ML19319B770: Difference between revisions
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{{#Wiki_filter:. | {{#Wiki_filter:. | ||
- .- m__.~. - | - .- m__.~. - | ||
J -m.._._ | J -m.._._ | ||
2 _ _ _ _- | 2 _ _ _ _- | ||
m . | m . | ||
5 . | 5 . | ||
. LICE..,NSEE | . LICE..,NSEE | ||
-; EVENT REPORT - . . - | -; EVENT REPORT - . . - | ||
.Y CO*d stiot OL OCf. l_ [ j l l l] | .Y CO*d stiot OL OCf. l_ [ j l l l] | ||
e 6 b'a aa't' " t ect**st se s,wot a ''',"e't'' | e 6 b'a aa't' " t ect**st se s,wot a ''',"e't'' | ||
i | i E ,"d e"c' | ||
E ,"d e"c' | |||
@i)10 !H I DILLSjl] 10 j.pt-j 010 ! Ml P jF i -!O l 3J l 4 i lj,1,11! 1 J 10_L,A 3 | @i)10 !H I DILLSjl] 10 j.pt-j 010 ! Ml P jF i -!O l 3J l 4 i lj,1,11! 1 J 10_L,A 3 | ||
1 9 74 ' 85 ,a N A : | 1 9 74 ' 85 ,a N A : | ||
Line 45: | Line 33: | ||
. LJ, [ ,(01 | . LJ, [ ,(01 | ||
., 5 ! O t -1 0: 3 r4 1 .1 ., 1,01 5 ~ | ., 5 ! O t -1 0: 3 r4 1 .1 ., 1,01 5 ~ | ||
t VI NT Of 1:nie TIO** , | |||
@i]! Auxiliary Feedwater Pump Turbine (AFFT) 1-2 failed to start on Stea= j 7 89 . so | @i]! Auxiliary Feedwater Pump Turbine (AFFT) 1-2 failed to start on Stea= j 7 89 . so | ||
@i]l Feedwater Rupture Control System actuation si:;nal. The disconnect : | @i]l Feedwater Rupture Control System actuation si:;nal. The disconnect : | ||
Line 53: | Line 41: | ||
[gg L_ (NF-33-77-45) ! | [gg L_ (NF-33-77-45) ! | ||
> e5 m LUD L. i | > e5 m LUD L. i | ||
* IU,n" | * IU,n" | ||
- '<'4,? c n en~, ~, c oo. | - '<'4,? c n en~, ~, c oo. | ||
(d!kIh"' ../PJ:";;','d'n',,, v.o. ... | (d!kIh"' ../PJ:";;','d'n',,, v.o. ... | ||
@IJLCJ.H.J (Aj 'W | @IJLCJ.H.J (Aj 'W i C IK 1T 13 I RJ.K j' LZJ t z_1 Z I Z ! Z I 3 29 to 66 12 IJ 43 e4 43 43 CAWT OtsCneptioN switch was suspected to have been bucced out of 1 J {@0,lij L The It disconnect 9 g m | ||
i C IK 1T 13 I RJ.K j' LZJ t z_1 Z I Z ! Z I 3 29 to 66 12 IJ 43 e4 43 43 | |||
jj(l copifign is located in a narrow corridor, a high traffic area ! | jj(l copifign is located in a narrow corridor, a high traffic area ! | ||
7 89 m 81 | 7 89 m 81 | ||
Line 69: | Line 51: | ||
7 0 LBJ 9 | 7 0 LBJ 9 | ||
LO.JLLDJ to 12 | LO.JLLDJ to 12 | ||
(__NA IJ | (__NA IJ 44 I LAj di | ||
44 I LAj di | |||
[ | [ | ||
afo NA | afo NA j | ||
20 eu. o.c. | |||
eu. o.c. | |||
ac iv co... | ac iv co... | ||
8 m asoveel Of ac t evet y tOCaisose c.r at t C asC | 8 m asoveel Of ac t evet y tOCaisose c.r at t C asC | ||
~ 38 't49^%tU l_Zj . | ~ 38 't49^%tU l_Zj . | ||
LZj i NA osseat.tAst I l NA I 7 9 to Ie 64 ab W Ptnsoaea tt t aroSUAES wveeie n sveg of.sC a eveon 3 LG 7 89 1 d 11.] L7J la 12 l NA 13 g J | LZj i NA osseat.tAst I l NA I 7 9 to Ie 64 ab W Ptnsoaea tt t aroSUAES wveeie n sveg of.sC a eveon 3 LG 7 89 1 d 11.] L7J la 12 l NA 13 g J | ||
Ptn50*egt t ar#Junst s | Ptn50*egt t ar#Junst s h uu e t a et sc enet son | ||
'' NA l e3 talc!Gl o Ii2 w | '' NA l e3 talc!Gl o Ii2 w | ||
_ Lt 7 Stif CONSt Gtti NCES | _ Lt 7 Stif CONSt Gtti NCES | ||
'5 NA. l 7 [9 | '5 NA. l 7 [9 | ||
* a Lo55 OH DAM AGE TO 8 ACILilY ot s e n ,e ,,o., | * a Lo55 OH DAM AGE TO 8 ACILilY ot s e n ,e ,,o., | ||
3 ,v et Z 8 NA | 3 ,v et Z 8 NA l | ||
l | |||
. > a % o | . > a % o | ||
. x - | . x - | ||
rueucity | rueucity | ||
@l e, NA | @l e, NA | ||
.3 l | .3 l | ||
ADD;110N AL f Actons | ADD;110N AL f Actons | ||
[ex @ l. NA | [ex @ l. NA l | ||
(v)' * ** na F, I'3,,1,. . | |||
______ _.,, i Jacque Ling,enfelter/ Rich Chesko (419) ' 259-5000, f .:. . J.d 8 0 01270 2t/O , | |||
______ _.,, i Jacque Ling,enfelter/ Rich Chesko (419) ' 259-5000, f .:. . J.d | |||
8 0 01270 2t/O , | |||
'.[\ | '.[\ | ||
* TOLEDO EDISON COMPANY | * TOLEDO EDISON COMPANY | ||
) DAVIS-BESSE UNIT ONE UUCLEAR POWER STATION , | ) DAVIS-BESSE UNIT ONE UUCLEAR POWER STATION , | ||
SUPPLEMENTAL Il: FORMATION FOR LER NP-33-77-45 . | SUPPLEMENTAL Il: FORMATION FOR LER NP-33-77-45 . | ||
DATE OF EVENT: August 6, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF O'CCURRENCE: Auxiliary Feedwater Pump Turbine (AFPT) 1-2 did net start a Steam Feedwater Rupture Control System (SFRCS) actuation. | DATE OF EVENT: August 6, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF O'CCURRENCE: Auxiliary Feedwater Pump Turbine (AFPT) 1-2 did net start a Steam Feedwater Rupture Control System (SFRCS) actuation. | ||
Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0. | Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0. | ||
Description of Occurrence: On August 6, 1977 at 0329 hours, while performing a section of IP 600.11, " Auxiliary Feedwater and Once Thru Steam Generator Control Systems", AFPT 1-2 did not start on an SFRCS loss of feedwater signal. | Description of Occurrence: On August 6, 1977 at 0329 hours, while performing a section of IP 600.11, " Auxiliary Feedwater and Once Thru Steam Generator Control Systems", AFPT 1-2 did not start on an SFRCS loss of feedwater signal. | ||
Both Steam Generators did isolate as required, but AFPT l-2 did not start, placing the Station in Action Statement of Technical Specification 3.7.1.2. | Both Steam Generators did isolate as required, but AFPT l-2 did not start, placing the Station in Action Statement of Technical Specification 3.7.1.2. | ||
Line 134: | Line 93: | ||
) ment Isolation Valve was partially caused by a disconnect switch being in " LOCAL", | ) ment Isolation Valve was partially caused by a disconnect switch being in " LOCAL", | ||
NP-33-77-38. | NP-33-77-38. | ||
f | f | ||
---}} | ---}} |
Latest revision as of 05:32, 1 February 2020
ML19319B770 | |
Person / Time | |
---|---|
Site: | Davis Besse |
Issue date: | 08/31/1977 |
From: | Chesko R, Lingenfelter J TOLEDO EDISON CO. |
To: | |
Shared Package | |
ML19319B674 | List: |
References | |
NUDOCS 8001270240 | |
Download: ML19319B770 (2) | |
Text
.
- .- m__.~. -
J -m.._._
2 _ _ _ _-
m .
5 .
. LICE..,NSEE
-; EVENT REPORT - . . -
.Y CO*d stiot OL OCf. l_ [ j l l l]
e 6 b'a aa't' " t ect**st se s,wot a ',"e't
i E ,"d e"c'
@i)10 !H I DILLSjl] 10 j.pt-j 010 ! Ml P jF i -!O l 3J l 4 i lj,1,11! 1 J 10_L,A 3
1 9 74 ' 85 ,a N A :
c a t a cca *T*E("' is .It noc.etsuvuote e st N e tia t e accos t om e t 6 (0 18t0i6 1717,. 8 131 1 1 7g CON'I t,, ,
. LJ, [ ,(01
., 5 ! O t -1 0: 3 r4 1 .1 ., 1,01 5 ~
t VI NT Of 1:nie TIO** ,
@i]! Auxiliary Feedwater Pump Turbine (AFFT) 1-2 failed to start on Stea= j 7 89 . so
@i]l Feedwater Rupture Control System actuation si:;nal. The disconnect :
e9 y
[~E]t switch for Valve MS107 was found out of the " Remote" position. (
) e9 a
[gg L_ (NF-33-77-45) !
> e5 m LUD L. i
- IU,n"
- '<'4,? c n en~, ~, c oo.
(d!kIh"' ../PJ:";;','d'n',,, v.o. ...
@IJLCJ.H.J (Aj 'W i C IK 1T 13 I RJ.K j' LZJ t z_1 Z I Z ! Z I 3 29 to 66 12 IJ 43 e4 43 43 CAWT OtsCneptioN switch was suspected to have been bucced out of 1 J {@0,lij L The It disconnect 9 g m
jj(l copifign is located in a narrow corridor, a high traffic area !
7 89 m 81
- s9 durinst construction. . i
,,3 ss 2IOS s covee a oses astaavs ossbo uw otSc ovt *t s Dt3C n ert soav 8
7 0 LBJ 9
LO.JLLDJ to 12
(__NA IJ 44 I LAj di
[
afo NA j
20 eu. o.c.
ac iv co...
8 m asoveel Of ac t evet y tOCaisose c.r at t C asC
~ 38 't49^%tU l_Zj .
LZj i NA osseat.tAst I l NA I 7 9 to Ie 64 ab W Ptnsoaea tt t aroSUAES wveeie n sveg of.sC a eveon 3 LG 7 89 1 d 11.] L7J la 12 l NA 13 g J
Ptn50*egt t ar#Junst s h uu e t a et sc enet son
NA l e3 talc!Gl o Ii2 w
_ Lt 7 Stif CONSt Gtti NCES
'5 NA. l 7 [9
- a Lo55 OH DAM AGE TO 8 ACILilY ot s e n ,e ,,o.,
3 ,v et Z 8 NA l
. > a % o
. x -
rueucity
@l e, NA
.3 l
ADD;110N AL f Actons
[ex @ l. NA l
(v)' * ** na F, I'3,,1,. .
______ _.,, i Jacque Ling,enfelter/ Rich Chesko (419) ' 259-5000, f .:. . J.d 8 0 01270 2t/O ,
'.[\
- TOLEDO EDISON COMPANY
) DAVIS-BESSE UNIT ONE UUCLEAR POWER STATION ,
SUPPLEMENTAL Il: FORMATION FOR LER NP-33-77-45 .
DATE OF EVENT: August 6, 1977 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF O'CCURRENCE: Auxiliary Feedwater Pump Turbine (AFPT) 1-2 did net start a Steam Feedwater Rupture Control System (SFRCS) actuation.
Conditions Prior to Occurrence: The plant was in Mode 3, with Power (MWT) = 0 and Load (MWE) = 0.
Description of Occurrence: On August 6, 1977 at 0329 hours0.00381 days <br />0.0914 hours <br />5.439815e-4 weeks <br />1.251845e-4 months <br />, while performing a section of IP 600.11, " Auxiliary Feedwater and Once Thru Steam Generator Control Systems", AFPT 1-2 did not start on an SFRCS loss of feedwater signal.
Both Steam Generators did isolate as required, but AFPT l-2 did not start, placing the Station in Action Statement of Technical Specification 3.7.1.2.
Investigation of the occurrence found that the disconnect switch for Valve MS107, AFPT 1-2 Main Steam Supply, had been bumped slightly out of tne " Remote"
^
position. The disconnect switch was repositioned in the " Remote" position
[( returning AFPT 1-2 to operability at 0333 hours0.00385 days <br />0.0925 hours <br />5.505952e-4 weeks <br />1.267065e-4 months <br /> on August 6, 1977.
Designation of Apparent Cause of Occurrence: The disconnect switch for MS107 is on a panel in a narrow corridor. Ihis area is a high traffic area during construction, but will have limited traffic during normal operations. It is suspected that an unknown person bumped the discennect switch slightly out of the " Remote" position taking control of MS107 away.
Analysis of Occurrence: Since the Reactor had not reached initial criticality, and there was no decay heat in the Reactor core, there was no threat to the health and safety of the public or to Station staff.
Corrective Action: The disconnect switch was repositioned and personnel were instructed to use care while passing through close quarters in ene plant and to be observant of switch positions being in "Re=ote". A Facility Change Request FCR 77-234 has been issued to install a cover over these panels to prevent recurrence.
s Failure Data: No previous Auxiliary Feed Pump inoperabilities were caused by disconnect switches being repositioned. One previous inoperability of a Contain-s_ e
) ment Isolation Valve was partially caused by a disconnect switch being in " LOCAL",
NP-33-77-38.
f
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