ML19330B424: Difference between revisions

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Pdtsawgn. Pa.
Pdtsawgn. Pa.
               ' 53''                                                            DUQUESNE LIGHT COMPANY Beaver Valley Power Station Post Office Boic 4 Shippingport, PA 15077 July 28, 1980 BVPS: JAW:920
               ' 53''                                                            DUQUESNE LIGHT COMPANY Beaver Valley Power Station Post Office Boic 4 Shippingport, PA 15077 July 28, 1980 BVPS: JAW:920
                              .
* Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-052/OlP Mr. B. H. Grier, Director of Regulation United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406
* Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-052/OlP Mr. B. H. Grier, Director of Regulation
* United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406


==Dear Mr. Grier:==
==Dear Mr. Grier:==
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At approximately 1737 hours on July 26, 1980, the diesel fire pump auto-started on low pressure. With no fire alarms present, an operator was directed to shut down the diesel. At 1757 hours, the operator reported to the Shift Supervisor that the diesel fire pump was running at below the rated RPM and pressure. The pump was shut down and the temporary fire pump was tested because the motor-driven fire pump was out of service. The fuel oil was sampled for water and none was found.            The fuel oil filter was changed.
At approximately 1737 hours on July 26, 1980, the diesel fire pump auto-started on low pressure. With no fire alarms present, an operator was directed to shut down the diesel. At 1757 hours, the operator reported to the Shift Supervisor that the diesel fire pump was running at below the rated RPM and pressure. The pump was shut down and the temporary fire pump was tested because the motor-driven fire pump was out of service. The fuel oil was sampled for water and none was found.            The fuel oil filter was changed.
The diesel was started up and tested successfully at 2038 hours.
The diesel was started up and tested successfully at 2038 hours.
The plant motor-driven fire pump is presently out of service; however, a
The plant motor-driven fire pump is presently out of service; however, a temporary fire pump is hooked up for service and it is felt that degradation l              to the system is minimized because of this backup pump.
,
temporary fire pump is hooked up for service and it is felt that degradation l              to the system is minimized because of this backup pump.
                                                                   ~
                                                                   ~
Very truly yours, kl!d
Very truly yours, kl!d
,
[    J. A. Werling S.per1nt.ne.nt i
[    J. A. Werling S.per1nt.ne.nt i
8008 0 4,0 C)/ 3
8008 0 4,0 C)/ 3


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          . .                                                                              - - _ -- _
Mr. B. H. Grier                                                                          i July 28, 1980                                                                            l BVPS: JAW:920 Page 2 cc: Director Of Management & Program Analysis United States Nuclear Regulatory Commission Washington, D. C. 20555 W. J. Ross, BVPS Licensing Project Manager v#'
                                                                                        --
United States Nuclear Regulc.cory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatary Commission, BVPS Eite Inspector C. A. Olson, Secretary, Prime Movers Committee - EEI Nuclear Safety Analysis Center, Palo Alto, California Mr. John Alford, PA Public Utilities Commission, Harrisburg, PA l
  . . .
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1 Mr. B. H. Grier                                                                          i July 28, 1980                                                                            l
                                                                                                        '
BVPS: JAW:920 Page 2 cc: Director Of Management & Program Analysis United States Nuclear Regulatory Commission Washington, D. C. 20555 W. J. Ross, BVPS Licensing Project Manager v#'
United States Nuclear Regulc.cory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatary Commission, BVPS Eite Inspector
* C. A. Olson, Secretary, Prime Movers Committee - EEI Nuclear Safety Analysis Center, Palo Alto, California Mr. John Alford, PA Public Utilities Commission, Harrisburg, PA l
                          .
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Latest revision as of 19:25, 31 January 2020

RO 80-052/01P:on 800726,diesel Fire Pump auto-started Below Rated RPM & Pressure.No Specific Cause Found.Fuel Oil Filter Changed & Pump Tested Successfully
ML19330B424
Person / Time
Site: Beaver Valley
Issue date: 07/28/1980
From: Werling J
DUQUESNE LIGHT CO.
To:
References
BVPS:JAW:920, NUDOCS 8008040013
Download: ML19330B424 (2)


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Pdtsawgn. Pa.

' 53 DUQUESNE LIGHT COMPANY Beaver Valley Power Station Post Office Boic 4 Shippingport, PA 15077 July 28, 1980 BVPS: JAW:920

  • Beaver Valley Power Station, Unit No. 1 Docket No. 50-334, License No. DPR-66 LER 80-052/OlP Mr. B. H. Grier, Director of Regulation United States Nuclear Regulatory Commission Region 1 631 Park Avenue King of Prussia, Pennsylvania 19406

Dear Mr. Grier:

In accordance with Appendix A, Beaver Valley Technical Specifications, Licensee Event Report 80-052/0lP, Technical Specification 3.7.14.1.a, Fire Suppression, is submitted. This occurrence was reported to Mr. D. A. Beckman, the Beaver Valley Unit 1 NRC Resident Inspector, at 0900 hours0.0104 days <br />0.25 hours <br />0.00149 weeks <br />3.4245e-4 months <br /> on July 28, 1980.

At approximately 1737 hours0.0201 days <br />0.483 hours <br />0.00287 weeks <br />6.609285e-4 months <br /> on July 26, 1980, the diesel fire pump auto-started on low pressure. With no fire alarms present, an operator was directed to shut down the diesel. At 1757 hours0.0203 days <br />0.488 hours <br />0.00291 weeks <br />6.685385e-4 months <br />, the operator reported to the Shift Supervisor that the diesel fire pump was running at below the rated RPM and pressure. The pump was shut down and the temporary fire pump was tested because the motor-driven fire pump was out of service. The fuel oil was sampled for water and none was found. The fuel oil filter was changed.

The diesel was started up and tested successfully at 2038 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.75459e-4 months <br />.

The plant motor-driven fire pump is presently out of service; however, a temporary fire pump is hooked up for service and it is felt that degradation l to the system is minimized because of this backup pump.

~

Very truly yours, kl!d

[ J. A. Werling S.per1nt.ne.nt i

8008 0 4,0 C)/ 3

, -4 l 1

Mr. B. H. Grier i July 28, 1980 l BVPS: JAW:920 Page 2 cc: Director Of Management & Program Analysis United States Nuclear Regulatory Commission Washington, D. C. 20555 W. J. Ross, BVPS Licensing Project Manager v#'

United States Nuclear Regulc.cory Commission Washington, D. C. 20555 D. A. Beckman, Nuclear Regulatary Commission, BVPS Eite Inspector C. A. Olson, Secretary, Prime Movers Committee - EEI Nuclear Safety Analysis Center, Palo Alto, California Mr. John Alford, PA Public Utilities Commission, Harrisburg, PA l

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