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{{#Wiki_filter:Nhc F Oui LJ U. S. NUCLE AR REGUL ATOP.Y CCl.'
{{#Wiki_filter:Nhc F Oui
:J;0N*17-77'F LICENSEE EVENT REPORT CONTROL OLOCK: l llllll(PLE ASE PRINT OR TYPE ALL REQUIRED INFORP.1ATION) o li l l L l Q l A l 0l 1 l@l 0 l 0 l 0 l - 10 0 l 0 l - l 0 l 0 l 0 l@l 4 l 1 l I l 1 1 l@lll@7 8 9 LICENSEE CODE 14 15 LICENSE NUVdER
* LJ                                                                                                           U. S. NUCLE AR REGUL ATOP.Y CCl.'         :J;0N 17-77'               F LICENSEE EVENT REPORT CONTROL OLOCK: l                 l    l      l    l  l      l                (PLE ASE PRINT OR TYPE ALL REQUIRED INFORP.1ATION) o li               l l LLICENSEE lQlA              l 0l 114l@l150 l 0 l 0 l - 10                 0 l 0 l - l 0 l 0 l 0.6l@l264 l 1               l I l 1 1 l@l51 CAl T 5dl@
.6 26 LICENSE TYPE 40 51 CA T 5d CON'T o1i 3M L @l 01 5101010 l 2 l 5 l 4 l@l 1 012101719 l@l 11 Il 0l Il 7191@
7           8 9                           CODE                                       LICENSE NUVdER                                     LICENSE TYPE 40 CON'T 7
" 7 8 60 61 OOCK ET NUMBER 6d 69 ist ENT O ATE 74 75 RE* ORT DATE 83 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES o 2 l While evaluating piping restraints in accordance with NRC IE Bulletin 79-02, i.O 3lStandby Gas Treatment Systems A and B were declared inoperable at 11: 30 a.m. on lOctober 20, 1979 Analyses indicated that piping restraint 1/2-7509-R149 had a lo 4 o 5 safety factor of less than 2.
o1i 8
The Standby Gas Treatment Systems were at all times l0 e j functional and the requirements of Technical Specification 3.7.B.I.b were met.
3M 60 L @l6101 5101010         OOCK ET NUMBER l 2 l 5 l 6d4 l@l 69 1 ist012101719 ENT O ATE          74 l@l 11RE*IlORT 75 0lDATE Il 7191@   83 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES o     2 l           While evaluating piping restraints in accordance with NRC IE Bulletin 79-02,                                                                                 i O     3      l      Standby Gas Treatment Systems A and B were declared inoperable at 11: 30 a.m. on                                                                             l o    4              October 20, 1979                       Analyses indicated that piping restraint 1/2-7509-R149 had a                                                         l o     5             safety factor of less than 2.                               The Standby Gas Treatment Systems were at all times                                             l 0    e         j     functional and the requirements of Technical Specification 3.7.B.I.b were met.                                                                                 [
[o> llo18ll7 8 9 80 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUCCODE COVPCNENT CODE SUSCODE SUSCCCEl Sl Cl@ l Bl@ l A l@ l Sl Ul Pl 0l Rl Tl@ l B l@ lZ @
o     > l                                                                                                                                                                          l o18          l                                                                                                                                                                    l 7            8 9                                                                                                                                                                   80 SYSTEM             CAUSE         CAUSE                                                     COMP.           VALVE CODE             CODE       SUCCODE                 COVPCNENT CODE                   SUSCODE           SUSCCCE                              '
'o 9 7 8 9 10 11 12 13'8 19 20 ,,.SE QUENTI AL OCCURRENCE REPCRT REVISICN LEA a0 EVENT YE AR REPORT NO.
7 o    9 8                          9 l Sl Cl@ l Bl@ l A l@ l Sl Ul Pl 0l Rl Tl@ l B l@ lZ @
CODE TYPE NO.@ Ng.g 17l91 l-l 1013 3I l/l 0111 i Tl L-J 10 1 a 21 22 23 24 26 27 23 23 Ju 31 32 T K A ON ON PLANT T N0URS SS I FOR8 8-5 PPLIE MAN FA 7 ReR lF l@l Z l@
10         11           12             13                           '8           19             20
Zl@lZl@l 0l 0l 0l 0l l Yl@Nl@lAl@Gl2l515l@33 34 35 36 37 40 4 42 43 44 47 CAUSE DESCRIPTICN AND COPRECTIVE ACTIONS h i o!l Evaluation of the design of restraint 1/2-7509-R149 found the design safety factors
                                        ,,.                                       SE QUENTI AL                     OCCURRENCE           REPCRT                       REVISICN LEA a0         EVENT YE AR                           REPORT NO.                           CODE                 TYPE                       NO.
][i li ;to be less conservative than originally analyzed. The restraint was modified to a I , , j safety factor of greater than 4, and at 4:56 a.m. , October 21, 1979, the Standby Gas l lTreatment systems were declared operable.
                    @ Ng.g a 17l91               l-l           1013 3I               l/l               0111               i Tl         L-J           10 1 21       22         23           24             26     27             23       23           Ju             31           32 T K         A     ON             ON PLANT             T                   N0URS         SS I               FOR8     8-     5 PPLIE             MAN FA 7 ReR lF 33 l@l34Z l@                 35 Zl@           lZl@
l, , i 4 1 I 7 8 9 30 STA S NPOWER OTwER S TATUS OtSCOV RY DISCOVERY CESCR:PTION l E l@ l 0l 9 l 8 l@l NAllD l@lExternal Source l1 5, ACTIVITY CC TENT Av0unT or ACTiviTv @
36 l 0l 0l 0l 0l 37 l4 Yl@             Nl@             lAl@             Gl2l515l@
asuEAsED csnELEasE LOCATION OF RELE ASE Z l @ l Zl@l NA NA i 6 7 8 9 10 11 44 45 60 PERSCNNEL EXPOSUAES NUMBER TYPh DESCR'PTCN 29 101010 l@l Z l@l NAli.'' ''''8 PEnsONNe'L mu' dies r 1 -. 5 i Af o oesCn4 Tion 8 3 NuverR FT'l 1010 l 0 l@l NA j e 8 3*1';p3 LOSS OF QA D AMAGE TO F ACILITY TYPE C E SC AIPTION vlZl@lNA i o 7 4 9 19 39 b NRC W CNLY Si7CnPru;N@
40                     42                 43             44             47 CAUSE DESCRIPTICN AND COPRECTIVE ACTIONS h i o!l Evaluation of the design of restraint 1/2-7509-R149 found the design safety factors                                                                                         ]
791119>t msuElNlNAllle l; ;;;;,;;2''i i 3 IU 6d 63.s;.309-654-2241, Ext. 178
[i li ;                 to be less conservative than originally analyzed. The restraint was modified to a                                                                             I
: J. Kopacz.m..rc-en.p3r--
      ,     , j           safety factor of greater than 4, and at 4:56 a.m. , October 21, 1979, the Standby Gas l l
,  
Treatment systems were declared operable.                                                                                                                     l i   4         1                                                                                                                                                                   I 7           8 9                                                                                                                                                                   30 STA S                 NPOWER                       OTwER S TATUS             OtSCOV RY                           DISCOVERY CESCR:PTION 5,                                                          NA 1
.~_2.1.LER NUMBER: LER/RO-79-31/01T-0 ll.LICENSEE NAME: Commonwealth Edison Company
l E l@ l 0l 9 l 8 l@l                                                       l    lD l@l          External Source                                                   l ACTIVITY         CC TENT asuEAsED csnELEasE                            Av0unT or ACTiviTv @                                                   LOCATION OF RELE ASE i    6                                                            NA                                          NA 7          8 9 Z l @ l10Zl@l               11                                       44         45                                                                         60 PERSCNNEL EXPOSUAES NUMBER                 TYPh       DESCR'PTCN 29 i
.Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV.DOCKET NUMBER: 050-254
101010 l@l         '
.V.EVENT DESCRIPTION:
Z l@l                 NA                                                                                                              l
While reevaluating restraint safety factors in accordance with NRC IE Bulletin 79-02, 1/2-7509-R149 was found to have a safety factor of less than 2.
                                                          ''                                                                                                 r                    8 PEnsONNe'L mu' dies NuverR                oesCn4 Tion 8                                                                          1 3-. 5 i         Af o                         j FT'l 81010 e                3 l 0 l@l
Analyzing the system stress with this restraint deleted, the ultimate stress on the system was found to be greater than 1/2.-At this time, 11:30 a.m. , October 20, 1979, the"A" and"B" Standby Gas Treatment (SBGT) systems were declared inoperable and the con-ditions of Technical Specification 3 7.B.1.b were placed into effect.
                                    *1         ';
VI.PROBABLE CONSEQUENCES OF THE OCCURRENCE:
NA p3 LOSS OF QA D AMAGE TO F ACILITY TYPE         C E SC AIPTION                 v NA 7
i   o 4 9 lZl@l      19                                                                                                                                                   39 b           NRC W CNLY 2    ''
msuE lN Si7CnPru;N@
l                                      NA 791119>t                                   ; ;;;;,;;
l    lle l i             i 3             IU                                                                                                                 6d 63                           .s     ;
                                .m..rc-en.p3r--
J. Kopacz                                                        ,
309-654-2241, Ext. 178                    :
 
    .   ~
2
: 1. LER NUMBER: LER/RO-79-31/01T-0 ll. LICENSEE NAME: Commonwealth Edison Company         .
Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV. DOCKET NUMBER: 050-254 V. EVENT DESCRIPTION:
While reevaluating restraint safety factors in accordance with NRC IE Bulletin 79-02, 1/2-7509-R149 was found to have a safety factor of less than 2. Analyzing the system stress with this restraint deleted, the ultimate stress on the system was found to be greater than 1/2.         -
At this time, 11:30 a.m. , October 20, 1979, the "A" and "B" Standby Gas Treatment (SBGT) systems were declared inoperable and the con-ditions of Technical Specification 3 7.B.1.b were placed into effect.
VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:
The Standby Gas Treatment systems were mechanically sound at the time of this occurrence, and all piping and equipment were fully functional.
The Standby Gas Treatment systems were mechanically sound at the time of this occurrence, and all piping and equipment were fully functional.
Also, primary aid secondary containments were fully operable and in effect.Safe plant operation was not compromised by this occurrence.
Also, primary aid secondary containments were fully operable and in effect. Safe plant operation was not compromised by this occurrence.
Vll. CAUSE:
Vll. CAUSE:
An evaluation of the design of restraint 1/2-7509-R149, in accordance with NRC IE Bulletin 79-02, found the design safety factors to be less conservative than originally analyzed.
An evaluation of the design of restraint 1/2-7509-R149, in accordance with NRC IE Bulletin 79-02, found the design safety factors to be less conservative than originally analyzed.
.Vill. CORRECTIVE ACTION:
Vill. CORRECTIVE ACTION:
The restraint was modified to a safety factor of greater than 4, and at 4:56 a.m., October 21, 1979, the SBGT systems were declared oper-able.1354 346.%o}}
The restraint was modified to a safety factor of greater than 4, and at 4:56 a.m., October 21, 1979, the SBGT systems were declared oper-able.
1354 346 o}}

Latest revision as of 05:30, 2 February 2020

LER 79-033/01T-0:on 791020,piping Restraint 1/2-7509-R149 Had Safety Factor of Less than Two.Standby Gas Treatment Sys a & B Declared Inoperable.Caused by Improper Design Safety Factors.Restraint Modified
ML19210C684
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 11/01/1979
From: Kopacz J
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19210C672 List:
References
LER-79-033-01T, LER-79-33-1T, NUDOCS 7911190425
Download: ML19210C684 (2)


Text

Nhc F Oui

  • LJ U. S. NUCLE AR REGUL ATOP.Y CCl.' :J;0N 17-77' F LICENSEE EVENT REPORT CONTROL OLOCK: l l l l l l l (PLE ASE PRINT OR TYPE ALL REQUIRED INFORP.1ATION) o li l l LLICENSEE lQlA l 0l 114l@l150 l 0 l 0 l - 10 0 l 0 l - l 0 l 0 l 0.6l@l264 l 1 l I l 1 1 l@l51 CAl T 5dl@

7 8 9 CODE LICENSE NUVdER LICENSE TYPE 40 CON'T 7

o1i 8

3M 60 L @l6101 5101010 OOCK ET NUMBER l 2 l 5 l 6d4 l@l 69 1 ist012101719 ENT O ATE 74 l@l 11RE*IlORT 75 0lDATE Il 7191@ 83 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES o 2 l While evaluating piping restraints in accordance with NRC IE Bulletin 79-02, i O 3 l Standby Gas Treatment Systems A and B were declared inoperable at 11: 30 a.m. on l o 4 October 20, 1979 Analyses indicated that piping restraint 1/2-7509-R149 had a l o 5 safety factor of less than 2. The Standby Gas Treatment Systems were at all times l 0 e j functional and the requirements of Technical Specification 3.7.B.I.b were met. [

o > l l o18 l l 7 8 9 80 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUCCODE COVPCNENT CODE SUSCODE SUSCCCE '

7 o 9 8 9 l Sl Cl@ l Bl@ l A l@ l Sl Ul Pl 0l Rl Tl@ l B l@ lZ @

10 11 12 13 '8 19 20

,,. SE QUENTI AL OCCURRENCE REPCRT REVISICN LEA a0 EVENT YE AR REPORT NO. CODE TYPE NO.

@ Ng.g a 17l91 l-l 1013 3I l/l 0111 i Tl L-J 10 1 21 22 23 24 26 27 23 23 Ju 31 32 T K A ON ON PLANT T N0URS SS I FOR8 8- 5 PPLIE MAN FA 7 ReR lF 33 l@l34Z l@ 35 Zl@ lZl@

36 l 0l 0l 0l 0l 37 l4 Yl@ Nl@ lAl@ Gl2l515l@

40 42 43 44 47 CAUSE DESCRIPTICN AND COPRECTIVE ACTIONS h i o!l Evaluation of the design of restraint 1/2-7509-R149 found the design safety factors ]

[i li ; to be less conservative than originally analyzed. The restraint was modified to a I

, , j safety factor of greater than 4, and at 4:56 a.m. , October 21, 1979, the Standby Gas l l

Treatment systems were declared operable. l i 4 1 I 7 8 9 30 STA S NPOWER OTwER S TATUS OtSCOV RY DISCOVERY CESCR:PTION 5, NA 1

l E l@ l 0l 9 l 8 l@l l lD l@l External Source l ACTIVITY CC TENT asuEAsED csnELEasE Av0unT or ACTiviTv @ LOCATION OF RELE ASE i 6 NA NA 7 8 9 Z l @ l10Zl@l 11 44 45 60 PERSCNNEL EXPOSUAES NUMBER TYPh DESCR'PTCN 29 i

101010 l@l '

Z l@l NA l

r 8 PEnsONNe'L mu' dies NuverR oesCn4 Tion 8 1 3-. 5 i Af o j FT'l 81010 e 3 l 0 l@l

  • 1 ';

NA p3 LOSS OF QA D AMAGE TO F ACILITY TYPE C E SC AIPTION v NA 7

i o 4 9 lZl@l 19 39 b NRC W CNLY 2

msuE lN Si7CnPru;N@

l NA 791119>t  ; ;;;;,;;

l lle l i i 3 IU 6d 63 .s  ;

.m..rc-en.p3r--

J. Kopacz ,

309-654-2241, Ext. 178  :

. ~

2

1. LER NUMBER: LER/RO-79-31/01T-0 ll. LICENSEE NAME: Commonwealth Edison Company .

Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV. DOCKET NUMBER: 050-254 V. EVENT DESCRIPTION:

While reevaluating restraint safety factors in accordance with NRC IE Bulletin 79-02, 1/2-7509-R149 was found to have a safety factor of less than 2. Analyzing the system stress with this restraint deleted, the ultimate stress on the system was found to be greater than 1/2. -

At this time, 11:30 a.m. , October 20, 1979, the "A" and "B" Standby Gas Treatment (SBGT) systems were declared inoperable and the con-ditions of Technical Specification 3 7.B.1.b were placed into effect.

VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

The Standby Gas Treatment systems were mechanically sound at the time of this occurrence, and all piping and equipment were fully functional.

Also, primary aid secondary containments were fully operable and in effect. Safe plant operation was not compromised by this occurrence.

Vll. CAUSE:

An evaluation of the design of restraint 1/2-7509-R149, in accordance with NRC IE Bulletin 79-02, found the design safety factors to be less conservative than originally analyzed.

Vill. CORRECTIVE ACTION:

The restraint was modified to a safety factor of greater than 4, and at 4:56 a.m., October 21, 1979, the SBGT systems were declared oper-able.

1354 346 o