ML19270F684: Difference between revisions

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CONTHOL OLOCK: l                l    l      l        l  l      l                  . (PLEASE PRINT OR TYPE ALL REQUIRED INFORMAllON)
CONTHOL OLOCK: l                l    l      l        l  l      l                  . (PLEASE PRINT OR TYPE ALL REQUIRED INFORMAllON)
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                                                                     .e _ .m . . ~a s                        ao l l !w 1  .1 19 aI 719 t@l ao f 2,e l,116 i                      T ; m ! 7191@    a Ev:, ::.            m-    ~ x.c .        _..gLE ccwEcues.c;n @
                                                                     .e _ .m . . ~a s                        ao l l !w 1  .1 19 aI 719 t@l ao f 2,e l,116 i                      T ; m ! 7191@    a Ev:, ::.            m-    ~ x.c .        _..gLE ccwEcues.c;n @
:      L. While performing local Icak rate testing, the Reactor Core Isolation Cooling System                                                                                              i e      ;3        ;      (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate                                                                                          i 7                      of 396.3 SCFH.                    In the event of a high suppression chamber pressure, stop check                                                                            :
:      L. While performing local Icak rate testing, the Reactor Core Isolation Cooling System                                                                                              i e      ;3        ;      (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate                                                                                          i 7                      of 396.3 SCFH.                    In the event of a high suppression chamber pressure, stop check                                                                            :
  '
s; i          valve 1-1301-41 was available and also could have been manually shut to minimize                                                                                            1 Ji                  leakage back to the RCIC turbine.                                      The leakage through_CV 1-1301-41 d i d _no t,,r,e nde r                                    .
s; i          valve 1-1301-41 was available and also could have been manually shut to minimize                                                                                            1 Ji                  leakage back to the RCIC turbine.                                      The leakage through_CV 1-1301-41 d i d _no t,,r,e nde r                                    .
                                                                                                                                                                                                ..
t
t
{
{
  ,
         .*l      L the RCIC incapable of performing its intended function.                                                                                                                          t s      i                                                                                                                                                                                  I
         .*l      L the RCIC incapable of performing its intended function.                                                                                                                          t s      i                                                                                                                                                                                  I
   *                                                                                                                                                                                                $J d 9 09 0 TE'A            C U.3E            CA J-i                                                              ;            'c q -
   *                                                                                                                                                                                                $J d 9 09 0 TE'A            C U.3E            CA J-i                                                              ;            'c q -
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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1
Ol            The valve internals were found to be di rty. thus preventina a good disc-to-seat seal,                                                                                        I l: lil l                The valve internals were cleaned and the valve reassembled.                                                                  A local leak rate test                          I jil7j l                  was then performed and the leak rate was found to be 0.0 SCFH.                                                                                                                I 1  3      l
Ol            The valve internals were found to be di rty. thus preventina a good disc-to-seat seal,                                                                                        I l: lil l                The valve internals were cleaned and the valve reassembled.                                                                  A local leak rate test                          I jil7j l                  was then performed and the leak rate was found to be 0.0 SCFH.                                                                                                                I 1  3      l 11 141 l                                                                                                                                                                                              l 7            8 9                                                                                                                                                                                    30 A JS          % POWER                            OTHER STATUS                  IS          Y                            DISCOVERY DESCntPTION 1-1    L 8 9 W@ l o10 l o l 0 l@l              12      11 NA 44 l      lBl@l 45          46 Local Leak Rate Testing EO i
                    .
ACitVI TY CON TENT RELEASED OF nELEASE                          AMOUNT OF ACTIVITY                                                                LOCATION OF RELEASE
11 141 l                                                                                                                                                                                              l
* 7            8 9                                                                                                                                                                                    30 A JS          % POWER                            OTHER STATUS                  IS          Y                            DISCOVERY DESCntPTION 1-1    L 8 9 W@ l o10 l o l 0 l@l              12      11 NA 44 l      lBl@l 45          46 Local Leak Rate Testing EO i
ACitVI TY CON TENT
                                                                                                                                                                              '
RELEASED OF nELEASE                          AMOUNT OF ACTIVITY                                                                LOCATION OF RELEASE
!1 3
!1 3
6 h 9 W @ WQl        10            13 HA 44 l            l 45 NA 60 l
6 h 9 W @ WQl        10            13 HA 44 l            l 45 NA 60 l
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2_lli8 Lal81 A              9            to nA                                                                        I cs 69                                LO ;
NAYE OF PnrPAPER                                      M. Kooi                                              pggyg.}09-654-2241, ext. 252                                  {
NAYE OF PnrPAPER                                      M. Kooi                                              pggyg.}09-654-2241, ext. 252                                  {
  *
,
        ..
    '
      .
: l. LER NUMBER:      LER/R0 79-03/03L-0 ll. LICENSEE NAME:  Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV. DOCKET NUMBER:  050-254 V. EVENT DESCRIPTION:
: l. LER NUMBER:      LER/R0 79-03/03L-0 ll. LICENSEE NAME:  Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV. DOCKET NUMBER:  050-254 V. EVENT DESCRIPTION:
On January 19, 1979, while performing Local Leak Rate Testing, the Reactor Core Isolation Cooling System (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate of 396.3 SCFH. The test was performed according to procedure QTS 100-21 by closing the 1-1301-64 stop check valve and pressurizing the volume between the two valves. The Technical Specification leak rate limit for any one primary containment isolation valve is 18.36 SCFH. Work request 357-79 was written to repair the valve.
On January 19, 1979, while performing Local Leak Rate Testing, the Reactor Core Isolation Cooling System (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate of 396.3 SCFH. The test was performed according to procedure QTS 100-21 by closing the 1-1301-64 stop check valve and pressurizing the volume between the two valves. The Technical Specification leak rate limit for any one primary containment isolation valve is 18.36 SCFH. Work request 357-79 was written to repair the valve.

Latest revision as of 19:33, 1 February 2020

LER 79-003/03L-0 on 790119:reactor Core Isoloation Cooling Sys Turbine Steam Exhaust Check Valve Cv 1-1301-41 Was Leaking.Caused by Dirty Valve Internals.Valve Internals Cleaned & Valve Reassembled
ML19270F684
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 02/16/1979
From: Kooi M
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17296A304 List:
References
LER-79-003-03L-09, LER-79-3-3L-9, NUDOCS 7903070386
Download: ML19270F684 (2)


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L. While performing local Icak rate testing, the Reactor Core Isolation Cooling System i e ;3  ; (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate i 7 of 396.3 SCFH. In the event of a high suppression chamber pressure, stop check  :

s; i valve 1-1301-41 was available and also could have been manually shut to minimize 1 Ji leakage back to the RCIC turbine. The leakage through_CV 1-1301-41 d i d _no t,,r,e nde r .

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CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1

Ol The valve internals were found to be di rty. thus preventina a good disc-to-seat seal, I l: lil l The valve internals were cleaned and the valve reassembled. A local leak rate test I jil7j l was then performed and the leak rate was found to be 0.0 SCFH. I 1 3 l 11 141 l l 7 8 9 30 A JS  % POWER OTHER STATUS IS Y DISCOVERY DESCntPTION 1-1 L 8 9 W@ l o10 l o l 0 l@l 12 11 NA 44 l lBl@l 45 46 Local Leak Rate Testing EO i

ACitVI TY CON TENT RELEASED OF nELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE

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NAYE OF PnrPAPER M. Kooi pggyg.}09-654-2241, ext. 252 {

l. LER NUMBER: LER/R0 79-03/03L-0 ll. LICENSEE NAME: Commonwealth Edison Company Quad-Cities Nuclear Power Station Ill. FACILITY NAME: Unit One IV. DOCKET NUMBER: 050-254 V. EVENT DESCRIPTION:

On January 19, 1979, while performing Local Leak Rate Testing, the Reactor Core Isolation Cooling System (RCIC) turbine steam exhaust check valve CV 1-1301-41 was found to have a leak rate of 396.3 SCFH. The test was performed according to procedure QTS 100-21 by closing the 1-1301-64 stop check valve and pressurizing the volume between the two valves. The Technical Specification leak rate limit for any one primary containment isolation valve is 18.36 SCFH. Work request 357-79 was written to repair the valve.

VI. PROBABLE CONSEQUENCES OF THE OCCURRENCE:

The purpose of check valve CV 1-1301-41 is to prevent the back flow of steam from the pressure suppression chamber into the RCIC system.

In the event of a high suppression chamber pressure, stop check valve 1-1301-41 was operable. It also could have been manually shut to minimize leakage back to the RCIC turbine. The leakage through CV 1-1301-41 did not render the RCIC system inoperable, nor incap-able of performing its intended function when needed.

Vll. CAUSE:

Upon disassembly, the valve internals were inspected and the valve disc and seating surfaces were found to be dirty, thus preventing a good disc-to-seat seal. Further inspection revealed no other abnormalities which could have caused the failure. Check valve CV 1-1301-41 is an 8 inch, 150 pound swing check valve manufactured by Crane Company.

Vill, CORRECTIVE ACTION:

The valve internals were c1 caned and the valve was reassembled. A local leak rate test was then performed and the leak rate was found to be 0.0 SCFH.