ML19317G281: Difference between revisions
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Oi ' | Oi ' | ||
: u. s. =ves.s An ascutArony commissiers | : u. s. =ves.s An ascutArony commissiers | ||
# sac acau aos | # sac acau aos LICENSEE EVENT REPORT EXHl8IT A | ||
LICENSEE EVENT REPORT EXHl8IT A | |||
! cominos stocc: I, i 1 I I I l@ , | ! cominos stocc: I, i 1 I I I l@ , | ||
cettAsa per on Tves ALL stouinao imponatArnous ._.. . _ | cettAsa per on Tves ALL stouinao imponatArnous ._.. . _ | ||
r.o'Til IF l oc.u..c LI Q Rt2.Pi 3..lg[0101- a t O !mOr s. 0~ l... 0: 0 ; -go i 0lgg a a Lt .1,1oc ,a | r.o'Til IF l oc.u..c LI Q Rt2.Pi 3..lg[0101- a t O !mOr s. 0~ l... 0: 0 ; -go i 0lgg a a Lt .1,1oc ,a | ||
;l l 1 n.. a | ;l l 1 n.. a | ||
;gg. i . ; g - -- | ;gg. i . ; g - -- | ||
i, w | i, w con'T ~ | ||
con'T ~ | |||
_ _ _ Wa. i . | _ _ _ Wa. i . | ||
g; Qgt u 050-0 | g; Qgt u 050-0 r 3:0 t 2 gi 0:3 i 0 : 5: 7 I agl0n r3 li! r317:a m . . , s_ . . . . . .. . . s , s. r. 1. ...o o.r. | ||
r 3:0 t 2 gi 0:3 i 0 : 5: 7 I agl0n r3 li! r317:a m . . , s_ . . . . . .. . . s , s. r. 1. ...o o.r. | |||
er -- | er -- | ||
svaar osscairrios Ano anosasts cousscusscas | svaar osscairrios Ano anosasts cousscusscas | ||
Line 47: | Line 35: | ||
The instantaneous release race was 5% of the :nost restrictive noble gas | The instantaneous release race was 5% of the :nost restrictive noble gas | ||
_ , g,j , | _ , g,j , | ||
_ g , limit. Redundancy NA. No safety hazard to the plant or public. This is | _ g , limit. Redundancy NA. No safety hazard to the plant or public. This is | ||
. ._ . . _. _ . r5TO I the 7th occurrence of this event. , | . ._ . . _. _ . r5TO I the 7th occurrence of this event. , | ||
. . . Io iil f f __. | . . . Io iil f f __. | ||
@f ., | @f ., | ||
f O. C00. S'. : 8 Cov8.s4%* 038 ,I 28 8e . [ | f O. C00. S'. : 8 Cov8.s4%* 038 ,I 28 8e . [ | ||
. _ _ _ iot. | . _ _ _ iot. | ||
l Pi a @' ]@ Q @ [Z l 3 Z i ZI Z l Zi@ g,, @ [,Zj g_ | l Pi a @' ]@ Q @ [Z l 3 Z i ZI Z l Zi@ g,, @ [,Zj g_ | ||
c::... : . . . , ..m, u | c::... : . . . , ..m, u | ||
. ..r.... ..c.2 | . ..r.... ..c.2 | ||
.. . s,m, :: s ~.. ,o | .. . s,m, :: s ~.. ,o 6 ,a;'.;;; .. 1718I | ||
6 ,a;'.;;; .. 1718I | |||
.,. = | .,. = | ||
Wu 1 10 i 81 | Wu 1 10 i 81 | ||
:. u W | :. u W | ||
v 101 41 | v 101 41 W | ||
u 8, . l ol W.'n Ws' a%'Rr *%2W - ., nn ' , % p ' .;;.',2 , 'i.','h i;' :::2;?::,, | |||
W.'n Ws' a%'Rr *%2W - ., nn ' , % p ' .;;.',2 , 'i.','h i;' :::2;?::,, | |||
L...D6 W@ . | L...D6 W@ . | ||
laZ.J O >I o i 0: a' 0 gj@ | laZ.J O >I o i 0: a' 0 gj@ | ||
Wg w@ u[ ZI 919'i 9fg | Wg w@ u[ ZI 919'i 9fg | ||
., ., ~ | ., ., ~ | ||
cAuse oescaieries amo conatern r Aertas @ ~ | cAuse oescaieries amo conatern r Aertas @ ~ | ||
_,, ._ _ g (_'The cause of this event was personnel error. Temporary changes to OP-205 , _ | _,, ._ _ g (_'The cause of this event was personnel error. Temporary changes to OP-205 , _ | ||
, were not followed. Supervision and concerned personnel have been mada _ | , were not followed. Supervision and concerned personnel have been mada _ | ||
_ , , , , , , , aware of the consequences 'of not following approved procedures both , | _ , , , , , , , aware of the consequences 'of not following approved procedures both , | ||
I i.,3II temporary and permanent. Discrepancy Report #C-00834 has been initiated. t_ . | I i.,3II temporary and permanent. Discrepancy Report #C-00834 has been initiated. t_ . | ||
t'!4 1.3 [ | t'!4 1.3 [ | ||
'#.'W : .. e,.. . . . , @ s',7di!' | '#.'W : .. e,.. . . . , @ s',7di!' | ||
. .,::...,.,,....,, g | . .,::...,.,,....,, g L,.11J Lgj@ l d o f ol@l NA l [A,,J@! Operator observation l | ||
L,.11J Lgj@ l d o f ol@l NA l [A,,J@! Operator observation l | |||
*fr.,,,, ds... | *fr.,,,, ds... | ||
" u ~ a | " u ~ a | ||
* u | * u | ||
Line 107: | Line 68: | ||
.u .... | .u .... | ||
(~ .! . i LGj (h,(..u. | (~ .! . i LGj (h,(..u. | ||
128 curies nobl@e [ ds Aux 111ar.,.3s..u.,,@ | 128 curies nobl@e [ ds Aux 111ar.,.3s..u.,,@ | ||
7 Building NJ l | 7 Building NJ l | ||
.. c.m'd | .. c.m'd | ||
,s .. . | ,s .. . | ||
3".. .gl | 3".. .gl I , ! 1 1010 10 'CLZ.J@l NA l ~ | ||
I , ! 1 1010 10 'CLZ.J@l NA l ~ | |||
' * ' " a | ' * ' " a | ||
. .,:sa'.v.1.,,,, :......se s..... | . .,:sa'.v.1.,,,, :......se s..... | ||
._ l' l 1, I,O!0 i Ol@l NA l - | ._ l' l 1, I,O!0 i Ol@l NA l - | ||
..2 ''* "' @ | ..2 ''* "' @ | ||
W' :' :'lL';';.'ls NA Ii6'.I | W' :' :'lL';';.'ls NA Ii6'.I | ||
. d. @l .. " | . d. @l .. " | ||
l sac tst c . . | l sac tst c . . | ||
e G.. I;31' G,'.. .. os @ NA # : ieet ,et tt [ | e G.. I;31' G,'.. .. os @ NA # : ieet ,et tt [ | ||
Avs er 7.tramtr' l- Gener / .n 904 ) 795-6486 ya (SEE ATTACIIED SUPPLE.'!F.NTAP.T INFOC!ATION SEIEET) | Avs er 7.tramtr' l- Gener / .n 904 ) 795-6486 ya (SEE ATTACIIED SUPPLE.'!F.NTAP.T INFOC!ATION SEIEET) 8002 280 7CQ ;i | ||
8002 280 7CQ ;i | |||
[ SUPPLEMENTARY INPORMATION | [ SUPPLEMENTARY INPORMATION | ||
\ | \ | ||
. Report No.: 50-302/78-008/04T-0 2. | . Report No.: 50-302/78-008/04T-0 2. | ||
Facility: Crystal River Unit #3 | Facility: Crystal River Unit #3 | ||
: 3. Report Date: 13 March 1978 | : 3. Report Date: 13 March 1978 | ||
: 4. Occurrence Date: 5 March 1978 | : 4. Occurrence Date: 5 March 1978 | ||
Line 156: | Line 94: | ||
Mode 5 cold shutdown operation. | Mode 5 cold shutdown operation. | ||
: 7. Description of Occurrence: | : 7. Description of Occurrence: | ||
At 1410, an unplanned gas release occurred during plant cooldown. While desassing - | At 1410, an unplanned gas release occurred during plant cooldown. While desassing - | ||
Reactor Coolant System, in preparation for RCS draindown, the Wasta Gas Surge tank ; | Reactor Coolant System, in preparation for RCS draindown, the Wasta Gas Surge tank ; | ||
was isolated by a temporary change to the Hydrogen Addition and Degasification " | was isolated by a temporary change to the Hydrogen Addition and Degasification " | ||
Procedure (OP-205) . The purpose of the change was to put all the high activity gasses into one waste gas decay tank. After completion of degasification, the waste gas header was over-pressurized blowing the Auxiliary Building loop seals.- | Procedure (OP-205) . The purpose of the change was to put all the high activity gasses into one waste gas decay tank. After completion of degasification, the waste gas header was over-pressurized blowing the Auxiliary Building loop seals.- | ||
A total of 128 curies of noble gasses, primarily Ze-133, was released. The instantan- | A total of 128 curies of noble gasses, primarily Ze-133, was released. The instantan-g acus release rate was 5% .of the most restrictive noble gas limit set forth in Environ-mental Technical Specification.2.4.2.A(1). . . | ||
g acus release rate was 5% .of the most restrictive noble gas limit set forth in Environ-mental Technical Specification.2.4.2.A(1). . . | |||
: 8. Designation of Apparent Cause: - | : 8. Designation of Apparent Cause: - | ||
The cause of this event was personnel error, in that the' camporary procedure change to OP-205 was not followed and the gas header was over-pressurized, blowing the | The cause of this event was personnel error, in that the' camporary procedure change to OP-205 was not followed and the gas header was over-pressurized, blowing the Aux 111nry Building loop seals. l l | ||
Aux 111nry Building loop seals. l l | |||
: 9. Analysis of Occurrence: | : 9. Analysis of Occurrence: | ||
The health and safaty of the public was not affected in that the instantaneous release rate was 5% of the most restrictive noble gas limit. | The health and safaty of the public was not affected in that the instantaneous release rate was 5% of the most restrictive noble gas limit. | ||
Line 174: | Line 106: | ||
Supervision & concerned personnel have been made aware of the consequences of not following approved procedures both temporary and per:anent. Discrepancy Reper | Supervision & concerned personnel have been made aware of the consequences of not following approved procedures both temporary and per:anent. Discrepancy Reper | ||
#C o0834 has been initiated. | #C o0834 has been initiated. | ||
: 11. Failure Data: | : 11. Failure Data: | ||
This is the 7th occurrence of this event due to blown loop seals. | This is the 7th occurrence of this event due to blown loop seals. |
Latest revision as of 16:48, 21 February 2020
ML19317G281 | |
Person / Time | |
---|---|
Site: | Crystal River |
Issue date: | 03/13/1978 |
From: | Cooper J FLORIDA POWER CORP. |
To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
Shared Package | |
ML19317G278 | List: |
References | |
LER-78-008-04T, LER-78-8-4T, NUDOCS 8002280902 | |
Download: ML19317G281 (2) | |
Text
.. - .-_.___-- _ _ _
Oi '
- u. s. =ves.s An ascutArony commissiers
- sac acau aos LICENSEE EVENT REPORT EXHl8IT A
! cominos stocc: I, i 1 I I I l@ ,
cettAsa per on Tves ALL stouinao imponatArnous ._.. . _
r.o'Til IF l oc.u..c LI Q Rt2.Pi 3..lg[0101- a t O !mOr s. 0~ l... 0: 0 ; -go i 0lgg a a Lt .1,1oc ,a
- l l 1 n.. a
- gg. i . ; g - --
i, w con'T ~
_ _ _ Wa. i .
g; Qgt u 050-0 r 3:0 t 2 gi 0:3 i 0 : 5: 7 I agl0n r3 li! r317:a m . . , s_ . . . . . .. . . s , s. r. 1. ...o o.r.
er --
svaar osscairrios Ano anosasts cousscusscas
,. _ _ ___ .,_ g in Mode 5 operation, while degas g the Reactor Coolant System, the wasta ,
_. _ g ,g gas header was over-pressurized blowing the Auxiliary. Building loop seals.,
The instantaneous release race was 5% of the :nost restrictive noble gas
_ , g,j ,
_ g , limit. Redundancy NA. No safety hazard to the plant or public. This is
. ._ . . _. _ . r5TO I the 7th occurrence of this event. ,
. . . Io iil f f __.
@f .,
f O. C00. S'. : 8 Cov8.s4%* 038 ,I 28 8e . [
. _ _ _ iot.
l Pi a @' ]@ Q @ [Z l 3 Z i ZI Z l Zi@ g,, @ [,Zj g_
c::... : . . . , ..m, u
. ..r.... ..c.2
.. . s,m, :: s ~.. ,o 6 ,a;'.;;; .. 1718I
.,. =
Wu 1 10 i 81
- . u W
v 101 41 W
u 8, . l ol W.'n Ws' a%'Rr *%2W - ., nn ' , % p ' .;;.',2 , 'i.','h i;' :::2;?::,,
L...D6 W@ .
laZ.J O >I o i 0: a' 0 gj@
Wg w@ u[ ZI 919'i 9fg
., ., ~
cAuse oescaieries amo conatern r Aertas @ ~
_,, ._ _ g (_'The cause of this event was personnel error. Temporary changes to OP-205 , _
, were not followed. Supervision and concerned personnel have been mada _
_ , , , , , , , aware of the consequences 'of not following approved procedures both ,
I i.,3II temporary and permanent. Discrepancy Report #C-00834 has been initiated. t_ .
t'!4 1.3 [
'#.'W : .. e,.. . . . , @ s',7di!'
. .,::...,.,,....,, g L,.11J Lgj@ l d o f ol@l NA l [A,,J@! Operator observation l
- fr.,,,, ds...
" u ~ a
- u
..:.m :...-.,u n c
.u ....
(~ .! . i LGj (h,(..u.
128 curies nobl@e [ ds Aux 111ar.,.3s..u.,,@
7 Building NJ l
.. c.m'd
,s .. .
3".. .gl I , ! 1 1010 10 'CLZ.J@l NA l ~
' * ' " a
. .,:sa'.v.1.,,,, :......se s.....
._ l' l 1, I,O!0 i Ol@l NA l -
..2 * "' @
W' :' :'lL';';.'ls NA Ii6'.I
. d. @l .. "
l sac tst c . .
e G.. I;31' G,'.. .. os @ NA # : ieet ,et tt [
Avs er 7.tramtr' l- Gener / .n 904 ) 795-6486 ya (SEE ATTACIIED SUPPLE.'!F.NTAP.T INFOC!ATION SEIEET) 8002 280 7CQ ;i
[ SUPPLEMENTARY INPORMATION
\
. Report No.: 50-302/78-008/04T-0 2.
Facility: Crystal River Unit #3
- 3. Report Date: 13 March 1978
- 4. Occurrence Date: 5 March 1978
- 5. Identification of Occurrence:
Unplanned radioactive gas release to the atmosphere reported in accordance with 10 CFR 20.403.
- 6. Conditions Prior to Occurrence:
Mode 5 cold shutdown operation.
- 7. Description of Occurrence:
At 1410, an unplanned gas release occurred during plant cooldown. While desassing -
Reactor Coolant System, in preparation for RCS draindown, the Wasta Gas Surge tank ;
was isolated by a temporary change to the Hydrogen Addition and Degasification "
Procedure (OP-205) . The purpose of the change was to put all the high activity gasses into one waste gas decay tank. After completion of degasification, the waste gas header was over-pressurized blowing the Auxiliary Building loop seals.-
A total of 128 curies of noble gasses, primarily Ze-133, was released. The instantan-g acus release rate was 5% .of the most restrictive noble gas limit set forth in Environ-mental Technical Specification.2.4.2.A(1). . .
- 8. Designation of Apparent Cause: -
The cause of this event was personnel error, in that the' camporary procedure change to OP-205 was not followed and the gas header was over-pressurized, blowing the Aux 111nry Building loop seals. l l
- 9. Analysis of Occurrence:
The health and safaty of the public was not affected in that the instantaneous release rate was 5% of the most restrictive noble gas limit.
- 10. Corrective Action:
Supervision & concerned personnel have been made aware of the consequences of not following approved procedures both temporary and per:anent. Discrepancy Reper
- C o0834 has been initiated.
- 11. Failure Data:
This is the 7th occurrence of this event due to blown loop seals.
1 1
i 1
- , - . . -_ .-- .