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PNO-II-96-081, on 961112,Unit 2 Experienced Turbine Generator Trip from 100% Power.Investigation Into Cause of Turbine Generator Trip Revealed Ground Fault on Main Generator Stator Phase a Windings.Addl Followup Will Be Performed13 November 1996PNO-II-96-081:on 961112,Unit 2 Experienced Turbine Generator Trip from 100% Power.Investigation Into Cause of Turbine Generator Trip Revealed Ground Fault on Main Generator Stator Phase a Windings.Addl Followup Will Be Performed
PNO-II-92-020, on 920327,hot Particle Was Detected on Forehead of Health Physics Technician When Exiting Radiation Control Area.No Erythema Was Oberved & Employee Scheduled to Visit Company Physician as Precaution30 March 1992PNO-II-92-020:on 920327,hot Particle Was Detected on Forehead of Health Physics Technician When Exiting Radiation Control Area.No Erythema Was Oberved & Employee Scheduled to Visit Company Physician as Precaution
PNO-II-89-066A, updates Status of Hurricane Hugo for Nuclear Facilities in Southeast.Manning of Incident Response Ctr by Region II Continuing21 September 1989PNO-II-89-066A:updates Status of Hurricane Hugo for Nuclear Facilities in Southeast.Manning of Incident Response Ctr by Region II Continuing
PNO-II-89-026, 80,000 1b Reactor Coolant Pump Motor Enroute to Cheswick,Pa Collapsed One Side of Low Boy Trailer Resulting in Small Brush Fire.Surveys at Site Confirmed No Contamination.Commonwealth of VA Health Dept Notified27 March 1989PNO-II-89-026:80,000 1b Reactor Coolant Pump Motor Enroute to Cheswick,Pa Collapsed One Side of Low Boy Trailer Resulting in Small Brush Fire.Surveys at Site Confirmed No Contamination.Commonwealth of VA Health Dept Notified
PNO-II-89-015A, on 890225,primary to Secondary Steam Generator Tube Leak at Plant.Caused by Mechanical Failure. Eddy Current & Boroscopic Insps of Affected Tube Will Be Conducted Following Removal of Plug10 March 1989PNO-II-89-015A:on 890225,primary to Secondary Steam Generator Tube Leak at Plant.Caused by Mechanical Failure. Eddy Current & Boroscopic Insps of Affected Tube Will Be Conducted Following Removal of Plug
PNO-II-89-015, on 890125,Unit 1 Tripped Due to Ruptured Air Line to Main Feedwater Regulating Valve.Subsequent to Trip, Radiation Monitor Indications & Increased Charging Flow Revealed primary-to-secondary Leak from C Steam Generator27 February 1989PNO-II-89-015:on 890125,Unit 1 Tripped Due to Ruptured Air Line to Main Feedwater Regulating Valve.Subsequent to Trip, Radiation Monitor Indications & Increased Charging Flow Revealed primary-to-secondary Leak from C Steam Generator
PNO-II-88-022, on 880405,low Levels of Radioactive Matl Detected in Demineralizer Beds for Plant Makeup Water.Caused by Concentrating Effect of Radionuclides.Licensee Currently Storing Spent Demineralizer Beds Onsite Until NRC Approval6 April 1988PNO-II-88-022:on 880405,low Levels of Radioactive Matl Detected in Demineralizer Beds for Plant Makeup Water.Caused by Concentrating Effect of Radionuclides.Licensee Currently Storing Spent Demineralizer Beds Onsite Until NRC Approval
PNO-II-88-004, on 880113,licensee Identified Resin Intrusion from Powdex Demineralizer Sys Into Secondary Side of Steam Generator.Resin Causes Formation of Sulphates,Believed to Be Prime Cause of Steam Generator Tube Failures14 January 1988PNO-II-88-004:on 880113,licensee Identified Resin Intrusion from Powdex Demineralizer Sys Into Secondary Side of Steam Generator.Resin Causes Formation of Sulphates,Believed to Be Prime Cause of Steam Generator Tube Failures
PNO-II-87-079, on 871128,North Anna Unit 1 Was Taken Off Line Due to Excessive Seal Leakage on B Reactor Coolant Pump. Outage Planned for 10 Days to Replace Seal Package & Inspect Lower Radial Bearing on Pump.Commonwealth of VA Informed1 December 1987PNO-II-87-079:on 871128,North Anna Unit 1 Was Taken Off Line Due to Excessive Seal Leakage on B Reactor Coolant Pump. Outage Planned for 10 Days to Replace Seal Package & Inspect Lower Radial Bearing on Pump.Commonwealth of VA Informed
PNO-II-87-070, on 871013,NRC Authorized Startup & Operation Limited to 50% Power for Facility,Down Since 870715 Following Steam Generator Tube Rupture.No Evidence of Steam Generator Tube Leakage Noted13 October 1987PNO-II-87-070:on 871013,NRC Authorized Startup & Operation Limited to 50% Power for Facility,Down Since 870715 Following Steam Generator Tube Rupture.No Evidence of Steam Generator Tube Leakage Noted
PNO-II-87-060, on 870719,hot Particle Recovered from Skin of Left Shoulder Blade of Contract Health Physics Technician & Determined to Be 1.6 Uci of C-60.Investigation Continuing. Technician Restricted from Radiation Control Zone20 August 1987PNO-II-87-060:on 870719,hot Particle Recovered from Skin of Left Shoulder Blade of Contract Health Physics Technician & Determined to Be 1.6 Uci of C-60.Investigation Continuing. Technician Restricted from Radiation Control Zone
PNO-II-87-053A, on 870730,State of Ny,Dept of Environ Conservation & Dept of Radiation Health Completed Survey of Miscellaneous Boxes & Equipment W/Markings from VEPCO Found in Abandoned Bldg in Springwater,Ny.No Problems Noted30 July 1987PNO-II-87-053A:on 870730,State of Ny,Dept of Environ Conservation & Dept of Radiation Health Completed Survey of Miscellaneous Boxes & Equipment W/Markings from VEPCO Found in Abandoned Bldg in Springwater,Ny.No Problems Noted
PNO-II-87-053, on 870728,licensee Notified That Fireman Discovered Miscellaneous Boxes & Equipment in Abandoned Bldg Outside Springwater,Ny.Matl Might Be Clean Surplus Matl Disposed of After Cancellation of North Anna 329 July 1987PNO-II-87-053:on 870728,licensee Notified That Fireman Discovered Miscellaneous Boxes & Equipment in Abandoned Bldg Outside Springwater,Ny.Matl Might Be Clean Surplus Matl Disposed of After Cancellation of North Anna 3
PNO-II-87-049, on 870716,augmented Insp Team Formed After Licensee Calculated Possible Leak Rate of 600 Gpm.Util Will Visually Inspect Steam Generator for More Precise Reading on Occurrence & Reconstructing Circumstances of Event17 July 1987PNO-II-87-049:on 870716,augmented Insp Team Formed After Licensee Calculated Possible Leak Rate of 600 Gpm.Util Will Visually Inspect Steam Generator for More Precise Reading on Occurrence & Reconstructing Circumstances of EventSafe Shutdown
PNO-II-87-048, on 870715,cold Shutdown Reached & Util Downgraded from Alert Status to Recovery Mode.Nrc Inspectors Will Remain Onsite to Follow Up on Licensee Actions & Assess Sequence of Events.Pno Updates PNO-II-87-04715 July 1987PNO-II-87-048:on 870715,cold Shutdown Reached & Util Downgraded from Alert Status to Recovery Mode.Nrc Inspectors Will Remain Onsite to Follow Up on Licensee Actions & Assess Sequence of Events.Pno Updates PNO-II-87-047
PNO-II-87-047, on 870715,unit Experienced Steam Generator Tube Leak.Util Reported Estimated Release of Radioactive Matl to Atmosphere Less than 1.3% of Tech Spec Release Limit.Release Path Isolated15 July 1987PNO-II-87-047:on 870715,unit Experienced Steam Generator Tube Leak.Util Reported Estimated Release of Radioactive Matl to Atmosphere Less than 1.3% of Tech Spec Release Limit.Release Path Isolated
PNO-II-87-043, on 870702,util Shutdown Facility for Longer than 48 Hs to Repair Manual Isolation Valve.Util Plans to Bring Plant to Hot Shutdown & Repair Valve.Svc Will Resume in Several Days2 July 1987PNO-II-87-043:on 870702,util Shutdown Facility for Longer than 48 Hs to Repair Manual Isolation Valve.Util Plans to Bring Plant to Hot Shutdown & Repair Valve.Svc Will Resume in Several Days
PNO-II-86-074, on 861013,licensee Issued News Release Stating That Investigation of Alleged Offsite Drug Use Resulted in Dismissal or Voluntary Resignation of 13 Security Officers or Employees,Including Supervisor of Security at Surry14 October 1986PNO-II-86-074:on 861013,licensee Issued News Release Stating That Investigation of Alleged Offsite Drug Use Resulted in Dismissal or Voluntary Resignation of 13 Security Officers or Employees,Including Supervisor of Security at Surry
PNO-II-86-061, on 860827,turbine & Reactor Manually Tripped Due to High Bearing Vibration on Main Turbine.Caused by Damage to Some Turbine Blades on Last Stage of Low Pressure Turbine.Corrective Action Being Evaluated29 August 1986PNO-II-86-061:on 860827,turbine & Reactor Manually Tripped Due to High Bearing Vibration on Main Turbine.Caused by Damage to Some Turbine Blades on Last Stage of Low Pressure Turbine.Corrective Action Being Evaluated
PNO-II-86-056, on 860804,unidentified Leakage of 1.31 Gpm Noted.Power Reduced to Allow Containment Entry to Identify Leakage.Three Valves,Including Loop Stop Valve,Found Leaking.On 860805,reactor Shut Down to Repair Leak7 August 1986PNO-II-86-056:on 860804,unidentified Leakage of 1.31 Gpm Noted.Power Reduced to Allow Containment Entry to Identify Leakage.Three Valves,Including Loop Stop Valve,Found Leaking.On 860805,reactor Shut Down to Repair Leak
PNO-II-86-051, media Interest Developed Re Denial of Plant Access to Eight Painting Contractor Employees Following Internal Licensee Investigation of Possible Illegal Drug Use.No Charges Filed17 July 1986PNO-II-86-051:media Interest Developed Re Denial of Plant Access to Eight Painting Contractor Employees Following Internal Licensee Investigation of Possible Illegal Drug Use.No Charges Filed
PNO-II-86-029, on 860411,reactor Tripped While Unit Operating at 70%,due to Loss of Permanent Magnet Generator in Exciter Unit.Repairs Will Be Completed by 860415.During Shutdown, Cooldown Rate Higher than Expected14 April 1986PNO-II-86-029:on 860411,reactor Tripped While Unit Operating at 70%,due to Loss of Permanent Magnet Generator in Exciter Unit.Repairs Will Be Completed by 860415.During Shutdown, Cooldown Rate Higher than Expected
PNO-II-86-023, on 860326,reactor Tripped from 100% Power Due to ESF Activation Which Occurred on High Steam Line Flow Coincident W/Low Steam Line Pressure.Caused by Closure of Loop B Main Steam Trip Valve.Investigation Underway26 March 1986PNO-II-86-023:on 860326,reactor Tripped from 100% Power Due to ESF Activation Which Occurred on High Steam Line Flow Coincident W/Low Steam Line Pressure.Caused by Closure of Loop B Main Steam Trip Valve.Investigation Underway
PNO-II-86-020, on 851031,bushings Were Installed During Outage Following Engine Failure in Diesel Generator of Plant Unit 25 March 1986PNO-II-86-020:on 851031,bushings Were Installed During Outage Following Engine Failure in Diesel Generator of Plant Unit 2
PNO-II-86-002, on 851229,shutdown Initiated Due to RCS Leakage Exceeding Tech Spec Limits.Pressure Vessel Head Will Be Removed for Repair of Reactor Pressure Vessel Head Seals.Unit Will Be Out of Svc for Addl 16 Days7 January 1986PNO-II-86-002:on 851229,shutdown Initiated Due to RCS Leakage Exceeding Tech Spec Limits.Pressure Vessel Head Will Be Removed for Repair of Reactor Pressure Vessel Head Seals.Unit Will Be Out of Svc for Addl 16 Days
PNO-II-85-122, on 851228,surveillance Test Determined That Unit 1 RCS Unidentified Leak Rate to Be Approx 0.28 Gpm in Excess of 1.0 Gpm TS Limit.Leakage Suspected to Be Coming from in-core Thermocouple Electrical Connection Seal30 December 1985PNO-II-85-122:on 851228,surveillance Test Determined That Unit 1 RCS Unidentified Leak Rate to Be Approx 0.28 Gpm in Excess of 1.0 Gpm TS Limit.Leakage Suspected to Be Coming from in-core Thermocouple Electrical Connection Seal
PNO-II-85-100, on 851024,480-volt Circuit Breaker or Associated Components for One Battery Room Exhaust Ventilation Fan Failed,Causing Trip of Another Breaker. Plant Gradually Shut Down24 October 1985PNO-II-85-100:on 851024,480-volt Circuit Breaker or Associated Components for One Battery Room Exhaust Ventilation Fan Failed,Causing Trip of Another Breaker. Plant Gradually Shut Down
PNO-II-85-095, on 851011,unit Shut Down Following Failure of One Emergency Diesel Generator to Pass Routine Checks While Down for Maint.Restart Procedures Underway.Pistons & Two Cylinders replaced.Post-repair Review & Testing Completed15 October 1985PNO-II-85-095:on 851011,unit Shut Down Following Failure of One Emergency Diesel Generator to Pass Routine Checks While Down for Maint.Restart Procedures Underway.Pistons & Two Cylinders replaced.Post-repair Review & Testing Completed
PNO-II-85-089, on 850911,leak in Excess of Tech Specs Discovered in Reactor Coolant Loop Bypass Valve.Cause Not Stated.Valve Backseated & Leakage Reduced.Evaluation & Repairs Performed12 September 1985PNO-II-85-089:on 850911,leak in Excess of Tech Specs Discovered in Reactor Coolant Loop Bypass Valve.Cause Not Stated.Valve Backseated & Leakage Reduced.Evaluation & Repairs Performed
PNO-II-85-075, on 850802,plant Shut Down Before Leakage in Steam Generator 14 Exceeded Tech Spec Limit of 500 Gallons Per Day in Single Steam Generator.Plant Remained Out of Svc for 14 Days to Repair Steam Generator Leaks5 August 1985PNO-II-85-075:on 850802,plant Shut Down Before Leakage in Steam Generator 14 Exceeded Tech Spec Limit of 500 Gallons Per Day in Single Steam Generator.Plant Remained Out of Svc for 14 Days to Repair Steam Generator Leaks
PNO-II-85-061, on 850613,unplanned Release of Radioactive Gases Occurred.Caused by Relief Valves Lifting as Result of Water Filling Surge Drum That Removes Radioactive Gas from Primary Coolant.Offsite Doses Negligible14 June 1985PNO-II-85-061:on 850613,unplanned Release of Radioactive Gases Occurred.Caused by Relief Valves Lifting as Result of Water Filling Surge Drum That Removes Radioactive Gas from Primary Coolant.Offsite Doses Negligible
PNO-II-84-042, on 840705,contractor Employee Sustained Back Injuries When Falling 10 Feet While Performing Decontamination Work.Employee Transported to Hosp.Evidence of Contamination,Cracked Rib & Back Injuries Identified5 July 1984PNO-II-84-042:on 840705,contractor Employee Sustained Back Injuries When Falling 10 Feet While Performing Decontamination Work.Employee Transported to Hosp.Evidence of Contamination,Cracked Rib & Back Injuries Identified
PNO-II-82-078B, updating PNO-II-82-078A Re Status of Thermal Sleeves in RCS by Nondestructive Tests.Unit 2 to Remain Shut Down Approx 2 Wks to Remove Thermal Sleeves.Unit 1 Outage Extended to Sept to Replace Control Rod Guide Tube20 July 1982PNO-II-82-078B:updating PNO-II-82-078A Re Status of Thermal Sleeves in RCS by Nondestructive Tests.Unit 2 to Remain Shut Down Approx 2 Wks to Remove Thermal Sleeves.Unit 1 Outage Extended to Sept to Replace Control Rod Guide Tube
ML20055B57513 July 1982Updated PNO-II-82-078A:on 820707,insp of Steam Generator a Revealed That Recently Reinstalled Tube Lane Blocking Device on Secondary Side Was Loose Due to Improper Installation. Steam Generators B & C Devices Found Rigid
PNO-II-82-078, on 820707,unit Shutdown to Investigate Low Level Noise.Noise Discovered to Be Vibration on Secondary Side of Steam Generator.No Corrective Actions Noted.Restart Rescheduled for 8207128 July 1982PNO-II-82-078:on 820707,unit Shutdown to Investigate Low Level Noise.Noise Discovered to Be Vibration on Secondary Side of Steam Generator.No Corrective Actions Noted.Restart Rescheduled for 820712
PNO-II-82-064B, Westinghouse Has Completed Evaluation of Two Metal Objects Found in a & C Steam Generator Hot Leg Plenums.Both Objects Identified as Inconel Nuts from Control Guide Tube Hold Down Pins.Pins Replaced Prior to Startup1 July 1982PNO-II-82-064B:Westinghouse Has Completed Evaluation of Two Metal Objects Found in a & C Steam Generator Hot Leg Plenums.Both Objects Identified as Inconel Nuts from Control Guide Tube Hold Down Pins.Pins Replaced Prior to Startup
PNO-II-82-064A, on 820609,tube End Damage Reported Below Tube Sheet on Hot Leg Side of Steam Generators a & C W/Peening Damage Over 75% of Sheet Area.Evaluation Continuing22 June 1982PNO-II-82-064A:on 820609,tube End Damage Reported Below Tube Sheet on Hot Leg Side of Steam Generators a & C W/Peening Damage Over 75% of Sheet Area.Evaluation Continuing
PNO-II-82-064, on 820606,during Regular Inservice Insp Licensee Observed Peening Damage on Primary Side of Tube Ends in Steam Generators a & C.Damage Being Evaluated by Licensee & Westinghouse9 June 1982PNO-II-82-064:on 820606,during Regular Inservice Insp Licensee Observed Peening Damage on Primary Side of Tube Ends in Steam Generators a & C.Damage Being Evaluated by Licensee & Westinghouse
PNO-II-80-034, on 800226,small Leak Observed from Reactor Water Storage Tank Cooling Sys.Estimated 270 Gallons of Water Contaminated Ground.Licensee Sampling of Storm Drain Sys Showed No Release.Contaminated Matl to Be Shipped27 February 1980PNO-II-80-034:on 800226,small Leak Observed from Reactor Water Storage Tank Cooling Sys.Estimated 270 Gallons of Water Contaminated Ground.Licensee Sampling of Storm Drain Sys Showed No Release.Contaminated Matl to Be Shipped
PNO-II-80-030A, on 800220,util Issued Press Release on Reactor Trip.Westinghouse & Licensee Have Completed Initial Set of Noise Measurement Tests & Will Compare Results W/Normal Operation Testing to Locate Noise22 February 1980PNO-II-80-030A:on 800220,util Issued Press Release on Reactor Trip.Westinghouse & Licensee Have Completed Initial Set of Noise Measurement Tests & Will Compare Results W/Normal Operation Testing to Locate Noise
PNO-II-80-030, on 800220,reactor Inadvertently Tripped When Input Breaker to nonsafety-related Rod Drive Motor/Generator Set 1-1 Opened.Caused by Custodial Personnel.Investigating Possible Loose Parts in Steam Generator C21 February 1980PNO-II-80-030:on 800220,reactor Inadvertently Tripped When Input Breaker to nonsafety-related Rod Drive Motor/Generator Set 1-1 Opened.Caused by Custodial Personnel.Investigating Possible Loose Parts in Steam Generator C
PNO-II-79-001C, on 791005,completed Investigation Into Cause of Overpressurization of Vol Control Tank & Release of Radioactive Gases Into Bldg.Caused by High Influx of Water from Primary Sys10 October 1979PNO-II-79-001C:on 791005,completed Investigation Into Cause of Overpressurization of Vol Control Tank & Release of Radioactive Gases Into Bldg.Caused by High Influx of Water from Primary Sys
ML20217A1178 November 1978PNO-78-191:informs That Virginia Sunshine Alliance Plans Caravan Against VEPCO on 781111-12.VEPCO Notified State & Local Officials & Commonwealth of Virginia.Region II Received Notification of Event on 781108
ML20216K0233 November 1978PNO-78-186:on 781102,unplanned Release of Radioactive Gases, Mostly Xe-133,occurred as Result of Spill of Three Gallons of Radioactive Liquid.Radioactive Release Activated Alarms & Workers Were Evacuated.Region II Notified on 781102
ML20216J75326 October 1978PNO-78-182:on 781024,following Completion of Valve Maintenance & While Returning Charging Sys to Operation,Two Drain Valves Inadvertently Left Open.Thirteen Individuals Received Low Level Contamination & Decontaminated Onsite
ML20249A6611 August 1978PNS-78-037A:on 780731,newscast Indicated That Local Environ Group Planning Antinuclear Demonstration on 780805. Size of Group & Reason for Demonstration Not Indicated
ML20248F14626 May 1978PNO-78-116:on 780427,planned Surveys Conducted Inside Reactor Containment During Startup Testing Program Revealed Neutron & Gamma Radiation Levels in Excess of Those Predicted in FSAR
ML20248K9825 April 1978PNO-78-071:on 780405,initial Criticality Was Achieved.Region II Inspectors Reported That Actual Control Rod Configuration & Boron Concentration Were in Close Agreement W/Predicted Values.News Release Planned by Licensee
ML20248L90216 March 1978PNO-78-049:on 780315,letdown Valve Failed Closed W/Rcs in Solid Water,Cold Shutdown Condition & Average Temp of 158 Degrees F.Analysis Reveals No Excessive Stresses Were Incurred by Reactor Vessel or RCS Piping
ML20248L1216 March 1978PNO-78-040:on 780303,licensee Reported That Architect Engineer,Stone & Webster Engineering Corp,Used Incorrect Allowable Stresses When Designing Piping Support Lugs for safety-related Piping for Units 1 & 2