|
|
Line 53: |
Line 53: |
| Attachment to HNP-94-018 REPLY TO A NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50400/93-25 Re orted Violation A: | | Attachment to HNP-94-018 REPLY TO A NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50400/93-25 Re orted Violation A: |
| 10 CFR 50, Appendix B, Criterion XVIrequires that measures shall be established to assure conditions adverse to quality, such as failures, malfunctions,'deficiencies, deviations, and non-confor'mance are properly identified and corrected. | | 10 CFR 50, Appendix B, Criterion XVIrequires that measures shall be established to assure conditions adverse to quality, such as failures, malfunctions,'deficiencies, deviations, and non-confor'mance are properly identified and corrected. |
| The licensee's Corporate Quality Assurance Manual, Section 12, requires that significant conditions adverse to quality be identified and that corrective actions be determined which | | The licensee's Corporate Quality Assurance Manual, Section 12, requires that significant conditions adverse to quality be identified and that corrective actions be determined which will preclude repetition of the condition. |
| -
| |
| will preclude repetition of the condition. | |
| Contrary to the above, following the failure of an auxiliary feedwater system valve in November 1992, the identification and determination of corrective actions for deficiencies noted in the motor control center wiring of auxiliary feedwater system motor operated valves was not sufficient to preclude the repetition of another auxiliary feedwater system valve failure on December 14, 1993. | | Contrary to the above, following the failure of an auxiliary feedwater system valve in November 1992, the identification and determination of corrective actions for deficiencies noted in the motor control center wiring of auxiliary feedwater system motor operated valves was not sufficient to preclude the repetition of another auxiliary feedwater system valve failure on December 14, 1993. |
| This is a Severity Level IV violation (Supplement g. | | This is a Severity Level IV violation (Supplement g. |
Line 89: |
Line 87: |
| Technical Specification 6.8.1(a) requires that written procedures be properly established and implemented covering procedures outlined in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. | | Technical Specification 6.8.1(a) requires that written procedures be properly established and implemented covering procedures outlined in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978. |
| Regulatory Guide 1.33, Appendix A, paragraph 2.f requires procedures for changing turbine load, Operating Procedure OP-131.01, Main Turbine, Section 7.1 provides specific guidance for reducing turbine load. | | Regulatory Guide 1.33, Appendix A, paragraph 2.f requires procedures for changing turbine load, Operating Procedure OP-131.01, Main Turbine, Section 7.1 provides specific guidance for reducing turbine load. |
| ,
| |
| Ccr~ avg to the above, on December 31, 1993, the directions provided in procedure OP-131.01 were determined to be inadequate and could not be performed in the sequerice specified to reduce the turbine load. | | Ccr~ avg to the above, on December 31, 1993, the directions provided in procedure OP-131.01 were determined to be inadequate and could not be performed in the sequerice specified to reduce the turbine load. |
| This is a Severity Level V violation (Supplement I). | | This is a Severity Level V violation (Supplement I). |
|
---|
Category:CORRESPONDENCE-LETTERS
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20216G3501999-09-29029 September 1999 Confirms Conversations Re NRC Staff Voluntary Response to Orange County Discovery Requests.Staff Will Voluntarily Answer Discovery Requests & Will Not Waive Any Objection or Privilege Under NRC Regulations.Related Correspondence ML20212M1081999-09-29029 September 1999 Confirms Intent to Meet with Utils on 991025 in Atlanta,Ga to Discuss Pilot Plants,Shearon Harris & Sequoyah Any Observations & Lessons Learned & Recommendations Re Implementation of Pilot Program ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML20212H7741999-06-23023 June 1999 Responds to Re Petition Filed by Orange County Board of Commissioners Re Proposed Expansion of Sf Storage Capacity at Shearon Harris Npp.Public Meeting Will Be Held at Later Date.With Certificate of Svc.Served on 990624 ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML20206R2511999-05-19019 May 1999 Responds to Addressed to Chairman Jackson Requesting That NRC Grant Standing to Orange County Board of Commissioners in Shearon Harris Proceeding Currently Before Board.With Certificate of Svc.Served on 990519 ML20206Q5281999-05-17017 May 1999 Responds to 990304 Request for Two Rail Routes to Be Used for Transport of Spent Fuel from Brunswick Steam Electric Plant,Southport,Nc & Hb Robinson Steam Electric Plant, Hartsville,Sc to Shearon Harris Npp,Near New Hill,Sc ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9601999-05-11011 May 1999 Forwards Resolution Adopted by Carrboro Board of Aldermen at 990504 Meeting.Resolution Expresses Town Concern Re Util Plans to Double high-level Nuclear Waste Storage at Shnpp ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl IR 05000400/19982011999-04-12012 April 1999 Discusses Safeguards Insp Rept 50-400/98-201 (Operational Safeguards Response Evaluation) on 980908-11.No Violations Noted.Licensee Performance During Evaluation Indicated Excellent Overall Contingency Response Capability 1999-09-08
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML18017A9241999-10-15015 October 1999 Provides Supplemental Info Re 981223 Lar,Placing Plant Spent Fuel Pools 'C' & 'D' in Service.Info Provided Does Not Change Util Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18017A9141999-10-12012 October 1999 Forwards Addl Info Re Second 10-year ISI Program Plan Relief Requests,As Requested During 990923 Telcon ML18017A9131999-10-0606 October 1999 Provides Notification That Three SROs Licensed at Shnpp Have Been Reassigned from Position for Which Util Previously Certified Need for SRO License.Name,Docket Number & License Number for Subject Sros,Encl.Encl Withheld ML18017A8911999-09-30030 September 1999 Submits Comment on Encl 2 to 990617 Memo Titled Summary of Meeting with Nuclear Energy Inst. Encl 2 Was Titled Draft Technical Study of Spent Fuel Pool Accidents for Decommissioning Plants. Rept Which Provides Info Encl Also ML20212J0741999-09-29029 September 1999 Refers to Proposed License Amend for Harris NPP Which Would Allow Licensee to Activate Two of Plant Spent Fuel Pools.Serves Copy of Orange County Second Set of Document Requests to NRC Staff,Dtd 990929.Related Correspondence ML18017A8941999-09-29029 September 1999 Forwards Response to NRC 990414 RAI Re GL 95-07, Pressure- Locking & Thermal-Binding of SR Power-Operated Gate Valves. ML18017A8881999-09-27027 September 1999 Submits Info Re Estimated Effect of Changes or Errors in ECCS Evaluation Models or in Application of Models,Per 10CFR50.46(a)(3)(ii) ML18017A8861999-09-21021 September 1999 Forwards Response to NRC Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Examinations. ML18017A8821999-09-14014 September 1999 Provides Notification That RO Licensed on Harris Plant No Longer Meets Requirements of 10CFR50.21,effective 990826. Name,Docket Number & License Number for Individual Provided in Encl.Encl Withheld,Per 10CFR2.790(a)(6) ML18017A8651999-09-0808 September 1999 Requests Relief from Section XI,IWA-5242(a) Requirement for HNP Class 2 Bolted Connections in Borated Sys.Compliance with Requirement Would Result in Unusual Difficulty Without Compensating Increase in Level of Quality & Safety ML18017A8581999-09-0303 September 1999 Provides Response to NRC 990805 RAI Re Amend Request to Increase Fuel Storage Capacity ML18017A8551999-09-0101 September 1999 Forwards Marked Up Copy of Approved FSAR Section 17.3 with Applicable Duplicated TS Requirements,As Committed to in 990602 Application for Rev to TS ML18017A8541999-08-20020 August 1999 Submits Closure Info for Rev 1,Suppl 1 to GL 92-01, Reactor Vessel Structural Integrity. Identified Discrepancies from Review of NRC Rvid Provided HNP-99-134, Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.211999-08-18018 August 1999 Forwards Rev 11 to Physical Security & Safeguards Contingency Plan,Iaw 10CFR50.54(p)(2) & 10CFR50.4(b)(4). Description of Changes Is Provided as Encl 2 to Ltr.Rev Withheld,Per 10CFR73.21 ML18017A8351999-08-10010 August 1999 Corrects Statement Made in 980923 Ltr,By Clarifying That Operation of Inner & Outer Pal Doors Can Be Operated by Control Panels Located Inside & Outside Containment ML18016B0531999-08-0606 August 1999 Forwards Exercise Scenario with Controller Info & Simulation Data for Harris Nuclear Plant Emergency Preparedness Exercise Scheduled for 990921.Without Encl ML18016B0461999-08-0404 August 1999 Forwards LER 99-006-01 Describing Condition Which Resulted in Exceeding TS Requirements for CIVs & TS 4.0.4 for Generic Requirements for Surveillance Testing.Rev Includes Results of Investigation Into Failure to Recognize TS Requirements ML18016B0421999-07-30030 July 1999 Informs That in Ltr Dtd 950330 CP&L Committed to Complete Assessment of Severe Accident Mgt Capabilities & Make Any Identified Enhancements by 981231.Actions Were Completed in July 1998 ML18016B0391999-07-30030 July 1999 Forwards Rev 35 to PLP-201, Emergency Plan. Rev Replaces All Pages of Previous Rev with Exception of EAL Flow Path, Side 1 & 2 & Annex H,Operations Map & Aperature Card. Changes Made by Rev,Listed ML18016B0221999-07-26026 July 1999 Informs That CP&L Proposes to Provide Response to NRC 990414 RAI Re GL 95-07, Pressure-Locking & Thermal-Binding of SR Power-Operated Gate Valves, by 990930 ML18016B0171999-07-16016 July 1999 Forwards Corrected Pages to Annual Radioactive Effluent Release Rept, for 1998 for HNP ML18016B0051999-07-0101 July 1999 Informs of Scheduled Emergency Preparedness Exercise for Shnpp on 990921,per Requirements of 10CFR50,App E.List of 26 Objectives Selected for Evaluation During Exercise,Encl. Without Encl ML18016A9871999-06-14014 June 1999 Forwards Response to NRC 990429 RAI Re License Amend Request to Place Spent Fuel Pools C & D in Service,Dtd 981223.Info Does Not Change Initial Determination That Proposed License Amend Represents No Significant Hazards Consideration ML18016A9831999-06-10010 June 1999 Submits Notification That Reactor Operator Licensed at HNP Has Terminated Employment with Cp&L.Reactor Operator Info Encl.Effective 990528,individuals License Is No Longer Required & CP&L Requests That License Be Terminated ML20212H7521999-06-0404 June 1999 Encourages NRC to Schedule Open Public Forum Which Would Allow Local Citizens to Express Concerns Re Proposed Expansion of high-level Radwaste Storage Capacity at Shearon Harris Npp.With Certificate of Svc.Served on 990624 ML18016A9721999-05-28028 May 1999 Responds to 990309 RAI Re GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs. ML18016B0011999-05-26026 May 1999 Forwards Ltr Received from Hj Jaffe Expressing Concern Re Cpl Proposal to NRC on Dec of 1998 to Make Harris Nuclear Plant Largest Storage Area for High Level Nuclear Waste in Nation ML18016A9631999-05-25025 May 1999 Forwards Periodic Update to FSAR for Hnp.Amend 49 Is Current Through 981128 (End of RFO 8).Some Changes & Analysis Completed After 981128 Have Also Been Included in Amend ML18016A9511999-05-13013 May 1999 Submits Info Re Estimated Effect of Change to ECCS Evaluation Model,As Required by 10CFR50.46 ML18016A9481999-05-0606 May 1999 Forwards NRC Form 396, Certification of Medical Examination by Facility Licensee, for Senior Reactor Operator Licensed to Operate Hnp.Individuals Info Is Proprietary & Is Being Withheld from Public Disclosure,Per 10CFR2.790(a)(6) ML20206R2611999-05-0505 May 1999 Requests That NRC Grant Standing to Intervention Sought by Orange County Board of Commissioners Re Proposal by CP&L to Expand Storage of Hlrw at Shnpp.With Certificate of Svc. Served on 990519 ML18016A9451999-05-0404 May 1999 Provides Proprietary Notification That One SRO Has Been Reassigned from Position for Which Util Certified Need for SRO License & Another SRO Has Terminated Employment with Util.Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9441999-05-0404 May 1999 Notifies NRC of Util Completion of Actions Re GL 96-01, Testing of Safety-Related Logic Circuits at Plant ML18016A9351999-04-30030 April 1999 Forwards Info Requested in 990324 RAI as Suppl to 981223 Application for Amend to License NPF-63 for Alternative Plan for Spent Fuel Pool Cooling & Cleanup Sys Piping ML18016A9311999-04-30030 April 1999 Forwards Annual Radioactive Effluent Release Rept for Jan- Dec 1998 & Rev 11 to ODCM for Shnpp HNP-99-068, Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld1999-04-28028 April 1999 Forwards Rev 0 to Physical Security & Safeguards Contingency Plan. Description of Changes Provided.Encl Withheld ML18016A9221999-04-27027 April 1999 Forwards Proprietary Notification That SRO Licensed on Shnpp Has Terminated Employment with Cp&L,Per 10CFR50.74(b). Proprietary Info Withheld,Per 10CFR2.790(a)(6) ML18016A9211999-04-27027 April 1999 Provides Rev 2 to ISI Relief Request 2RG-008, ISI of Class 1,2 & 3 Snubbers (Code Category F-A) Per Plant TS in Lieu of ASME Code Section XI, in Response to 990408 Telcon with NRC ML18016A9161999-04-22022 April 1999 Forwards Proprietary NRC Form 396, Certification of Medical Exam by Facility Licensee, for SRO Licensed to Operate Hnp. License for Individual Should Be Amended IAW Change Noted on Form.Proprietary Encl Withheld,Per 10CFR2.790(a)(6) ML18016A9201999-04-20020 April 1999 Informs of HNP Personnel Changes to Facilitate Proper Distribution of Correspondence.Records Should Be Updated to Reflect Noted Change ML18016A9121999-04-12012 April 1999 Forwards Diskette Containing Data Re Annual Exposure Rept for Individual Monitoring for Personnel Shnpp,Per 10CFR20.2206(b).Without Encl ML18016A9021999-04-12012 April 1999 Forwards Rev 34 to PLP-201, Shearon Harris NPP Emergency Plan, Replacing All Pages of Previous Rev with Exception of EAL Flow Path,Side 1 & 2 & Annex H Operations Map & Aperture Card.Changes,Listed.Rev Summary,Encl ML18016A8911999-04-0505 April 1999 Forwards non-proprietary App 4A,pages 20-25 & Proprietary Page 4-6 to re-issued Rev 3 of Holtec International Licensing Rept HI-971760.Pages Were Inadvertently Omitted from Reissued Rept.Proprietary Page 4-6 Withheld ML18016A8891999-04-0101 April 1999 Forwards Rev 99-1 to Plant EALs for NRC Review & Approval, Per 10CFR50,App E.Encl Provides Comparison of Currently Approved EALs & Proposed Rev 99-01.Approval of EALs Prior to June 1999,requested.With Four Oversize Drawings ML18016A8811999-03-31031 March 1999 Responds to NRC 990301 Ltr Re Violations Noted in Insp Rept 50-400/98-11.Corrective Actions:Post Trip/Safeguards Actuation Rept for 981023,RT Was Corrected,Required Reviews Completed & Approval Obtained on 990219 ML18016A8671999-03-19019 March 1999 Submits Response to RAI Re Spent Fuel Pool Water Level & Revised Fuel Handling Accident Analyses,Per 990317 Telcon with NRC ML18016A8631999-03-19019 March 1999 Forwards Shnpp Operator Training Simulator,Simulator Certification Quadrennial Rept, IAW 10CFR55.45(b)(5)(ii). NRC Form 474 & Required Info Re Simulator Performance Test Results & Schedules Also Encl ML18016A8691999-03-18018 March 1999 Forwards Resolution Adopted by Lee County,North Carolina Board of Commissioners Re Proposed Expansion of high-level Radioactive Waste Storage Facilities at Carolina Power & Light Shearon Harris Nuclear Power Plant ML18016A8511999-03-15015 March 1999 Forwards Proprietary & non-proprietary Version of Rev 3 to HI-971760, Licensing Rept for Expanding Storage Capacity in Harris SFPs 'C' & 'D'. Repts Are Reissued to Reflect Reduction in Proprietary Info.Proprietary Info Withheld ML18016A8601999-03-15015 March 1999 Informs NRC of Mod to Commitment for Hnp,Re Comprehensive Review of Implementation of TS Sr.Upon Completion of Listed Reviews,Surveillance Procedure Review Project Will Be Considered Complete 1999-09-08
[Table view] |
Text
ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRXBUTION SYSTEM (RXDS)
CESSION NBR:9403140274 DOC.DATE: 94/03/07 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME ROBINSON,W.R.
'UTHOR AFFILIATXON Carolina Power & Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Responds to NRC 940203 ltr re violations'oted in insp rept 50-400/93-25.Corrective actions:tie wraps will be installed on field cables in two dc distribution panels & PSU-111 D connectors replaced.
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Violation R sponse NOTES:Application for permit renewal filed. 05000400 A RECIPIENT COPIES D RECIPIENT COPIES ID CODE/NAME LTD ENCL ID CODE/NAME LTTR ENCL D
PD2-1 PD 1 ( 1 LE,N 1 1 INTERNAL: ACRS 2 2 AEOD/DE IB 1 1 AEOD/DSP/ROAB 1 1 AEOD/DSP/TPAB 1 1 AEOD/TTC 1 1 DEDRO 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PEPB 1 1 NRR/PMAS/ILPB1 1 1 NRR/PMAS/ILPB2 1 1 NUDOCS-ABSTRACT OGC/HDS1 RES/HFB 1
1 1
1 1
1 OEM
%EG RGN2
~
FILE 02 01 1
1 1
1 1
1 EXTERNAL: EG&G/BRYCE,J.H. 1 1 NRC PDR 1 1 NSIC 1 1 D
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOiVI Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24
tJ
<jy CPA.L Carolina Power 8 Light Company William R. Robinson PO Box 165 Vice President New Hill NC 27562 Harris Nuclear Plant
, MAR -"f lgg File: HO-.940507 Serial: HNP-94-018 10CFR2.201 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT DOCKET NO. 50400/LICENSE NO. NPF-63 REPLY TO A NOTICE OF VIOLATION Gentlemen:
In reference to your letter of February 3, 1994, referring to NRC Inspection Report 50-400/93-25, the attached is Carolina Power Bc Light Company's reply to the
~ ~ ~
violations identified in Enclosure 1.
II It is considered that the corrective actions taken/planned are satisfactory for resolution of the violations. Questions regarding this matter may be referred to Mr. D. C. McCarthy at (919) 362-2100.
Very truly yours, W. R. Robinson SDC:sdc Attachment c: Mr. S. D. Ebneter (NRC-RII)
M . N. S. Z (NRR)
Mr. J. E. Tedrow (NRC-SHNPP) 9403140274 940307 PDR ADOCK 05000400 9 PDR State Road1134 New Hill NC Tel 919362-2502 Fax 919362-6950
Attachment to HNP-94-018 REPLY TO A NOTICE OF VIOLATION NRC INSPECTION REPORT NO. 50400/93-25 Re orted Violation A:
10 CFR 50, Appendix B, Criterion XVIrequires that measures shall be established to assure conditions adverse to quality, such as failures, malfunctions,'deficiencies, deviations, and non-confor'mance are properly identified and corrected.
The licensee's Corporate Quality Assurance Manual, Section 12, requires that significant conditions adverse to quality be identified and that corrective actions be determined which will preclude repetition of the condition.
Contrary to the above, following the failure of an auxiliary feedwater system valve in November 1992, the identification and determination of corrective actions for deficiencies noted in the motor control center wiring of auxiliary feedwater system motor operated valves was not sufficient to preclude the repetition of another auxiliary feedwater system valve failure on December 14, 1993.
This is a Severity Level IV violation (Supplement g.
Denial or Admission:
The violation is admitted.
Reason for the Violation:
Plant Change Request PCR-3551 was initiated for the DC electrical distribution system in August 1988 by the Technical Support Unit to disposition concerns of loose electrical connector strips found in DC distribution panels DP-1A2-SA and DP-1B2-SB'. The connectors of concern were Connectron Model PSU-111, separable modular plugs. The PCR prompted an investigation to discern the scope of potential problem(s) with the connectors. A review of records found no equipment failures resulting f'rom these connectors coming loose. It was believed that the PCR was initiated as a result of problems experienced f'rom movement of the cables associated with activities within the DC" distribution panels during construction of the facility. Given that no documented failures could be associated with these connectors after commencement of plant operations, PCR-3551 was canceled in August 1990.
Meanwhile, on July 18, 1989, the Operations Unit issued a Standing Order and mounted placards on the access doors of the two DC distribution panels to heighten operations and maintenance personnel awareness of concerns associated with these connectors. The There are a total of five valves routed through the distribution panels DP-1A24A and DP-1B2-SB.
MEM/HO 940507/OS1
4 Attachment to HNP-94-018 tw Standing Order required verifying proper operation of each valve whose control circuitry is
~ ~ ~ ~ ~
routed through a DC distribution panel in which work is done in the breaker cubicle or to
~ ~ ~ ~
the access doors. ~
PCR-5511 was initiated in September 1990 by the Operations Vnit based on the same concerns that resulted in initiation of PCR-3551. Subsequently, a single failure attributable to a loose PSU-111 connector occurred on November 26, 1992 in the control circuit of valve 1MS-70'. The engineering review stemming from the failure'concluded that the design of the distribution panels, including the PSV-111 terminals, was sufficient if the cables are supported in accordance with design requirements., Further, the review stated that the terminal blocks unlatch due to forces on them f'rom supporting cable weight and pulling forces exerted by the moving of cables. The pull-apart terminal blocks used in the two DC
.~'.".l~hu<3on. g~a~ls have s>>fficient frictional force holding them together such that without the introduction of outside forces the terminal blocks would not pull apart.
Investigation of PCR 5511 prompted another review to discern if there had been any changes since the previous PCR's review. This review identified the single failure on November 26, 1992 in the control circuit of valve 1MS-70 as the only failure. However, given the population of greater than 3500 PSU-111 terminal blocks in service for seven years of operation, a single failure attributable to a loose PSU-111 connection was not considered to be sufficient cause to warrant any design changes. Therefore, PCR-5511 was also canceled on November 12, 1993 and no additional actions were taken.
On December 14, 1993, valve 1AF-137 failed. The root-cause investigation attributed the failure to a loose PSU-111 connector resulting from movement of the cables, possibly by settling, given that the cables had been recently disturbed and were not properly supported by tie-wraps.
The PSU-111 separable modular connectors are used in the two DC distribution panels as well as in other AC Motor Control Centers (MCC). Carolina Power & Light Company believes that the component inoperability concern is limited to the two DC distribution panels because 1) inspection of several AC MCCs confirmed that the cables were appropriately supported by tie-wraps, 2) the AC distribution panels are not entered for routine testing comparable to the two DC panels, and 3) there have been no documented problems with loose connectors within the AC MCCs. The combination of the cables being disturbed to acquire current test readings for DC motor driven MOVs and the lack of supporting tie-wraps has been determined as the probable cause of the two terminal block failures.
Note: A second failure of 1MS-70, on March 8, 1993, referred to in the Inspection Report 93-25 Details Section Paragraph b.(2) was the result of a main contactor problem with the motor operator for valve iMS-70. It did not have any correlation to loose PSU-111 connectors.
MEM/HO940507/osi
Attachment to HNP-94-018 Corrective Ste s Taken and Results Achieved:
Since the failure of 1MS-70, revision to the Root Cause Investigation Procedure (AP-605) requires a more rigorous root cause evaluation. That more rigorous process was followed for the 1AF-137 valve failure investigation. As a result of the failure of 1AF-137 on December 14, 1993, Adverse Condition Report (ACR)93-594 was initiated. Investigation reconfirmed the findings of the engineering review performed in association with PCR-5511, i.e., that the design of the distribution panels was sufficient ifthe cables are tie-wrapped and not disturbed. To that end, the ACR requires the installation of tie-wraps on field cables in the two DC distribution panels.
Corrective Ste s To Be Taken to Prevent Further Violations:
As stated above, tie-wraps will be installed on the field cables in the two DC distribution panels. In addition, Carolina Power & Light Company willreplace the PSU-111 connectors in the DC distribution panels DP-1A2-SA and DP-1B2-SB with a non separable connector.
Date When Full Com liance Will Be Achieved:
Full compliance is expected upon completion of the corrective actions described above. The reinstallation of tie-wraps willbe completed by March 25, 1994. The replacement of the DC panels PSU-111 connectors willbe performed during the upcoming outage. This action will be completed by May 15, 1994.
MEM/H0940507/Osl
Attachment to HNP-94-018 Re orted Violation B:
Technical Specification 6.8.1(a) requires that written procedures be properly established and implemented covering procedures outlined in Appendix A of Regulatory Guide 1.33, Revision 2, February 1978.
Regulatory Guide 1.33, Appendix A, paragraph 2.f requires procedures for changing turbine load, Operating Procedure OP-131.01, Main Turbine, Section 7.1 provides specific guidance for reducing turbine load.
Ccr~ avg to the above, on December 31, 1993, the directions provided in procedure OP-131.01 were determined to be inadequate and could not be performed in the sequerice specified to reduce the turbine load.
This is a Severity Level V violation (Supplement I).
Denial or Admission:
The violation is admitted.
Reason for the Violation:
On December 31, 1993, the plant was to reduce power to perform required testing. In preparation to reduce load, the Control Operator added 50 gallons of boric acid (about an 8 ppm increase in the RCS boron concentration). When the boron took effect, approximately 10 minutes after injection, the turbine load reduction was to start per OP-131.01. While preparing for the power down, the Balance of Plant (BOP) Operator saw that two procedure steps in OP 131.01 were out of sequence. OP-131.01 gives instructions for changing turbine load with the DEH control panel. Step 7.1.2.1.g should have directed the enabling of the Megawatt and Turbine Impulse'ressure feedback loops and then inputting the desired load change. However, the steps were reversed, which would result v the ioac coiiilnand oeing deleted upon activation of the feedback control.
A check of the Operator Feedback Report (OFR) database showed that the problem was already identified. At the time the OFR was initiated, the time frame for revising the procedure was not considered to be critical given the operator knowledge of this evolution through training and experience, plus the fact that this evolution was correctly sequenced in General Operating Procedure GP-006. Hence, the information was in the procedure working file to be added to the procedure during the next revision. However, in October 1993, this work sequence was removed from GP-006 since it was believed to be redundant to OP-131.01.
Management in the Control Room directed the BOP Operator to reduce load based on his knowledge of how to reduce turbine load. The plant load reduction was subsequently completed, but no action was taken to immediately correct OP-131.01. Thus the violation MEM/HO 94507/os1
Attachment to HNP-94-018 Ct occurred because the identified procedure defect was not corrected when first identified.
'econdly, the rediscovery of the error was not appropriately addressed. Proper application of plant procedural use and adherence requirements (AP-100) allows achieving safe stable conditions. In this event, performing a load decrease to maintain RCS average temperature at the program value would be acceptable. However, this should have been immediately followed'with a temporary change to OP-131.01.
Corrective Ste s Taken and Results Achieved:
Procedures have been revised to incorporate the correct sequence of steps for reducing turbine load. This was completed by January 20, 1994.
~
. b.~..~. >iv~ ~> .;,s, Yaken to Prevent Further Violations:
The individuals involved were counseled on the proper response to the discovery of errors in procedures. A discussion of compliance with AP-100 was presented by the Manager-Operations in a Shift Supervisor - Nuclear meeting held on February 8, 1994.
The Operations Unit procedure revision working files were reviewed and seven additional procedure revisions were identified. The seven procedures were subsequently revised.
Date When Full Com liance Will Be Achieved:
Full compliance was achieved as described above by February 14, 1994.
MEM/HO940507/osl
0