ML19210D703: Difference between revisions

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{{#Wiki_filter:E0 -3% ;5 cro,so y ae stj?. ace W.bh 0 T-,g1,3gecr>..L,,1no ceen'November 12, 1979 hW pate--TO: U. S. Nuclear Regulatory Commission qine_Office of Inspection and Enforcement initia 'Region III Attention: Tom Tambling
{{#Wiki_filter:E0 -3% ;5 cro,so y November 12, 1979 ceen  ae stj?. ace W T-,g1,3gecr>..L,,1no 0
_, W-
                                                                                      .bh pate-                 hW TO:   U. S. Nuclear Regulatory Commission       qine            _
Office of Inspection and Enforcement     initia '
Region III Attention: Tom Tambling W-


==SUBJECT:==
==SUBJECT:==
Reportable Occurrence Per Technical Specification 6.9.1.8.1
Reportable Occurrence Per Technical Specification 6.9.1.8.1           .
.On November 9, 1979 at 1400 hours, it was determined a reportable event existed in that the Steam and Feedwater Rupture Control System steam generator low level trip setpoint was less conservative than was recuired by Technical Specification 3.3.2.2 Table 3.3-12.
On November 9, 1979 at 1400 hours, it was determined a reportable event existed in that the Steam and Feedwater Rupture Control System steam generator low level trip setpoint was less conservative than was recuired by Technical Specification 3.3.2.2 Table 3.3-12. It was determined by Tolea0 Edison personnel during comple-tion of the response to I.E. Bulletin 79-21 that the level transmitter setpoint was not properly compensated for the hot operating conditions.
It was determined by Tolea0 Edison personnel during comple-tion of the response to I.E. Bulletin 79-21 that the level transmitter setpoint was not properly compensated for the hot operating conditions.
Design work is proceeding to correct the setpoint for hot ambient conditions. The setpoint will be modified prior to the unit entering Mode 3 from the present unit outage.
Design work is proceeding to correct the setpoint for hot ambient conditions. The setpoint will be modified prior to the unit entering Mode 3 from the present unit outage.Onsite inspector, Luis Reyes was notified at 1645 hours on November 9, 1979.
Onsite inspector, Luis Reyes was notified at 1645 hours on November 9, 1979.
D Terry D. Murray Station Superintendent
D Terry D. Murray Station Superintendent
*Davis-Besse Nucler Power Station Toledo Edison Company TDM/SN8/ljk
* Davis-Besse Nucler Power Station Toledo Edison Company TDM/SN8/ljk I
*b.I.yoL 66becL-N/279//mg_.
b.
ge{o 1399 133 y7/'l 7911270 3}}
yoL 66becL-               N/279//mg_.                     ge{o 1399 133 7911270 y7/
                                                                                    'l 3}}

Latest revision as of 05:14, 2 February 2020

Ro:On 791109,steam & Feedwater Rupture Control Sys Steam Generator Low Level Trip Setpoint Discovered Less Conservative than Tech Spec Requirements.Caused by Level Transmitter Setpoint Drift.Design Work Underway
ML19210D703
Person / Time
Site: Davis Besse  Cleveland Electric icon.png
Issue date: 11/12/1979
From: Murray T
TOLEDO EDISON CO.
To:
References
NUDOCS 7911270471
Download: ML19210D703 (1)


Text

E0 -3% ;5 cro,so y November 12, 1979 ceen ae stj?. ace W T-,g1,3gecr>..L,,1no 0

.bh pate- hW TO: U. S. Nuclear Regulatory Commission qine _

Office of Inspection and Enforcement initia '

Region III Attention: Tom Tambling W-

SUBJECT:

Reportable Occurrence Per Technical Specification 6.9.1.8.1 .

On November 9, 1979 at 1400 hours0.0162 days <br />0.389 hours <br />0.00231 weeks <br />5.327e-4 months <br />, it was determined a reportable event existed in that the Steam and Feedwater Rupture Control System steam generator low level trip setpoint was less conservative than was recuired by Technical Specification 3.3.2.2 Table 3.3-12. It was determined by Tolea0 Edison personnel during comple-tion of the response to I.E. Bulletin 79-21 that the level transmitter setpoint was not properly compensated for the hot operating conditions.

Design work is proceeding to correct the setpoint for hot ambient conditions. The setpoint will be modified prior to the unit entering Mode 3 from the present unit outage.

Onsite inspector, Luis Reyes was notified at 1645 hours0.019 days <br />0.457 hours <br />0.00272 weeks <br />6.259225e-4 months <br /> on November 9, 1979.

D Terry D. Murray Station Superintendent

  • Davis-Besse Nucler Power Station Toledo Edison Company TDM/SN8/ljk I

b.

yoL 66becL- N/279//mg_. ge{o 1399 133 7911270 y7/

'l 3