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| issue date = 03/03/1989
| issue date = 03/03/1989
| title = Followup Part 21 Rept Re Failures of Closing Mechanisms in Two Bbc Brown Boveri,Inc,Type 5HJK250 Circuit Breakers Installed in Safety Sys at Plant.Initially Reported on 890301.Maint Procedure Will Be Revised
| title = Followup Part 21 Rept Re Failures of Closing Mechanisms in Two Bbc Brown Boveri,Inc,Type 5HJK250 Circuit Breakers Installed in Safety Sys at Plant.Initially Reported on 890301.Maint Procedure Will Be Revised
| author name = ALEXICH M P
| author name = Alexich M
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name = MURLEY T E
| addressee name = Murley T
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| docket = 05000315, 05000316
| docket = 05000315, 05000316
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:-AC CELEBRATED Dl Bt'Tl 04 DEMON~TR O.i Fr'PTER REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:8903100446 DOC.DATE: 89/03/03 NOTARIZED:
{{#Wiki_filter:-AC CELEBRATED         Dl                     Bt'Tl 04   DEMON ~TR       O.i     Fr'PTER REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
NO DOCKET FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana&05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana&05000316 AUTH.NAME AUTHOR AFFILIATION ALEXICH,M.P.
ACCESSION NBR:8903100446                         DOC.DATE: 89/03/03   NOTARIZED: NO           DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana                           & 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana                           & 05000316 AUTH. NAME           AUTHOR AFFILIATION ALEXICH,M.P.         Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME           RECIPIENT AFFILIATION MURLEY,T.E.           Document Control Branch (Document Control Desk)                                 R
Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME RECIPIENT AFFILIATION MURLEY,T.E.
Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Part 21 rept re failure of circuit breakers, manufactured by BBC,Inc,during testing.DISTRIBUTION CODE: IE19D COPIES RECEIVED:LTR ENCL SIZE: TITLE: Part 21 Rept (50 DKT)NOTES: R RECIPIENT ID CODE/NAME PD3-1 LA STANG,J INTERNAL: AEOD/DOA ARM TECH ADV NRR CRUTCHFIELD NRR/DEST/ADE 8H NRR/DLPQ/QAB 10 N~/~B 9D RGN3 RGN5 EXTERNAL: INPO RECORD CTR NRC PDR COPIES LTTR ENCL 1 0 1 1 1 1 1 1 1 1 1'1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME PD3-1 PD AEOD/DS P/TPAB IRM/DAB NRR VARGA,S NRR/DEST/ADS 7E NRR/DOEA/GCB 11 NUDOCS-ABSTRACT RES/DSIR/EIB RGN2 RGN4 LPDR NS I C S I LVER g E COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1~1 R I NOTE'IO ALL"RIDS" RECIPZERIS'PLEASE HELP US IO REDUCE WASTE!CCNTACI'IHE
Part 21 rept re failure of circuit breakers, manufactured by BBC,Inc,during testing.
~ENI'OPIBOL DESK, ROOM Pl-37 (EXT.20079)KO ZXiDGXLTB YOUR NAME FMH DISTRIBUTION LISTS FOR DOCUMENIS YOU DON'T NEEDt D D S TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 25 Indiana Michigan Power Company P.O.Box 16631 Coiumbus, OH 43216 AEP'NRC:0971F Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 10 CFR 21 REPORT: FAILURE OF CIRCUIT BREAKERS MANUFACTURED BY BBC BROWN BOVERI, INC.DURING TESTING U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.20555 Attn: T.E.Murley March 3, 1989
DISTRIBUTION CODE: IE19D                       COPIES RECEIVED:LTR     ENCL     SIZE:
TITLE: Part 21 Rept (50             DKT)
NOTES:
RECIPIENT                          COPIES          RECIPIENT         COPIES ID   CODE/NAME                       LTTR ENCL    ID  CODE/NAME      LTTR ENCL PD3-1 LA                               1    0    PD3-1 PD              1      1 STANG,J                                 1    1 INTERNAL: AEOD/DOA                                 1    1    AEOD/DS P/TPAB        1      1 ARM TECH ADV                           1    1    IRM/DAB              1      1 NRR CRUTCHFIELD                         1    1    NRR VARGA,S          1      1 NRR/DEST/ADE 8H                         1  '1    NRR/DEST/ADS 7E      1      1 NRR/DLPQ/QAB 10                         1    1    NRR/DOEA/GCB 11      1      1 N~/~         B 9D                     1     1   NUDOCS-ABSTRACT      1       1 1     1   RES/DSIR/EIB          1       1 1     1   RGN2                  1       1 RGN3                                    1     1   RGN4                  1       1 RGN5                                    1     1 EXTERNAL: INPO RECORD CTR                          1     1   LPDR                  1       1 NRC PDR                                1     1     I    I NS C S LVER g E       1 ~
1 R
I D
D NOTE 'IO ALL "RIDS" RECIPZERIS'PLEASE S
HELP US IO REDUCE WASTE! CCNTACI'IHE             ~ENI'OPIBOL DESK, ROOM Pl-37 (EXT. 20079) KO ZXiDGXLTB YOUR NAME             FMH DISTRIBUTION LISTS FOR DOCUMENIS YOU DON'T NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR                       26   ENCL   25


==Dear Dr.Murley:==
Indiana Michigan Power Company P.O. Box 16631 Coiumbus, OH 43216 AEP'NRC:0971F Donald C. Cook Nuclear Plant Units      1 and 2 Docket Nos. 50-315 and 50-316 License Nos. DPR-58 and DPR-74 10 CFR 21 REPORT:      FAILURE OF CIRCUIT BREAKERS MANUFACTURED BY BBC BROWN BOVERI, INC. DURING TESTING U.S. Nuclear Regulatory Commission Attn:    Document  Control Desk Washington, D.C. 20555 Attn:      T. E. Murley March 3, 1989
Introduction (10 CFR 21.21(b)(3)(i), (ii)and (iii))A This letter constitutes a follow-up report, as required by,."'10 CFR 21.21, of information provided to your staff via telephone'n March 1, 1989.This report is being submitted by Indiana Michigan Power Company, P.O.Box 16631, Columbus,Ohio 43216.The 10 CFR 21 report concerns observed failures of closing mechanisms in two BBC Brown Boveri, Inc.type 5HK250 circuit breakers installed in safety systems in Cook Nuclear Plant Unit 1.On February 8, 1989, during the conduct of routine cleaning and inspection of circuit breakers installed in the 4KV distribution system for Cook Nuclear Plant Unit 1, a BBC Brown Boveri (BBC)5HK250 breaker that had been removed from service for testing failed to close as required when the closing circuit was energized.
 
The breaker supplies the Unit 1 east residual heat removal (RHR)pump and is required to close to perform its safety function.Subsequent investigation showed the cause of the failure to be aging and dirt contamination of the grease used for lubrication of the breaker closing mechanism.
==Dear Dr. Murley:==
After cleaning and relubrication of the closing mechanism the breaker functioned properly.The failure of the breaker to close was considered to be an isolated event since the breaker in question, as well as other safety-related breakers, of the same type, had previously passed all in-service surveillance tests.However, the breaker servicing described below in the discussion section was initiated at the time this'ailure was observed.On February 27, 1989, a second BBC 5HK250 breaker 8903100446 890303 PDR ADOCK 05000315 S PDC 0 P C I'e J V Dr.T.E.Hurley-2-AEP:NRC:0971F also failed to close during routine testing performed on the breaker while out of service.The cause of the second failure was determined to be the same as in the first case.After cleaning and relubricating of the breaker closing mechanism, the breaker functioned properly.The observation of two failures of the same type due to the same cause, in conjunction with the knowledge that breakers of the same type and similar age are used in safety-related applications elsewhere in the industry, prompted submittal of this 10 CFR 21 report.Discussion (10 CFR 21.21(b)(3)(vi) and (vii))As part of the investigation of the first breaker failure discussed above, BBC was contacted and assistance from a BBC service representative was requested.
 
When the cause of the breaker's failure to close was determined, the BBC representative recommended a procedure for cleaning and lubricating the closing mechanism in order to provide for proper functioning of the breaker.It should be noted that the observed failures during testing affected only the breaker's ability to close when required, and not the ability to open.As a result, all safety-related BBC 5HK250 breakers in both Units 1 and 2 at Cook Nuclear Plant that are required to close in order to perform their safety function have been serviced in accordance with the BBC representative's recommendations in order to ensure they will function properly.At the Cook Nuclear Plant this involved 18 BBC breakers in each unit.These breakers serve safety injection, auxiliary feedwater, containment spray, RHR, essential service water, component cooling water and centrifugal charging pumps, and the emergency diesel feed.As an additional part of our investigation and corrective actions associated with the events described above, we have reviewed the maintenance procedures applicable to the BBC 5HK circuit breakers.This review was intended to assess to what extent procedural requirements may have contributed to the events and what, if any, procedural revisions could be made to prevent recurrence.
Introduction (10     CFR 21.21(b)(3)(i), (ii) and (iii))
It should be noted that the applicable maintenance procedure was prepared based on the instructions supplied with the breakers by the breaker manufacturer (I.T.E.instruction'No.
letter constitutes     follow-up report, as required by,. "
1B-8.2.7-2).
A This                          a 10   CFR 21.21, of information provided to your staff via       telephone'n March 1, 1989. This report is being submitted by Indiana Michigan Power Company, P.O. Box 16631, Columbus,Ohio 43216. The 10 CFR 21 report concerns observed failures of closing mechanisms in two BBC Brown Boveri, Inc. type 5HK250 circuit breakers installed in safety systems in Cook Nuclear Plant Unit 1.
Discussions with the BBC representative revealed that periodic cleaning and lubrication of the closing mechanism was not addressed in the applicable BBC technical manual because the lubrication performed at the factory was considered to be permanent and was meant to last for the life of the unit.Therefore, review concluded that because the manufacturer's instructions contained no requirements for periodic lubrication of the breaker closing mechanism, our maintenance procedure similarly did not require this to be done during routine maintenance activities.
On   February 8, 1989, during the conduct of routine cleaning and inspection of circuit breakers installed in the 4KV distribution system for Cook Nuclear Plant Unit 1, a BBC Brown Boveri (BBC) 5HK250 breaker that had been removed from service for testing failed to close as required when the closing circuit was energized.
Dr.T.E.Murley-3-AEP:NRC:0971F Conclusion (10 CFR 21.21(b)(3)(vii) and (viii))In accordance with the BBC service representative's recommendations, actions have been completed to correct the breaker closing mechanism failures discussed above and all other BBC safety-related breakers installed in Cook Nuclear Plant Units 1 and 2 whose safety function is to close when called upon have similarly been serviced according to BBC's recommendations.
The breaker supplies the Unit 1 east residual heat removal (RHR) pump and is required to close to perform its safety function.
In order to prevent recurrence of the events discussed in this report, our maintenance procedure will be revised to include cleaning and lubrication of the breaker closing mechanism on a periodic basis as part of our maintenance program.This point may be of interest to other licensees who, as in the case of the Cook Nuclear Plant, have developed their maintenance procedures for the BBC breakers based on the manufacturer's instructions'his document has been prepared following Corporate procedures that incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.
Subsequent investigation showed the cause of the failure to be aging and dirt contamination of the grease used for lubrication of the breaker closing mechanism. After cleaning and relubrication of the closing mechanism the breaker functioned properly. The failure of the breaker to close was considered to be an isolated event since the breaker in question, as well as other safety-related breakers, of the same type, had previously passed all in-service surveillance tests. However, the breaker servicing described below in the discussion section was initiated at the time this'ailure was observed.     On February 27, 1989, a second   BBC 5HK250         breaker 8903100446 890303 PDR     ADOCK 05000315 S                     PDC
Sincerely, M.P.Ale ich Vice President ldp Attachment cc: D.H.Williams, Jr.W.G.Smith, Jr.-Bridgman R.C.Callen G.Charnoff A.B.Davis NRC Resident Inspector G.Bruchmann}}
 
0       P C
I'e J
V
 
Dr. T. E. Hurley                                   AEP:NRC:0971F also failed to close   during routine testing performed on the breaker while out of   service. The cause of the second failure was determined to be the   same as in the first case. After cleaning and relubricating of the breaker closing mechanism, the breaker functioned properly. The observation of two failures of the same type due to the same   cause, in conjunction with the knowledge that breakers of the same   type and similar age are used in safety-related applications elsewhere in the industry, prompted submittal of this 10 CFR 21 report.
Discussion (10 CFR 21.21(b)(3)(vi)   and (vii))
As part of the investigation of the   first breaker failure discussed above, BBC was contacted and assistance from a BBC service representative was requested. When the cause of the breaker's failure to close was determined, the BBC representative recommended a procedure for cleaning and lubricating the closing mechanism in order to provide for proper functioning of the breaker.
It should be noted that the observed failures during testing affected only the breaker's ability to close when required, and not the ability to open. As a result, all safety-related BBC 5HK250 breakers in both Units 1 and 2 at Cook Nuclear Plant that are required to close in order to perform their safety function have been serviced in accordance with the BBC representative's recommendations in order to ensure they will function properly. At the Cook Nuclear Plant this involved 18 BBC breakers in each unit.
These breakers serve safety injection, auxiliary feedwater, containment spray, RHR, essential service water, component cooling water and centrifugal charging pumps, and the emergency diesel feed.
As an additional part of our investigation and corrective actions associated with the events described above, we have reviewed the maintenance procedures applicable to the BBC 5HK circuit breakers.
This review was intended to assess to what extent procedural requirements may have contributed to the events and what,     if any, procedural revisions could be made to prevent recurrence. It should be noted that the applicable maintenance procedure was prepared based on the instructions supplied with the breakers by the breaker manufacturer (I.T.E. instruction'No. 1B-8.2.7-2).
Discussions with the BBC representative revealed that periodic cleaning and lubrication of the closing mechanism was not addressed in the applicable BBC technical manual because the lubrication performed at the factory was considered to be permanent and was meant to last for the life of the unit. Therefore, review concluded that because the manufacturer's instructions contained no requirements for periodic lubrication of the breaker closing mechanism, our maintenance procedure similarly did not require this to be done during routine maintenance activities.
 
Dr. T. E. Murley                                           AEP:NRC:0971F Conclusion (10   CFR 21.21(b)(3)(vii)   and (viii))
In accordance with the BBC service representative's recommendations, actions have been completed to correct the breaker closing mechanism failures discussed above and all other BBC safety-related breakers installed in Cook Nuclear Plant Units 1 and 2 whose safety function is to close when called upon have similarly been serviced according to BBC's recommendations.
In order to prevent recurrence of the events discussed in this report, our maintenance procedure will be revised to include cleaning and lubrication of the breaker closing mechanism on a periodic basis as part of our maintenance program. This point may be of interest to other licensees who, as in the case of the Cook Nuclear Plant, have developed their maintenance procedures for the BBC breakers based on the manufacturer's     instructions'his document has been prepared   following Corporate procedures that incorporate   a reasonable set of controls to ensure         its accuracy and completeness prior to signature by the undersigned.
Sincerely, M. P. Ale ich Vice President ldp Attachment cc:   D. H. Williams, Jr.
W. G. Smith, Jr. - Bridgman R. C. Callen G. Charnoff A. B. Davis NRC Resident Inspector G. Bruchmann}}

Latest revision as of 00:55, 4 February 2020

Followup Part 21 Rept Re Failures of Closing Mechanisms in Two Bbc Brown Boveri,Inc,Type 5HJK250 Circuit Breakers Installed in Safety Sys at Plant.Initially Reported on 890301.Maint Procedure Will Be Revised
ML17326B550
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/03/1989
From: Alexich M
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Murley T
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
REF-PT21-89, REF-PT21-89-044-000 AEP:NRC:0971F, AEP:NRC:971F, PT21-89-044-000, PT21-89-44, NUDOCS 8903100446
Download: ML17326B550 (5)


Text

-AC CELEBRATED Dl Bt'Tl 04 DEMON ~TR O.i Fr'PTER REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8903100446 DOC.DATE: 89/03/03 NOTARIZED: NO DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana & 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana & 05000316 AUTH. NAME AUTHOR AFFILIATION ALEXICH,M.P. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION MURLEY,T.E. Document Control Branch (Document Control Desk) R

SUBJECT:

Part 21 rept re failure of circuit breakers, manufactured by BBC,Inc,during testing.

DISTRIBUTION CODE: IE19D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: Part 21 Rept (50 DKT)

NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 0 PD3-1 PD 1 1 STANG,J 1 1 INTERNAL: AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 ARM TECH ADV 1 1 IRM/DAB 1 1 NRR CRUTCHFIELD 1 1 NRR VARGA,S 1 1 NRR/DEST/ADE 8H 1 '1 NRR/DEST/ADS 7E 1 1 NRR/DLPQ/QAB 10 1 1 NRR/DOEA/GCB 11 1 1 N~/~ B 9D 1 1 NUDOCS-ABSTRACT 1 1 1 1 RES/DSIR/EIB 1 1 1 1 RGN2 1 1 RGN3 1 1 RGN4 1 1 RGN5 1 1 EXTERNAL: INPO RECORD CTR 1 1 LPDR 1 1 NRC PDR 1 1 I I NS C S LVER g E 1 ~

1 R

I D

D NOTE 'IO ALL "RIDS" RECIPZERIS'PLEASE S

HELP US IO REDUCE WASTE! CCNTACI'IHE ~ENI'OPIBOL DESK, ROOM Pl-37 (EXT. 20079) KO ZXiDGXLTB YOUR NAME FMH DISTRIBUTION LISTS FOR DOCUMENIS YOU DON'T NEEDt TOTAL NUMBER OF COPIES REQUIRED: LTTR 26 ENCL 25

Indiana Michigan Power Company P.O. Box 16631 Coiumbus, OH 43216 AEP'NRC:0971F Donald C. Cook Nuclear Plant Units 1 and 2 Docket Nos. 50-315 and 50-316 License Nos. DPR-58 and DPR-74 10 CFR 21 REPORT: FAILURE OF CIRCUIT BREAKERS MANUFACTURED BY BBC BROWN BOVERI, INC. DURING TESTING U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C. 20555 Attn: T. E. Murley March 3, 1989

Dear Dr. Murley:

Introduction (10 CFR 21.21(b)(3)(i), (ii) and (iii))

letter constitutes follow-up report, as required by,. "

A This a 10 CFR 21.21, of information provided to your staff via telephone'n March 1, 1989. This report is being submitted by Indiana Michigan Power Company, P.O. Box 16631, Columbus,Ohio 43216. The 10 CFR 21 report concerns observed failures of closing mechanisms in two BBC Brown Boveri, Inc. type 5HK250 circuit breakers installed in safety systems in Cook Nuclear Plant Unit 1.

On February 8, 1989, during the conduct of routine cleaning and inspection of circuit breakers installed in the 4KV distribution system for Cook Nuclear Plant Unit 1, a BBC Brown Boveri (BBC) 5HK250 breaker that had been removed from service for testing failed to close as required when the closing circuit was energized.

The breaker supplies the Unit 1 east residual heat removal (RHR) pump and is required to close to perform its safety function.

Subsequent investigation showed the cause of the failure to be aging and dirt contamination of the grease used for lubrication of the breaker closing mechanism. After cleaning and relubrication of the closing mechanism the breaker functioned properly. The failure of the breaker to close was considered to be an isolated event since the breaker in question, as well as other safety-related breakers, of the same type, had previously passed all in-service surveillance tests. However, the breaker servicing described below in the discussion section was initiated at the time this'ailure was observed. On February 27, 1989, a second BBC 5HK250 breaker 8903100446 890303 PDR ADOCK 05000315 S PDC

0 P C

I'e J

V

Dr. T. E. Hurley AEP:NRC:0971F also failed to close during routine testing performed on the breaker while out of service. The cause of the second failure was determined to be the same as in the first case. After cleaning and relubricating of the breaker closing mechanism, the breaker functioned properly. The observation of two failures of the same type due to the same cause, in conjunction with the knowledge that breakers of the same type and similar age are used in safety-related applications elsewhere in the industry, prompted submittal of this 10 CFR 21 report.

Discussion (10 CFR 21.21(b)(3)(vi) and (vii))

As part of the investigation of the first breaker failure discussed above, BBC was contacted and assistance from a BBC service representative was requested. When the cause of the breaker's failure to close was determined, the BBC representative recommended a procedure for cleaning and lubricating the closing mechanism in order to provide for proper functioning of the breaker.

It should be noted that the observed failures during testing affected only the breaker's ability to close when required, and not the ability to open. As a result, all safety-related BBC 5HK250 breakers in both Units 1 and 2 at Cook Nuclear Plant that are required to close in order to perform their safety function have been serviced in accordance with the BBC representative's recommendations in order to ensure they will function properly. At the Cook Nuclear Plant this involved 18 BBC breakers in each unit.

These breakers serve safety injection, auxiliary feedwater, containment spray, RHR, essential service water, component cooling water and centrifugal charging pumps, and the emergency diesel feed.

As an additional part of our investigation and corrective actions associated with the events described above, we have reviewed the maintenance procedures applicable to the BBC 5HK circuit breakers.

This review was intended to assess to what extent procedural requirements may have contributed to the events and what, if any, procedural revisions could be made to prevent recurrence. It should be noted that the applicable maintenance procedure was prepared based on the instructions supplied with the breakers by the breaker manufacturer (I.T.E. instruction'No. 1B-8.2.7-2).

Discussions with the BBC representative revealed that periodic cleaning and lubrication of the closing mechanism was not addressed in the applicable BBC technical manual because the lubrication performed at the factory was considered to be permanent and was meant to last for the life of the unit. Therefore, review concluded that because the manufacturer's instructions contained no requirements for periodic lubrication of the breaker closing mechanism, our maintenance procedure similarly did not require this to be done during routine maintenance activities.

Dr. T. E. Murley AEP:NRC:0971F Conclusion (10 CFR 21.21(b)(3)(vii) and (viii))

In accordance with the BBC service representative's recommendations, actions have been completed to correct the breaker closing mechanism failures discussed above and all other BBC safety-related breakers installed in Cook Nuclear Plant Units 1 and 2 whose safety function is to close when called upon have similarly been serviced according to BBC's recommendations.

In order to prevent recurrence of the events discussed in this report, our maintenance procedure will be revised to include cleaning and lubrication of the breaker closing mechanism on a periodic basis as part of our maintenance program. This point may be of interest to other licensees who, as in the case of the Cook Nuclear Plant, have developed their maintenance procedures for the BBC breakers based on the manufacturer's instructions'his document has been prepared following Corporate procedures that incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.

Sincerely, M. P. Ale ich Vice President ldp Attachment cc: D. H. Williams, Jr.

W. G. Smith, Jr. - Bridgman R. C. Callen G. Charnoff A. B. Davis NRC Resident Inspector G. Bruchmann