
                                                        '" ~',,      ''',,:.'                     "*-'
+Point&#x17d; -Sizing *Inspection not required per technical specification alternate repair criteria.
Existing             Tube Wear           Anti-Vibration Bars         Bobbin - Detection and Sizing Bobbin and +Point'- Detection Existing             OD Pitting         Top-of-Tubesheet
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14 d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified.
                                                                                      +Point' - Sizing Bobbin - Detection Existing             Tube Wear           Tube Support Plate
Tables 3 through 6 provide information regarding these indications.
                                                                                      +Point' - Sizing Tube Wear                                       Bobbin and +Point' - Detection Existing                                Freespan and TIS (foreign objects)                                         +Point' - Sizing ODSCC Potential                             Hot Leg Top-of-Tubesheet       +Point' - Detection and Sizing PWSCC Potential               PWSCC                 Tube Ends                           NIA*
Table 3 -AVB Indications for SG A SGA 25 57 AV2 16 21 SGA 26 ' 9 AV4 12 10 I SGA 26 ' 86 AV3 17 21 SGA 29 28 AV3 NR 13 SGA 29 70 AV2 11 11 SGA 30 12 AV1 10 10 , ,,;:-... $GA 30 64 AV2 7 8 ----* SGA 33 26 AV4 NR 12 SGA 36 62 AV2 24* 21 I SGA 36 62 AV3 14 16 SGA 36 62 AV4 27 31 SGA 36 66 AV2 12 16 I SGA 36 66 ' AV3 " 10 13 i *' *:.::* . . -..... -SGA 37 20 AV1 13 12 .. --* -SGA 37 20 AV4 12 10 SGA 38 57. AV1 13 13 SGA 38 70 AV3 NR 11 SGA 38 72 AV4 23 26 SGA 38 74 AV4 17 22 SGA 40 25 AV4 12 8. SGA 40 49 AV1 11 15 SGA 40 49 AV2 10 10 SGA 40 49 AV3 11 11 SGA 40 65 AV2 18 21 SGA 40 65 AV3 10 15 SGA 40 65 AV4 10 9 SGA 40 66 AV3. 9 14 " -**--.....
Bobbin - Detection Potential             Tube Wear         Flow Distribution Baffle
-
                                                                                      +Point' - Sizing Bulges, Dents, Manufacturing ODSCC           Anomalies, and Above-Potential                                                            +Point' - Detection and Sizing PWSCC         Tubesheet Overexpansions (OVR)
-*-b
Tubesheet Crevice in Potential              ODSCC                                        +Point' - Detection and Sizing Tubes With NTEs Potential           Tube Slippage         Within Tubesheet                 Bobbin Detection Tubesheet Potential               PWSCC                                         +Point' - Detection and Sizing Overexpansions (OXP)
* tlli (&deg;AT\IW ** '/i: *.eP.':* o* .... *:**** '* ETSS '96041':1  
ODSCC Potential                               Row 1 and 2 Li-bends         +Point' - Detection and Sizing PWSCC Bobbin - Detection Potential               ODS CC       Freespan and Tube Supports
',*
                                                                                      +Point' - Sizing
; : *;)2012: ..
        *Inspection not required per technical specification alternate repair criteria.
* 201,:s .. SGA 42 62 AV3 NR 10 SGA 44 35 AV1 NR 10 SGA 44 38 AV2 11 9 SGA 45 44 AV2 11 11 SGA 46 45 AV1 13 10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C :::):*:: .....
 
j-r**"' .,, : J, ' "
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14
*  
: d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified. Tables 3 through 6 provide information regarding these indications.
(% TW).*. * **  
Table 3 -AVB Indications for SG A SGA       25       57   AV2   16       21 26 '                                   I                                      "
; L -,.SG.-. " -_;. ' .: ETSs,' 96041'..:l Row Col '\  
SGA                  9   AV4   12       10 SGA       26       86 ' AV3   17       21 SGA       29       28   AV3   NR       13 SGA       29       70   AV2   11       11 SGA       30       12   AV1   10       10                       ~--
' ' ' _,._-No. ' ': : ; ' ' . 20tf5'; . **;<<.*' ._: ..... *;**. SGC 24' 8 AV4 9 10 SGC 25 9 AV1 8 8 SGC 25 9 AV3 11 10 SGC 25 27 AV1 18 17 SGC . 25 27 AV2 32 32 SGC 25 27 AV3 13 12 SGC 25 29 AV2 12 8 -SGC 25 29 AV3 26 20 SGC 26 26 AV3 17 19 SGC 26 26 AV4 17 17 -SGC 26 39 AV3 20 15 SGC 27 84 AV4 11 7 SGC 31 65 AV2 17 13 SGC 31 69 AV2 26 19 SGC 31 69 AV3 20 17 SGC 31 75 AV3 11 13 SGC 31 75 AV4 16 13 SGC 33 59 AV3 21 19 SGC 33 59 AV4 11 12 SGC 33 67 AV3 NR 10 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14 T
                                                                                              ,,;:- ... ~
---.... . ..;..... 
                      $GA       30       64   AV2     7       8                                               -~v SGA       33       26   AV4   NR       12 SGA       36       62   AV2   24*     21     I SGA       36       62   AV3   14       16 SGA       36       62   AV4   27       31 SGA       36       66   AV2   12       16     I                                       -~--
,, " " ' ,"*" -**
SGA       36       66 ' AV3 " 10         13     i                   *'
\: . .Row **-Col . *,*. __ ,. -.*>< ' ,,_*No.*** . ' . ' *, :: . ': ' ' ' ,,, ,; '! ;:.'*:> .;.. SGC 33 68 AV1 SGC 33 68 AV2 SGC 33 69 AV1 SGC. 33 69 AV2 SGC 33 70 AV1 SGC 33 70 AV3 SGC 34 29 AV3 SGC 34 29 AV4 SGC 34 79 AV1 SGC 35 77 AV2 SGC 35 77 AV3 SGC 37 63 AV2 SGC 37 73 AV3 SGC 37 75 AV3
SGA       37       20   AV1   13       12                       .. ~.                -~,:
* SGC. 38 28 AV1 SGC 38 28 AV3 SGC 38 30 AV2 SGC 38 43 AV3 SGC *38 73 AV1 SGC 38 73 AV2 SGC 38 74 AV2 SGC 39 50 AV3 SGC 39 ' 53 AV3 SGC 39 55 AV3 SGC 39 55 AV3 SGC ' 39 55 AV4 SGC 39 71 AV3 SGC 39 72 AV4 SGC 40 33 AV2 SGC 40 33 AV3 SGC 40 63 AV2 SGC 40 63 AV3 SGC 40 63 AV4 ' . c:>ep111:4,(%
SGA       37       20   AV4   12       10 SGA       38       57. AV1   13       13 SGA       38       70   AV3   NR       11 SGA       38       72   AV4   23       26 SGA       38       74   AV4   17       22 SGA       40       25   AV4   12       8.
ffl):. *.
SGA       40       49   AV1   11       15 SGA       40       49   AV2   10       10 SGA       40       49   AV3   11       11 SGA       40       65   AV2   18       21 SGA       40       65   AV3   10       15 SGA       40       65   AV4   10       9 SGA       40       66   AV3. 9       14
* ETSS. 9604 t .. * -: ; ,::2012 ,:, '20f5. 18 20 20 19 10 9 13 11 10 8 16 16 11 12 17 16 8 11 10 11 10 10 13 11 15 17 12 11 10 7 17 14 12 13 15 11 11 9 9 8* 8 8 14 13 30 28 27 25 18 12 26 25 12 8 5 10 23 24 23 25 9 9 19 15 19 16 Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 -ii
 
--Y.;,.:-, ....... *:-11. , .. .[., .... :;. .. :;;,; ('. -r;-
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14
., .,.:
                                                                                        -*-b*.eP.':*
.* AVB Depth (% TW) . **s8 Row Col No. ' E:TSS 96041.1 * ' ' ' . 201'2 2015 SGC 41 35 AV3 NR 11 SGC 41 64 AV1 11 9 SGC 41 . 66 AV3 12 14 SGC 41 68 AV4 10 10 SGC 43 39 AV2 16 13 SGC 43 61 AV1 25 22 SGC 43 63 AV1 14 15 SGC 44 61 AV1 11 10 SGC 45 58 AV3 NR 13 SGC 46 45 AV2 8 11 SGC 46 45 AV3 NR 10 SGC 46 46 AV1 NR 10 SGC 46 46 AV2 NR 12 SGC 46 46 AV3 NR 13 SGC 46 46 AV4 NR 10 NR = Not Reported du!"ing the previous outage Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14
                                                                                        '/i:
'
* tlli (&deg;AT\IW o* .... *:******
':.bi l.'.\ ',c-113; ,, c;: 
                                                                                      '* ETSS '96041':1
' .* . . .. SG Row Col Location . . TSC+0.82 A 4 37 TSC+1.81 A 6 60 5H-0.59 A 11 45 TSH+0.96 A 15 16 TSH+0.23 A 17 16 TSH+0.04 A 18 16 TSH+0.02 A 32 27 TSC+0.02 A 33 27 TSC+0.12 A 39 24 TSH+0.45 A 42 52 TSC+0.26 A 43 61 BPH+0.56 A 43 64 BPH+0.62 Table 5 -Summary of Non-AVB Volumetric Degradation Identified
                      ,.-~
.* '" k . Signal Present prior to . . *
                                                                                    ;: *;)2012: ~: .
* Foreign ... ETSS Initially Cause Object {f,oTW) Repor;ted
* 201,:s .
*,, Current Outage? Remaining?
SGA                           42               62                 AV3               NR             10 SGA                           44               35                 AV1               NR             10 SGA                           44               38                 AV2               11               9 SGA                           45               44                 AV2                 11             11 SGA                           46               45                 AV1               13             10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C
I*, . ' .. *. ' ... 27901.1 20%TW 2015 Yes. No signal change Foreign No since 1995. Object 27901.1 27%TW 2015 Yes. No signal change Foreign No since 1995. Object 96910.1 13%TW 2009 Yes. No signal TSP Wear N/A change since 2002. 27901.1 27%TW 2012 Yes. No signal Foreign No change since 2006. Object 27901.1 25%TW 2012 No signal present Foreign No in 2006 exam. Object 27901.1 31 %TW 2002 Yes. No signal Foreign No change. Object 27901.1 30%TW 2002 Yes. No signal Foreign No change. Object 27901.1 20%TW 2006 Yes. No signal Foreign No change. Object 27901.1 25%TW 2006 Yes. No signal Foreign No change. Object 27901.1 20%TW 2009 Yes. No signal Foreign No change since 2006. Object 27901.1 20%TW 2009 Yes. No signal change Foreign No since 2009. Object 27901.1 23%TW 2009 Yes. No signal Foreign No change since 2002. Object .. Yes. Possible minor Foreign 27901.1 '24%TW 2009 sigriai'\;iiange 2002 to No 2009. No change since. Object Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Plugged? ' No No No No No No No No No No No No 1.1 ' '*Max Depth SG Row Col Location ETSS Initially***
:::):*::..... {~ii j-r**"' .,,
(%TW) ,
- ,.SG.- .
3C+0.47 96910.1 4%TW 2011 c 3 72 3C+0.48 96910.1 2%TW 2011 c 28 22 TSH+0.17 27901.1 29%TW 2014 TSH+0.52 27901.1 29%TW 2014 c 28 23 TSH+0.21 27901.1 29%TW 2014 c 28 71 TSH+0.27 27901.1 24%TW 2009 c 28 84 03H+0.50 96910.1 5%TW 2014 c 30 48 BPH+0.58 27901.1 20%TW 2015 c 30 74 TSH+6.47 27901.1 20%TW 2014 c 32 36 BPH+0.58 27901.1 19%TW 2009 c 33 17 TSH+2.69 27901.1 20%TW 2005 c 34 18 TSH+0.97 27901.1 22%TW 2005 c 34 20 TSH+0.91 27901.1 25%TW 2005 c 34 74 TSH+0.06 27901.1 27%TW 2005 ' .. c 35 19 TSH+0.32 27901.1 29%TW 2005 '. 'Signal*
: ~'"~~"'"' ~ J,
Prior to ,, , '; ci:rrent Outage?. Yes, in 1996 bobbin data. No RPC. Yes. No change since initial detection.
                                                '-'!;'~:,"':: ;
Yes. No change since initial detection.
L
Yes. No change since initial detection.
                                                                        ~xva~
Yes. No signal change since 1996. Yes, based on lookup. Unchanged since 1996. Yes. Present in 2014 X-Probe data with no change. Yes, based on lookup. Unchanged since 1996. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. No signal change. * ..
* r'*.~~bepM; (% TW).*. ***
No signal change. Cause TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Object ,,. .  
                                                                                      .: ETSs,' 96041'..:l
.. N/A No No No No N/A No No No No No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 " Plugged? No No No No No No No No No No No No No No   
'\**;<<.*' "-,~:.*,
.SG Row Col " 'ErSS l.,ocation, ' .. c 35 22 TSH+1.03 27901.1 c 35 30 TSH+0.11 27901.1 c 36 32 BPH+0.55 27901.1 c 36 68 TSH+0.17 27902.1 c 37 31 TSH+0.09 27901.1 c 37 32 TSH+0.02 27901.1 c 37 33 TSH+0.04 27901.1 c 37 34 TSH-0.06 27901.1 c 37 35 BPH+0.60 27901.1 c 37 54 TSH+0.12 27901.1 7C-0.48 96910.1 c 37 73 7C-0.52 96910.1 c 38 32 BPH+0.60 27901.1 c 38 53 TSH+0.08 27901.1 BPH+0.61 27901.1 ,* .. c 39 32 BPH+0.60 27901.1 '. *,Max Depth I* Initially' Signal Present P.rior.,to
              ~ "'~ '~1 '~ '
(%TW) k Reportecl
Row
* 'Current Outage? '*,*"' << " 29%1W 2005 Yes. No signal change. 35%TW 2005 Yes. No signal change. 21 %1W 2015 Yes. No change since 2008. 26%1W 2005 Yes. No signal change. 26%1W 2011 Yes, in 1996 3-coil data. No change. 23%1W 2011 Yes, in 2005 +Point&#x17d; data. No change. 26%1W 2011 Yes, in 1996 3-coil data. No change. 26%1W 2009 Yes. No signal change since 1996. 33%1W 2005 Yes. No signal change. 24%1W 2005 Yes. No signal change. 13%1W 2005 Yes. No change since initial detection.
: .;~
6%1W 2011 26%1W 2011 Yes, present in 2005 bobbin data. No RPC. 22%1W 2005 Yes. No signal change. 22%1W 2011 ":-* Yes,:*1:i'resent in 2005 bobbin data. No RPC. 24%1W 2011 . \'*, ;_; . '. (;:,. '* ...... ,-*, *' Cause Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Object Re1J1aining?
Col
No No No No No No No No No No N/A No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14 . Plugged? No No No No No No No No No No No No No No No 
                                            '>~:~\:;._
' *.i .. ' Maxbepth*
_,._-No.
*Initially SG Row
                                                                ' ' ' ~~~~A'   ~-t  ~":*201.2.,~:- . 20tf5'; .
* Co( Locatio*n ETSS (%TW) .Reported
T J~~
*,* ' .. '**'* . ' i* c 39 34 BPH+0.57 27901.1 24%TW 2011 c 40 34 BPH+0.60 27901.1 22%TW 2011 c 44 42 TSH+0.12 27901.1 24%TW 2005 c 44 43 TSH+0.19 27901.1 26%TW 2005 c 44 47 TSH+0.06 27901.1 26%TW 2005 c 44 60 BPH+0.17 96910.1 7%1W 2015 c 45 42 TSH+0.26 27901.1 19%TW 2015 TSH+0.23 27901.1 23%TW c 45 43 TSH+0.24 27901.1 24%TW 2005 TSH+0.72 27901.1 20%TW c 45 47 TSH+0.17 27901.1 23%TW 2005 *.*. .
                                                                                                                                      ~1;,:
Present Prior to' ' ,-Current Outage? . . ' . Yes, present in 2005 bobbin data. No RPC. Yes, present in 2005 bobbin data. No RPC. Yes. No signal change. Yes. No signal change. Yes. No signal change. Yes. Present in 2014 bobbin data with no change. Present in 2005 +Point&#x17d; data with no change. Yes. No signal change. Yes. No signal change. '*
SGC                          24'                  8                AV4                9              10 SGC                         25                 9                 AV1                 8               8
* l'i' .. "' Cause. .. Foreign Object Foreign Object Foreign Object Foreign Object Foreign Object TSP Wear Foreign Object Foreign Object Foreign Object Foreign Object Remaining?
                                                                                                                                              .... -~
No No No No No N/A No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 Plugged? . No No No No No No No No No Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14 e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation.
SGC                         25                 9                 AV3               11             10                                       ~ ~
The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times. Table 6 -Circumferential PWSCC Indications
SGC                         25               27                   AV1               18             17 SGC                     . 25                   27                   AV2               32             32
><' : .+PointtM
                                                                                                                                                      *~
'
SGC                         25               27                   AV3               13             12                                     :.,---
* Max '* Arc: ; SG*,'.* Row *C.ol 'Ind* ' 1 l.ocatfon
                                                                                                                                                    ~~:*
* ' >'' >*' ,, '* .:J' , 1;:*t0r.9 tt\ * : 1 PD'1\, "' '' " ,*
SGC                        25                 29                   AV2               12             8
* Volts. ( '' . SGC 6 41 SCI TEH +18.25" 0.88 65%TW 85&deg; 15 SGC 7 46 SCI TEH +15.56" 0.78 50%TW 78&deg; 11 SGC 27 65 SCI TEH +16.04" 1.30 60%TW 99&deg; 17 f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator.  
  - SGC                         25                 29                   AV3               26             20 SGC                         26                 26                   AV3               17             19 SGC                         26                 26                   AV4               17 -            17 SGC                         26                 39                   AV3               20             15 SGC                         27                 84                   AV4               11             7 SGC                         31               65                   AV2               17             13 SGC                         31               69                   AV2               26             19 SGC                         31               69                   AV3               20             17 SGC                         31               75                   AV3               11             13 SGC                         31               75                   AV4               16             13 SGC                         33               59                   AV3               21             19 SGC                         33               59                   AV4               11             12 SGC                         33               67                   AV3               NR             10
., * }, Table 7 provides the plugging totals and percentages to date. SGA SG B SGC Total Table 7 -Tube Plugging Summary 3,342 3,342 3,342 10,026 .Tube's Plugged, :., * *. To Date* .* , .. 30 (0.9%) 19 (0.6%) 50 (1.5%) 99 (1.0%) g. The results of condition monitoring, including the results of tube pulls and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity.
 
Further, the results from the current outage inspection validate prior outage operational assessment assumptions.
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 I~:      ,"*" ,,
Tube pulls and in-situ pressure testing were not required during the current outage.
                                        ~'! .~"~~J* \: . -:~VB:
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14 h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.
c:>ep111:4,(%ffl):. *. *
During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG. i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident.
*,*..;_*s~:~:*:
* j. The results of the monitoring for tube axial displacement (slippage).
__ ,. .Row                **-Col . ,,_*No.***
If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
ETSS.; 9604 t ..:~ *
No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data 'j
                                                                              -    :           ~*
* from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 5 r-* 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were . identified) and will again be screened during the Spring 2017 RFO.
  .   ' . ~<~- '   '   ,,, ,; ' !   *,  :: . ':    '  ;:.'*:> .;.. ,::2012 ,:, '20f5.
AVB BPC BPH C/l ECT EFPM ETSS FOSAR GPD H/L MRPC NSAL NTE OD ODSCC OVR OXP PARC PLP PWSCC SC! SG SSC TEC TEH TSC TSH TSP TTS TW Acronyms Anti-Vibration Bar Baffle Plate Cold Baffle Plate Hot Cold Lea Eddy Current Testina Effective Full Power Month Eddy Current Technical Specification Sheets Foreiqn Obiect Search and Retrieval Gallons Per Dav Hot Lea Motorized Rotatina Pancake Coil Nuclear Safetv Advisory Letter No tube Exoansion Outer Diameter Outside Diameter Stress Corrosion Crackinq Over Roll Over Expansion Permanent Alternate Reoair Criteria Possible Loose Part Primary Water Stress Corrosion Crackina Single Circumferential Indication Steam Generator Stress Corrosion Crackina Tube End Cold-lea Tube End Hot-lea Top of Tube Sheet Cold-lea Top of Tube Sheet Hot-leq Tube Support Plate Top of Tube&heet Throuqh Wall Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14
  ~      '  ~'
' '}}
SGC              33                     68               AV1            18          20 SGC              33                    68                AV2           20          19 SGC             33                     69               AV1           10          9 SGC.             33                     69               AV2           13          11 SGC             33                     70               AV1           10          8 SGC               33                     70               AV3           16          16 SGC             34                     29               AV3           11          12 SGC             34                     29               AV4           17          16 SGC             34                     79               AV1             8          11 SGC               35                     77               AV2           10          11 SGC             35                     77               AV3           10          10 SGC             37                     63               AV2           13          11 SGC             37                     73                 AV3           15          17
                                                                                                                      -ii              , ..
                                                                                                                        ;~
                                                                                                                                        .,~
                                                                                                                                        .[.,
SGC              37                      75                AV3            12          11                                      ....  :;.
                                                                                                        ':~i                      .. :;;,;
* SGC. 38                                 28               AV1             10          7                                        ('.
                                                                                                                              -r;- ~-=J~~
SGC              38                    28                AV3           17          14                                            ~~
SGC               38                     30                 AV2           12          13
                                                                                                                                  ~'
SGC               38                     43               AV3           15          11
:,~Hr'.~
SGC             *38                     73               AV1           11          9        --Y.;,.:-,                    ::~:~
SGC              38                    73                AV2            9          8*                      .......        -~--r:_
                                                                                                                      *:-11.
SGC              38                    74                AV2           8          8                                          .,
SGC               39                     50               AV3           14          13 SGC               39 '                   53                 AV3           30          28 SGC               39                     55               AV3           27          25 SGC               39                     55               AV3           18          12 SGC ' 39                                 55               AV4           26          25 SGC               39                     71                 AV3           12          8 SGC               39                     72                 AV4           5          10 SGC             40                     33               AV2           23          24 SGC             40                     33               AV3           23          25 SGC             40                     63               AV2             9          9 SGC             40                     63               AV3           19          15 SGC             40                     63               AV4           19          16
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14 Depth (% TW) .
**s8      Row    Col    .* AVB '  E:TSS 96041.1
* No.
    ' '                          . 201'2    2015 SGC      41      35        AV3    NR        11 SGC      41      64        AV1    11         9 SGC      41    . 66        AV3    12       14 SGC      41      68        AV4    10       10 SGC      43      39        AV2    16        13 SGC      43      61        AV1    25        22 SGC      43      63        AV1    14        15 SGC      44      61        AV1    11       10 SGC      45      58        AV3    NR        13 SGC      46      45        AV2      8        11 SGC      46      45        AV3    NR        10 SGC      46      46        AV1    NR        10
                                                                  .)~1 SGC      46      46        AV2    NR        12
                                                                ' ~,;:;'.. l.'.\
SGC      46      46        AV3    NR        13
                                                    ':.bi                  ',c-113; SGC      46      46        AV4    NR        10                            ,,
c;:
NR = Not Reported du!"ing the previous outage
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Table 5 - Summary of Non-AVB Volumetric Degradation Identified
        . .  .* ..            .*        '"  k    .
M~Depth      Initially    Signal Present prior to
                                                                                                            .  . *
* Foreign ...
SG  Row    Col  Location          ETSS                                                                Cause        Object      Plugged?
  ~
                        .. I*,              .'
{f,oTW) Repor;ted
                                                                        *,,    Current Outage?
                                                                                                            .. Remaining?
Yes. No signal change    Foreign TSC+0.82        27901.1          20%TW      2015                                                    No            No since 1995.         Object A   4     37 Yes. No signal change    Foreign TSC+1.81         27901.1          27%TW      2015                                                    No            No since 1995.        Object Yes. No signal A    6    60    5H-0.59        96910.1          13%TW      2009                                  TSP Wear        N/A           No change since 2002.
Yes. No signal        Foreign A    11     45   TSH+0.96         27901.1          27%TW      2012                                                    No            No change since 2006.      Object No signal present      Foreign A    15     16   TSH+0.23         27901.1          25%TW        2012                                                  No            No in 2006 exam.        Object Yes. No signal        Foreign A   17     16   TSH+0.04         27901.1          31 %TW      2002                                                  No            No change.          Object Yes. No signal        Foreign A   18      16  TSH+0.02         27901.1          30%TW        2002                                                  No          ~No change.          Object Yes. No signal        Foreign A   32    27   TSC+0.02        27901.1          20%TW        2006                                                  No            No change.          Object Yes. No signal        Foreign A   33    27  TSC+0.12        27901.1          25%TW        2006                                                  No            No change.           Object Yes. No signal        Foreign A    39    24  TSH+0.45        27901.1          20%TW        2009                                                  No            No change since 2006.       Object Yes. No signal change    Foreign A    42    52  TSC+0.26        27901.1          20%TW        2009                                                  No            No since 2009.         Object Yes. No signal        Foreign A    43    61  BPH+0.56        27901.1         23%TW       2009                                                  No            No change since 2002.       Object
                                                ..                           Yes. Possible minor Foreign A    43      64  BPH+0.62        27901.1       '24%TW         2009        sigriai'\;iiange 2002 to                  No            No Object 2009. No change since.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 1.1 '                                                                                              For~ign
                                  '*Max Depth      Initially***    'Signal* Pres~nf Prior to ,, ,                    ,,.
SG Row Col      Location  ETSS                                                                    Cause      Object     Plugged?
(%TW) , Reporte~              ci:rrent Outage?.
                                                                ';  ~
                                                                                                          . R~maining? ..
3C+0.47  96910.1       4%TW       2011                        Yes, in TSP c  3 72                                                                1996 bobbin data.                     N/A          No Wear 3C+0.48  96910.1       2%TW         2011                      No RPC.
Yes. No change since       Foreign c  28 22      TSH+0.17  27901.1       29%TW         2014                                                      No          No initial detection. Object Yes. No change since        Foreign TSH+0.52  27901.1       29%TW         2014                                                      No           No initial detection. Object c  28 23 Yes. No change since        Foreign TSH+0.21  27901.1      29%TW        2014                                                        No          No initial detection. Object Yes. No signal        Foreign c  28 71      TSH+0.27  27901.1       24%TW         2009                                                       No           No change since 1996.       Object Yes, based on lookup.        TSP c  28 84      03H+0.50 96910.1         5%TW        2014 Unchanged since 1996.        Wear N/A          No Yes. Present in 2014 Foreign c  30 48      BPH+0.58  27901.1       20%TW         2015              X-Probe data with no Object No          No change.
Yes, based on lookup.       Foreign c 30 74      TSH+6.47  27901.1       20%TW         2014                                                       No          No Unchanged since 1996.      Object Yes. No signal        Foreign c  32 36      BPH+0.58  27901.1       19%TW         2009 change.          Object No          No Yes. No signal        Foreign c 33 17      TSH+2.69  27901.1       20%TW         2005 change.            Object No          No Yes. No signal        Foreign c 34 18      TSH+0.97  27901.1       22%TW         2005 change.            Object No          No Yes. No signal        Foreign c 34 20      TSH+0.91  27901.1       25%TW         2005 change.           Object No          No Yes. No signal        Foreign c 34 74       TSH+0.06  27901.1       27%TW         2005 change.           Object No          No
                                    ' ~ ..                             *. '<yej'~<< No signal      Foreign c 35 19      TSH+0.32  27901.1       29%TW         2005 change.            Object No          No
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14
                      "                *,Max Depth I* Initially' Signal Present P.rior.,to
                                                                                                                        *t=or~ign
.SG Row  Col l.,ocation, 'ErSS                                                                              Cause        Object    Plugged?
(%TW)      k Reportecl *               'Current Outage?
Re1J1aining?
Yes. No signal      Foreign c  35  22  TSH+1.03    27901.1          29%1W            2005 change. Object No          No Foreign c  35  30  TSH+0.11    27901.1          35%TW          2005              Yes. No signal change.
Object No          No Yes. No change since         Foreign c  36  32  BPH+0.55    27901.1          21 %1W          2015 2008. Object No          No Yes. No signal      Foreign c  36  68  TSH+0.17    27902.1          26%1W            2005 change. Object No          No Yes, in 1996 3-coil data.     Foreign c  37  31  TSH+0.09    27901.1          26%1W            2011 No change.       Object No          No Yes, in 2005 +Point'        Foreign c  37  32  TSH+0.02    27901.1          23%1W            2011 data. No change.       Object No         No Yes, in 1996 3-coil data.      Foreign c  37  33  TSH+0.04    27901.1          26%1W            2011 No change.       Object No          No Yes. No signal      Foreign c  37  34  TSH-0.06    27901.1          26%1W            2009 change since 1996.       Object No         No Yes. No signal      Foreign c  37  35  BPH+0.60    27901.1          33%1W            2005 change. Object No         No Yes. No signal      Foreign c  37  54  TSH+0.12    27901.1         24%1W            2005 change. Object No         No 7C-0.48    96910.1          13%1W          2005 Yes. No change since          TSP c  37 73 initial detection. Wear N/A        No 7C-0.52      96910.1           6%1W          2011 Yes, present in 2005      Foreign c 38  32 BPH+0.60    27901.1         26%1W            2011 bobbin data. No RPC.          Object No          No Yes. No signal      Foreign c 38  53  TSH+0.08    27901.1         22%1W            2005 change.     Object No          No BPH+0.61    27901.1         22%1W            2011                                                          No          No
                                  ..,*    ":-*                                  Yes,:*1:i'resent in 2005  Foreign c 39  32 bobbin data. No RPC.        Object BPH+0.60     27901.1           24%1W          2011                                                          No          No
                                                  . \'*,          ?~ ;_; . '. (;:,. '* ,~ . . . ,-
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 SG
  ' Row*.i* Co(
Locatio*n    ETSS Maxbepth*   *Initially     . ~ignat. Present Prior to' ' ,-    "'
Cause.
Foreign Object  Plugged?
(%TW)     .Reported              Current Outage? .
              *,* ' ''~      ..         '**'* . '  i*                                      . . '
                                                                                                        ..     Remaining?
Yes, present in 2005          Foreign c    39    34      BPH+0.57    27901.1  24%TW          2011 bobbin data. No RPC.          Object No        No Yes, present in 2005         Foreign c    40    34      BPH+0.60    27901.1  22%TW          2011 bobbin data. No RPC.           Object No        No Yes. No signal       Foreign c    44    42      TSH+0.12    27901.1  24%TW          2005 change.            Object No        No Yes. No signal       Foreign c    44    43      TSH+0.19    27901.1  26%TW          2005 change.            Object No        No Yes. No signal       Foreign c    44    47      TSH+0.06    27901.1  26%TW          2005 change.             Object No       No Yes. Present in 2014 c    44    60      BPH+0.17    96910.1  7%1W         2015              bobbin data with no        TSP Wear    N/A      No change.
Present in 2005 +Point'        Foreign c    45    42      TSH+0.26    27901.1  19%TW          2015 data with no change.         Object No        No TSH+0.23    27901.1  23%TW Yes. No signal        Foreign c    45    43      TSH+0.24    27901.1  24%TW          2005 change.             Object No        No TSH+0.72    27901.1  20%TW Yes. No signal        Foreign c    45    47      TSH+0.17    27901.1  23%TW          2005 change.             Object No        No
                                            *.*.                ~ '*
* l'i' ..
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14
: e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation. The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times.
Table 6 - Circumferential PWSCC Indications
: .+PointtM '
* Max        '* Arc:
SG*,'.* Row  *C.ol 'Ind* '    1l.ocatfon * ,*' >''* Volts.
                                                                  >*' ,, '* .:J'
                                                                              ~    ,:*.DE{~th'1** 1;:*t0r. 9 tt\ *:
1
                                                                                                                    ~
PD'1\,
(
SGC        6    41    SCI    TEH +18.25"              0.88              65%TW             85&deg;            15 SGC        7    46    SCI    TEH +15.56"              0.78              50%TW             78&deg;            11 SGC      27    65    SCI    TEH +16.04"              1.30              60%TW             99&deg;            17
: f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator.                                                                             .,          * },
Table 7 provides the plugging totals and percentages to date.
Table 7 - Tube Plugging Summary
                                                                              .Tube's Plugged, :., *
                                                                                *. To  Date* .* ,. ~
SGA                    3,342                                  30 (0.9%)
SG B                    3,342                                  19 (0.6%)
SGC                    3,342                                  50 (1.5%)
Total                  10,026                                  99 (1.0%)
: g. The results of condition            monitoring,      including          the        results      of    tube        pulls  and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity. Further, the results from the current outage inspection validate prior outage operational assessment assumptions. Tube pulls and in-situ pressure testing were not required during the current outage.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14
: h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.
During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG.
: i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from other~.sources is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from belo~(the H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields      a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident. *
: j. The results of the monitoring for tube axial displacement (slippage). If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
                                                                                    **~!.
No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data            'j
* from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 20~ 5      r- * 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were
. identified) and will again be screened during the Spring 2017 RFO.
 
Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14 Acronyms AVB  Anti-Vibration Bar BPC  Baffle Plate Cold BPH  Baffle Plate Hot C/l Cold Lea ECT  Eddy Current Testina EFPM  Effective Full Power Month ETSS  Eddy Current Technical Specification Sheets FOSAR  Foreiqn Obiect Search and Retrieval GPD  Gallons Per Dav H/L Hot Lea MRPC  Motorized Rotatina Pancake Coil NSAL  Nuclear Safetv Advisory Letter NTE  No tube Exoansion OD  Outer Diameter ODSCC  Outside Diameter Stress Corrosion Crackinq OVR  Over Roll OXP  Over Expansion PARC  Permanent Alternate Reoair Criteria PLP  Possible Loose Part PWSCC  Primary Water Stress Corrosion Crackina                        ?:.~
SC!  Single Circumferential Indication                                  ''
SG Steam Generator SSC  Stress Corrosion Crackina TEC  Tube End Cold-lea TEH  Tube End Hot-lea TSC  Top of Tube Sheet Cold-lea TSH  Top of Tube Sheet Hot-leq TSP  Tube Support Plate TTS  Top of Tube&heet TW  Throuqh Wall}}

Latest revision as of 22:53, 24 February 2020

Inspection Report for the Fall 2015 Refueling Outage
ML16141A117
Person / Time
Site: Surry  Dominion icon.png
Issue date: 05/10/2016
From: Lawrence D
Virginia Electric & Power Co (VEPCO)
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
16-196
Download: ML16141A117 (17)


Text

VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission Serial No.16-196 Attention: Document Control Desk SPS-LIC/CGL RO Washington, DC 20555-0001 Docket No. 50-281

If you have any questions concerning this information, please contact Mrs. Candee G. Lovett at (757) 365-2178.

Douglas Lawrence Director S ation Safety & Licensing Surry Power Station

Attachment:

Surry Unit 2 Steam Generator Tube Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None

Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager- Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager - North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station

Serial No.: 16-196 Docket No.: 50-281 ATTACHMENT 1 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting

  • requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C.

This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM).

Surry Unit 2 exceeded 200°F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.

In the discussion below bold italicized wording represents TS verbiage and the required

. information is provided directly below each reporting requirement. A list of acronyms is attac;;hed at the end of this report. "

A report shall be submitted Within 180 days after Tavg exceeds -~JJ0 9F: following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program. 11 The report shall include:

a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is RfOY,id~d in ~

,}

Table 1.

  • The only scope expansions required in SG A and SG C were those ne.ce§sary. to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications. The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.

No bobbin inspections or cold leg tubesheet inspections were performed.

The primary side work scope also included as-found and as-left visual examinations in the hot

  • and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations.

Serial No. : 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 Secondary Side During the Surry Unit 2 Fall 2015 RFO, a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed. This included all accessible steam drum components and structures, including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insertions through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs . Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A, B, and C at the top of the tubesheet, in the annulus, and in the no-tube lane as necessary.

Table 1 - Eddy Current Testing Examination Scope SG Scope Description Extent SGA SGC B

Bobbin Coil Exams Full Length TEHTEC 2849 2831 H/L CandyCane (Row 3-5) 07CTEH 278 282 H/L Straight (R 1-2) 07HTEH 185 182 H/L Straiqht Restricted 07HTEH 1 C/L CandyCane Restricted 02HTEC 1 C/L Straight Restricted 07CTEC 1 2 C/L Straight (R1-5) 07CTEC 462 463 Array Exams H/L TSH Array (Non-Baffle Plate) TSH01H 834 444 843 H/L TSH Array (Baffle Plate) TSHBPH 2478 1260 2453 C/L TSC Array (Non-Baffle Plate) TSC01C 834 842 C/L TSC Array (Baffle Plate) TSCBPC 2478 2453 MRPC Exams Ubend +Point' (Row 1-2) 07H07C 185 182 MRPC Special Interest H/L Previous Indications Various 120 172 H/L Previous Restricted 02H03 1 C/L Previous Restricted Various 8 H/L Current Indications Various 97 7 92 Ubend Current Indications Various 2 1 C/L Previous Indications Various 8 7 C/L Current Indications Various 36 20 Indications For Mag8ias Probe Various 1 2 Additional RPC TEHTSH 2 Total 10848 1713 10838

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14

b. Degradation mechanisms found Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage.
c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.

Table 2 - Inspection Method for Applicable Degradation Modes

' *Degradation Classification.'  : Mechanism, ..

  • Loi;ation .Probe

. Type..

'" ~',, ,,:.' "*-'

Existing Tube Wear Anti-Vibration Bars Bobbin - Detection and Sizing Bobbin and +Point'- Detection Existing OD Pitting Top-of-Tubesheet

+Point' - Sizing Bobbin - Detection Existing Tube Wear Tube Support Plate

+Point' - Sizing Tube Wear Bobbin and +Point' - Detection Existing Freespan and TIS (foreign objects) +Point' - Sizing ODSCC Potential Hot Leg Top-of-Tubesheet +Point' - Detection and Sizing PWSCC Potential PWSCC Tube Ends NIA*

Bobbin - Detection Potential Tube Wear Flow Distribution Baffle

+Point' - Sizing Bulges, Dents, Manufacturing ODSCC Anomalies, and Above-Potential +Point' - Detection and Sizing PWSCC Tubesheet Overexpansions (OVR)

Tubesheet Crevice in Potential ODSCC +Point' - Detection and Sizing Tubes With NTEs Potential Tube Slippage Within Tubesheet Bobbin Detection Tubesheet Potential PWSCC +Point' - Detection and Sizing Overexpansions (OXP)

ODSCC Potential Row 1 and 2 Li-bends +Point' - Detection and Sizing PWSCC Bobbin - Detection Potential ODS CC Freespan and Tube Supports

+Point' - Sizing

  • Inspection not required per technical specification alternate repair criteria.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14

d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified. Tables 3 through 6 provide information regarding these indications.

Table 3 -AVB Indications for SG A SGA 25 57 AV2 16 21 26 ' I "

SGA 9 AV4 12 10 SGA 26 86 ' AV3 17 21 SGA 29 28 AV3 NR 13 SGA 29 70 AV2 11 11 SGA 30 12 AV1 10 10 ~--

,,;:- ... ~

$GA 30 64 AV2 7 8 -~v SGA 33 26 AV4 NR 12 SGA 36 62 AV2 24* 21 I SGA 36 62 AV3 14 16 SGA 36 62 AV4 27 31 SGA 36 66 AV2 12 16 I -~--

SGA 36 66 ' AV3 " 10 13 i *'

SGA 37 20 AV1 13 12 .. ~. -~,:

SGA 37 20 AV4 12 10 SGA 38 57. AV1 13 13 SGA 38 70 AV3 NR 11 SGA 38 72 AV4 23 26 SGA 38 74 AV4 17 22 SGA 40 25 AV4 12 8.

SGA 40 49 AV1 11 15 SGA 40 49 AV2 10 10 SGA 40 49 AV3 11 11 SGA 40 65 AV2 18 21 SGA 40 65 AV3 10 15 SGA 40 65 AV4 10 9 SGA 40 66 AV3. 9 14

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14

-*-b*.eP.':*

'/i:

  • tlli (°AT\IW o* .... *:******

'* ETSS '96041':1

,.-~

*;)2012
~: .
  • 201,:s .

SGA 42 62 AV3 NR 10 SGA 44 35 AV1 NR 10 SGA 44 38 AV2 11 9 SGA 45 44 AV2 11 11 SGA 46 45 AV1 13 10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C

):*::..... {~ii j-r**"' .,,

- ,.SG.- .

~'"~~"'"' ~ J,

'-'!;'~:,"':: ;

L

~xva~

  • r'*.~~bepM; (% TW).*. ***

.: ETSs,' 96041'..:l

'\**;<<.*' "-,~:.*,

~ "'~ '~1 '~ '

Row

.;~

Col

'>~:~\:;._

_,._-No.

' ' ' ~~~~A' ~-t ~":*201.2.,~:- . 20tf5'; .

T J~~

~1;,:

SGC 24' 8 AV4 9 10 SGC 25 9 AV1 8 8

.... -~

SGC 25 9 AV3 11 10 ~ ~

SGC 25 27 AV1 18 17 SGC . 25 27 AV2 32 32

  • ~

SGC 25 27 AV3 13 12  :.,---

~~:*

SGC 25 29 AV2 12 8

- SGC 25 29 AV3 26 20 SGC 26 26 AV3 17 19 SGC 26 26 AV4 17 - 17 SGC 26 39 AV3 20 15 SGC 27 84 AV4 11 7 SGC 31 65 AV2 17 13 SGC 31 69 AV2 26 19 SGC 31 69 AV3 20 17 SGC 31 75 AV3 11 13 SGC 31 75 AV4 16 13 SGC 33 59 AV3 21 19 SGC 33 59 AV4 11 12 SGC 33 67 AV3 NR 10

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 I~: ,"*" ,,

~'! .~"~~J* \: . -:~VB:

c:>ep111:4,(%ffl):. *. *

  • ,*..;_*s~:~:*:

__ ,. .Row **-Col . ,,_*No.***

ETSS.; 9604 t ..:~ *

-  : ~*

. ' . ~<~- ' ' ,,, ,; ' ! *,  :: . ': '  ;:.'*:> .;.. ,::2012 ,:, '20f5.

~ ' ~'

SGC 33 68 AV1 18 20 SGC 33 68 AV2 20 19 SGC 33 69 AV1 10 9 SGC. 33 69 AV2 13 11 SGC 33 70 AV1 10 8 SGC 33 70 AV3 16 16 SGC 34 29 AV3 11 12 SGC 34 29 AV4 17 16 SGC 34 79 AV1 8 11 SGC 35 77 AV2 10 11 SGC 35 77 AV3 10 10 SGC 37 63 AV2 13 11 SGC 37 73 AV3 15 17

-ii , ..

~

.,~

.[.,

SGC 37 75 AV3 12 11 ....  :;.

':~i .. :;;,;

  • SGC. 38 28 AV1 10 7 ('.

-r;- ~-=J~~

SGC 38 28 AV3 17 14 ~~

SGC 38 30 AV2 12 13

~'

SGC 38 43 AV3 15 11

,~Hr'.~

SGC *38 73 AV1 11 9 --Y.;,.:-,  ::~:~

SGC 38 73 AV2 9 8* ....... -~--r:_

  • -11.

SGC 38 74 AV2 8 8 .,

SGC 39 50 AV3 14 13 SGC 39 ' 53 AV3 30 28 SGC 39 55 AV3 27 25 SGC 39 55 AV3 18 12 SGC ' 39 55 AV4 26 25 SGC 39 71 AV3 12 8 SGC 39 72 AV4 5 10 SGC 40 33 AV2 23 24 SGC 40 33 AV3 23 25 SGC 40 63 AV2 9 9 SGC 40 63 AV3 19 15 SGC 40 63 AV4 19 16

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14 Depth (% TW) .

    • s8 Row Col .* AVB ' E:TSS 96041.1
  • No.

' ' . 201'2 2015 SGC 41 35 AV3 NR 11 SGC 41 64 AV1 11 9 SGC 41 . 66 AV3 12 14 SGC 41 68 AV4 10 10 SGC 43 39 AV2 16 13 SGC 43 61 AV1 25 22 SGC 43 63 AV1 14 15 SGC 44 61 AV1 11 10 SGC 45 58 AV3 NR 13 SGC 46 45 AV2 8 11 SGC 46 45 AV3 NR 10 SGC 46 46 AV1 NR 10

.)~1 SGC 46 46 AV2 NR 12

' ~,;:;'.. l.'.\

SGC 46 46 AV3 NR 13

':.bi ',c-113; SGC 46 46 AV4 NR 10 ,,

c;:

NR = Not Reported du!"ing the previous outage

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Table 5 - Summary of Non-AVB Volumetric Degradation Identified

. . .* .. .* '" k .

M~Depth Initially Signal Present prior to

. . *

  • Foreign ...

SG Row Col Location ETSS Cause Object Plugged?

~

.. I*, .'

{f,oTW) Repor;ted

  • ,, Current Outage?

.. Remaining?

Yes. No signal change Foreign TSC+0.82 27901.1 20%TW 2015 No No since 1995. Object A 4 37 Yes. No signal change Foreign TSC+1.81 27901.1 27%TW 2015 No No since 1995. Object Yes. No signal A 6 60 5H-0.59 96910.1 13%TW 2009 TSP Wear N/A No change since 2002.

Yes. No signal Foreign A 11 45 TSH+0.96 27901.1 27%TW 2012 No No change since 2006. Object No signal present Foreign A 15 16 TSH+0.23 27901.1 25%TW 2012 No No in 2006 exam. Object Yes. No signal Foreign A 17 16 TSH+0.04 27901.1 31 %TW 2002 No No change. Object Yes. No signal Foreign A 18 16 TSH+0.02 27901.1 30%TW 2002 No ~No change. Object Yes. No signal Foreign A 32 27 TSC+0.02 27901.1 20%TW 2006 No No change. Object Yes. No signal Foreign A 33 27 TSC+0.12 27901.1 25%TW 2006 No No change. Object Yes. No signal Foreign A 39 24 TSH+0.45 27901.1 20%TW 2009 No No change since 2006. Object Yes. No signal change Foreign A 42 52 TSC+0.26 27901.1 20%TW 2009 No No since 2009. Object Yes. No signal Foreign A 43 61 BPH+0.56 27901.1 23%TW 2009 No No change since 2002. Object

.. Yes. Possible minor Foreign A 43 64 BPH+0.62 27901.1 '24%TW 2009 sigriai'\;iiange 2002 to No No Object 2009. No change since.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 1.1 ' For~ign

'*Max Depth Initially*** 'Signal* Pres~nf Prior to ,, , ,,.

SG Row Col Location ETSS Cause Object Plugged?

(%TW) , Reporte~ ci:rrent Outage?.

'; ~

. R~maining? ..

3C+0.47 96910.1 4%TW 2011 Yes, in TSP c 3 72 1996 bobbin data. N/A No Wear 3C+0.48 96910.1 2%TW 2011 No RPC.

Yes. No change since Foreign c 28 22 TSH+0.17 27901.1 29%TW 2014 No No initial detection. Object Yes. No change since Foreign TSH+0.52 27901.1 29%TW 2014 No No initial detection. Object c 28 23 Yes. No change since Foreign TSH+0.21 27901.1 29%TW 2014 No No initial detection. Object Yes. No signal Foreign c 28 71 TSH+0.27 27901.1 24%TW 2009 No No change since 1996. Object Yes, based on lookup. TSP c 28 84 03H+0.50 96910.1 5%TW 2014 Unchanged since 1996. Wear N/A No Yes. Present in 2014 Foreign c 30 48 BPH+0.58 27901.1 20%TW 2015 X-Probe data with no Object No No change.

Yes, based on lookup. Foreign c 30 74 TSH+6.47 27901.1 20%TW 2014 No No Unchanged since 1996. Object Yes. No signal Foreign c 32 36 BPH+0.58 27901.1 19%TW 2009 change. Object No No Yes. No signal Foreign c 33 17 TSH+2.69 27901.1 20%TW 2005 change. Object No No Yes. No signal Foreign c 34 18 TSH+0.97 27901.1 22%TW 2005 change. Object No No Yes. No signal Foreign c 34 20 TSH+0.91 27901.1 25%TW 2005 change. Object No No Yes. No signal Foreign c 34 74 TSH+0.06 27901.1 27%TW 2005 change. Object No No

' ~ .. *. '<yej'~<< No signal Foreign c 35 19 TSH+0.32 27901.1 29%TW 2005 change. Object No No

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14

" *,Max Depth I* Initially' Signal Present P.rior.,to

  • t=or~ign

.SG Row Col l.,ocation, 'ErSS Cause Object Plugged?

(%TW) k Reportecl * 'Current Outage?

Re1J1aining?

Yes. No signal Foreign c 35 22 TSH+1.03 27901.1 29%1W 2005 change. Object No No Foreign c 35 30 TSH+0.11 27901.1 35%TW 2005 Yes. No signal change.

Object No No Yes. No change since Foreign c 36 32 BPH+0.55 27901.1 21 %1W 2015 2008. Object No No Yes. No signal Foreign c 36 68 TSH+0.17 27902.1 26%1W 2005 change. Object No No Yes, in 1996 3-coil data. Foreign c 37 31 TSH+0.09 27901.1 26%1W 2011 No change. Object No No Yes, in 2005 +Point' Foreign c 37 32 TSH+0.02 27901.1 23%1W 2011 data. No change. Object No No Yes, in 1996 3-coil data. Foreign c 37 33 TSH+0.04 27901.1 26%1W 2011 No change. Object No No Yes. No signal Foreign c 37 34 TSH-0.06 27901.1 26%1W 2009 change since 1996. Object No No Yes. No signal Foreign c 37 35 BPH+0.60 27901.1 33%1W 2005 change. Object No No Yes. No signal Foreign c 37 54 TSH+0.12 27901.1 24%1W 2005 change. Object No No 7C-0.48 96910.1 13%1W 2005 Yes. No change since TSP c 37 73 initial detection. Wear N/A No 7C-0.52 96910.1 6%1W 2011 Yes, present in 2005 Foreign c 38 32 BPH+0.60 27901.1 26%1W 2011 bobbin data. No RPC. Object No No Yes. No signal Foreign c 38 53 TSH+0.08 27901.1 22%1W 2005 change. Object No No BPH+0.61 27901.1 22%1W 2011 No No

..,* ":-* Yes,:*1:i'resent in 2005 Foreign c 39 32 bobbin data. No RPC. Object BPH+0.60 27901.1 24%1W 2011 No No

. \'*,  ?~ ;_; . '. (;:,. '* ,~ . . . ,-

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 SG

' Row*.i* Co(

Locatio*n ETSS Maxbepth* *Initially . ~ignat. Present Prior to' ' ,- "'

Cause.

Foreign Object Plugged?

(%TW) .Reported Current Outage? .

  • ,* ' ~ .. '**'* . ' i* . . '

.. Remaining?

Yes, present in 2005 Foreign c 39 34 BPH+0.57 27901.1 24%TW 2011 bobbin data. No RPC. Object No No Yes, present in 2005 Foreign c 40 34 BPH+0.60 27901.1 22%TW 2011 bobbin data. No RPC. Object No No Yes. No signal Foreign c 44 42 TSH+0.12 27901.1 24%TW 2005 change. Object No No Yes. No signal Foreign c 44 43 TSH+0.19 27901.1 26%TW 2005 change. Object No No Yes. No signal Foreign c 44 47 TSH+0.06 27901.1 26%TW 2005 change. Object No No Yes. Present in 2014 c 44 60 BPH+0.17 96910.1 7%1W 2015 bobbin data with no TSP Wear N/A No change.

Present in 2005 +Point' Foreign c 45 42 TSH+0.26 27901.1 19%TW 2015 data with no change. Object No No TSH+0.23 27901.1 23%TW Yes. No signal Foreign c 45 43 TSH+0.24 27901.1 24%TW 2005 change. Object No No TSH+0.72 27901.1 20%TW Yes. No signal Foreign c 45 47 TSH+0.17 27901.1 23%TW 2005 change. Object No No

  • .*. ~ '*
  • l'i' ..

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14

e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation. The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times.

Table 6 - Circumferential PWSCC Indications

.+PointtM '
  • Max '* Arc:

SG*,'.* Row *C.ol 'Ind* ' 1l.ocatfon * ,*' >* Volts.

>*' ,, '* .:J'

~ ,:*.DE{~th'1** 1;:*t0r. 9 tt\ *:

1

~

PD'1\,

(

SGC 6 41 SCI TEH +18.25" 0.88 65%TW 85° 15 SGC 7 46 SCI TEH +15.56" 0.78 50%TW 78° 11 SGC 27 65 SCI TEH +16.04" 1.30 60%TW 99° 17

f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator. ., * },

Table 7 provides the plugging totals and percentages to date.

Table 7 - Tube Plugging Summary

.Tube's Plugged, :., *

  • . To Date* .* ,. ~

SGA 3,342 30 (0.9%)

SG B 3,342 19 (0.6%)

SGC 3,342 50 (1.5%)

Total 10,026 99 (1.0%)

g. The results of condition monitoring, including the results of tube pulls and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity. Further, the results from the current outage inspection validate prior outage operational assessment assumptions. Tube pulls and in-situ pressure testing were not required during the current outage.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14

h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.

During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG.

i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from other~.sources is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from belo~(the H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident. *
j. The results of the monitoring for tube axial displacement (slippage). If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
    • ~!.

No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data 'j

  • from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 20~ 5 r- * 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were

. identified) and will again be screened during the Spring 2017 RFO.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14 Acronyms AVB Anti-Vibration Bar BPC Baffle Plate Cold BPH Baffle Plate Hot C/l Cold Lea ECT Eddy Current Testina EFPM Effective Full Power Month ETSS Eddy Current Technical Specification Sheets FOSAR Foreiqn Obiect Search and Retrieval GPD Gallons Per Dav H/L Hot Lea MRPC Motorized Rotatina Pancake Coil NSAL Nuclear Safetv Advisory Letter NTE No tube Exoansion OD Outer Diameter ODSCC Outside Diameter Stress Corrosion Crackinq OVR Over Roll OXP Over Expansion PARC Permanent Alternate Reoair Criteria PLP Possible Loose Part PWSCC Primary Water Stress Corrosion Crackina  ?:.~

SC! Single Circumferential Indication

SG Steam Generator SSC Stress Corrosion Crackina TEC Tube End Cold-lea TEH Tube End Hot-lea TSC Top of Tube Sheet Cold-lea TSH Top of Tube Sheet Hot-leq TSP Tube Support Plate TTS Top of Tube&heet TW Throuqh Wall

VIRGINIA ELECTRIC AND POWER COMPANY RICHMOND, VIRGINIA 23261 May 10, 2016 United States Nuclear Regulatory Commission Serial No.16-196 Attention: Document Control Desk SPS-LIC/CGL RO Washington, DC 20555-0001 Docket No. 50-281

If you have any questions concerning this information, please contact Mrs. Candee G. Lovett at (757) 365-2178.

Douglas Lawrence Director S ation Safety & Licensing Surry Power Station

Attachment:

Surry Unit 2 Steam Generator Tube Inspection Report for the Fall 2015 Refueling Outage Commitments made in this letter: None

Serial No.: 16-196 Docket No.: 50-281 Page 2 of 2 cc: U.S. Nuclear Regulatory Commission Region II Marquis One Tower 245 Peachtree Center Avenue NE Suite 1200 Atlanta, Georgia 30303-1257 Ms. K. R. Cotton Gross NRC Project Manager- Surry U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 Dr. V. Sreenivas NRC Project Manager - North Anna U.S. Nuclear Regulatory Commission One White Flint North Mail Stop 08 G-9A 11555 Rockville Pike Rockville, Maryland 20852-2738 NRC Senior Resident Inspector Surry Power Station Mr. R. A. Smith Authorized Nuclear Inspector Surry Power Station

Serial No.: 16-196 Docket No.: 50-281 ATTACHMENT 1 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE VIRGINIA ELECTRIC AND POWER COMAPNY (DOMINION)

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 1 of 14 SURRY UNIT 2 STEAM GENERATOR TUBE INSPECTION REPORT FOR THE FALL 2015 REFUELING OUTAGE The following satisfies the Surry Power Station Technical Specification (TS) reporting

  • requirement section 6.6.A.3 .. During the Surry Unit 2 Fall 2015 refueling outage (RFO), steam generator (SG) inspections in accordance with TS 6.4.Q were completed for SG A and SG C.

This was the third inspection in the 4th inspection period which has a duration of 72 effective full power months (EFPM).

Surry Unit 2 exceeded 200°F on November 28, 2015; therefore, this report is required to be submitted by May 26, 2016. At the time of this inspection, the Unit 2 SGs had operated for 333.0 EFPM since the first inservice inspection.

In the discussion below bold italicized wording represents TS verbiage and the required

. information is provided directly below each reporting requirement. A list of acronyms is attac;;hed at the end of this report. "

A report shall be submitted Within 180 days after Tavg exceeds -~JJ0 9F: following completion of an inspection performed in accordance with the Specification 6.4.Q, "Steam Generator (SG)Program. 11 The report shall include:

a. The scope of inspections performed on each SG Primary Side A summary of the eddy current tube examinations performed during the outage is RfOY,id~d in ~

,}

Table 1.

  • The only scope expansions required in SG A and SG C were those ne.ce§sary. to bound foreign objects and foreign object related degradation, *as well as to resolve ;;:imbig1,.1ous indications. The inspection scope. was expanded into SG B based on the findil'.lg of circumferential primary water stress corrosion cracking (PWSCC) within the-hot leg tubesheet of SG C (see item e below for more detail). The eddy current scope in SG B was focused on the detection of stress corrosion cracking (SCC) in susceptible locations in the hot leg tubesheet; therefore, a 50% sample of the hot leg tubesheet locations with array probes was examined.

No bobbin inspections or cold leg tubesheet inspections were performed.

The primary side work scope also included as-found and as-left visual examinations in the hot

  • and cold leg primary side channel heads in SGs A, B, and C. The examination included the divider plate, welds, cladding, the "mouse-hole" region per NSAL-12-1, previously installed plugs, and manway flanges. No abnormal or degraded conditions were identified from these examinations.

Serial No. : 16-196 Docket No.: 50-281 Attachment 1 Page 2 of 14 Secondary Side During the Surry Unit 2 Fall 2015 RFO, a visual inspection of upper steam drum moisture separator components, feedring components , and top of bundle U-bend region components through the secondary manway in SG A was performed. This included all accessible steam drum components and structures, including the feedring exterior, the upper tube bundle, and ?'h tube support plate (TSP) via probe insertions through the primary moisture separators. No degradation or adverse conditions were noted during these inspections. Sludge lancing was performed in all three SGs . Foreign Object Search and Retrieval (FOSAR) examinations were performed in SGs A, B, and C at the top of the tubesheet, in the annulus, and in the no-tube lane as necessary.

Table 1 - Eddy Current Testing Examination Scope SG Scope Description Extent SGA SGC B

Bobbin Coil Exams Full Length TEHTEC 2849 2831 H/L CandyCane (Row 3-5) 07CTEH 278 282 H/L Straight (R 1-2) 07HTEH 185 182 H/L Straiqht Restricted 07HTEH 1 C/L CandyCane Restricted 02HTEC 1 C/L Straight Restricted 07CTEC 1 2 C/L Straight (R1-5) 07CTEC 462 463 Array Exams H/L TSH Array (Non-Baffle Plate) TSH01H 834 444 843 H/L TSH Array (Baffle Plate) TSHBPH 2478 1260 2453 C/L TSC Array (Non-Baffle Plate) TSC01C 834 842 C/L TSC Array (Baffle Plate) TSCBPC 2478 2453 MRPC Exams Ubend +Point' (Row 1-2) 07H07C 185 182 MRPC Special Interest H/L Previous Indications Various 120 172 H/L Previous Restricted 02H03 1 C/L Previous Restricted Various 8 H/L Current Indications Various 97 7 92 Ubend Current Indications Various 2 1 C/L Previous Indications Various 8 7 C/L Current Indications Various 36 20 Indications For Mag8ias Probe Various 1 2 Additional RPC TEHTSH 2 Total 10848 1713 10838

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 3 of 14

b. Degradation mechanisms found Degradation mechanisms targeted by the inspection plan included anti-vibration bar (AVB) wear, pitting, foreign object wear, tube support wear and sec at various locations within the steam generator tube bundle. AVB wear, foreign object wear, tube support plate wear, and PWSCC were detected during the current outage.
c. Nondestructive examination techniques utilized for each degradation mechanism The inspection program focused on the degradation mechanisms listed in Table 2 and utilized the referenced eddy current techniques.

Table 2 - Inspection Method for Applicable Degradation Modes

' *Degradation Classification.'  : Mechanism, ..

  • Loi;ation .Probe

. Type..

'" ~',, ,,:.' "*-'

Existing Tube Wear Anti-Vibration Bars Bobbin - Detection and Sizing Bobbin and +Point'- Detection Existing OD Pitting Top-of-Tubesheet

+Point' - Sizing Bobbin - Detection Existing Tube Wear Tube Support Plate

+Point' - Sizing Tube Wear Bobbin and +Point' - Detection Existing Freespan and TIS (foreign objects) +Point' - Sizing ODSCC Potential Hot Leg Top-of-Tubesheet +Point' - Detection and Sizing PWSCC Potential PWSCC Tube Ends NIA*

Bobbin - Detection Potential Tube Wear Flow Distribution Baffle

+Point' - Sizing Bulges, Dents, Manufacturing ODSCC Anomalies, and Above-Potential +Point' - Detection and Sizing PWSCC Tubesheet Overexpansions (OVR)

Tubesheet Crevice in Potential ODSCC +Point' - Detection and Sizing Tubes With NTEs Potential Tube Slippage Within Tubesheet Bobbin Detection Tubesheet Potential PWSCC +Point' - Detection and Sizing Overexpansions (OXP)

ODSCC Potential Row 1 and 2 Li-bends +Point' - Detection and Sizing PWSCC Bobbin - Detection Potential ODS CC Freespan and Tube Supports

+Point' - Sizing

  • Inspection not required per technical specification alternate repair criteria.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 4of14

d. Location, orientation (if linear}, and measured sizes (if available) of service induced indications As stated in item b above, service* induced indications were identified. Tables 3 through 6 provide information regarding these indications.

Table 3 -AVB Indications for SG A SGA 25 57 AV2 16 21 26 ' I "

SGA 9 AV4 12 10 SGA 26 86 ' AV3 17 21 SGA 29 28 AV3 NR 13 SGA 29 70 AV2 11 11 SGA 30 12 AV1 10 10 ~--

,,;:- ... ~

$GA 30 64 AV2 7 8 -~v SGA 33 26 AV4 NR 12 SGA 36 62 AV2 24* 21 I SGA 36 62 AV3 14 16 SGA 36 62 AV4 27 31 SGA 36 66 AV2 12 16 I -~--

SGA 36 66 ' AV3 " 10 13 i *'

SGA 37 20 AV1 13 12 .. ~. -~,:

SGA 37 20 AV4 12 10 SGA 38 57. AV1 13 13 SGA 38 70 AV3 NR 11 SGA 38 72 AV4 23 26 SGA 38 74 AV4 17 22 SGA 40 25 AV4 12 8.

SGA 40 49 AV1 11 15 SGA 40 49 AV2 10 10 SGA 40 49 AV3 11 11 SGA 40 65 AV2 18 21 SGA 40 65 AV3 10 15 SGA 40 65 AV4 10 9 SGA 40 66 AV3. 9 14

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 5 of 14

-*-b*.eP.':*

'/i:

  • tlli (°AT\IW o* .... *:******

'* ETSS '96041':1

,.-~

*;)2012
~: .
  • 201,:s .

SGA 42 62 AV3 NR 10 SGA 44 35 AV1 NR 10 SGA 44 38 AV2 11 9 SGA 45 44 AV2 11 11 SGA 46 45 AV1 13 10 NR =Not Reported during the previous outage Table 4 -AVB Indications for SG C

):*::..... {~ii j-r**"' .,,

- ,.SG.- .

~'"~~"'"' ~ J,

'-'!;'~:,"':: ;

L

~xva~

  • r'*.~~bepM; (% TW).*. ***

.: ETSs,' 96041'..:l

'\**;<<.*' "-,~:.*,

~ "'~ '~1 '~ '

Row

.;~

Col

'>~:~\:;._

_,._-No.

' ' ' ~~~~A' ~-t ~":*201.2.,~:- . 20tf5'; .

T J~~

~1;,:

SGC 24' 8 AV4 9 10 SGC 25 9 AV1 8 8

.... -~

SGC 25 9 AV3 11 10 ~ ~

SGC 25 27 AV1 18 17 SGC . 25 27 AV2 32 32

  • ~

SGC 25 27 AV3 13 12  :.,---

~~:*

SGC 25 29 AV2 12 8

- SGC 25 29 AV3 26 20 SGC 26 26 AV3 17 19 SGC 26 26 AV4 17 - 17 SGC 26 39 AV3 20 15 SGC 27 84 AV4 11 7 SGC 31 65 AV2 17 13 SGC 31 69 AV2 26 19 SGC 31 69 AV3 20 17 SGC 31 75 AV3 11 13 SGC 31 75 AV4 16 13 SGC 33 59 AV3 21 19 SGC 33 59 AV4 11 12 SGC 33 67 AV3 NR 10

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 6of14 I~: ,"*" ,,

~'! .~"~~J* \: . -:~VB:

c:>ep111:4,(%ffl):. *. *

  • ,*..;_*s~:~:*:

__ ,. .Row **-Col . ,,_*No.***

ETSS.; 9604 t ..:~ *

-  : ~*

. ' . ~<~- ' ' ,,, ,; ' ! *,  :: . ': '  ;:.'*:> .;.. ,::2012 ,:, '20f5.

~ ' ~'

SGC 33 68 AV1 18 20 SGC 33 68 AV2 20 19 SGC 33 69 AV1 10 9 SGC. 33 69 AV2 13 11 SGC 33 70 AV1 10 8 SGC 33 70 AV3 16 16 SGC 34 29 AV3 11 12 SGC 34 29 AV4 17 16 SGC 34 79 AV1 8 11 SGC 35 77 AV2 10 11 SGC 35 77 AV3 10 10 SGC 37 63 AV2 13 11 SGC 37 73 AV3 15 17

-ii , ..

~

.,~

.[.,

SGC 37 75 AV3 12 11 ....  :;.

':~i .. :;;,;

  • SGC. 38 28 AV1 10 7 ('.

-r;- ~-=J~~

SGC 38 28 AV3 17 14 ~~

SGC 38 30 AV2 12 13

~'

SGC 38 43 AV3 15 11

,~Hr'.~

SGC *38 73 AV1 11 9 --Y.;,.:-,  ::~:~

SGC 38 73 AV2 9 8* ....... -~--r:_

  • -11.

SGC 38 74 AV2 8 8 .,

SGC 39 50 AV3 14 13 SGC 39 ' 53 AV3 30 28 SGC 39 55 AV3 27 25 SGC 39 55 AV3 18 12 SGC ' 39 55 AV4 26 25 SGC 39 71 AV3 12 8 SGC 39 72 AV4 5 10 SGC 40 33 AV2 23 24 SGC 40 33 AV3 23 25 SGC 40 63 AV2 9 9 SGC 40 63 AV3 19 15 SGC 40 63 AV4 19 16

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 7 of 14 Depth (% TW) .

    • s8 Row Col .* AVB ' E:TSS 96041.1
  • No.

' ' . 201'2 2015 SGC 41 35 AV3 NR 11 SGC 41 64 AV1 11 9 SGC 41 . 66 AV3 12 14 SGC 41 68 AV4 10 10 SGC 43 39 AV2 16 13 SGC 43 61 AV1 25 22 SGC 43 63 AV1 14 15 SGC 44 61 AV1 11 10 SGC 45 58 AV3 NR 13 SGC 46 45 AV2 8 11 SGC 46 45 AV3 NR 10 SGC 46 46 AV1 NR 10

.)~1 SGC 46 46 AV2 NR 12

' ~,;:;'.. l.'.\

SGC 46 46 AV3 NR 13

':.bi ',c-113; SGC 46 46 AV4 NR 10 ,,

c;:

NR = Not Reported du!"ing the previous outage

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 8of14 Table 5 - Summary of Non-AVB Volumetric Degradation Identified

. . .* .. .* '" k .

M~Depth Initially Signal Present prior to

. . *

  • Foreign ...

SG Row Col Location ETSS Cause Object Plugged?

~

.. I*, .'

{f,oTW) Repor;ted

  • ,, Current Outage?

.. Remaining?

Yes. No signal change Foreign TSC+0.82 27901.1 20%TW 2015 No No since 1995. Object A 4 37 Yes. No signal change Foreign TSC+1.81 27901.1 27%TW 2015 No No since 1995. Object Yes. No signal A 6 60 5H-0.59 96910.1 13%TW 2009 TSP Wear N/A No change since 2002.

Yes. No signal Foreign A 11 45 TSH+0.96 27901.1 27%TW 2012 No No change since 2006. Object No signal present Foreign A 15 16 TSH+0.23 27901.1 25%TW 2012 No No in 2006 exam. Object Yes. No signal Foreign A 17 16 TSH+0.04 27901.1 31 %TW 2002 No No change. Object Yes. No signal Foreign A 18 16 TSH+0.02 27901.1 30%TW 2002 No ~No change. Object Yes. No signal Foreign A 32 27 TSC+0.02 27901.1 20%TW 2006 No No change. Object Yes. No signal Foreign A 33 27 TSC+0.12 27901.1 25%TW 2006 No No change. Object Yes. No signal Foreign A 39 24 TSH+0.45 27901.1 20%TW 2009 No No change since 2006. Object Yes. No signal change Foreign A 42 52 TSC+0.26 27901.1 20%TW 2009 No No since 2009. Object Yes. No signal Foreign A 43 61 BPH+0.56 27901.1 23%TW 2009 No No change since 2002. Object

.. Yes. Possible minor Foreign A 43 64 BPH+0.62 27901.1 '24%TW 2009 sigriai'\;iiange 2002 to No No Object 2009. No change since.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 9 of 14 1.1 ' For~ign

'*Max Depth Initially*** 'Signal* Pres~nf Prior to ,, , ,,.

SG Row Col Location ETSS Cause Object Plugged?

(%TW) , Reporte~ ci:rrent Outage?.

'; ~

. R~maining? ..

3C+0.47 96910.1 4%TW 2011 Yes, in TSP c 3 72 1996 bobbin data. N/A No Wear 3C+0.48 96910.1 2%TW 2011 No RPC.

Yes. No change since Foreign c 28 22 TSH+0.17 27901.1 29%TW 2014 No No initial detection. Object Yes. No change since Foreign TSH+0.52 27901.1 29%TW 2014 No No initial detection. Object c 28 23 Yes. No change since Foreign TSH+0.21 27901.1 29%TW 2014 No No initial detection. Object Yes. No signal Foreign c 28 71 TSH+0.27 27901.1 24%TW 2009 No No change since 1996. Object Yes, based on lookup. TSP c 28 84 03H+0.50 96910.1 5%TW 2014 Unchanged since 1996. Wear N/A No Yes. Present in 2014 Foreign c 30 48 BPH+0.58 27901.1 20%TW 2015 X-Probe data with no Object No No change.

Yes, based on lookup. Foreign c 30 74 TSH+6.47 27901.1 20%TW 2014 No No Unchanged since 1996. Object Yes. No signal Foreign c 32 36 BPH+0.58 27901.1 19%TW 2009 change. Object No No Yes. No signal Foreign c 33 17 TSH+2.69 27901.1 20%TW 2005 change. Object No No Yes. No signal Foreign c 34 18 TSH+0.97 27901.1 22%TW 2005 change. Object No No Yes. No signal Foreign c 34 20 TSH+0.91 27901.1 25%TW 2005 change. Object No No Yes. No signal Foreign c 34 74 TSH+0.06 27901.1 27%TW 2005 change. Object No No

' ~ .. *. '<yej'~<< No signal Foreign c 35 19 TSH+0.32 27901.1 29%TW 2005 change. Object No No

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 10 of 14

" *,Max Depth I* Initially' Signal Present P.rior.,to

  • t=or~ign

.SG Row Col l.,ocation, 'ErSS Cause Object Plugged?

(%TW) k Reportecl * 'Current Outage?

Re1J1aining?

Yes. No signal Foreign c 35 22 TSH+1.03 27901.1 29%1W 2005 change. Object No No Foreign c 35 30 TSH+0.11 27901.1 35%TW 2005 Yes. No signal change.

Object No No Yes. No change since Foreign c 36 32 BPH+0.55 27901.1 21 %1W 2015 2008. Object No No Yes. No signal Foreign c 36 68 TSH+0.17 27902.1 26%1W 2005 change. Object No No Yes, in 1996 3-coil data. Foreign c 37 31 TSH+0.09 27901.1 26%1W 2011 No change. Object No No Yes, in 2005 +Point' Foreign c 37 32 TSH+0.02 27901.1 23%1W 2011 data. No change. Object No No Yes, in 1996 3-coil data. Foreign c 37 33 TSH+0.04 27901.1 26%1W 2011 No change. Object No No Yes. No signal Foreign c 37 34 TSH-0.06 27901.1 26%1W 2009 change since 1996. Object No No Yes. No signal Foreign c 37 35 BPH+0.60 27901.1 33%1W 2005 change. Object No No Yes. No signal Foreign c 37 54 TSH+0.12 27901.1 24%1W 2005 change. Object No No 7C-0.48 96910.1 13%1W 2005 Yes. No change since TSP c 37 73 initial detection. Wear N/A No 7C-0.52 96910.1 6%1W 2011 Yes, present in 2005 Foreign c 38 32 BPH+0.60 27901.1 26%1W 2011 bobbin data. No RPC. Object No No Yes. No signal Foreign c 38 53 TSH+0.08 27901.1 22%1W 2005 change. Object No No BPH+0.61 27901.1 22%1W 2011 No No

..,* ":-* Yes,:*1:i'resent in 2005 Foreign c 39 32 bobbin data. No RPC. Object BPH+0.60 27901.1 24%1W 2011 No No

. \'*,  ?~ ;_; . '. (;:,. '* ,~ . . . ,-

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 11of14 SG

' Row*.i* Co(

Locatio*n ETSS Maxbepth* *Initially . ~ignat. Present Prior to' ' ,- "'

Cause.

Foreign Object Plugged?

(%TW) .Reported Current Outage? .

  • ,* ' ~ .. '**'* . ' i* . . '

.. Remaining?

Yes, present in 2005 Foreign c 39 34 BPH+0.57 27901.1 24%TW 2011 bobbin data. No RPC. Object No No Yes, present in 2005 Foreign c 40 34 BPH+0.60 27901.1 22%TW 2011 bobbin data. No RPC. Object No No Yes. No signal Foreign c 44 42 TSH+0.12 27901.1 24%TW 2005 change. Object No No Yes. No signal Foreign c 44 43 TSH+0.19 27901.1 26%TW 2005 change. Object No No Yes. No signal Foreign c 44 47 TSH+0.06 27901.1 26%TW 2005 change. Object No No Yes. Present in 2014 c 44 60 BPH+0.17 96910.1 7%1W 2015 bobbin data with no TSP Wear N/A No change.

Present in 2005 +Point' Foreign c 45 42 TSH+0.26 27901.1 19%TW 2015 data with no change. Object No No TSH+0.23 27901.1 23%TW Yes. No signal Foreign c 45 43 TSH+0.24 27901.1 24%TW 2005 change. Object No No TSH+0.72 27901.1 20%TW Yes. No signal Foreign c 45 47 TSH+0.17 27901.1 23%TW 2005 change. Object No No

  • .*. ~ '*
  • l'i' ..

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 12 of 14

e. Number of tubes plugged during the inspection outage for each degradation mechanism Three tubes (see Table 6) required plugging as a result of circumferential cracks from PWSCC which was identified during the Fall 2015 RFO. One additional tube (SG C R20 C62) was preventatively plugged. This tube was inspected full length and determined to have no degradation. The tube was plugged because the tube is dented at the th TSP making it difficult to inspect without examining the tube several times.

Table 6 - Circumferential PWSCC Indications

.+PointtM '
  • Max '* Arc:

SG*,'.* Row *C.ol 'Ind* ' 1l.ocatfon * ,*' >* Volts.

>*' ,, '* .:J'

~ ,:*.DE{~th'1** 1;:*t0r. 9 tt\ *:

1

~

PD'1\,

(

SGC 6 41 SCI TEH +18.25" 0.88 65%TW 85° 15 SGC 7 46 SCI TEH +15.56" 0.78 50%TW 78° 11 SGC 27 65 SCI TEH +16.04" 1.30 60%TW 99° 17

f. The number and percentage of tubes plugged to date, and the effective plugging p,ercentage in each steam generator. ., * },

Table 7 provides the plugging totals and percentages to date.

Table 7 - Tube Plugging Summary

.Tube's Plugged, :., *

  • . To Date* .* ,. ~

SGA 3,342 30 (0.9%)

SG B 3,342 19 (0.6%)

SGC 3,342 50 (1.5%)

Total 10,026 99 (1.0%)

g. The results of condition monitoring, including the results of tube pulls and in-situ testing Based on the results of the primary and secondary side inspections performed during this outage, all degradation identified during the Fall 2015 inspection satisfied condition monitoring requirements for SG tube structural and leakage integrity. Further, the results from the current outage inspection validate prior outage operational assessment assumptions. Tube pulls and in-situ pressure testing were not required during the current outage.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 13of14

h. The primary to secondary LEAKAGE rate observed in each SG (if it is not practical to assign the LEAKAGE to an individual SG, the entire primary to secondary LEAKAGE should be conservatively assumed to_be from one SG) during the cycle preceding the inspection which is the subject of the report, Routine primary-to-secondary leak monitoring is conducted in accordance with station procedures.

During the cycle preceding the Fall 2015 RFO, no measurable primary-to-secondary leakage (i.e., >1 GPO) was observed in any Unit 2 SG.

i. The calculated accident induced LEAKAGE rate from the portion of the tubes below 17.89 inches from the top of the tubesheet for the most limiting accident in the most limiting SG. In addition, if the calculated accident induced LEAKAGE rate from the most limiting accident is less than 1.80 times the maximum operational primary to secondary LEAKAGE rate, the report should describe how it was determined, The permanent alternate repair criteria (PARC) requires that the component of operational leakage from the prior cycle from below the H-star distance be multiplied by a factor of 1.8 and added to the total accident leakage from any other source, and compared to the allowable accident induced leakage limit. Since there is reasonable assurance that no tube degradation identified during this outage would have resulted in leakage during an accident, the contribution to accident leakage from other~.sources is zero. Assuming that the prior cycle operational leakage of <1 GPO originated from belo~(the H-star distance, and multiplying this leakage by a factor of 1.8 as required by the PARC, yields a*ii accident induced leakage value of <1.8 GPO. This value is well below the 470 GPO limit for.the limiting SG and provides reasonable assurance that the accident induced leakage performance criteria would not have been exceeded during a limiting design basis accident. *
j. The results of the monitoring for tube axial displacement (slippage). If slippage is discovered, the implications of the discovery and corrective action shall b.e provided.
    • ~!.

No indications of tube slippage were identified during the evaluation of bobbin probe examjpation data 'j

  • from SGs A or C. Note that no bobbin probe examinations were performed in SG B during tf.ie Fall 20~ 5 r- * 'y RFO. All tubes in SG B were screened for slippage during the Spring 2014 (no indications were

. identified) and will again be screened during the Spring 2017 RFO.

Serial No.: 16-196 Docket No.: 50-281 Attachment 1 Page 14 of 14 Acronyms AVB Anti-Vibration Bar BPC Baffle Plate Cold BPH Baffle Plate Hot C/l Cold Lea ECT Eddy Current Testina EFPM Effective Full Power Month ETSS Eddy Current Technical Specification Sheets FOSAR Foreiqn Obiect Search and Retrieval GPD Gallons Per Dav H/L Hot Lea MRPC Motorized Rotatina Pancake Coil NSAL Nuclear Safetv Advisory Letter NTE No tube Exoansion OD Outer Diameter ODSCC Outside Diameter Stress Corrosion Crackinq OVR Over Roll OXP Over Expansion PARC Permanent Alternate Reoair Criteria PLP Possible Loose Part PWSCC Primary Water Stress Corrosion Crackina  ?:.~

SC! Single Circumferential Indication

SG Steam Generator SSC Stress Corrosion Crackina TEC Tube End Cold-lea TEH Tube End Hot-lea TSC Top of Tube Sheet Cold-lea TSH Top of Tube Sheet Hot-leq TSP Tube Support Plate TTS Top of Tube&heet TW Throuqh Wall